IR 05000320/1977020

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IE Insp Rept 50-320/77-20 on 770523-26.No Noncompliance Noted.Major Areas Inspected:Quality Records Re Electrical & Instrumentation Cable Installation & Termination
ML19220C298
Person / Time
Site: Crane Constellation icon.png
Issue date: 06/07/1977
From: Finkel A, Mcgaughy R, Narrow L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML19220C291 List:
References
50-320-77-20, NUDOCS 7904300153
Download: ML19220C298 (8)


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U.S. NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT

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Region I

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Report No. 50-320/77-20 Docket No. 50-320

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License No. CPPR-66 Priority

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Category n

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Licensee:

fietropolitan Edison Comoany Box 542 Reading, Pennsylvania 19603 Facility Name:

Three Mile Island 2 Inspection at:

Middletown, Per.nsylvania i

Inspection conducted: May 23-26,1977 h# [#,k (7thZ/07 Inspectors:

u' date digned

).. Harrow,,RgorInspector 0. W h P4 7 ff 77 c

A. Finkel, Reactor Inspector V

dat6 signed date signed Approved by:

N / MA 7,877 R. W. McGaugfydhief, Construction date' signed Projects Section, Reactor Construction and Engineering Support Branch Insoection Summary:

Inspection on itay 23-26, 1977 (Recort No. 50-320/77-20)

Areas Inspected: Routine, unannounced inspection of work performance and quality records concerning electrical and instrumentation cable installation and termina-tion; quality records of instrumentation components; and licensee action on noncoutine events he had previously reported. The inspection involved 54 inspector hours onsite by two NRC inspectors.

Results: No items of noncompliance were identified.

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Region I Form 12

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(Rev. April 77)

"I904300153

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OETAILS 1.

Persons Contacted a.

Principal Licensee Employees

  • R. F. Fenti, QA Auditor
  • S. Levin, Project Engineer
  • R. L. Wayne, Construction QA Manager
  • J. E. Wright, Site QA Manager b.

United Engineers and Constructors, Inc.

  • J. J. Carrabba, Field Supervisor QC/ Construction D. Lambert, QC Supervisor c.

Burns & Roe, Inc.

G. T. Harper, Jr., Site Project Engineer

  • denotes those present at the exit interview.

The inspector also talked with several other licensee em-ployees as well as enployees of the Architect-Engineer and the constructor.

2.

Diesel Generator 4160 Volt Cable Terminations The inspector examined the diesel generators (DG-X-1 A and DF-X-1B)

4160 volt cable teminations from the output of the generators to the bus connector located within the diesel generator teminal box.

The inspector found that the six 4160 volt cables from the DF-X-1 A generator unit had no cable temination lugs, while the six 4160 volt cables from the DF-X-1B generatur unit were terminated in 1/0 - 4/0 UIT (set screw-type cannector).

The inspector reviewed the Colt Industry drawing 11856085, Sheet 1, Revision 6 (B&R File #4300-0110) which specifies Burndy YA-34-2LN lugs for 500 MCM crimp type cable terminals.

The licensee recorded this deviation on Deviation Report 0764 datt.d May 25,1977.

The method of terminating the 4160 volt cables fre.n the diesel generators and mounting the cables onto the three i phase bus in the diesel generator teminal box was under review by engineering during this inspection period.

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This matter is considered to be unresolved (320/77-20-01).

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3.

Vendor Documentation For DH-3-LT-1 The inspector exmnined receiving inspection reports for the Borated Water Storage Tank Level Transmitter No. DH-3-LT-1 and observed that no vendor documentation had been required to be submitted.

This iten was identified on the instrument classification printout as Quality Class 4 and Seismic Class I (for mounting only). The Purchase Order requirements for documentation had not been estab-lished prior to completion of the inspection.

This item is considered to be unresolved (320/77-20-02).

4.

Responsibility for Storage and Cleanliness During Partial Turnover The inspector observed that the responsibility for storage and cleanliness during partial turnover had not been documented in procedures or instructions although in many cases parts of equip-ment had beca turned over to startup.

As exmnples, certain cables within cabinets were turned over to startup as part of a system while the remaining cables and the cabinet itself had not been turned over.

This item is considered to be unresolved (320/77-20-03).

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5.

OC Records of Instrument Components The inspector examined the records shown below f'r conformance to the requirements of the applicable specification s and procedures.

a.

Receiving Inspection and Vendor Documentation Receiving inspection reports and required vendor documentation including performance tests, seismic qualification tests, equipment calibration reports, and certificates of conformance were examined for the following items:

(1)

Pressurizer Level Transmitters RC-1-LT-2 and RC-1-LT-3 (2) Liquid Radiation Monitors DC-R-3399 and DC-R-3400 (3) Gaseous Radiation Monitors WDG-R-1480 and WDG-R-1485 (4)

Intennediate Closed Cooling Water Pressure Indicator IC-Pl-470 (5) Intermediate Closed Cooling Water Temperature Indicator I C-T1-468 i

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Storage, Installation, and Calibration Records QC records of storage, identification, and installation and of field calibration, were required, for the following instruments were examined:

(1) Pressurizer Level Transmitters RC-1-LT-2 and RC-1-LT-3 (2) Borated Water Storage Tank Level Transmitter DH-3-LT-1 (3)

Intermediate Closed Cooling Water Pressure Indicator IC-Pl-470 (4)

Intermediate Closed Cooling Water Tenperature Indicator IC T1-468 (5) Liquid Radiation Monitors DC-R-3399 and DC-R-3400 No items of noncompliance were identified.

