IR 05000280/2015009

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IR 05000280/2015009, 05000281/2015009; 07/13-17/2015 and 07/27-30/2015; Surry Power Station, Units 1 and 2; Biennial Inspection of Problem Identification and Resolution Program
ML15239A719
Person / Time
Site: Surry  Dominion icon.png
Issue date: 08/26/2015
From: Masters A
Reactor Projects Branch 7
To: Heacock D
Dominion Nuclear, Virginia Electric & Power Co (VEPCO)
References
IR 2015009
Download: ML15239A719 (15)


Text

UNITED STATES ust 26, 2015

SUBJECT:

SURRY POWER STATION - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000280/2015009 AND 05000281/2015009

Dear Mr. Heacock:

On July 30, 2015, the U. S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution biennial inspection at your Surry Power Station Units 1 and 2. The enclosed report documents the inspection results which were discussed on July 30, 2015, with Mr. R. Simmons and other members of your staff.

Based on the inspection samples, the inspectors determined that your staffs implementation of the corrective action program supported nuclear safety. In reviewing your corrective action program, the inspectors assessed how well your staff identified problems at a low threshold, your staffs implementation of the stations process for prioritizing and evaluating these problems, and the effectiveness of corrective actions taken by the station to resolve these problems. In each of these areas, the inspectors determined that your staffs performance was adequate to support nuclear safety.

The inspectors also evaluated other processes your staff used to identify issues for resolution.

These included your use of audits and self-assessments to identify latent problems and your incorporation of lessons learned from industry operating experience into station programs, processes, and procedures. The inspectors determined that your stations performance in each of these areas supported nuclear safety.

Finally, the inspectors determined that your stations management maintains a safety-conscious work environment adequate to support nuclear safety. Based on the inspectors observations, your employees are willing to raise concerns related to nuclear safety through at least one of the several means available. The NRC inspectors did not identify any findings or violations of more than minor significance.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Anthony D. Masters, Chief Reactor Projects Branch 7 Division of Reactor Projects Docket Nos.: 50-280, 50-281 License Nos.: DPR-32, DPR-37

Enclosure:

Inspection Report

05000280/2015009 and 05000281/2015009 w/Attachment: Supplemental Information

REGION II==

Docket Nos.: 50-280, 50-281 License Nos.: DPR-32, DPR-37 Report No.: 05000280/2015009 and 05000281/2015009 Licensee: Virginia Electric and Power Company Facility: Surry Power Station, Units 1 and 2 Location: 5850 Hog Island Rd Surry, VA 23883 Dates: July 13 - 17, 2015 July 27 - 30, 2015 Inspectors: R. Rodriguez, Senior Project Engineer (Team Leader)

N. Staples, Senior Project Inspector M. Coursey, Reactor Inspector K. Steddenbenz, Construction Inspector Approved by: Anthony D. Masters, Chief Reactor Projects Branch 7 Division of Reactor Projects Enclosure

SUMMARY

IR 05000280/2015009, 05000281/2015009; 07/13/2015 - 07/30/2015; Surry Power Station,

Units 1 and 2; Biennial Inspection of Problem Identification and Resolution Program.

The inspection was conducted by one senior project engineer, one senior project inspector, one reactor inspector, and a construction inspector. No findings were identified. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.

Identification and Resolution of Problems The inspectors concluded that, in general, problems were properly identified, evaluated, prioritized, and corrected. The licensee was effective at identifying problems and entering them into the corrective action program (CAP) for resolution, as evidenced by the relatively few number of deficiencies identified by external organizations (including the NRC) that had not been previously identified by the licensee, during the review period. Generally, prioritization and evaluation of issues were adequate, formal root cause evaluations for significant problems were adequate, and corrective actions specified for problems were acceptable. Overall, corrective actions developed and implemented for issues were generally effective and implemented in a timely manner.

The inspectors determined that overall, audits and self-assessments were adequate in identifying deficiencies and areas for improvement in the CAP, and appropriate corrective actions were developed to address the issues identified. Operating experience usage was found to be generally acceptable and integrated into the licensees processes for performing and managing work, and plant operations.

Based on discussions and interviews conducted with plant employees from various departments, the inspectors determined that personnel at the site felt free to raise safety concerns to management and use the CAP to resolve those concerns.

The NRC inspectors did not identify any findings or violations of more than minor significance.

