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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217L0421999-10-21021 October 1999 Forwards Insp Rept 50-382/99-20 on 990815-0925 & Notice of Violation.Two Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217N2111999-10-19019 October 1999 Forwards Insp Rept 50-382/99-14 on 990913-17 & 1004-08.No Violations Noted.Licensed Operator Requalification Program, Effective,Utilized Systems Approach to Training & Showed Continued Improvements Over Previous Insp Findings ML20217L0101999-10-18018 October 1999 Provides Update of Waterford 3 Effort for Review of Ufsar. Info Listed Includes Background Mgt Expectations,Review Status & Results,Clarifications Re Review & Conclusions ML20217L0141999-10-18018 October 1999 Submits Update to NRC Staff Re Circumstances & Plans for Submitting Certification Rept on Waterford 3 Plant Specific Simulator ML20217G7051999-10-14014 October 1999 Forwards Comments on Four of NRC RO Examination Questions for Exam Administered During Week of 991004 05000382/LER-1999-014, Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal1999-10-12012 October 1999 Forwards LER 99-014-00,providing Details of Reactor Shutdown Due to Loss of RCP Controlled bleed-off Flow.Attached Commitment Identification/Voluntary Enhancement Form Identifies All Commitments Contained in Submittal ML20217D5151999-10-0707 October 1999 Forwards Application for Renewal of SRO License for C Fugate License SOP-43039-3,IAW 10CFR55.57.Without Encls ML20217C6251999-10-0505 October 1999 Informs That NRC Reviewed Util Ltr & Encl Exercise Scenario Package for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Based on Review,Nrc Determined That Exercise Appropriate to Meet Objectives ML20212J6921999-09-29029 September 1999 Forwards Insp Rept 50-382/99-18 on 990830-0902.One Noncited Violation Identified Re Failure to Follow Procedural Instructions to Ensure That Members on Fire Brigade Shift Were Qualified ML20216G2441999-09-27027 September 1999 Forwards Insp Rept 50-382/99-19 on 990830-0903.No Violations Noted 05000382/LER-1999-013, Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form1999-09-23023 September 1999 Forwards LER 99-013-00,providing Details of Exceeding TS Limits for RCS Cooldown Rates.All Commitments Contained in Submittal Are Identified on Encl Commitment Identification/ Voluntary Enhancement Form IR 05000382/19993011999-09-21021 September 1999 Informs That NRC License Exam Previously Associated with NRC Insp Rept 50-382/99-301 Will Be Incorporated Into NRC Insp Rept 50-382/99-14 ML20212D8761999-09-16016 September 1999 Informs That on 990818,NRC Staff Completed Midcycle PPR of Waterford 3.During Assessment Period,Number of Personnel Errors Occurred,Which Demonstrated Lack of Attention to Detail by Plant Personnel.Historical Listing of Issues,Encl ML20212C2471999-09-16016 September 1999 Forwards Five Final Applications for RO Licenses for G Esquival,Jm Hearn,Md Lawson,Re Simpson & PI Wood.Written Exam & Operating Test to Be Administered,Is Requested. Encls Withheld ML20212C2391999-09-16016 September 1999 Requests Cancellation of SRO Licenses for Bn Coble,License SOP-43835,due to Job Assignment Location & CA Rodgers, License SOP-43537-1,due to Resignation from Company, Effective 990901 ML20212C5881999-09-14014 September 1999 Forwards Insp Rept 50-382/99-15 on 990719-23 with Continuing in Ofc Insp Until 0819.No Violations Noted ML20211Q4421999-09-0909 September 1999 Forwards Insp Rept 50-382/99-07 on 990601-11.Three Violations Being Treated as Noncited Violations ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) ML20211M8391999-09-0303 September 1999 Forwards Revised Epips,Including Rev 25 to EP-001-020,rev 24 to EP-001-030,rev 25 to EP-001-040,rev 30 to EP-002-100,rev 22 to EP-001-010,rev 27 to EP-002-010,rev 26 to EP-002-102 & Rev 16 to EP-002-190.Listed Proprietary Revs