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Category:CORRESPONDENCE-LETTERS
MONTHYEAR1CAN109906, Forwards Framatome Technologies,Inc non-proprietary TR BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheet of Once-Through Sgs, Rev 11999-10-19019 October 1999 Forwards Framatome Technologies,Inc non-proprietary TR BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheet of Once-Through Sgs, Rev 1 ML20217J4971999-10-18018 October 1999 Requests Addl Info Re Results of Util Most Recent Steam Generator Insp at ANO-2 & Util Methodology Used to Predict Future Performance of SG Tubes ML20217J3871999-10-15015 October 1999 Informs That Topical Rept BAW-10235P, Management Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through SG, Rev 0 Marked as Proprietary Will Be Withheld from Public Disclosure 2CAN109902, Submits Withdrawal of Code Case N-593 for ANO-2 Replacement SGs1999-10-15015 October 1999 Submits Withdrawal of Code Case N-593 for ANO-2 Replacement SGs ML20217J3601999-10-15015 October 1999 Informs That Topical Rept BAW-10235P, Management Program for Volumetric Outer Diameter Integranular Attack in Tubesheets of Once-Through SG, Rev 1 Marked as Proprietary Will Be Withheld from Public Disclosure 2CAN109903, Forwards Response to RAI Re Proposed Tech Specs Change for Special SG Insp1999-10-14014 October 1999 Forwards Response to RAI Re Proposed Tech Specs Change for Special SG Insp ML20217D1721999-10-0808 October 1999 Forwards RAI Re 990729 Request for Amend to TSs Allowing Special SG Insp for Plant,Unit 2.Questions Re Proposed Insp Scope for Axial Cracking Degradation in Eggcrate Support Region Submitted.Response Requested by 991015 1CAN109905, Discusses Insp of Once Through SG Tubing Surveillance Performed During 1R15 Scheduled RFO on 990910.Category C-3 Results,Included1999-10-0404 October 1999 Discusses Insp of Once Through SG Tubing Surveillance Performed During 1R15 Scheduled RFO on 990910.Category C-3 Results,Included ML20212L0621999-10-0101 October 1999 Forwards Safety Evaluation & Exemption from Certain Requirements of 10CFR50,App R,Section III.G.2, Fire Protection of Safe Shutdown Capability 1CAN099908, Withdraws 990919 Exigent TS Change Request to Allow Continued Installation of re-rolls for One Cycle of Operation Through End of Cycle 16 in Conjunction with Addl Insp Criteria1999-09-30030 September 1999 Withdraws 990919 Exigent TS Change Request to Allow Continued Installation of re-rolls for One Cycle of Operation Through End of Cycle 16 in Conjunction with Addl Insp Criteria 2CAN099902, Requests That NRC Assign CENPD-132,Suppl 4-P, Calculative Methods for Abb Cenp Large Break LOCA Evaluation Model, Review Priority So That Approval Will Be Granted No Later than Oct 31,20001999-09-29029 September 1999 Requests That NRC Assign CENPD-132,Suppl 4-P, Calculative Methods for Abb Cenp Large Break LOCA Evaluation Model, Review Priority So That Approval Will Be Granted No Later than Oct 31,2000 1CAN099903, Forwards Rev 0 to COLR for ANO-1 Cycle 16, IAW TS 6.12.31999-09-27027 September 1999 Forwards Rev 0 to COLR for ANO-1 Cycle 16, IAW TS 6.12.3 1CAN099907, Requests That Alternative Be Allowed in Accordance with 10CFR50.55a(a)(3)(i) & (II) as Discussed in Encl 1.Encl 2 & 3 Stress Analysis & Flaw Evaluation Summaries Ref in Encl Alternative1999-09-26026 September 1999 Requests That Alternative Be Allowed in Accordance with 10CFR50.55a(a)(3)(i) & (II) as Discussed in Encl 1.Encl 2 & 3 Stress Analysis & Flaw Evaluation Summaries Ref in Encl Alternative 1CAN099906, Forwards 1R15 Growth Data Obtained & Analyzed Through 990922 & Includes Plus Point Voltages,Axial Extent & Circumferential Extent