REPORT DETAILS

OTHER ACTIVITIES

4OA2 Problem Identification and Resolution

a. Assessment of the Corrective Action Program

(1) Inspection Scope The inspectors reviewed the licensees corrective action program (CAP) procedures which described the administrative process for initiating and resolving problems primarily through the use of condition reports (CRs). To verify that problems were being properly identified, appropriately characterized, and entered into the CAP, the inspectors reviewed CRs that had been issued between July 2013 and June 2015 including a detailed review of selected CRs associated with the following risk-significant systems:

Safety Injection System, Ventilation System for the Emergency Switchgear Rooms and the Auxiliary Building, and Auxiliary Feedwater System. Where possible, the inspectors independently verified that the corrective actions were implemented as intended. The inspectors also reviewed selected common causes and generic concerns associated with root cause evaluations to determine if they had been appropriately addressed. To help ensure that samples were reviewed across all cornerstones of safety identified in the NRCs Reactor Oversight Process, the inspectors selected a representative number of CRs that were identified and assigned to the major plant departments, including operations, engineering, health physics, chemistry, emergency preparedness, and security. These CRs were reviewed to assess each departments threshold for identifying and documenting plant problems, thoroughness of evaluations, and adequacy of corrective actions. The inspectors reviewed selected CRs, verified corrective actions were implemented, and attended meetings where CRs were screened for significance to determine whether the licensee was identifying, accurately characterizing, and entering problems into the CAP at an appropriate threshold.

The inspectors conducted plant walkdowns of equipment associated with the selected systems and other plant areas to assess the material condition and to look for any deficiencies that had not been previously entered into the CAP. The inspectors reviewed CRs, maintenance history, completed work orders/work requests for the systems, and reviewed associated system health reports. These reviews were performed to verify that problems were being properly identified, appropriately characterized, and entered into the CAP. Items reviewed generally covered a two-year period of time; however, in accordance with the inspection procedure, a five-year review was performed for selected systems for age-dependent issues.

The main control room (MCR) deficiency list was assessed to ascertain if deficiencies were entered into the CAP and tracked to resolution. Operator Workarounds and Operator Burden screenings were reviewed, and the inspectors verified compensatory measures for deficient equipment which were being implemented.

The inspectors conducted a detailed review of selected CRs to assess the adequacy of the root cause and apparent cause evaluations of the problems identified. The inspectors reviewed these evaluations against the descriptions of the problem described in the CRs and the guidance in licensee procedures PI-AA-300-3001, Root Cause Evaluation, and PI-AA-300-3002, Apparent Cause Evaluation. The inspectors assessed if the licensee had adequately determined the cause(s) of identified problems, and had adequately addressed operability, reportability, common cause, generic concerns, extent-of-condition, and extent-of-cause. The review also assessed if the licensee had appropriately identified and prioritized corrective actions to prevent recurrence where applicable.

The inspectors reviewed selected industry operating experience items, including NRC generic communications to verify that they had been appropriately evaluated for applicability and that issues identified through these reviews had been entered into the CAP.

The inspectors reviewed site trend reports to determine if the licensee effectively trended identified issues and initiated appropriate corrective actions when adverse trends were identified.

The inspectors attended various plant meetings to observe management oversight functions of the corrective action process. These included CR Review Team meetings and Corrective Action Review Board meetings.

Documents reviewed are listed in the Attachment.

(2) Assessment Identification of Issues The inspectors determined that the licensee was generally effective in identifying problems and entering them into the CAP and there was a low threshold for entering issues into the CAP. This conclusion was based on the type of problems entered into the CAP; the review of licensee requirements for initiating CRs as described in licensee procedure PI-AA-200, Corrective Action; the management expectation that employees were encouraged to initiate CRs for any issue that is not meeting performance expectations regardless of whether it is a potential, suspect, or actual problem; a review of system health reports; and inspectors observations during plant walkdowns.

Trending was generally effective in monitoring equipment performance. Site management was actively involved in the CAP and focused appropriate attention on significant plant issues.

Based on reviews and walkdowns of accessible portions of the selected systems, the inspectors determined that system deficiencies were being identified and placed in the CAP.

Prioritization and Evaluation of Issues Based on the review of CRs sampled by the inspection team during the onsite period, the inspectors concluded that problems were generally prioritized and evaluated in accordance with the licensees CAP procedure as described in the CR severity level determination guidance in PI-AA-200, Corrective Action. The inspectors determined that overall, each CR was assigned an adequate severity level at the CRT meetings, and adequate consideration was given to system or component operability and associated plant risk.

The inspectors determined that station personnel had conducted root cause and apparent cause analyses in compliance with the licensees CAP procedures and assigned cause determinations were appropriate, considering the significance of the issues being evaluated. A variety of causal-analysis techniques were used depending on the type and complexity of the issue consistent with licensee procedures PI-AA-300, Cause Evaluation; PI-AA-300-3001, Root Cause Evaluation; PI-AA-300-3002, Apparent Cause Evaluation; PI-AA-300-3003, Common Cause Evaluation; and PI-AA-300-3004, Cause Evaluation Methods. The inspectors determined that the licensee had performed evaluations that were technically accurate and of sufficient depth.