to Epips,Encl ML20211L3681999-09-0202 September 1999 Forwards Five Preliminary Applications for Reactor Operator Licenses for Individuals Listed,Iaw 10CFR55.31.Encls Withheld ML20211K9741999-09-0101 September 1999 Forwards Insp Rept 50-382/99-16 on 990704-0814.Two Severity Level IV Violations Identified & Being Treated as Noncited Violations,Consistent with App C of Enforcement Policy 05000382/LER-1999-011, Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form1999-08-31031 August 1999 Forwards LER 99-011-00,providing Details of Reactor Shutdown Due to Loss of Controlled bleed-off Flow.All Commitments Contained in Submittal Identified on Attached Commitment Identification/Voluntary Enhancement Form ML20211M3641999-08-30030 August 1999 Forwards Written Examination,Operating Tests & Supporting Ref Matl Identified in Attachment 2 of ES-210,in Response to NRC .Encl Withheld ML20211G5751999-08-27027 August 1999 Forwards RAI Re IPEEE Submittal.Please Provide RAI within 60 Days of Receipt of Ltr,Per Util Response to GL 88-20,suppl 4 ML20211E3281999-08-26026 August 1999 Forwards fitness-for-duty Performance Data for Period of 990101-0630,IAW 10CFR26.71(d).Ltr Does Not Contain Commitments 05000382/LER-1999-009, Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately1999-08-26026 August 1999 Forwards LER 99-009-00 Re Discovery of Condition of Noncompliance with App R Involving Inadequate Separation of Essential Cables Routed in Fire Area RAB-30 in Rab. Compensatory Measures Were Established Immediately 05000382/LER-1999-010, Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form1999-08-26026 August 1999 Forwards LER 99-010-00,providing Details of Inadequate Pumping Capacity in Dry Cooling Tower Area.All Commitments Contained in Submittal Are Identified on Attached Commitment Identification Voluntary Enhancement Form ML20211F5421999-08-24024 August 1999 Forwards Proposed marked-up TS Page Xviii, Index Administrative Controls, Correcting Page Number Re TS Change Request NPF-38-220.Editorial Changes for TS Change NPF-38-221 Discussed ML20211F3561999-08-24024 August 1999 Forwards CTS Pages & TS Proposed marked-up Pages for Insertion Into TS Change Request NPF-38-207 Re Efas, Originally Submitted on 980702.Original NSHC Determination Continues to Be Applicable ML20211F4611999-08-24024 August 1999 Informs That NRC Reviewed Ltr & Encl Objectives for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Exercise Objectives Appropriate to Meet Emergency Plan Requirements ML20211G1731999-08-23023 August 1999 Informs That Info Submitted in ,B&W Rept 51-1234900-00,will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 ML20210T9791999-08-18018 August 1999 Discusses Which Responded to Reconsideration of Violation Denial (EA 98-022) Enforcement Action Detailed in .Concludes That Violation Occurred as Stated ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl ML20210S0561999-08-12012 August 1999 Submits Voluntary Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for NRC Fys 2000 & 2001 for Waterford 3 ML20210Q6161999-08-12012 August 1999 Forwards Corrected Copy of Monthly Operating Rept for July 1999 for Waterford 3.Original Rept,Submitted with ,Contained Typos ML20217F2661999-08-12012 August 1999 Forwards Copy of 1999 Waterford 3 Biennial Exercise Package to Be Performed Using Waterford 3 CR Simulator ML20210R9231999-08-11011 August 1999 Forwards Insp Rept 50-382/99-10 on 990719-23.Violations Noted.Nrc Has Determined That One Severity Level IV Violation of NRC Requirements Occurred ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams 05000382/LER-1999-008, Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl1999-07-29029 July 1999 Forwards LER 99-008-00,re Failure to Perform Testing of ESF Filtration Units Per TS Srs.Commitments Made by Util Also Encl ML20210H4291999-07-29029 July 1999 Forwards Response to NRC Rai,Associated with TS