Patches,As Well as Preliminary Growth Conclusions Based on Analysis of Data1999-09-24024 September 1999 Forwards 1R15 Growth Data Obtained & Analyzed Through 990922 & Includes Plus Point Voltages,Axial Extent & Circumferential Extent Patches,As Well as Preliminary Growth Conclusions Based on Analysis of Data 2CAN099901, Informs That G Kendrick,License SOP-43658,no Longer Has Need to Maintain Operating License on Ano,Unit 2.Entergy Requests That License for Individual Be Withdrawn,Due to Resignation, Effective 9908271999-09-24024 September 1999 Informs That G Kendrick,License SOP-43658,no Longer Has Need to Maintain Operating License on Ano,Unit 2.Entergy Requests That License for Individual Be Withdrawn,Due to Resignation, Effective 990827 2CAN099904, Forwards Ano,Unit 2 10CFR50.59 Rept for Time Period Ending 990225.Rept Contains Brief Description of Changes in Procedures & in Facility as Described in Sar,Tests & Experiments Conducted & Other Changes to SAR1999-09-23023 September 1999 Forwards Ano,Unit 2 10CFR50.59 Rept for Time Period Ending 990225.Rept Contains Brief Description of Changes in Procedures & in Facility as Described in Sar,Tests & Experiments Conducted & Other Changes to SAR ML20212F5031999-09-22022 September 1999 Forwards SER Granting Relief Requests 1-98-001 & 1-98-002 Which Would Require Design Mods to Comply with Code Requirements,Which Would Impose Significant Burden Pursuant to 10CFR50.55a(g)(6)(i) 1CAN099905, Submits Supplemental Info in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria.Proposed TS Rev & Info Related to Use of Alternate Repair Discussed in Attachments1999-09-17017 September 1999 Submits Supplemental Info in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria.Proposed TS Rev & Info Related to Use of Alternate Repair Discussed in Attachments ML20212D9961999-09-16016 September 1999 Informs That on 990818,NRC Completed Midcycle PPR of Arkansas Nuclear One.Nrc Plan to Conduct Core Insps at Facility Over Next 7 Months.Details of Insp Plan Through March 2000 Encl 1CAN099902, Forwards Proprietary Rev 1 to Topical Rept BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs, in Response to 990831 Rai.Proprietary Encl Withheld1999-09-15015 September 1999 Forwards Proprietary Rev 1 to Topical Rept BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs, in Response to 990831 Rai.Proprietary Encl Withheld 2CAN099905, Informs That Jk Caery,License OP-42589 & as Bates,License OP-42506,no Longer Need to Maintain Operating License at Ano,Unit 2.Withdrawal of Licenses Is Requested1999-09-0909 September 1999 Informs That Jk Caery,License OP-42589 & as Bates,License OP-42506,no Longer Need to Maintain Operating License at Ano,Unit 2.Withdrawal of Licenses Is Requested 1CAN099901, Forwards Responses to 990831 RAI Containing follow-up Questions Discussed on 990823-26,in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria. Revs to Proposed TSs Included in Attachments1999-09-0707 September 1999 Forwards Responses to 990831 RAI Containing follow-up Questions Discussed on 990823-26,in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria. Revs to Proposed TSs Included in Attachments ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) 0CAN099906, Forwards Comments on Ano,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid,Version 2,in Response to NRC 990708 & 0715 Ltrs1999-09-0101 September 1999 Forwards Comments on Ano,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid,Version 2,in Response to NRC 990708 & 0715 Ltrs ML20211L4901999-09-0101 September 1999 Forwards Insp Repts 50-313/99-12 & 50-368/99-12 on 990711- 0821.No Violations Noted ML20211J2351999-08-31031 