IR 05000010/1985001

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SALP Repts 50-010/85-01,50-237/85-01 & 50-249/85-01 for June 1984 - Sept 1985
ML20136F718
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 01/03/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20136F717 List:
References
50-010-85-01, 50-10-85-1, 50-101-85-1, 50-237-85-01, 50-237-85-1, 50-249-85-01, 50-249-85-1, NUDOCS 8601070477
Download: ML20136F718 (38)


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SALP 5 SALP BOARD REPORT U. S. NUCLEAR REGULATORY COMMISSION

REGION III

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SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE t

SG-10/85001; 50-237/85001; 50-249/85001

Inspection Report

Comonwealth Edison Company

Name of Licensee

Dresden Nuclear Power Station

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Name of Facility

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June 1, 1984 through September 30, 1985

Assessment Period

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I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data on a

periodic basis and to evaluate licensee performance based upon this information.

SALP is supplemental to normal regulatory processes used to ensure compliance

to NRC rules and regulations.

SALP is intended to be sufficiently diagnostic

to provide a rational basis for allocating NRC resources and to provide

meaningful guidance to the licensee's management to promote quality and safety

of plant construction and operation.

A NRC SALP Board, composed of staff members listed below, met on November 19,

1985, to review the collection of performance observations and data to assess

the licensee's performance in accordance with the guidance in NRC Manual

Chapter 0516, " Systematic Assessment of Licensee Performance." A summary of

the guidance and evaluation criteria is provided in Section II of this report.

This report is the SALP Board's assessment of the licensee's safety perforu nce

at the Dresden Nuclear Power Station for the period June 1, 1984 thrcJgh

September 30, 1985.

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SALP Board for Dresden Nuclear Power Station:

Name

Title

J. A. Hind

Director, Division of Radiological

Safety and Safeguards

C. E. Norelius

Director, Division of Reactor Projects

C. J. Paperiello

Director, Division of Reactor Safety

E. G. Greenman

Deputy Director, Division of Reactor

Projects

N. J. Chrissotimos

Chief, Reactor Projects Branch 2

L. A. Reyes

Chief, Operations Branch

G. C. Wright

Chief, Reactor Projects Section 2C

E. R. Schweibinz

Chief, Technical Support Section

D. H. Danielson

Chief, Materials and Processes Section

F. Hawkins

Chief, Quality Assurance Programs Section

R. L. Gregor

Chief, Facilities Radiation Protection

Section

M. C. Schumacher

Chief, Indepentent Measurements and

Environmental Protection Section

J. R. Creed

Chief, Safeguards Section

R. A. Gilbert

Licensing Project Manager, NRR

T. M. Tongue

Senior Resident Inspector, Braidwood

L. McGregor

Senior Resident Inspector, Dresden

R. B. Landsman

ProjectManager,ReactorProjects

Section 2C

P. R. Rescheske

Reactor Inspector

D. Miller

Senior Radiation Specialist

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II.

CRITERIA

The licensee's performance is assessed in selected functional areas

depending on whether the facility is in a construction, preoperational,

or operating phase.

Each functional area normally represents areas

significant to nuclear safety and the environment, and are normal

programmatic areas.

Some functional areas may not be assessed because

of little or no licensee activities or lack of meaningful observations.

Special areas may be added to highlight significant observations.

One or more of the following evaluation criteria were used to assess

each functional area:

1.

Management involvement in assuring quality.

2.

Approach to resolution of technical issues from a safety standpoint.

3.

Responsiveness to NRC initiatives.

4.

Enforcement history.

5.

Reporting and analysis of reportable events.

6.

Staffing (including management).

7.

Training effectiveness and qualification.

However, the SALP Board is not limited to these criteria and others may

have been used where appropriate.

Based upon the 5 ALP Board's assessment, each functional area evaluated is

classified into one of three performance categories.

The definition of

these performance categories is:

Category 1:

Reduced NRC attention may be appropriate.

Licensee management

attention and involvement are aggressive and oriented toward nuclear

safety.

Licensee resources are ample and effectively used so that a high

level of perform 1nce with respect to operational safety or construction

is being achieved.

Category 2:

NRC attention should be maintained at normal levels.

Licensee

management attention and involvement are evident and management is

concerned with nuclear safety.

Licensee resources are adequate and are

reasonably effective such that satisfactory performance with respect to

operational safety or construction is being achieved.

Category 3:

Both NRC and licensee attention should be increased.

Licensee

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management attention and involvement is acceptable and considers nuclear

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safety, but weaknesses are evident.

Licensee resources appear to be

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strained or not effcetively used so that minimally satisfactory performance

with respect to operational safety or construction is being achieved.

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Trend: The SALP Board has also categorized the performance trend in each

functional area rated over the course of the SALP assessment period.

The

categorization describes the general or prevailing tendency (the perfor-

mance gradient) during the SALP period.

The performance trends are defined

as follows:

Improved:

Licenseeperformancehasgenerallyimprovedoverthecourse

of the SALP assessment period.

<

Same:-

Licensee performance has remained essentially constant over

the course of the SALP assessment period.

Declined:

Licensee performance has generally declined over the course

of the SALP assessment period.

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III. SUfMARY OF RESULTS

The overall regulatory performance of your facility has improved during

the current SALP period. We are encouraged by the improved performance

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in the areas of radiological controls, maintenance / modifications,

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security, and licensing activities.

However, performance in the areas

of surveillance and inservice testing declined from a Category 1 to a

Category 2 and the performance trend in the areas of plant operations and

fire protection / housekeeping also declined. Your performance in these

areas will be monitored and discussed in the next SALP Board assessment

for your facility.

Rating Last

Rating This

Functional Area

Period

Period

Trend

'A.

Plant Operations

2

Declining

B.

Radiological Controls

2

Improving

C.

Maintenance /

Modifications

2

Improving

D.

Surveillance and

Inservice Testing

2

Same

E.

Fire Protection /

Housekeeping

2

Declining

F.

Emergency Preparedness

1

Same

G.

Security

2

Improving

H.

Refueling

1

Same

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Quality Programs and

Administrative Controls 2

Same

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Licensing Activities

1

Improving

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IV.

PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

This functional area was routinely inspected by the resident

inspectors throughout the evaluation period. One special

inspection was conducted by the resident inspectors related to

three personnel errors that occurred in a short period of time.

Six violations were identified as follows:

SeverityLevehIV-Inadequatecorrectiveactionsresulting

a.

in a second occurrence where the corner room submarine

doors were.found open and unattended (237/84012-03).

b.

Severity Level V - Failure to investigate and evaluate

multiple alarms and indications in the control room where

secondary containment was in question (237/84016-01;

249/84015-01).

c.

Severity Level V - Failure to report scrams in accordance

with 10 CFR 50.73 (249/84021-01).

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d.

Severity Level IV - High Pressure Coolant Injection (HPCI)

room cooler service water found valved-out resulting in

HPCI being inoperable (249/85009-01).

e.

Severity Level IV - Loss of undervoltage protection on

Emergency diesel bus 34-1 for about four and one-half

minutes (249/85009-03).

f.

Severity Level IV - Suppression pool water sample line

found open allowing water to flow from the suppression

pool in containment to the secondary containment

(249/85009-02).

The violations did not appear to be programmatic or to have

generic implications to the plant.

Although the licensee's

response to all of the violations was generally prompt and

effective with consideration given to longterm corrective

actions, the responses to d, e, and f above were exceptionally

good.

The number of violations issued during this assessment

period was comparable to the number issued during the last

assessment period.

During the SALP 5 period, the licensee experienced 35

unscheduled reactor scrams (21 on Unit 2 and 14 on Unit 3).

Fourteen of the scrams occurred while the reactors were in

a shutdown condition with all rods fully inserted.

Nine

scrams resulted directly from personnel errors, of which

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one was caused by a nonlicensed operator, five by licensed

operators, and the remaining three by maintenance or other

personnel.

Three scrams during SALP 5 were due to defective

procedures, with the balance of the scrams attributed to

component failures.

During the later portion of the assessment

period, recognizing that the number of scrams being experienced

were becoming excessive, the licensee formed a scram reduction

committee chaired by the assistant superintendent for operations.