Change Request NPF-38-208,proposing to Replace Ref to Supplement 1 with Ref to Supplement 2 of Calculative Methods for CE Small Break LOCA Evaluation Model, in ACs Section of TSs ML20210F9451999-07-27027 July 1999 Forwards Proprietary & non-proprietary Version of Rev 29 to EPIP EP-002-100, Technical Support Ctr Activation,Operation & Deactivation. Proprietary Info Withheld,Per 10CFR2.790 ML20210D3171999-07-23023 July 1999 Submits Proposal for Final Resolution of Reracking Spent Fuel Pool at Plant,Per License Amend 144,issued by NRC in .No New Commitments Are Contained in Ltr 05000382/LER-1999-007, Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached1999-07-23023 July 1999 Forwards LER 99-007-00,providing Details of Operation Outside Tornado Missile Protection Licensing Basis for turbine-driven Emergency Feedwater Pump Exhaust Stack & Steam Supply Piping.All Commitments Identified on Attached ML20210D8701999-07-23023 July 1999 Forwards Safety Evaluation Re First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 Through ISI-020 for Entergy Operations,Inc,Unit 3 ML20210B1521999-07-15015 July 1999 Forwards Insp Rept 50-382/99-13 on 990523-0703.Three Violations Being Treated as Noncited Violations ML20209G9771999-07-13013 July 1999 Forwards Objectives & Guidelines for Waterford 3 Emergency Preparedness Exercise Scheduled for 991013.List of Objectives cross-referenced Where Applicable to Relevant Sections of NUREG-0654 IR 05000382/19990081999-07-12012 July 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-382/99-08 Issued on 990503 ML20209E5231999-07-0909 July 1999 Informs That as Result of NRC Review of Util Responses to GL-92-01,rev 1 & Suppl 1,staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2.This Closes Staff Efforts Re TAC MA0583 ML20209D4051999-07-0707 July 1999 Forwards Revised TS Pages to Replace Attachment C,Entirely in Original TS Change Request NPF-38-207,per 990519 Discussion with C Patel of Nrc.Changes to Action 20 Delete Word Requirement & Revise Word Modes to Mode 1999-09-09
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217L0421999-10-21021 October 1999 Forwards Insp Rept 50-382/99-20 on 990815-0925 & Notice of Violation.Two Severity Level IV Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217N2111999-10-19019 October 1999 Forwards Insp Rept 50-382/99-14 on 990913-17 & 1004-08.No Violations Noted.Licensed Operator Requalification Program, Effective,Utilized Systems Approach to Training & Showed Continued Improvements Over Previous Insp Findings ML20217C6251999-10-0505 October 1999 Informs That NRC Reviewed Util Ltr & Encl Exercise Scenario Package for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Based on Review,Nrc Determined That Exercise Appropriate to Meet Objectives ML20212J6921999-09-29029 September 1999 Forwards Insp Rept 50-382/99-18 on 990830-0902.One Noncited Violation Identified Re Failure to Follow Procedural Instructions to Ensure That Members on Fire Brigade Shift Were Qualified ML20216G2441999-09-27027 September 1999 Forwards Insp Rept 50-382/99-19 on 990830-0903.No Violations Noted IR 05000382/19993011999-09-21021 September 1999 Informs That NRC License Exam Previously Associated with NRC Insp Rept 50-382/99-301 Will Be Incorporated Into NRC Insp Rept 50-382/99-14 ML20212D8761999-09-16016 September 1999 Informs That on 990818,NRC Staff Completed Midcycle PPR of Waterford 3.During Assessment Period,Number of Personnel Errors Occurred,Which Demonstrated Lack of Attention to Detail by Plant Personnel.Historical Listing of Issues,Encl ML20212C5881999-09-14014 September 1999 Forwards Insp Rept 50-382/99-15 on 990719-23 with Continuing in Ofc Insp Until 0819.No Violations Noted ML20211Q4421999-09-0909 September 1999 Forwards Insp Rept 50-382/99-07 on 990601-11.Three Violations Being Treated as Noncited Violations ML20211K9741999-09-0101 September 1999 Forwards Insp Rept 