6.

Deviation Reports

The inspector examined seven Instrument Deviation Reports and observed that they were complete, legible, readily retreivable, had been reviewed by the Deviation Review Board, dispositioned the corrective work promptly performed and verified by QC.

No items of noncompliance were identified.

7.

Installation and Termination of Power and Control Cables The inspector examined the installation and tennination of the power and control cables listed below and reviewed the procedures and records associated with those cabics.

Circuit No.

System HHlP 9ecay Heat Removal System MA3C MA10C MA336C HH10C HGlP b

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Circuit No.

System HG30P Emergency Feedwater Systen HH30P MA212C MA488C HH54P1 Makeup and Purification Systen HG55P HG45P HH20P Reactor Building Spray System HG20P MA130P Reactor Building Emergency Cooling Rf er Water System IT2903C 1T2904C MA58C MA97C MA226C

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MB74C GA50P Red Diesel Switchgear - 2DG1 GA51P GA52P The inspection included examination of handling and it;entification of cable, use of specified materials, cable tennination, separation, tray loading, grounding and conformance to work procedures and QC proc edures. The inspector reviewed documentation of the final construction inspection and verified that incomplete and noncon-forming condf' ions had been included on the punch lists of the packages for aver to startup.

No items of noncompliance were identified.

8.

Installation and Termination of Instrument Cables The inspector examined installation and termination of instrument cables associated with the DG control panel, radiation monitoring, safe shutdown, and display instrumentation as listed below:

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DG Controls Circuit Cabinet GA81C Red Switchgear Instrumentation GA3C Bus 2-IE to Bus Tie ETB 1, 2, 3, 4, and 5 GA14P GA29C Radiation Monitoring Circuit M874C M876C M930C M933C M944C M956C Display Instrumentaticq Circuit Cabinet Terminal Glock Containment Isolation Cabinet DV No. 35, 36 Cabinet #15 Control Room Unit 2-45, and 46 Safe Shutdcwn Systems Circuit Termination M932C AH-V101, AH-V102, AH-V105 and AH-V107 Indication M934C AH-V105 and AH-V107 Control and Indication M930C AH-V101, AH-V102, AH-V105 and AH-V107 Interlock (

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The inspector examined handling and identification of cable, use of specified material,' cable terminations, separation, grounding, tray loading and conformance to work and QC procedures. The inspector also reviewed the final construction inspection records and verified that incomplete and nonconforming items were included on the punch lists of the package for turnover to startup.

No items of noncanpliance were identified.

10. Plant Tour The inspector walked through various areas of the plant and observed work in progress and adherence to QC requirements for control and protection of equipment.

The inspector observed some deterioration in maintenance of cleanli-ness in cabinets containing circuits which had been turned over to startup.

No items of noncompliance were identified.

11. Review of Nonroutine Events Reported by the Licensee

a.

Galling of Vent Valve Studs On February 20, 1976, the licensee had reported galling of vent valve studs during removal of the valves. The inspector exanined Deviation Reports (DRs) No. 0729 and 0564 which identified the problem and its disposition. The inspector also examined QC reports of the corrective work and replace-ment of two valves which had been damaged.

The inspector had no further questions on this matter.

b.

Short Circuit in Unit Substation 2-21E On November 17, 1976, the licensee had reported i fire caused by a short circuit in unit substation 2-21E had damaged one section of the substation and f everal adjacent circuits.

The inspector examined Deviation Report No. 0658 which described the damage and its disposition and QC records of cleanup of the substation, replacement and testing of damaged wiring and tests of the replacement section of the substation.

The inspector had no further questions on this matter.

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c.

Modification of Reactor Internals Guide Blocks On April 19, 1977, the licensee had reported a field installa-tion problem with the reactor internal guide blocks and lugs as a Significant Deficiency in accordance with 10 CFR 50.55(e).

The inspector audited the Babcock and Wilcox (B&W) Field Construction Procedures which had been prepared for removal, inspection, and repositioning of the guide blocks and lugs.

The inspector also audited material certifications, welding records, and welder qualification records and reviewed QC records of work performance.

No items of noncompliance were identified.

12. Unresolved Items Unresolved items are matters about which more information is required in order to ascertain.whether they are acceptable items, items of noncompliance, or deviations. Unresolved items disclosed during the inspection are discussed in Paragraphs 2, 3, and 4 of this report.

i 13. Exit Interview The inspector met with licensee representatives (denotes in Paragraph 1) at the conclusicn of the inspection on May 26, 1977. The inspector summarized the scope and findings of the inspection.

The licensee representative had no comments.

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