IR 05000320/1977040
| ML19220A529 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 11/04/1977 |
| From: | Davis A, Kellogg P, Rebelowski T NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML19220A516 | List: |
| References | |
| 50-320-77-40, NUDOCS 7904230047 | |
| Download: ML19220A529 (9) | |
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U.S. NUCLEAR REGULATORY COM.% SION
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OFFICE OF INSPECTION AND ENFORCEMENT Regfon I Report No.
77-40 Docket No.50-32J B1 License No.
CP9R-66 Priority Category
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Licensee:
Metropolitan Edison Ccmpany
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P. O. Box 542 Reading, Pennsylvania Three Mile Island Nuclear Station, Unit 2 Facility thme:
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Middletown, Pennsylvania Inspection at:
tr r / 6, 10-14, 1977 Inspection conducted
[/ h 77 Inspectors:
M pate/si Qf n Yu. e tor eM/gned77 P. j ' * Wa c i T. Rebelowsk Reactor Inspector
/dyte/ signed cate signed h
'7 7 Approved by:
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.(&. Davis, Chiet, Reactor Projects cate/ signed
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Section No.1, RO&NS Branch Insoection Summary:
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4-6,10-14,1977 (Recort No. 50-320/77-40)
Inscection on October Routine, unannounced inspection of preoperational hot functional Ay as Inspected:
tetting plant status; test results verification; test results review; witness of hot functional testing in progress; and review of previously unresolved items.
The inspector involved 79 inspector-hours onsite by two NRC inspectors and other acccmpanying personnel.
Resul ts: No items of noncompliance were identified.
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Region I Form 12 (Rev. April 77)
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,~DU4$3cc.77
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DETAILS 1.
Persons Contacted Metrocolitan Edison Cccoany
- Mr. M. Beailla, PORC Secretary
- Mr. J. Floyd, Supervisor of Operations
- Mr. J. Hilbish, Senior Reactor Engineer
- Mr. J. Seelir.ger, Unit Superintendent - Technical Suoport General Public Utilities Service Corcoration (GPUSC)
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Mr. A. Dominguez, Shift Test Engineer
- Mr.
R. Fenti, Lead Site QA Auditor Mr. J. Garrison, Shift Test Engineer
- Mr. C. Gatto, Lead Mechanical Engineer
- Mr. T. Hawkins, Assistant Test Superintendent
- Mr. M. Nelson, Technical Engineer Mr. S. Poje, Shift Test Engineer Mr. I. Porter, Lead Engineer
- Mr. R. Toole, Test Superintendent Mr. J. Ulrich, Shift Test Engineer
- denotes those present at exit interview on October 6,1977
- denotes those present at exit interview on October 14,1977
Licensee Action on Previous Insoection Findinas (Closed) Unresolved item (320/77-10-04): Replacement of BFD relays.
The licensee has installed and checked thirty-four relays identified as a result of IE Circular 76-02 actions.
(Closed) Unresolved item (320/77-17-02): Issuance of preoperational precedures.
lne licensee has approved Test Procedure 600/20, Loss of Electric Pcwer.
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G5-205
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Hot Functional Testing (HFT) - TP 600/28 3.
The licensee's hot functional test program consists of a sequence of tests performed on the reactor coolant system and various auxiliary systems as these systems are brought to the hot conditi The system and ccmponent performance during integrated operation.
first time.
2F, reactor coolant system (RCS) is heated to the ho The licensee's HFT pro-at 532 F for testing and then cooled down.cedure, TP 600/28
specifies the measurements required at the established temperatureDu 3500, 4500, and 5320F.
plateaus of 2500, licensee ccmpleted the HFT and a plant cooldown was com
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October 14, 1977.
of preoperational testing and the proposed technical specification surveillance requirements that would be required to be performed initially at 5320F.
No inadequacies were identified during this review, a.
Purpose The purpose of the inspection during HFT is to verify through
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independent observations, evaluation, and record review, that testing is conducted in accordance with established p included observations made in the control room, control and service and controls.
building, reactor building, auxiliary fuel handling building, and other areas of the plant.
b.