50-382/99-16 on 990704-0814.Two Severity Level IV Violations Identified & Being Treated as Noncited Violations,Consistent with App C of Enforcement Policy ML20211G5751999-08-27027 August 1999 Forwards RAI Re IPEEE Submittal.Please Provide RAI within 60 Days of Receipt of Ltr,Per Util Response to GL 88-20,suppl 4 ML20211F4611999-08-24024 August 1999 Informs That NRC Reviewed Ltr & Encl Objectives for Waterford 3 Emergency Plan Exercise Scheduled for 991013.Exercise Objectives Appropriate to Meet Emergency Plan Requirements ML20211G1731999-08-23023 August 1999 Informs That Info Submitted in ,B&W Rept 51-1234900-00,will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20210T9791999-08-18018 August 1999 Discusses Which Responded to Reconsideration of Violation Denial (EA 98-022) Enforcement Action Detailed in .Concludes That Violation Occurred as Stated ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl ML20210R9231999-08-11011 August 1999 Forwards Insp Rept 50-382/99-10 on 990719-23.Violations Noted.Nrc Has Determined That One Severity Level IV Violation of NRC Requirements Occurred ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams ML20210D8701999-07-23023 July 1999 Forwards Safety Evaluation Re First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 Through ISI-020 for Entergy Operations,Inc,Unit 3 ML20210B1521999-07-15015 July 1999 Forwards Insp Rept 50-382/99-13 on 990523-0703.Three Violations Being Treated as Noncited Violations IR 05000382/19990081999-07-12012 July 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-382/99-08 Issued on 990503 ML20209E5231999-07-0909 July 1999 Informs That as Result of NRC Review of Util Responses to GL-92-01,rev 1 & Suppl 1,staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2.This Closes Staff Efforts Re TAC MA0583 ML20196E6931999-06-22022 June 1999 Forwards Corrected Ltr Re Changes to Rev 19 to Emergency Plan.Original Ltr Had Error in Subject Line ML20196E0831999-06-21021 June 1999 Forwards Insp Rept 50-382/99-12 on 990524-27.No Violations Noted.Purpose of Insp Was to Conduct Assessment of Emergency Preparedness Program ML20196D9941999-06-18018 June 1999 Forwards Insp Rept 50-382/99-11 on 990524-28.No Violations Noted ML20195J8091999-06-17017 June 1999 Forwards Safety Evaulation Re First 10-yr Interval Inservice Insp Relief Request for Plant,Unit 3 ML20196C8711999-06-15015 June 1999 Discusses Insp Rept 50-382/99-08 & Forwards Notice of Violation Re Unescorted Access Which Was Mistakenly Granted to Individual Whose Background Investigation Indicated That He Had Failed Prior Drug Screening with Another Employer ML20196F3721999-06-0909 June 1999 Corrected Ltr Forwarding Rev 19 to Emergency Plan ML20195G3711999-06-0909 June 1999 Ack Receipt of Ltr Dtd 981223,which Transmitted Waterford 3 Steam Electric Station Emergency Plan,Rev 24,under Provisions of 10CFR50,App E,Section V.No Violations of 10CFR50.54(q) Identified During Review ML20207E8541999-06-0303 June 1999 Forwards SE Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressurizer Safety Valves at Plant,Unit 3 ML20207G3441999-06-0303 June 1999 Forwards Insp Rept 50-382/99-09 on 990411-0522 & Notice of Violation.One Violation Identified & Being Treated as Noncited Violation C ML20207D3771999-05-27027 May 1999 Ack Receipt of 990401 & 0504 Ltrs Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-382/99-01 on 990303 ML20207A5121999-05-24024 May 1999 Refers to Which Responded to NOV & Proposed Imposition of Civil Penalty Sent by .Violations A,B & E Withdrawn & Violations C & D Changed to Severity Level IV ML20206U7851999-05-18018 May 1999 Forwards Insp Rept 50-382/99-06 on 990405-09.Three Violations of NRC Requirements Occurred & Being Treated as non-cited Violations ML20206N6961999-05-11011 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization, Division of Licensing Project Management Created ML20206S4411999-05-10010 