Effectiveness of Corrective Actions Based on a review of corrective action documents, interviews with licensee staff, and verification of completed corrective actions, the inspectors determined that overall, corrective actions were timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected. For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence in that a review of performance indicators, CRs, and effectiveness reviews demonstrated that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence were sufficient to ensure corrective actions were properly implemented and were effective.

(3) Findings No findings of significance were identified.

b. Assessment of the Use of Operating Experience (OE)

(1) Inspection Scope The inspectors examined licensee programs for reviewing industry operating experience, reviewed licensee procedure PI-AA-100-1007, Operating Experience Program, and reviewed the licensees operating experience database to assess the effectiveness of how external and internal operating experience data was handled at the plant. In addition, the inspectors selected operating experience documents (e.g., NRC generic communications, 10 CFR Part 21 reports, licensee event reports, vendor notifications, and plant internal operating experience items, etc.), which had been issued since June 2011 to verify whether the licensee had appropriately evaluated each notification for applicability to the Surry plant, and whether issues identified through these reviews were entered into the CAP. Procedure PI-AA-100-1007, "Operating Experience Program,"

was reviewed to verify that the requirements delineated in the program were being implemented at the station. Documents reviewed are listed in the Attachment.

(2) Assessment Based on a review of documentation related to the review of operating experience issues, the inspectors determined that the licensee was generally effective in screening operating experience for applicability to the plant. Industry OE was evaluated by plant OE Coordinators and relevant information was then forwarded to the applicable department for further action or informational purposes. OE issues requiring action were entered into the CAP for tracking and closure. In addition, operating experience was included in all root cause evaluations in accordance with licensee procedure PI-AA-300, Cause Evaluation, PI-AA-300-3001, Root Cause Evaluation, and PI-AA-300-3002, Apparent Cause Evaluation.
(3) Findings No findings were identified.

c.

Assessment of Self-Assessments and Audits

(1) Inspection Scope The inspectors reviewed audit reports and self-assessment reports, including those which focused on problem identification and resolution, to assess the thoroughness and self-criticism of the licensee's audits and self-assessments. The inspectors also verified that problems identified through those activities were appropriately prioritized and entered into the CAP for resolution in accordance with licensee procedures PI-AA-100-1004, Self-Assessments.
(2) Assessment The inspectors determined that the scopes of assessments and audits were adequate.

Self-assessments were generally detailed and critical, as evidenced by findings consistent with the inspectors independent review. The inspectors verified that CRs were created to document all areas for improvement and findings resulting from the self-assessments, and verified that actions had been completed consistent with those recommendations. Generally, the licensee performed evaluations that were technically accurate. Site trend reports were thorough and a low threshold was established for evaluation of potential trends, as evidenced by the CRs reviewed that identified adverse trends.

(3) Findings No findings were identified.

d.

Assessment of Safety-Conscious Work Environment

(1) Inspection Scope The inspectors randomly interviewed several on-site workers regarding their knowledge of the corrective action program at Surry and their willingness to write CRs or raise safety concerns. During technical discussions with members of the plant staff, the inspectors conducted interviews to develop a general perspective of the safety-conscious work environment at the site. The interviews were also conducted to determine if any conditions existed that would cause employees to be reluctant to raise safety concerns. The inspectors reviewed the licensees Employee Concerns Program (ECP) and interviewed the ECP manager. Additionally, the inspectors reviewed a sample of ECP issues to verify that concerns were being properly reviewed and identified deficiencies were being resolved and entered into the CAP when appropriate.
(2) Assessment Based on the interviews conducted and the CRs reviewed, the inspectors determined that licensee management emphasized the need for all employees to identify and report problems using the appropriate methods established within the administrative programs, including the CAP and ECP. These methods were readily accessible to all employees.

Based on discussions conducted with a sample of plant employees from various departments, the inspectors determined that employees felt free to raise issues, and that management encouraged employees to place issues into the CAP for resolution. The inspectors did not identify any reluctance on the part of the licensee staff to report safety concerns.

(3) Findings No findings were identified.

4OA6 Meetings, Including Exit

On July 30, 2015, the inspectors presented the inspection results to Mr. R. Simmons and other members of the site staff. The inspectors confirmed that all proprietary information examined during the inspection had been returned to the licensee.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

K. Dunn, Engineering
B. Garber, Licensing Supervisor
M. Haduck, Manager Outage and Planning
D. Lawrence, Director of Nuclear Safety and Licensing
J. Pollard, Licensing Engineer
T. Sadler, Corrective Action Coordinator
R. Scanlan, Manager Maintenance
R. Simmons, Plant Manager
M. Smith, Manager Nuclear Organizational Effectiveness
D. Wilson, Assistant Operations Manager

NRC

C. Jones, Resident Inspector
P. McKenna, Senior Resident Inspector

LIST OF REPORT ITEMS

Opened and Closed

None

Closed

None

Discussed

None

LIST OF DOCUMENTS REVIEWED