The committee's function was to perform indepth reviews of every

scram and provide feedback of the analyses to the appropriate

personnel with the intention of preventing similar scrams.

Due

to the short time the committee has been in place, a determina-

tion of its effectiveness could not be made at the time of this

report.

As discussed in Section V.F.1, LER data indicates that the number

of personnel errors during the present assessment period have

substantially increased from the last assessment period.

Of the

93 LERs submitted this period 38 involved personnel errors, of

which 20 were attributable to the operations department.

This

is a significant increase over the SALP 4 data where, although

121 LERs were submitted, only 21 involved personnel errors and

only three of these were directly attributable to the operations

department.

During the assessment period, the licensee exhibited adequate

control over plant work activities as evidenced by well planned

daily assignments of priorities, use of followup and tracking

mechanisms to ensure required work was completed in a timely

manner, and adequately stated policies that insured appropriate

levels of station management review was involved when decisions

towards safety were made.

During daily (morning and afternoon)

planning meetings, operations personnel interfaced closely with

maintenance, health physics, and other station personnel to

set up work projects for the day and night shifts respectively

with emphasis given to determination of priorities.

Staffing was adequate during the period and vacancies were

generally filled quickly with qualified and motivsted personnel.

Overall, operators were attentive to their duties and ack-

nowledged and analyzed alarm conditions promptly and thoroughly.

On many occasions, the inspectors noted a seemingly large number

of annunciators "up" (acknowledged) in the control room.

Upon

questioning of the operators, it was generally found that the

causes for the annunciators were known or that equipment trouble-

shooting was underway to determine the cause.

Distractions,

such as. radios, televisions, or non-job related reading material

are not allowed in the control room.

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During the SALP period, the licensee completed construction of

a new shift supervisor's office / locker room area. The original

plant design had resulted in a.high personnel traffic flow

through the control room for access between the shift super-

visor's office and the plant.

The newly constructed additions

have considerably reduced this problem.

The Regulatory Performance Improvement Plan (RPIP) as described

in the previous SALP 4 report has resulted in supervisors and

union personnel being more aware of the need for attention to

detail. This has been accomplished through the use of weekly

meetings dealing with timely subjects and how they relate to

Dresden and by a greater onsite presence by station and

corporate management during both normal and off-normal work

hours.

The licensee identified and presented to the NRC, in a March 25,

1985 enforcement conference, a recurring problem involving an

overall increase in personnel errors that rince 1984 has

accompanied the restart of each Dresden uni

following its

respective refuel outage.

In recognition c.' this, and to help

correct it, the licensee has assigned additional personnel on

shift for operations, health physics, and quality assurance

during the Unit 3 refueling and recirculation piping replacement

project.

These personnel will aid in the outage work and their

experience and expertise should help to reduce personnel errors,

thus providing a smoother restart following completion of the

outage.

During the assessment period,12 Reactor Operator (RO) and 12

Senior Reactor Operator (SRO) examinations were administered

to Dresden personnel.

Two of the SR0 candidates were re-

applications.

The overall pass rate was 79%, which is very

close to the national average.

Requalification examinations

were not administered by Region III at Dresden during this

period.

2.

Conclusion

The licensee is rated Category 2.

Although the category rating

is the same given in the last SALP, due to the number of

personnel errors and reactor scrams, the trend in this area is

declining.

This is a significant change from the previous SALP

rating which judged the trend to be improving.

3.

Board Recommendations

The Board recommends that increased management attention should

be given to this area to reverse the declining trend.

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B.

Radiological Controls

1.

Analysis

Seven inspections were performed during the assessment period by

regional specialists.

The inspections included outage radiation

protection, radwaste management, operational radiation protec-

tion, and confirmatory measurements.

The resident inspectors

also inspected in this area.

The following violations were

identified:

a.

Severity Level IV - Uncontrolled liquid radioactive waste

release exceeded gross beta technical specification

concentration in Unit 1 discharge canal (10/84011-03).

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b.

Severity Level IV - Failure to adhere to radiation control

procedures for:

(1) location of personal film badges on

body, (2) performing required personal frisking, (3)

reporting out-of-specification radiochemistry results to

the Radiation / Chemistry Supervisor and Shift Engineer, and

(4) service water sampling requirements to confirm high

monitor readings (10/84011-01,02,04,05); 237/84013-01,02;

249/84012-01,02).

c.

Severity Level IV - Inadequate procedure for filling the

floor drain surge tank.

Procedures did not caution that

the level indicator was inaccurate, thereby causing a liquid

spill (237/84013-03; 249/84012-03).

d.

Severity Level IV - Transfer of contaminated gas cylinders

to persons not licensed to receive or possess radioactive

material (10/85002-03; 237/85005-05; 249/85004-05).

e.

Severity Level V - Failure to specify Tc-99, I-129, H-3,

and C-14 on shipment manifests as required by 10 CFR 20.311(b) (237/85021-01; 249/85017-01).

The Severity Level IV violations were indicative of minor

programmatic breakdowns.

Licensee corrective actions were

generally timely and effective but some procedural adherence

problems still exist.

The Severity Level V violation resulted

from an inappropriate instruction from the corporate office.

Corrective action was again timely and effective.

Overall,

licensee enforcement history improved from the previous SALP

rating period.

Both the extent and severity of violations has

diminished from previous SALP evaluations.

Staffing in this functional area remains adequate.

Vacant

positions are usually filled within a reasonable time.

Significant management changes, including replacement of the

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Rad / Chem Supervisor, Lead Health Physicist, and Lead Chemist

occurred during the period.

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Other staffing changes, including several new staff reporting

to the Lead Chemist, have also occurred.

Sufficient staffing

continuity appears to have been maintained.

The changes should

result in a net strengthening of the licensee's program.

Radiation protection support has also increased with appointment

of additional Radiation / Chemistry Foremen and technicians and

the addition of a new ALARA Section.

This new section consists

of a Lead Radiological Engineer, ALARA Coordinator, and ALARA

Decon Foreman and has resulted in improved pre-job planning, job

coverage, and post-job reviews.

However, several health physics

and engineering assistant positions are vacant owing to

promotions and transfers.

The licensee's policy of rotating

Radiation / Chemistry technicians (RCTs) between health physics

and laboratory assignments results in long intervals between

successive laboratory assignments.

This could limit RCT

proficiency in the laboratory.

Management oversight appeared

adequate during this period but the quality of the laboratory

program would be vulnerable to inappropriate management changes.

The licensee's management involvement has been pervasive.

Audits

are generally thorough and comprehensive; responses and correc-

tive actions are generally good and timely.

Health physics,

chemistry, and radwaste expertise is represented on both the

station and corporate QA audit teams.

Audit findings included

radwaste transport vehicle problems, records retrievability

problems, and isolated technical specification surveillance

problems.

In the radiological protection area, improvements

have been made in job-specific surveys, personal contamination

reports, solid radwaste handling, and supervisory overview of

ongoing work in radiologically significant areas.

Personal

monitoring equipment, personal decontamination facilities, and

respirator cleaning facilities and equipment have been improved.

Also, the management decisions to conduct chemical cleaning of

Unit 2 recirculating system piping before performance of

Inservice Inspection and Induction Heating Stress Improvement

work resulted in a significant reduction in total dose to workers

(ALARA).

However, it was noted during inspections that

administrative duties assigned the Radiation / Chemistry Foremen

occasionally hindered their timely response to radiological

technical matters.

The licensee's responsiveness to NRC initiatives in the radiation

protection area has been good during this assessment period as

evidenced by improvements in self-identification and correction

of radiation protection problems, management support for

implementation of radiation protection procedures, contamination

controls, and health physics coverage of radiologically signifi-

cantjobs.

Evidence of these improvements is noted by more

thorough licensee review of Radiological Occurrence Report and

personnel contamination events, stronger disciplinary actions

for offenders of radiation protection procedures, a reduction

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in dose at the station, and a dramatic reduction in the extent

of contaminated areas.

Also improved was ALARA pre-job planning,

job coverage, and post-job reviews.

The licensee's approach to

resolution of these issues has been technically sound and

thorough.

The training and qualification program contributes to an adequate

understanding of work and fair adherence to procedures with a

modest number of personnel errors.