May 1999 Forwards Insp Rept 50-382/99-05 on 990228-0410.Three Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20206H3841999-05-0707 May 1999 Informs That on 990407,NRC Administered Generic Fundamental Exam Section of Written Operator Licensing Exam.Licensee Facility Did Not Participate in Exam,However Copy of Master Exam,With Answer Key,Encl for Info.Without Encl ML20206K0951999-05-0606 May 1999 Discusses Insp Rept 50-382/99-08 Issued 990503 Without Cover Ltr Documenting EA Number & Subject Line Indicated NOV Which Was Incorrect.Corrected Cover Ltr Encl ML20206F4701999-05-0303 May 1999 Forwards Insp Rept 50-382/99-08 on 990405-07.One Apparent Violation Re Failure to Review & Consider Derogatory Access Authorization Background Info as Required by PSP Identified & Being Considered for Escalated Enforcement Action ML20206K1211999-05-0303 May 1999 Corrected Cover Ltr Forwarding Insp Rept 50-382/99-08 on 990405-07.One Violations Noted & Being Considered for Escalated EA ML20205N7251999-04-13013 April 1999 Forwards Summary of 990408 Meeting with EOI in Jackson, Mississippi Re EOI Annual Performance Assessment of Facilities & Other Issues of Mutual Interest.List of Meeting Attendees & Licensee Presentation Slides Encl ML20205M0561999-04-0909 April 1999 Forwards Insp Rept 50-382/99-04 on 990301-19.One Violation of NRC Requirements Occurred & Being Treated as Noncited Violation,Consistent with App C of Enforcement Policy ML20205J8781999-04-0505 April 1999 Forwards Insp Rept 50-382/99-02 on 990117-0227.No Violations Noted.Inspectors Determined That Six Violations Occurred & Being Treated as Noncited Violations Consistent with App C of Enforcement Policy ML20205J0901999-04-0202 April 1999 Informs That Info Submitted by & 970313 Affidavit Will Be Withheld from Public Disclosure,Per 10CFR2.790(b) (5) ML20205A4681999-03-26026 March 1999 Forwards Insp Rept 50-382/99-03 on 990308-12.Two Violations of Radiation Protection Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20205A6141999-03-25025 March 1999 Forwards SE Accepting Request to Use Mechanical Nozzle Seal Assemblies (Mnsas) as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Application at Plant,Unit 3 ML20205F3311999-03-19019 March 1999 Advises of Planned Insp Effort Resulting from Plant,Unit 3 PPR Review,Which Was Completed on 990211.Performance at Plant,Unit 3 Was Acceptable ML20204E4941999-03-17017 March 1999 Discusses TSs Bases Change Re 3/4.4.1,3/4.6.1.7,3/4.6.3, 3/4.7.12 & 3/4.8.4.Forwards Affected Bases Pp B 3/4 4-1, B 3/4 6-3,B 3/4 6-4,B 3/4 7-7 & B 3/4 8-3 ML20207F1251999-03-0303 March 1999 Forwards Insp Rept 50-382/99-01 on 990125-29 & 0208-12 & Notice of Violations ML20203H8501999-02-17017 February 1999 Forwards SE Accepting Licensee 970701 Submittal of Second Ten Year ISI Program & Associated Relief Request for Plant, Unit 3.Nine Relief Requests Had Been Authorized Previously & Proposed Alternatives Remain Authorized ML20203D7211999-02-11011 February 1999 Forwards Request for Addl Info Re Licensee 970317 & 990111 Responses to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves. Response Should Be Provided within 60 Days 1999-09-09
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Michael B. Sellman, Vice President Operations - Waterford Entergy Operations, In P.O. Box B Killona, Louisiana 70066 i
SUBJECT: NRC INSPECTION REPORT 50-382/96-11 :
Thank you for your letter of October 21,1996,in response to our letter and Notice of Violation dated September 20,1996. We have reviewed your reply and find it l
responsive to the concerns raised in our Notice of Violation. We will review the l
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OV J. E. Dyer, Director Division of Reactor Projects Docket No.: 50-382 License No.: NPF-38 cc:
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P.O. Box 82135 l Baton Rouge, Louisiana 70884-2135 Parish President !