August 1999 Forwards Request for Addl Info Re SG Outer Diameter Intergranular Attack Alternate Repair Criteria for Plant, Unit 1 ML20211E6161999-08-25025 August 1999 Forwards Amend 15 to ANO Unit 2,USAR,per 10CFR50.71(e) & 10CFR50.4(b)(6).Summary of 10CFR50.59 Evaluations Associated with Amend 15 of ANO Unit 2 SAR Will Be Provided Under Separate Cover Ltr with 30 Days 0CAN089905, Forwards Arkansas Nuclear One Units 1 & 2 FFD Program Performance Data for Period Jan-June 19991999-08-25025 August 1999 Forwards Arkansas Nuclear One Units 1 & 2 FFD Program Performance Data for Period Jan-June 1999 ML20211F4181999-08-25025 August 1999 Forwards SE Accepting Licensee 980603 & 990517 Requests for Approval of risk-informed Alternative to 1992 Edition of ASME BPV Code Section Xi,Insp Requirements for Class 1, Category B-J Piping Welds ML20211G0731999-08-19019 August 1999 Forwards Applications for Renewal of Operating License for Kw Canitz & Aj South.Without Encls 1CAN089904, Forwards Addl Info in Support of SG Tube End Cracking Alternate Repair Criteria,In Response to NRC 990728 Rai. Proposed TS Changes Encl1999-08-19019 August 1999 Forwards Addl Info in Support of SG Tube End Cracking Alternate Repair Criteria,In Response to NRC 990728 Rai. Proposed TS Changes Encl ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 ML20211A9501999-08-12012 August 1999 Discusses 990720-21 Workshop Conducted in Region IV Ofc,Re Exchange of Info in Area of Use of Risk Insights in Regulatory Activities.List of Attendees,Summary of Topic & Issues,Agenda & Copies of Handouts Encl 0CAN089903, Submits Addl Response to NRC Second RAI Re GL 95-07, Pressure Locking & Thermal Binding of Gate Valves1999-08-12012 August 1999 Submits Addl Response to NRC Second RAI Re GL 95-07, Pressure Locking & Thermal Binding of Gate Valves IR 05000368/19990111999-08-12012 August 1999 Forwards Insp Repts 50-313//99-11 & 50-368/99-11 on 990719-23.No Violations Noted.Insp Focused on Review of Licensed Operator Requalification Program & Observation of Requalification Exam Activities at Unit 1 2CAN089901, Forwards Description of Planned Scope & Expansion Criteria for Special SG Tube Insp,In Support of Proposed ANO-2 TS Amend for 2P99 Special SG Insp Submitted on 9907291999-08-0606 August 1999 Forwards Description of Planned Scope & Expansion Criteria for Special SG Tube Insp,In Support of Proposed ANO-2 TS Amend for 2P99 Special SG Insp Submitted on 990729 1CAN089902, Requests NRC Input on Encl Proposed Draft Format for ANO-1 License Renewal Application,Which Will Provide Option to Continue Operating Plant for Addl Twenty Years Beyond End of Current Operating License1999-08-0505 August 1999 Requests NRC Input on Encl Proposed Draft Format for ANO-1 License Renewal Application,Which Will Provide Option to Continue Operating Plant for Addl Twenty Years Beyond End of Current Operating License 2CAN089902, Informs That Tl Russell,License SOP-43587-1 & Jk Fancher, License OP-42300-1,no Longer Have Need to Maintain Operating License at ANO-2.Withdrawal of Licenses Requested1999-08-0404 August 1999 Informs That Tl Russell,License SOP-43587-1 & Jk Fancher, License OP-42300-1,no Longer Have Need to Maintain Operating License at ANO-2.Withdrawal of Licenses Requested ML20210L1461999-08-0303 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Requests Submittal of Ltr Identifying Individuals Taking Exam,Personnel Allowed Access to Exams & Mailing Address for Exams 0CAN089902, Submits 60 Day Response to GL 99-02, Laboratory Testing of Nuclear Grade Activated Charcoal. Proposed Actions That Will Be Taken on ANO Unit 1 RB Purge Filtration Sys & Unit 2 Containment