Tests Witnessed The inspector witnessed portions of the following hot functional tests and measurements:
(1) TP 600/20 Loss of Electric Power Tests The licensee performed sections of tests involving loss of Preliminary results two 230 KV Buses, Bus 4 and Bus 8.
indicated transfer of the bus loads was accomplished satis-The bus transfers factorily within the.10 sec criteria. Computer inputs and breaker occurred in.04 to.06 seconds.
target indicators did not reflect breaker positions accurately.
Further testing in this area will be performed by the licensee.
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GW 206
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TP 600/3 Soluble Poison Concentration Test _
(2)
The inspector witnessed the licensee test performance in the areas of boration and deboration and the validati of operating procedures and calculational techniques.
The following concerns were identified and require licensee action for resolution:
Revision of OP 2103-1.2 to include revised Baron Addition Pump Stroke vs Concentration Curves to reflect (a)
test data.
Modification to the agitator on Boric Acid mixing tank (b)
to aid in proper mixing.
All system flow paths were not demonstrated.
(c)
Heat tracing associated with borated lines was not (d)
complete.
Redundancy of boron addition pumps was not demonstrate (e)
The above items are grouped as an Unresolved Item (32
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A preliminary review of test results indicated that licensee has met the criteria for boration and deboration system operations.
(3) TP 600/17 CRDM Ooerational Test _
CRDM group pulls and drops were witnessed in the control r
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An intermittent loss of position The licensee and CRDM cabinet room.
indication on Rod 11 in Group 5 was identified.
repeated testing and could not duplicate the criteria had been met.
TP 600/23 Reactor Protection System Functional Test (4)
The inspector witnessed the establishmen Completion of the testing was delayed due to interference with other testing in progress.
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(5) TP 204/3 Reactor Buildina Soray Pumos The inspector witnessed the licensee's demonstration of the BS-P-1B spray pump in the area of head curves.
Three points were demonstrated and fell within the acceptance criteria. The maximum flow attained in the surveillance made of operation of recirculation was 1080 gpm.
Discussion with vendor field engineer indicated that the original icw flow problem was due to interposing the curves for BS-PIB with BS-PlA.
The BS-P-1B pump test curves did demonstrate that pump capability was in excess of 1500 gpm.
The results of testing of BS-PlA will be reviewed at a subsequent inspection.
c.
Parameters Observed The inspector observed the following parameters for each test witnessed:
Procedure Availability
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The inspector verified that the official copy of the approved procedure, TP 600/28, was available in the control room and used by test personnel.
The inspector verified that official approved copies of the test procedures were in use for all tests witnessed.
Crew Mannina
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The licensee established a shift test engineer to coordinate testing. Additionally a test engineer was assigned to cover each test procedure in progress.
The normal operations crew manned the control room and consisted of a Shift Foreman plus
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several control and equipment operators.
Prerecuisites and Initial Condition
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Extensive prerequisites and initial system conditions were contained in each test procedure (TP).
The inspector verified that prerequisites and initial conditions had been signed off or properly resolved by test exceptions or Test Change Notices.
The inspector verified by independent effort that selected prerequisites in the HFT program had been accomplished.
These prerequisites included system valve lineups, water chemistry specifications, and system operability.
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Soecial Test Ecuioment
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The inspector verified the special test equipment required by the TP's was in use and th?t current calibration stickers were affixed to the equipment.
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Test Performance The inspector verified, through observations of testing and a sampling review of TP's, that the testing was performed as required by the procedures.
The TP's were found to be properly documented to indicate changes, identify problems encountered an show adherence to procedural steps.
Crew Performance
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The inspector observed that test personnel engaged in the test program were briefed at each shift change and prior to the performance of testing.
Test personnel actions under planned and unplanned conditions, which were observed by the inspector, appeared to be ccrfucted in an orderly manner.
Communications were maintained between test and operations personnel during the conduct of the testing.