The policy of rotating RCTs

between health physics and laboratory assignments results in a

long interval between successive laboratory assignments and

requires a high degree of oversight and supervision.

However,

retraining has been enhanced by increasing scheduled formal

training sessions and broadening the scope of retraining to

include refresher training.

Insufficient time has elapsed to

assess effectiveness of the enhanced retraining.

The licensee's approach to resolution of technical issues

generally results in sound and timely resolutions with

appropriate emphasis on radiological safety.

Effectiveness

of the ALARA program has continued to improve during this

assessment period.

Increased ALARA awareness by the station

staff, addition of appropriate manpower to support the ALARA

organization, and greater management support have resulted in

more extensive pre-job planning, engineering controls, and

post-job reviews.

Total worker doses during this assessment period, about 890

person-rem per reactor in 1984 and estimated to be approximately

the same for 1985, represent significant decreases (30 to 35

percent) over the licensee's recent five year dose averages and

are about 20 percent below the national average for U.S. boiling

water reactors.

A further reduction for 1985 was not projected

because of Unit 3 recirculating system piping replacement

scheduled to begin during the fourth calendar quarter.

The licensee's radiological effluents continue to be about

average for U.S. boiling water reactors.

One unplanned liquid

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release above technical specification limits and one unplanned

release below technical specification limits occurred during the

assessment period.

There were no transportation incidents.

Laboratory performance continued to be satisfactory during this

period.

Instrument QC programs were satisfactory and analytical

instruments were operable and calibrated.

An ion chromatograph

obtained during the period-is expected to be put into use by

early 1986.

Laboratory procedures appeared satisfactory. The

licensee has implemented a program to check RCT analyses of blind

samples for conductivity, silica, chlorides, and pH prior to

their starting a three-week laboratory assignment.

The station

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also analyzed fluid samples provided by the corporate laboratory.

These programs should be strengthened and expanded to include

radiological samples to better check laboratory and individual

analyst performance.

Laboratory performance in confirmatory measurements continued

.to be very good with 28 agreements in 29 comparisons made during

the period.

Problems noted in the past with the Automated

Analytical Instrumentation Systems (AAIS) appeared to have been

resolved.

An experienced radiochemist with experience at the

plant provides good oversight for gamma spectroscopy.

2.

Conclusion

The licensee is rated Category 2 in this area.

This is an

improvement over the Category 3 achieved in SALP 4.

3.

Board Recommendations

None.

C.

Maintenance / Modifications

1.

Analysis

This functional area was inspected routinely throughout the

assessment period by both resident and regional inspectors.

In addition, six special inspections were conducted by regional

personnel.

The following violations were identified:

a.

Severity Level V - Hold points and work request forms

were not completed in accordance with approved procedures

(237/85008-01; 249/85007-01).

b.

Severity Level V - Failure of the control rod scram

surveillance procedure to provide for the review and

approval of test results (237/85032-03; 249/85028-03).

c.

Severity Level IV - Failure to perform adequate QC

inspection for piping suspension system n.odifications

to assure conformance to design documentation

(237/84027-01; 249/85013-01).

d.

Severity Level IV - Failure of the Architect Engineer

(AE) to conduct an adequate transient operability analysis

for the LPCI system snubber failure (237/84027-04).

e.

Severity Level IV - Failure to have prescribed standards

and procedures for Class IE cable splicing (237/85014-04a).

f.

Severity Level IV - Failure to assure that design basis

requirements are translated into specifications, drawings,

procedures, and instructions (237/85014-05b).

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One of_the special inspections conducted in this area was

performed.to provide for an indepth' review and evaluation of

the maintenance program and its implementation.

This was the

first in a planned series'of inspections of this type and

was prompted by the Category 3 -rating received in this func-

'tional area during the last assessment pericd (SALP 4).

As

part of the review an extensive sampling of work packages was

inspected, of which approximately 25% were found to have work

request forms not completed in accordance with approved

procedures.

This resulted in the issuance of violation a. as

described above.

Other concerns noted included:

A relatively large work request package backlog and the

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inadequate storage of incomplete packages.

The inability of Quality Control to support maintenance

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acti'/itics during periods when the workload is high.

Some craft personnel were not aware that maintenance

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procedures were required to be at the job site.

It should be noted that although violation a. above did not

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involve a significant' safety issue, the fact that such a'large

. proportion (25%) of the work packages were incomplete. reflects

poorly on the licensee's ability to control and evaluate work

activities. The licensee agreed that plant performance in

regard to the items identified required improvement.

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Another inspection in this functional area was conducted to

determine the adequacy of the licensee's program to meet the

requirements of Generic Letter 83-28, Required Actions Based

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on Generic Implications of Salem ATWS Events".

The inspection

addressed' equipment classification, vendor. interface, post-

maintenance testing,'and reactor trip system reliability.

Violation b. was issued as a result of this inspection; however,

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in' general the licensee's program adequately met the requirements

of Generic Letter 83-28 as ascertained from the areas inspected.

Inspections were conducted to examine the inservice inspection

program including review of activities related to:

(1) the

licensee's actions to satisfy requirements of NRC Generic Letter 84-11; (2) the licensee's actions related to-the Unit 2

Main Steamline-(MS) and Low Pressure Coolant Injection (LPCI)

piping snubber failures, including an independent review to

determine the cause of failure, and followup of Confirmatory

Action Letter 85-04; (3) the replacement of the Unit 2 Reactor

Water Cleanup System piping, including a review of procedures,

welder qualifications, radiographs, and other related documenta-

tion, and observations of piping spool fabrication and inprocess

welding; and (4) the licensee's actions to evaluate the effects

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of upgrading safety-related piping system supports that meet

IE Bulletin 79-14 location verification requirements.

As a

result of these inspections, violations c. and d. were

identified.

The violations were not repetitive of any identified

during the previous assessment period, and do not appear to have

generic or programmatic implications.

A significant causal

factor in the inspection discrepancies was the failure of

personnel to adhere to field change procedures.

Two inspections were conducted during the assessment period to

evaluate the Unit 2 125V DC system modification performed to

replace the degraded Unit 2 battery with the Unit 1 High

Pressure Coolant Injection Battery.

Two violations (e) and (f)

were identified to have occurred during the modification.

In summary, the licensee has shown overall improvement in this

functional area since the last assessment (SALP 4) as evidenced

by a significant reduction in the number of LERs issued as a

result of personnel errors by maintenance / modification work

groups (14 in SALP 4 as compared to 4 this period) and in a

reduction of NRC violations issued (11 violations in SALP 4 as

compared to 6 violations this SALP period).

However, further

improvements are required in the area of program implementation.

The licensee has dedicated additional resources to this area in

the form of management attention, training, and better communica-

tions with workers and first-line supervisors to create a

greater awareness of maintenance activities.

The licensee has continued to develop new procedures as necessary

and to use an extensive system of maintenance manuals (as

outlined in previous SALP reports) to aid maintenance activities

onsite.

Response to NRC initiatives is generally timely with

few longstanding issues attributable to the licensee.

Resolution

of technical issues from a safety perspective has been generally

conservative, sound, and thorough.

Maintenance records were generally complete, well maintained,

and available.

Maintenance personnel were adequately trained

and direct observations of work activities indicate the work

force has an adequate understanding of work practices and

procedures.

The inadequacy in the Architect Engineer's operability analysis

performed for the LPCI system snubber failure and the failure of

quality control to adequately inspect modifications to assure

conformance to the design documentation indcate that, although

there is an overall improvement in license- (

%rmance in this

functional area, a decline in performance.s %

rent in this

one narrow area.

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2.

Conclusion

The licensee is rated Category 2 in this area.

This is an

improvement over the Category 3 received in SALP 4.

3.

Board Recommendations

None.

D.

Surveillance and Inservice Testing

1.

Analysis

During the assessment period, the resident and regional inspectors

routinely inspected this area, concentrating on implementation

of procedures.

The inspectors also verified that procedures

were adequate, that test instrumentation was calibrated, that

limiting conditions for operation were met, that removal and

restoration of the affected components was accomplished, that

test results conformed with Technical Specifications and

procedure requirements and were reviewed by personnel other than

the individual directing the test, and that any deficiencies

identified during the testing were properly reviewed and resolved

by appropriate management personnel.