Purge & Exhaust Sys,Clarified1999-08-0202 August 1999 Submits 60 Day Response to GL 99-02, Laboratory Testing of Nuclear Grade Activated Charcoal. Proposed Actions That Will Be Taken on ANO Unit 1 RB Purge Filtration Sys & Unit 2 Containment Purge & Exhaust Sys,Clarified 0CAN089901, Forwards Info Re Estimate of licensee-originated Licensing Actions for ANO-1 & ANO-2,in Response to Administrative Ltr 99-02,dtd 9906031999-08-0202 August 1999 Forwards Info Re Estimate of licensee-originated Licensing Actions for ANO-1 & ANO-2,in Response to Administrative Ltr 99-02,dtd 990603 ML20210L3581999-07-29029 July 1999 Ltr Contract,Task Order 43, Arkansas Nuclear One Safety System Engineering Insp (Ssei), Under Contract NRC-03-98-021 1CAN079903, Forwards non-proprietary Addendum to Rev 0 of Topical Rept BAW-2346P,in Support of Proposed TS Changes Revising SG Tubing Surveillance Requirements to Provide Alternate Repair Criteria for Tube End Cracks1999-07-29029 July 1999 Forwards non-proprietary Addendum to Rev 0 of Topical Rept BAW-2346P,in Support of Proposed TS Changes Revising SG Tubing Surveillance Requirements to Provide Alternate Repair Criteria for Tube End Cracks ML20216D8131999-07-28028 July 1999 Forwards Request for Addl Info Re SG Tube End Cracking Alternate Repair Criteria for Plant,Unit 1 ML20216D3561999-07-23023 July 1999 Discusses non-cited Violation Identified in Insp Rept 50-313/98-21,involving Failure to Have Acceptable Alternative Shutdown Capability for ANO-1 ML20210C2191999-07-21021 July 1999 Forwards Insp Repts 50-313/99-08 & 50-368/99-08 on 990530-0710 at Arkansas Nuclear One,Units 1 & 2,reactor Facility.No Violations Noted.Conduct of Activities at Plant Generally Characterized by safety-conscious Operations ML20209H5251999-07-15015 July 1999 Informs That as Result of NRC Review of Licensee 980701 & 990311 Responses to GL 92-01,rev 1 & Suppl 1 & Suppl 1 RAI, Staff Revised Info in Reactor Vessel Integrity Database & Releasing Database as Rvid Version 2 1CAN079901, Forwards Proposed Changes to Current Util 990409 Submittal Re Rev to RB Structural Integrity Requirements Contained in Plant Ts.Proposed Revs Affect ACs & Applicable Bases Re ISI Reporting for Containment Structures,Tendons & Anchorages1999-07-14014 July 1999 Forwards Proposed Changes to Current Util 990409 Submittal Re Rev to RB Structural Integrity Requirements Contained in Plant Ts.Proposed Revs Affect ACs & Applicable Bases Re ISI Reporting for Containment Structures,Tendons & Anchorages 0CAN079902, Responds to NRC Telcon RAI Re Proposed Administrative Controls TS Changes.Revised TS Pages Which Replaces Pages Previously Provided in 981124 Submittal,Encl1999-07-14014 July 1999 Responds to NRC Telcon RAI Re Proposed Administrative Controls TS Changes.Revised TS Pages Which Replaces Pages Previously Provided in 981124 Submittal,Encl ML20209E5551999-07-0808 July 1999 Informs That as Result of NRC Review of Util Responses to GL 92-01,rev 1,suppl 1,staff Revised Info in Rv Integrity Database & Releasing Database as Rvid Version 2 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEAR1CAN109906, Forwards Framatome Technologies,Inc non-proprietary TR BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheet of Once-Through Sgs, Rev 11999-10-19019 October 1999 Forwards Framatome Technologies,Inc non-proprietary TR BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheet of Once-Through Sgs, Rev 1 2CAN109902, Submits Withdrawal of Code Case N-593 for ANO-2 Replacement SGs1999-10-15015 October 1999 Submits Withdrawal of Code Case N-593 for ANO-2 Replacement SGs 2CAN109903, Forwards Response to RAI Re Proposed Tech Specs Change for Special