Data Collection
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The inspector verified for those tests witnessed, that all data required by procedure was recorded on the appropriate data sheets and was completed to the intent allowable, based on the test completion status.
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Test Results
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The formal results of the testing had not been reviewed and
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approved by the licensee at the conclusion of this inspection.
These results will be reviewed during a subsequent inspection of the licensee's preoperational test program.
The inspector had no further questions on the tests witnessed except as noted in the above paragraphs.
4.
Reactor Coolant Pumos During the HFT program the RCPs exhibited leakage between the inner and outer flexitallic gasket joints at the pump machined lands to the reactor coolant loop volute. The resolution of this item will be reviewed during a subsequent inspection.
(320/77-40-02)
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5.
Carbon Steel in Boric Acid Containinc Svstems During a tour of the facility the inspector noted what appeared to. be carbon steel nuts and studs installed in stainless steel systems that contain boric acid. The specifications for the Architect-Engineer and NSSS were reviewed in this area.
It was noted the A-E's specifi-cation required the use of stainless steel nuts and studs in stainless steel systems. The NSSS specification allowed the use of steinless or carbon steel. The inspector indicated that this area would This item receive further review during a subsequent inspection.
is unresolved.
(320/77-40-03)
6.
Test Results Verification The test results of completed tests have been reviewed to determine that the licensee has:
Evaluated the test results to assure that the testing demon-
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strated that the systems met design requirements.
Test results were compared to acceptance criteria.
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A review of procedures has been in conformance with Test Manual, Test Instruction No. 18 Revision 5.
The approval of Test Working Group (TWG) which includes NSSS and AE representatives where indicated by the cognizance system
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under test.
The pro'edures verified include:
c TP 330/1 Control Rod Dr ve Pre-Op Calibration (MTX 38.2) aporoved d
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at TWG Meeting #80, September 29, 1977, and
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TP 260/3 Condenser Air Extraction Functional Test (MTX 26.5)
approved at TWG Meeting #80, September 29, 1977.
Findings The inspector identified one area of concern in his review of TP 260/3 Condenser Air Extraction Functional Test. The licensee has failed to demonstrate the ability of the standby air extraction pump to start at an increase in pressure of 5" Hg absolute. The calibration records and procedure content fail to support the requirements of system as (
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noted in FSAR Section 10.4.2.2.
The licensee stated that the pressure switches activating standby pump will be recalibrated and tested. This item is unresolved (320/77-40-04) pending ccmpletion of recalibration.
No other items of concern were identified.
7.
Test Results Evaluation The inspector's evaluation of licensee test results of TP 330/2 Control Rod Drive Control System Operational Test (MTX 38.3) in-cluded a:
Review of all test changes
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Review of all test deficiencies
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Review of the QA inspection records (Phase I testing)
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Review of the licensee test administrative and technical
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evaluation.
Findings The test Working Groco at meeting #80, September 29, 1977, reviewed and approved TP 330/2 Control Red Drive Control System Operational Test. The inspector reviewed twenty-five test exceptions including eleven test deficiencies. A sampling of the data of the test results identified no inspector concerns.
The QA inspection involve-ment in initial testing identified no concerns. The inspector has no further questions concerning the licensee's evaluation of test results.
8.
Outstanding Items Review A review of Region I open items and the licensee's construction completion was conducted to attempt to ascertain the status of the facility for the issuance of an operating license.
This review was performed by the Operations and Construction Project Inspectors in The results of conjunction with the Licensing Project Manager.
this review indicate an assessment of the open and inccmplete items is not meaningful at this time. This item will be followed during subsequent inspections.
9.
Unresolved Items -
Unresolved items are matters for which more information or additional time is required in order to ascertain whether they are acceptable, items of noncompliance or deviations. Unresolved items identified
during this inspection are discussed in paragraph 5 and 6.
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Exit Interview _
The inspector met with licensee representatives (denoted in paragraph 1) at the conclusien of the inspection on October 6 and O 1977.
and the findings.
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