During these inspections

the following six violations were identified:

a.

Severity Level V - Inadequate procedures resulting in no

'

precaution to operators on SBGTS flow and passive supports

for batteries being left off after maintenance (237/84018-

02A,'2B; 249/84017-02A, 28).

b.

Severity Level V - A number of examples of failure to adhere

to surveillance procedures (237/85016-01).

c.

Severity Level V - A number of examples of failure to

implement Quality Assurance procedures (237/85016-02).

d.

Severity Level IV - Failure to trend and evaluate valve

inservice testing data for Unit 3 during 1984 (249/

85005-07).

e.

Severity Level V - Failure to use calibrated measuring and

test equipment during surveillance testing (237/85006-06;

249/85005-06).

f.

Severity Level V - Failure to verify remote position

indicators for accessible valves and to measure pump

i

suction pressure with an idle pump as required by

Section XI of the ASME Code (237/85006-01; 249/85005-01).

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2This'is aLsignificant increase from.the previous assessment

-period when there were no violations and may be indicative of a

relaxed attitude and inattention to detail.' Furthermore, there

were several examples for two of the violations indicating that

there were more than six events.

Additionally, the events are

not limited to any specific functional area.but rather involve

diverse areas such as operational-surveillance, core performance

testing and inservice testing.

This may be indicative of a

-

.

programmatic weakness in surveillance testing.

'

.During inspection of core performance testing and startup

related activities it became evident that improvements are.

needed in the quality of surveillance records and implementation

of surveillance procedures (violations b. and c.).

While

evidence of management involvement exists, violations b. and c.

and.the necessary supplemental responses indicate increased

attention is required to not'only assure proper implementation

of procedures but to ensure timely and thorough evaluation and

response to identified concerns.

~The inspections relating to the inservice inspection (ISI) of

piping systems and the. functional testing of snubbers included a

review of the ISI program, procedures and drawings, equipment

and material certifications, personnel qualifications, records

and associated documentation for completed work, and selected

records'of nondestructive examinations performed during the

October 1984 to April 1985 refueling outage for Unit 2.

The

completeness, availability, and quality of the documentation

indicated the appropriate levels of management overview were-

being applied.

Except for violations (d), (e) and (f), the licensee had fully

implemented the inservice testing program f~ ?" ps and valves

and was conducting Letting in accordance with appropriate

schedules and approved test procedures.

Pump testing was

generally well defined and determination of operability was

made in a timely manner.

In addition to violation d., the

licensee was unable to verify or retrieve the valve test results

during the inspection.-

The licensee continues to show managerial involvement and the

approach to technical and NRC issues is appropriate and timely.

The licensee's responsiveness to inspection related concerns was

deemed very good.

The ifcensee submitted the required reports

and associated analyses within the time constraints imposed.'

The. licensee's training, staffing, and qualifications were

adequate.

Management control systems were effective in that

activities received prior planning and priorities had been

assigned.

Activities were controlled through the use of well

s

stated and defined procedures.

As stated previously, although

.

.:__a_________

_ _. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _. _ _. _ _. _ _ _ _ _ _ _. _ _ __ _ _ _ _. _ _ _ _ _ _. _ - _ _ _ - -.. _ _ _ _ _ _. _ _ _ _ _ _ _ _ _ _. _.. _ _ _ _ _ _ _. _ _ _ _ _ _ _ _ _ _ _ _. _ _. _ _ _. - _. _ _ _. _ _ _.. _ _ _ _ _ _ _ _ _ -..... - - _ _ _ _ _ _. _ _ _ _ _ _. _ _. _ _ _ - - _ _ _. _. _ _ _

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.

.

the licensee was unable to retrieve valve test results during an

inspection, overal records were found to be generally well

maintained and available.

The records also indicated that

equipment and material certifications were current and complete

and that personnel were trained and certified.

2.

Conclusion

The licensee is rated Category 2 in this area.

This is a

reduction from the rating received in the last SALP period.

This is primarily due to the increase in violations and the

apparent programmatic weaknesses indicated.

3.

Board Recommendations

None.

E.

Fire Protection / Housekeeping

1.

Analysis

Throughout the assessment period, the resident inspectors

observed the implementation of the licensee's fire protection

program.

One inspection involving a region based inspector was

also conducted to review the circumstances leading to Licensee

Event Report (LER) No. 85-029-0 and the corrective actions

related to the event.

Two violations were issued as follows:

a.

Severity Level IV - Failure to establish a continuous

fire watch in a timely manner (237/85028-01; 249/85023-01).

b.

Severity Level IV - Failure to test the automatic actuation

of the Master Cardox system valve (237/84011-02);

249/84010-02).

The first violation was identified as a result of a special

surveillance test in which three of five fire dampers failed in

the open position.

A major factor contributing to this event

was a lack of understanding of the Technical Specification

requirements for inoperable fire dampers on the part of the

Station Fire Marshall.

This resulted in a delay in notifying

the Operations Department of the failed dampers.

This is viewed

as a training deficiency. The Operations Department promptly

established the required fire watches upon notification of the

inoperable dampers.

Thus, the technical issues were properly

addressed once identified.

The LER itself was submitted in a

timely manner and contained the required information.

The

licensee was very cooperative in resolving the issues identified

in the LER.

No other violations or open items were identified.

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Housekeeping and plant appearance have improved throughout the

SALP period.

The licensee has established a special crew for

this purpose, supervised by an ex-shift foreman who holds an

SR0 license.

Along with general cleaning, the crew has the

responsibility of reducing the contaminated areas in the plant,

painting and generally improving appearances.

This has resulted

in. improved appearance in numerous areas in the plant and in a

number of areas that were made accessible without protective

clothing.

In spite of the foregoing, housekeeping at Dresden

remains a problem with craft personnel not picking up after

completion of a job and areas becoming recontaminated during

maintenance work.

In addition, it is common to see numerous

cigarette butts and loose trash in non-safety /non-health physics

controlled areas reflecting poor attitudes on the part of the

work force.

Station management has acknowledged this situation.

'Although housekeeping is an important factor in fire prevention,

the board also recognizes the necessity of maintaining the plant

as clean as reasonably possible to prevent dirt, dust, etc. from

intruding into safety-related systems and components since their

presence can ultimately challenge the reliability of system

operability.

The licensee should take steps to correct the

attitudes that have resulted in the poor housekeeping habits,

especially at the worker and f;irst line supervisor levels.

.c \\

With regard to final implemer.tation of the fire protection

requirements of 10 CFR 50 Appendix R, as they apply to Dresden,

,

there are a numtier of outstanding issues.

Thesd issues are the

. subject of ongoing discussion between the licensee and the NRC.

2.'

Co'nclusion

'

The licensee is rated Category 2 in this area.

The trend was

improving early in.the SALP perio'd and has shifted to declining

-later in the period.-

3.

Board Recommendations

s

The board noted that shortly after the close of the} SALP 5

'

period, a fire protection inspection was conducted which indi-

cated potentially significant weaknesses in the implementation

of existing. fire protection requirements.

These weaknesses,

some of which were. identified by the licensee, are currently

D

under review by the licensee in an effort to improve the program.

This effort will be closely monitored by. Region III.

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Emergency Preparedness-

1.

< Analysis

'

Three inspections were conducted during the. period to evaluate

the.following aspects of the. licensee's emergency preparedness

program:

(1) emergency detection and classification,

(2) protective. action decision' making,-(3) emergency notifications,

(4) emergency communications' systems, (5) shift augmentation

provisions, (6) emergency preparedness training, (7) independent

audits of emergency preparedness, and (8) implementation of

_

changes to the emergency-preparedness program.

Two of these

. inspections were observations-of annual emergency exercises.

No

violations or deviations from commitments were identified during

the period.

~Manag' ment involvement in the emergency preparedness program has

e

been adequate with evidence of assignment of prioritics and

explicit procedures for control of activities.

Independent

,

s

audits of:the emergency preparedness program were thorough,

being adequate.in scope, depth, and frequency. Audit records

were complete, well-maintained, and readily available.