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! . _d PR October 21,1996 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Subject: Waterford 3 SES Docket No. 50-382 License No. NPF-38 NRC Inspection Report 96-11 Reply to Notice of Violation Gentlemen:
In accordance with 10CFR2.201, Entergy Operations, Inc. hereby submits in Attachment 1 the response to the violation identified in Enclosure 1 of the subject l Inspection Repor ;
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The staff expressed concern with the violation in the cover letter of Inspection Report 96-11, because the susceptibility of the auxiliary component cooling water (ACCW)
system to a waterhammer had been addressed previously in inspection Report (IR) l 95-23. Additionally, concern arose because the written instructions for an instrument loop calibration activity were not sufficient to prevent a July 29,1996, inadvertent ACCW pump start and system waterhammer. Waterford 3 shares your concerns, and as detailed in IR 95-23, has taken comprehensive corrective actions to address those matters. These corrective actions included, among other things: (1)
instituting administrative controls to manually close ACCW pump discharge valves before starting the pumps at any time, and (2) operating the ACCW pumps continuously, with periodic venting to detect air intrusion. Those interim measures are intended to forestall future waterhammer events, until a more permanent solution (Design Change 3470) can be implemented during Refuel Outage 8.
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NRC Inspection Report 96-11 Reply to Notice of Violation W3F1-96-0173 ,
Page 2 October 21,1996 Regarding concern with respect to the inadvertent ACCW pump start and system waterhammer, due to the inadvertent nature of the pump start Operations was unable to first close and then throttle the associated discharge valves. Waterford 3 agrees that the Work Authorization Instructions should have been more prescriptiv The corrective action (including implementation of DC-3470) as outlined in the violation response should address this concer If you have any questions concerning this response, please contact me at (504) 739-6242 or Tim Gaudet at (504) 739-666 Very truly yours,
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dE W
/ J.J. Fisicaro h- %
l Director !
I Nuclear Safety JJF/ PRS /ssf Attachment
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cc: t O. Callan (NRC Region IV) -
C.P. Patel (NRC-NRR) l R.B. McGehee N.S. Reynolds NRC Resident inspectors Office l
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ATTACHMENT 1 l
ENTERGY OPERATIONS. INC. RESPONSE TO THE VIOLATION IDENTIFIED IN
' ENCLOSURE 1 OF INSPECTION REPORT 96-11 VIOLATION NO. 9611-03 Technical Specification 6.8.1.a requires, in part, that written procedures shall be
! maintained covering the applicable procedures recommended in Appendix A of
- Regulatory Guide 1.33, Revision 2, February 1978. Appendix A, Section 9, requires l that the licensee have maintenance procedures / written instructions appropriate to
! the circumstance Contrary to the above, on July 29,1996, Work Authorization (WA) 01149346, which provided written instructions for adjusting the process temperature meter for component cooling water temperature control loop manual / automatic station i . CC ITIC7070 B, was not appropriate to the circumstances in that the written instructions did not require returning the manual / automatic setpoint to its original state prior to returning the system to service and, as a result, Auxiliary Component Cooling Water Pump B inadvertently started automatically and caused a waterhammer in the syste This is a Severity Level IV violation (Supplement 1) (50-382/9611-03)
RESPONSE (1) Reason for the Violation Entergy believes the root causes of the violation are inadequate administrative controls and personnel error for the following reasons:
. Procedure Mi-005-563, Component Cooling Water Temperature Control Loop Calibration, Precaution Step 4.1.2 and Section 8.17, System Restoration, are misleading. This procedure provides instructions for the calibration of Control Loops CC IT7075A, CC IT7076A, CC IT7075B, and CCIT7076B. The procedure must be used for calibration or periodic j testing, and may be employed in troubleshooting suspected instrument
- malfunctions. Step 4.1.2 states, "When performing system restoration, the i Auxiliary Component Cooling Water Pump A or B may start if the Nuclear
} Plant Operator (NPO) has not returned the setpoint on Manual / Automatic i (M/A). Station CC ITIC7070 A or B to its original state, before connecting
- wires during performance of Section 8.17 (System Restoration)." The l Caution in Section 8.17 states, " Failure to perform Step 8.17.1 may result
- in starting of the ACCW pump." Step 8.17.1 states, "Have Operations
. return M/A station CC ITIC7070 A or B Setpoint to its original state." An
- l&C Technician could misconstrue from the wording that a reset of the i
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, associated setpoint is required only where a wiring reconnection is l necessary, since that is the only discussion. The caution, precaution, and ,
L restoration se;ction do not discuss action to be taken (setpoint reset) when j a card is removed and reinstalled as was the case in this event or for any ,
l other maintenance.