During

the period'the. licensee has improved its capability to monitor

corrective actions by utilizing effective tracking systems.

Administrative procedures were adhered to regarding the prepara-

' tion, review, and distribution of the emergency plan and its

~

implementing-procedures.

Plan'and procedure revisions were

consistent and did not decrease their effectiveness.

Training

recordkeeping improved during the period; however, updating of

records, with training performed,_in a timely manner remains as

a problem area.

Management involvement and control in assuring quality of the

emergency preparedness program is further evidenced by the

licensee's corrective action system, which promptly recognized

and addressed several nonreportable concerns..For example, a

Quality Assurance. Surveillance of.a Health Physics Drill iden-

tified the need for a timing device and a lack of heating where

low temperatures could cause adverse affects.

These items were

-brought to management attention and both were resolved in~a

timely manner.

The licensee's responsiveness to NRC initiatives has been

l

timely, with technically sound and thorough responses in almost

all. cases. Whenever the-licensee was required to formally-

,

respond-to-exercise weaknesses, they responded weil before the

due dates.

All proposed corrective actions were acceptable,

.

including the~ proposed completion schedules.

Effective

corrective _ actions on the majority of the previously identified

.open items were completed during the period.

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Records of eight activations of the emergency plan were evaluated

during the SALP period.

All emergency conditions were properly

classified.

Initial notifications to the NRC and State of

Illinois were completed in a timely manner following each

emergency declaration.

The licensee has maintained a prioritized roster of sufficient

numbers of qualified personnel to fill well-defined key positions

in the emergency organization.

Augmentation capabilities have

been adequately demonstrated by periodic drills.

The licensee

has involved both primary and alternate persons assigned to key

positions in emergency drills and exercises.

The licensee's training and qualification program contributes

to an adequate understanding of emergency responsibilities with

only a modest number of personnel errors, as evidenced by

exercise and walkthrough performances.

However, some areas

were identified which indicated a decrease in training emphasis.

In the Operational Support Center, the lack of adequate briefings

of teams has been identified in the last two exercise inspections.

Additionally, some radiological control personnel exhibited

insufficient knowledge of various tasks and associated procedures

during both exercises.

2.

Conclusion-

The licensee is rated Category 1 in this area, with the trend

being essentially the same throughout the period.

3.

Board Recommendations

None.

G.

Security

1.

Analysis

Two routine security inspections were conducted by region based

physical security inspectors during the assessment period.

In

addition, the resident inspectors routinely conducted observations

of security activities.

Two violations were identified relative

to the security program as follows:

a.

Severity Level IV - The licensee failed to adequately

implement a section of the background screening program

for contractor employees (10/85003-04; 237/85007-04;

249/85006-04).

b.

Severity Level V - The licensee failed to implement an

adequate compensatory measure (10/85003-02; 237/85007-02;

249/85006-02).

m

.

.

In addition to the two violations, a concern was identified

regarding an ineffective maintenance program for some security

related equipment.

Further, an anonymously written allegation was received by

Region III that dealt with an individual working onsite while

under the influence of alcohol and that he had been terminated

from other nuclear sites for alcohol and drug abuse.

The

inspectors determined that the licensee took adequate and

immediate followup action after receiving the information.

The allegation was not substantiated and no enforcement action

was required.

Regarding the compensatory measure violation, the implementation

of the compensatory measures for the failure of a perimeter

intrusion alarm zone was not effective, in that the CCTV being

used to monitor the affected zones was out of focus.

Therefore,

the guard posted to observe and monitor could not adequately

assess activities in the alarm zone.

The significance of this

violation was increased due to the fact that:

(1) a work

-request had apparently been written but not acted on for a long

time;'(2) guards apparently had become complacent and used a

less effective system; and (3) the importance of complete

implementation of compensatory measures should have-been recognized

as critical, based on the Severity Level III violation cited in

the last SALP period.

The violations identified were early in the assessment period,

were minor, and were corrected in a timely manner.

The item of concern identified the lack of timely action by

the electrical maintenance department to repair security-related

equipmyt.

Individually, none of the outstanding maintenance

items represented a significant failure of the security program;

however, the volume of items appeared to indicate a lack of

management action in assuring those items were corrected in a

timely manner.

Additionally, the licensee's preventative

maintenance program for the CCTV and protected area intrusion

alarm system was discontinued approximately two years ago due

to manpower shortages.

Based en this finding, the licensee was requested to respond to

the concern describing their short and long range program for

reducing the backlog of outstanding electrical maintenance

requests.

Additionally, the licensee was requested to

immediately re-establish a preventive maintenance program for

security-related electrical items and to keep the Region

informed of progress in the area. The licensee responded to

this concern in a timely manner and the corrective actions taken

appaar to be adequate.

.

.

There were no technical. issues involving physical security, from

a safety aspect, which required resolution during this assessment

period.

The licensee has provided a technically sound and thorough

response to NRC initiatives such as the development of a security

drill program to address all of the contingency events identified

in the Safeguards Contingency plan.

. Events reported under 10 CFR 73.71 were accurately identified

and reported in a timely manner.

The number of reportable

events-decreased significantly in this assessment period which

was attributed to improvements made to the security computer.

Positions within the security organization are identified and

responsibilities are defined.

The staffing levels for the

uniformed security force appeared adequate.

There is good

communication between the licensee and the contract guard force.

The training effectiveness and qualification of the guard force

is adequate.

This was demonstrated during the alert that occurred

during the assessment period, when the guards performed their

duties adequately and in a professional manner.

Corporate security involvement has increased during this

assessment period and has provided excellent support to site

security operations.

The licensee promoted from within to fill

vacancies at the corporate (Senior Nuclear Security Adminis-

trator) and site (Station Security Administrator) levels.

Both

individuals are knowledgeable of past and current security

practices at Dresden.

Due to his vast experience, the promotion

of the Station Security Administrator to a corporate security

level position should further enhance corporate involvement with

the site.

Good communication exists among corporate, site security,

and Region III NRC.

Except for the maintenance concern, senior management support

of security operations was made evident by the upgrading of

the security computer, the purchasing of new explosive detectors,

closed circuit television cameras, and the construction of new

nuclear security training facilities which include both

administrative offices and classrooms.

In summary, the contract security performance and corporate

security involvement in site activities has been strong and

consistent except in the electrical maintenance backlog of

. security equipment.

__

.

.

Conclusion

The licensee is rated Category 2 in this area, which is the

same SALP rating given in the previous assessment period.

A positive trend has been identified during this assessment

period in that the licensee continues to increase its efforts in

upgrading security.

3.

Board Recommendations

None.

H.

Refueling

1.

Analysis

Refueling activities we're inspected by the resident inspectors

during the refueling outage on Unit 2, and the return to power

on Unit 3.

The licensee continues to maintain their high

level of performance.

Personnel involved are well trained

and staffing is ample.

The licensee completed the remaining

shipments of Unit 1 spent fuel from West Valley, New York to

Dresden without incident.

One inspection of core physics and refueling was performed by

a Region III specialist.

No violations were identified.

The

inspection activities included a review of training records,

fuel handling equipment check out procedures, fuel handling and

surveillance test procedures, results of fuel reuse inspections

and fuel sipping operations, and several shifts of core alterations

for Unit 2.

The licensee continues to use a permanently assigned refueling

group that demonstrated the qualities of a well managed and

proficient fuel handling team.

There was evidence of prior

management attention and planning as the fuel movements were

handled safely and efficiently.

There was good coordination and

communication among the various licensee work groups that support

fuel handling.

Problems encountered were handled effectively

with minimal loss of time.

Personnel were knowledgeable of

their duties and staffing was adequate to support all fuel

handling evolutions.

2.

Conclusion

The licensee continues to be rated Category 1 in this area.

3.

Board Recommendations

None.

.

.

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~ Quality Programs and Admir.istrative Controls

H.

1.

Analysis

Routine observations by resident inspectors were made in this

area.. This functional area was also examined.by four region

based inspectors during two inspections within the assessment

period. These inspections were performed to determine the

adequacy of procurement, calibration, tests and experiments,

Lquality program control, records, and offsite review committee

and support staff activities.

The following violations were

identified:

a.

Severity Level IV'- Failure to evalu-te a possible

discrepancy for disposition in a timely manner

(237/84026-01; 249/84023-01).

b.

Severity Level IV - Three examples of failure to follow

'

procedures (237/84015-07; 249/84014-07).

c.

Severity Level V - Failure to perforr a seismic evaluation

on a substitute motor for the HPCI aue.iliary oil pump

(237/84015-08; 249/85014-08).

'd.

Severity. Level V - Failure to provide training on QA

program changes within the time frame specified by the

QA program (237/85029-02; 249/85024-02).

The-procurement inspection was a special inspection of the Ceco

procurement program and its implementation at all operating

sites.

During this inspection violations b. and c. specific

to Dresden were disclosed.

--With. regard to violation-b., the examples involved purchase

orders failing to impose'a. review for suitability of application

on-the vendor as required by the Ceco procurement program.

- While the individual examples had minor safety significance, the

multiple examples of the failure to impose programmatic

requirements indicated the need for added management attention

in this' area. 'With regard to violation c.,

the motor is

currently in a hold status pending a licensee decision on its

disposition. The licensee has implemented procedure changes

for both items,.which should preclude recurrence.

_InadditiontotheDresdenspecific.itemsaddressedabove,six

other items.were disclosed relating to the Ceco corporate

_

procurement program which apply to Dresden as well as the other

operating sites..These items were of~ concern, in that they

represented programmatic' weaknesses that provided a potential

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for the procurement, installation, and use of unqualified items.

-

The licensee's proposed action re' eating to these unresolved

items' appears to mitigate some of the weaknesses; however,

further NRC review is required before these items can be

  • ~

dispositioned.

With regard to violation d.on training, the licensee had a

commitment to train all appropriate personnel on changes to the

nuclear Quality Assurance Manual within 60 days of the date of

i

revisions so that the changes would be effectively implemented.

<

'

On one recent revision, there were over 20 job classifications

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-of site personnel who were not given the required training

'

within the specified' time period.

This failure was of concern

.

because.of the number of personnel who did not receive the

training in a timely manner.

Some of the changes were

administrative in nature without direct safety applications, so

the overall_ impact'of this' violation was_of limited safety

'

significance.

The. licensee's performance in the functional areas of

'

Calibration, Records, Offsite Review and Support Staff was -

a

found to be satisfactory.

No_ items of concern were identified

requiring further action by the licensee or the NRC in these

{

three areas.

In-' summary, the procurement area was controlled by a sometimes

.

.poorly stated program containing some weaknesses. Weaknesses

in program implementation indicated.the lack of management

-

. attention in this area and the need for more effective staff-

~

training.

The failure to provide training in QA program

~

changes also supported the need for more management attention.

The licensee has initiated corrective action to address these

,

issues.

The other area of inspection disclosed one minor item of concern

-in the functional area of Tests and Experiments.

The licensee.

will be conducting a special sampling review of completed

>

'

modification and maintenance work packages to verify that the

required technical evaluation had been completed on replacement

parts used in safety-related components.

'

2.

Conclusion

,

'

The licensee is-rated a Category 2 in this area.

,

3.

Board Recommendations

'

None.

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J.

Licensing Activities

~1.

Analysis

a.

Methodology

The basis for this appraisal was the licensee's performance

in support of licensing actions that were either completed

or had a significant level of activity during the current

rating period..These actions, consisted of amendment

requests, exemption requests, responses to generic letters,

TMI items, and other actions, including the following

specific items:

(1)_ Multiplant Action Items (MPAs) completed or having a

significant level of review action completed include:

NUREG-0737 Item (six items closed for D2 and D3,

one item (I.A.2.1) near closure for both units)

NUREG-0737 Technical Specifications - GL 83-36.

Completed except for Post Accident Sampling and

Control Room Habitability for the station

NUREG-0737 Supplement 1 Items:

SPDS in progress review, station

DCRDR in progress review, Final

Summary Report submitted

Procedures Generation Package (PGP)

for E0Ps.

RAI sent

Response to GL 81-04, NUREG-0313, completed

Control of Heavy Loads, Phase II, completed

Mark I Long Term Program, completed

GL 84-13 TS (Snubbers), completed

Environmental Qualification Schedular Extension,

completed

Radiological Effluents T.S. (RETS), completed

IST (2nd ten years) Relief Requests approved

GL 83-28, Salem ATWS Items 1.1, 3.1.1, 3.1.2,

3.1.3, 3.2.1, 3.2.2, 3.2.3, and 4.5.1 completed

IE Bulletin No. 84-01, Cracks in Mark I Contain-

ment Vent Headers completed

.

.

.

Response to GL 84-09, RAI sent

  • -

B-24, Containment Isolation Depenjability by

Demonstration of Purge and Vent Vilve Operability,

near closure

Response to GL 84-11, completed

Appendix R Schedular Exemptions - RAI sent,

near closure

(2) Plant Specific Action Items completed or having a

significant level of review include:

Reformatting of entire Technical Specification

.

for D2 and 03, completed

Emergency Preparedness Exercise Exemption, issued

Transfer of Dresden 1 Spent Fuel from West Valley

to Dresden Station, completed

-Decontamination of Dresden 1, completed except

for disposal

s

T.S. change relating to extension of MAPLHGR Curves,

D3,_ completed

T.S. for Cycle 10 Restart, D2, completed

Installation of Liquid H2 Storaga Tank at Dresden,

near completion

T.S. relating to Administrative Controls, D2 and

D3, completed

T.S. relating to SEP Topics VI-7.C.1 and XV-iS,

,

D2 and D3, completed

T.S. relating to Revision of T.S. Table 3.7.1, D2

and D3, completed

T.S. relating to Economic Generation Control, D2

and D3, completed

SEP Item - Thermal Overload Protection of M0Vs,

02, completed

T.S. - Deletion of Recirculation Equalizer Valves,

03, completed

Appendix J Exemptions, 03, completed

,

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b.

-Management Involvement and Control in Assuring' Quality.

Commonwealth Edison management has an awareness of the

various licensing issues by virtue of-its extensive

experience in the. industry, technical expertise, and active

participation in Owners Group and professional organization

activities.

Commonwealth management takes actions in a

,

timely manner to ensure safety issues are properly addressed.

These actions include. frequent. visits to NRC Headquarters

by the Director of Nuclear Licensing to discuss progress in

-

general on resolution of outstanding _ issues.

Specific

examples of this attribute in the report period are: (1)

the involvement of management all through the period

relative'to the req'uirements of Generic Letter 84-11 which

relates to the inspections of BWR stainless steel piping.

Because of management _ involvement with this issue,

Commonwealth's response to GL 84-11 was such that the staff

considered them acceptable relative to current IGSCC

concerns; (2) the response to NRC's need for effective

action and/or information regarding the loss of offsite

power event at Dresden 2 on August 16, 1985; and (3) the

care that Commonwealth took in evaluating the September 19,

1985 event where leaking scram solenoid valves caused

reactor: coolant to leak into the Reactor Building via the

vent and drain valves.

c.

Approach to Resolution of Technical Issues from a Safety

Standpoint

Commonwealth's responses to most technical issues are su:h

that few reviewer Request' for Additional Information (RAIs)

.

are needed. When RAIs are issued, Commonwealth's responses

are timely and technically accurate. The need for conference

calls to resolve issues are rare and, when~ conference calls

are made, Commonwealth has the proper technical expertise

available to respond to remaining staff concerns.

They

have a well qualified engineering staff and even a recent

licensing contact change did not interrupt the flow of

information to continue adequate review of outstanding

issues..This is an indication of the depth of quality of

Commonwealth's staff.

They also make appropriate use of

contractors when needed.

The resolution of the large number of multiplant issues

demonstrates that Commonw2alth's staff understands complex

technical issues in terms of' plant safety, plant operation,

and responsiveness to regulatory concerns.

.

.

During the report psiod several issues were identified for

which prompt and effective action was appropriate.

In each

case, the licensee promptly evaluated the problem and took

action to provide interim repairs or other appropriate

actions to satisfactorily resolve the issue from a

safety standpoint.

In each case Commonwealth Edison

furnished the staff promptly with the information required

to evaluate the possible safety concerns.