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. Standards, Policies, and Administrative Controls are not sufficiently l prescriptive. WA packages are planned in accordance UNT-005-l _015 " Work Authorization Preparation and implementation", MD-001-l 026 " Maintenance Work Center Planning," and the Planning i l Information Guide Notebook (PlGN). Requirements are in place i that specify that the planner assemble appropriate work instructions !
in the job plan. For this event, the planner may have been i influenced by the foreman's prior knowledge of the scope of the job, l since it appears that a thorough review of requirements was not 1 performed. Considering the importance and sensitivity of the system being worked on, this job plan warranted more specific '
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. The supervisor pre-job briefings did not include discussion on equipment l
restoration which might have been expected, but was not specifically required. The initial pre-job brief held on 7/18/96 to perform troubleshooting covered the precautions, limitations, and initial condition section of procedure Ml-005-563, but the supervisor did not cover the
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restoration section of Mi-005-563. Another briefing was conducted with a l new crew ten (10) days later on 7/28/96 to continue troubleshooting and j l corrective maintenance. This briefing also did not include discussion on i
the restoration section.
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. Operations failed to appropriately reset th 3 associated setpoint due to l inadequate turnover notes. The I & C Technician involved in completing the M/A Station meter adjustment verbally notified, just prior to Operation's l
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turnover, the NPO that work had been completed but did not communicate
- the need for setpoint restoration. During the Control Room Supervisor ,
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l (CRS) turnover from day shift to night shift the CRS noticed that the CCW y temperature setpoint needed to be reset and communicated that to the l ,
oncoming CRS. The oncoming CRS made a note on his list of turnover ;
items. Later that night, while reviewing his list of turnover items, the CRS l on duty noticed an item dealing with ACCW, but due to the lack of detail in q his notes failed to recognize that he needed to reset the setpoint.
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(2) Corrective Steos That Have Been Taken and the Results Achieved i a)- The ACC-126B setpoint was immediately readjusted to 85 F and the i ACCW Pump B was secure '
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b) Management expectations of what must be discussed in the course of pre-job briefings with respect to equipment restoration was ;
presented to all Maintenance Personnel via a September 26,1996 memorandum from the Maintenance Manage l c) Operations management reviewed this event with the operations crew i that was on shift when the ACCW Pump B inadvertently starte i
Corrective Steos Which Will Be Taken to Avoid Further Violations l (3)
a) ' Procedure Ml-005-563 will be revised to provide a clearer
, understanding of what the intent is and the consequences are for j restoring a M/A Station as described in Step 4. b) More guidance will be provided for the maintenance planners on when J more detailed work instructions are needed in a job plan, through revision of the Planning information Guide Notebook.
I i c) Operations will review the method by which turnovers are performe Particular emphasis will be placed on establishing how important items which have been discussed during the course of a turnover and which need to be performed at a later time in the shift are not overlooke d) All of the control loops in the plant that utilize NTD cards to generate setpoints will be identified and a review will be completed to determine
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whether procedure changes are required to ensure that the setpoints are restored properly following any maintenance.
l e) Management expectations of what must be discussed in the course of j pre-job briefings will be reiterated to the Maintenance Department l personnel through presentations at shop meeting (4) Date When Full Comoliance Will Be Achieved i
Based on the measures taken, Waterford 3 is in full compliance. Waterford 3 l will complete Corrective Steps 3(a),3(b), and 3(c) by 11/30/96, while
, Corrective Steps 3(d) and 3(e) will be finished by December 31,199 ! !
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