In addition, as

required for staff licensing actions, the necessary docu-

mentation was made available so that licensing deadlines

could be met without straining staff resources.

d.

Responsiveness to NRC Initiatives

Communication between NRC and Commonwealth generally occurs

between the respective licensing staffs.

However, on the

occasions where the need for information directly from

Dresden occurs, appropriate and technically competent

personnel have responded to staff concerns.

All technical

specification requests are initiated by the station and

the cooperation in satisfying staff documentation needs

during TS processing has been excellent.

This cooperation,

in fact, was extremely important during the reformatting of

the entire D2 and D3 Technical Specifications during the

evaluation period.

While Commonwealth responds to most staff concerns promptly

and is very cooperative when urgent safety issues appear,

they are much slower to respond to concerns that do not

effect them in an immediate way.

This causes reviews of

such concerns to remain outstanding longer than the staff

believes necessary.

Three specific items of this type

are:

(1) the closure of SEP items which will lead to the

Provisional Operating License-Full Term Operating Licensee

conversion for Dresden 2; (2) the licensing issues relating

to the use of the Mobile Volume Reduction System; and (3)

the approval of the use of the Liquid Hydrogen Storage Tank.

Resolution of these issues should be expedited during the

next rating period.

e.

Housekeeping

The NRR Project Manager has visited the site on numerous

occasions.

However, during the evaluation period the

visits involved issues which did not require an extensive

site tour. Visits to the Control Room were made in March

and June 1985. The Control Room appeared to be well

maintained and operated in a professional manner.

There

was no evidence of food and drink containers and all

reading material appeared related to operational needs.

In

earlier discussions with the Dresden Senior Resident

.

,

.

- _.

-. _ -

...

__

.

.

Inspector, a concern was expressed by him of housekeeping

problems at Dresden. However, more recent contacts

indicated that these concerns were being reduced.

f.

Fire Protection

Nearly all ~ plant modifications resulting from the NRC

staff fire protection review have been completed, and

exemptions were issued where appropriate.-

In late 1983, NRC issued a clarification of the

requirements of Appendix R.

In response to the NRC

clarification, the licensee then initiated an independent

review of their fire protection program, and additional

exemptions were requested beyond those resulting from the

original NRC fire protection review.

These are currently

under NRC staff review.

2.

Conclusion

The licensee is rated Category 1 in this area.

This is an

improvement from last years Category 2 and is due to improve-

ments in timeliness and resolution of licensing activities.

3.

Board Recommendations

None.

V.

SUPPORTING DATA AND SUMMARIES

A.

Licensee Activities

Unit 1 was officially declared " Retired in Place" on August 31, 1984.

Presently, the licensee is deliberating the disposition of the unit.

Chemical cleaning commenced on September 12, 1984.

"

Units 2 and 3 engaged in routine power operation throughout most

of SALP 5.

A major scheduled Unit 2 outage for plant refueling,

modification, and maintenance began on October 5, 1984 and was

completed on April 13, 1985.

A major unscheduled outage for

turbine repair was in progress at the beginning of the assessment

period for Unit 3 and was completed on July 21, 1984.

The remaining outages throughout the period are summarized below:

_U__ nit 2

June 21 to July 1, 1984

Repair 2A feed regulator valve

June 9 to June 13, 1985

Repair 2B MG set

June 18 to June 20, 1985

Repair EHC

-

.-

-. _ _ -.

_=

.

_- _

_-.

.

_

August 2 to August 6, 1985

Repair turbine oil reservoir

tank

August 16 to August 22, 1985

Repair auxiliary transformer

August 22 to August 25, 1985

Repair 2B feed pump

September 29 to October 10,

1985

Inspect snubbers

Unit 3

August 21 to August 22, 1984

Repair 3A feedwater valve

September 11, 1984

Repair EHC oil leak

September 25 to October 1, 1984

Repair main condenser leak

October 1 to October 4, 1984

Repair feedwater regulator

valve

October 4 to October 5, 1984

Repair EHC oil leak

October 20 to October 23, 1984

Feedwater regulator valve

problems

October 26 to November 2, 1984

Routine maintenance

January 12 to January 14, 1985

Oil trip solenoid valve on

turbine

April 26 to May 3, 1985

Repair feedwater heaters and

take measurements of recircula-

tion piping

Unit 2 scrammed twenty-one times (ten occurred while shutdown) and

Unit 3 fourteen times (four occurred while shutdown).

Fourteen of

the Unit 2 scrams and none of the Unit 3 scrams were attributed to

equipment malfunctions and required minor maintenance prior to

returning the units to service.

Two scrams occurred at power for

Unit 2 which were attributable to personnel error.

Three scrams

occurred at power for Unit 3 which were attributable to personnel

error. While both units were shut down, four scrams were attributed

to personnel error.

Three scrams during SALP 5 were due to defective

procedures.

The licensee formed a scram reduction committee late in this SALP

period because the number of scrams have approximately doubled each

of the last two SALP periods. The purpose of this committee is to

review each scram and provide feedback to all appropriate site

personnel to prevent similar scrams from occurring in the future.

-

-

-

- -

-

.

.

B.

Inspection Activities

A special NRC HQ's trial outage team inspection was begun on

September 5-6, 1985, to assess the stations' performance during

the Unit 3 recirculation pipe replacement. This is the second

of two NRC inspections to be performed on plants that will have

extended outages.

The inspection is being conducted in accordance

with a proposed NRC procedure to analyze details of new designs /

modifications for older sites.

Violation data for Dresden is presented in Table 1, which includes

Inspection Reports 84009 through 85014 for Unit 1, 84010 through

85032 for Unit 2, and 84009 through 85028 for Unit 3.

TABLE 1

INSPECTION ACTIVITY AND ENFORCEMENT

No. of Violations in Each Severity Level

Functional

Unit 1

Unit 2

Unit 3

Site

Areas

III

IV V

III

IV V

III

IV V

III

IV V

A.

Plant

Operations

1 1

3 2

4 2

B.

Radiological

Controls

3 1

3 1

4 1

C.

Maintenance /

Modifications

4 2

1 2

4 2

D.

Surveillance

and Inservice

Testing

1 3

1 5

E.

Fire Protection

2

F.

Emergency

Preparedness

G.

Security

1 1

1 1

1 1

1 1

H.

Refueling

I.

Quality Programs

and Administrative

Controls

2 2

2 2

2 2

J.

Licensing

Activities

TOTALS

4 1

13 12

13 11

18 13

.

.

C.

Investigations and Allegations Review

During a safeguards inspection, reviews were made as followups to

three anonymous allegations received on December 4, 1985 by the

Senior Resident Inspector.

The allegations concerned:

(1) DNI-

Radman suspected of alcohol use, (2) Commonwealth Edison Company

was told of the problem and did nothing,'and (3) Commonwealth

Edison Company needs a quality screening program.

The inspectors

determined that the licensee took adequate and immediate action

after receiving the information.

No violations of regulatory

requirements were identified and the allegation was not

substantiated.

On January 7,1985, a NRC contractor employee contacted the NRC

with concerns about an incident that occurred four years ago when

control rod drive pressure was too high, went offscale, and a rod

moved more than 1 notch.

A review of the incident determined that

the licensee reported.this in an LER which was followed by the

residents and closed in a routine inspection.

No violations of

regulatory requirements were identified.

D.

Escalated Enforcement Actions

There were no escalated enforcement actions during the assessment

period.

However, an Order imposing civil penalties in the cumulative

amount of $130,000 was issued in 1985 for violations occurring during

SALP 4.

E.

Management Conferences Held During Appraisal Period

1.

Confirmatory Action Letters (CAL)

A CAL was issued April 15, 1985 to confirm licensee action

regarding monitoring and surveillance actions required as a-

result of the damage sustained by several main steam piping

mechanical snubbers at Unit 2.

2.

Management Conferences

a.

September 7, 1984 (Glen Ellyn, Illinois)

Meeting to discuss licensee performance in regards to

'

their Regulatory Performance Improvement Plan (RPIP).

.

b.

September 17, 1984 (Glen Ellyn, Illinois)

Management meeting to review Systematic Assessment of

Licensee Performance (SALP 4).

s

-

c.

March 7, 1985 (Glen Ellyn, Illinois)

Meeting to discuss licensee performance in regard to

their RPIP.

d.

June 24. 1985 (LaSalle County Station)

Meeting to discuss licensee performance in regard to

their RPIP.

e.

July 16, 1985 (Glen Ellyn, Illinois)

Meeting to discuss additional aspects of the licensee's

RPIP.

3.

Enforcement Conferences

March 25, 1985 (Glen Ellyn, Illinois)

Meeting to discuss the increase in personnel errors and

HPCI inoperability.

F.

Review of Licensee Event Reports and 10 CFR 21 Reports

1.

Licensee Event Reports (LERs)

LER's issued during the 16 month SALP 5 period are presented

below:

Unit 2

Unit 3

LERs No.

LERs No.

84-05 through 84-25

84-05 through 84-23

85-01 through 85-34

85-01 through 85-16

Proximate Cause Code *

Number During Salp 5

Personnel Error (A)

Design Manufacturing,

Construction / Installation (B)

Defective Procedures (D)

Others (X)

Total

- TJ

  • Proximate cause is the cause assigned by the licensee according

to NUREG-1022, " Licensee Event Report System."

<

,

.

During the SALP 5 period, 93 Licensee Event Reports (LERs) which

were required by 10 CFR 50.73 were submitted.

Of these, two

-addressed occurrences on Unit 1, 56 were associated with Unit 2,

and 35 LERs were submitted relating to Unit 3.

In most cases,

the LERs were submitted in a timely manner and in accordance

with NUREG-1022, " Licensee Event Report System." However, in

four cases, LERs were submitted which exceeded the 30 day time

limit.

This was due, in part, to some initial confusion on the

part of the licensee as to what specifically constituted a

reportable occurrence following the change of the NRC reporting

requirements in January 1984.

The licensee conducted a review

of station deviation reports (DVRs) in the Fall of 1984 to

ascertain if all reportable items were issued as LERs and found

that some had been overlooked.

These were then subsequently

made into LERs and submitted.

During subsequent reviews, no

further problems in this area have been identified to date.

Because of the change in reporting requirements that occurred

in January 1984, a detailed comparison of LERs submitted during

SALP 4 and SALP 5 could not be made.

However, tha number of

LERs as a result of personnel errors have increased signifi-

cantly.

A portion of an enforcement conference discussed this

increase.

The number of component failures that were reportable

decreased during the last SALP period.

This is indicative of the

licensee's increased management attention in this area.

Of the 93 LER's submitted by the licensee during the SALP 5

period, 35 were due to unscheduled scrams or RPS actuation

which are discussed in this report under the Operations

Functional Area.

A review of the LERs identified that the

licensee has reported a number of ESF events even though the

actuation was anticipated and would therefore not be reportable.

During the SALP 5 period, where events are caused by personnel

error, and the licensee's investigation reveals that it was

carelessness or disregard by an individual, the licensee has

exercised stronger actions against the individuals who caused

the event.

This has been part of the effort to improve attitudes

and achieve a better sense of accountability to perconnel working

in the plant.

Notwithstanding the positive aspects of the licensee's reporting

system, an assessment by the Office for Analysis and Evaluation

of Operational Data (AEOD) of the quality of LERs submitted found

that the LERs were of barely acceptable quality based on the

requirements contained in 10 CFR 50.73.

The most significant

areas that need improvement are:

root cause discussions,

personnel error discussions, corrective actions to prevent

recurrence, safety assessment information, manufacturer and

<

model number information, date and time information, text

presentation consistency, text readability, and abstracts and

x

.

.

titles need to be written such that they better describe the

essence of the event.

A copy of the AE0D report has been

provided to the licensee so that the specific deficiencies noted

can be corrected in future LERs.

2.

10 CFR 21 Reports

No 10 CFR 21 reports were submitted during the assessment

period.

G.

Licensing Actions

1.-

NRR Site and Corporate Office Visits

March 17-20, 1985 - Site Visit, add RETS to Technical

Specifications and prepare an official version of the

reformatted Technical Specifications for Dresden 2 and 3.

June 9-11, 1985 - Corporate office visit on June 19, 1985, to

accompany J. Zwolinski and C. Jamerson on "get acquainted"

tour. Talked with corporate and technical personnel to ensure

that current regulatory requirements were well understood.

Site Visit on morning of June 11, 1985.

J. Zwolinski and

C. Jamerson met with station management, visited TSC, Control

Room, HRSS, and areas where MVRS is proposed to be placed and

where H Storage Tank is placed, but not approved for use.

J. Zwolinski and C. Jamerson also visited Commonwealth's

Training Center at Braidwood.

2.

Commission Briefing

None.

3.

Schedular Extension Granted

January 3, 1985, Equipment Qualification, Dresden Unit 3.

4.

Relief Granted

March 5, 1985 IST Program - Second 10 Year Interval.

5.

Exemptions Granted

August 14, 1984, - Emergency Preparedness Exercise Exemption,

02 and D3.

September 26, 1985 - Schedular Exemption from Requirements

of Appendix J, D3.

6.

License Amendments Issued

i

t

q;

=

.

...

..

%

. Unit 2-

'

' Amendment-No. 82, issued August-6, 1984, Reformatted Technical

- Specifications.

Amendment No. 83, issued November 16, 1984, Radiological

.

Effluent Technical Specifications.

~

Amendment No 84, issued January 17, 1985, Technical Specifica-

tion changes relating to the Cycle 10 Reload.

Amendment No. 85, issued February 27, 1985, Technical

Specification changes relating to Snubbers and Reflecting

- the_ guidance of Generic Letter 84-13.

Amendment No. 86,_ issued March 20, 1985,- -Technical Specification

changes Relating to Administrative Control and Reportability.

Amendment No.- 87, issued May 30, 1985, Technical Specification

Amendments Resolving-SEP Topics-VI-7.C.1 and XV-16.

- Amendment No. 88, issued May 30, 1985, Technical Specification

changes to Revise Table 3.7.1.

Amendment No. 89,. issued May 30, 1985, Technical Specifications:

Relating to Economic Generation Control.

Amendment No. 90, issued June 24, 1985, Technical Specifications

Relating to TMI Action Items Covered by Generic Letter 83-36.

Unit'3

Amendment No. 75, issued August 6, 1984, Reformatted Technical

Specifications.

Amendment No. 76, issued September 14, 1984, Technical

Specification changes Relating to the Extension of Certain

MAPLHGR Curves.

Amendment No. 77, issued November 16, 1984, Radiological

Effluent Technical Specifications.

Amendment No. 78, issued February 27, 1985, Technical

Specification changes Relating to Snubbers and Reflecting

the Guidance of Generic Letter 84-13.

Amendment No. 19, issued March 20, 1985, Technical

Specification changes Relating to Administrative Control

and Reportability.

~

cr

'..

.

Amendment-No. 80, issued May 30, 1985, Technical Specification

Amendments Resolving SE0 Topics VI-7.C.1 and SV-16.

Amendment No. 81, issued May 30, 1985, Technical Specification

changes to Revise Table 3.7.1.

Amendment No. 82,' issued May 30, 1985,-Technical Specifications

Relating to Econmic Generation Control.

Amendment No. 83, issued' June 24, 1985, Technical Specifications

Relating.to TMI Action Items Covered by Generic Letter 83-36.

Amendment No. 84, issued September 17, 1985, Technical

Specification and License changes Relating to Deletion of

Recirculation Equalizer Valves.

7.

Emergency / Exigent Technical Specification

Emergency Technical Specification for Dresden 3 on LPCI-Loop A -

Extension of LC0 was completed, (but not issued when Licensee was

able to complete the required repairs within the seven day period

specified in the existing Technical Specifications), for issuance.

by 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br />,- August 4, 1985.

8.

Orders Issued

A document entitled " Issuance of Order Confirming Licensee

Commitment on Emergency Response Capability" was issued on

June 12, 1984.

9.

NRR/ Licensee Management Conference

Conference in Bethesda on July 23, 1985 regarding the details

of Commonwealth's program for reactor coolant system piping

replacement during the next refueling outage scheduled to

start October 26, 1985.

,

.('

38