SG Insp1999-10-14014 October 1999 Forwards Response to RAI Re Proposed Tech Specs Change for Special SG Insp 1CAN109905, Discusses Insp of Once Through SG Tubing Surveillance Performed During 1R15 Scheduled RFO on 990910.Category C-3 Results,Included1999-10-0404 October 1999 Discusses Insp of Once Through SG Tubing Surveillance Performed During 1R15 Scheduled RFO on 990910.Category C-3 Results,Included 1CAN099908, Withdraws 990919 Exigent TS Change Request to Allow Continued Installation of re-rolls for One Cycle of Operation Through End of Cycle 16 in Conjunction with Addl Insp Criteria1999-09-30030 September 1999 Withdraws 990919 Exigent TS Change Request to Allow Continued Installation of re-rolls for One Cycle of Operation Through End of Cycle 16 in Conjunction with Addl Insp Criteria 2CAN099902, Requests That NRC Assign CENPD-132,Suppl 4-P, Calculative Methods for Abb Cenp Large Break LOCA Evaluation Model, Review Priority So That Approval Will Be Granted No Later than Oct 31,20001999-09-29029 September 1999 Requests That NRC Assign CENPD-132,Suppl 4-P, Calculative Methods for Abb Cenp Large Break LOCA Evaluation Model, Review Priority So That Approval Will Be Granted No Later than Oct 31,2000 1CAN099903, Forwards Rev 0 to COLR for ANO-1 Cycle 16, IAW TS 6.12.31999-09-27027 September 1999 Forwards Rev 0 to COLR for ANO-1 Cycle 16, IAW TS 6.12.3 1CAN099907, Requests That Alternative Be Allowed in Accordance with 10CFR50.55a(a)(3)(i) & (II) as Discussed in Encl 1.Encl 2 & 3 Stress Analysis & Flaw Evaluation Summaries Ref in Encl Alternative1999-09-26026 September 1999 Requests That Alternative Be Allowed in Accordance with 10CFR50.55a(a)(3)(i) & (II) as Discussed in Encl 1.Encl 2 & 3 Stress Analysis & Flaw Evaluation Summaries Ref in Encl Alternative 2CAN099901, Informs That G Kendrick,License SOP-43658,no Longer Has Need to Maintain Operating License on Ano,Unit 2.Entergy Requests That License for Individual Be Withdrawn,Due to Resignation, Effective 9908271999-09-24024 September 1999 Informs That G Kendrick,License SOP-43658,no Longer Has Need to Maintain Operating License on Ano,Unit 2.Entergy Requests That License for Individual Be Withdrawn,Due to Resignation, Effective 990827 1CAN099906, Forwards 1R15 Growth Data Obtained & Analyzed Through 990922 & Includes Plus Point Voltages,Axial Extent & Circumferential Extent Patches,As Well as Preliminary Growth Conclusions Based on Analysis of Data1999-09-24024 September 1999 Forwards 1R15 Growth Data Obtained & Analyzed Through 990922 & Includes Plus Point Voltages,Axial Extent & Circumferential Extent Patches,As Well as Preliminary Growth Conclusions Based on Analysis of Data 2CAN099904, Forwards Ano,Unit 2 10CFR50.59 Rept for Time Period Ending 990225.Rept Contains Brief Description of Changes in Procedures & in Facility as Described in Sar,Tests & Experiments Conducted & Other Changes to SAR1999-09-23023 September 1999 Forwards Ano,Unit 2 10CFR50.59 Rept for Time Period Ending 990225.Rept Contains Brief Description of Changes in Procedures & in Facility as Described in Sar,Tests & Experiments Conducted & Other Changes to SAR 1CAN099905, Submits Supplemental Info in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria.Proposed TS Rev & Info Related to Use of Alternate Repair Discussed in Attachments1999-09-17017 September 1999 Submits Supplemental Info in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria.Proposed TS Rev & Info Related to Use of Alternate Repair Discussed in Attachments 1CAN099902, Forwards Proprietary Rev 1 to Topical Rept BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs, in Response to 990831 Rai.Proprietary Encl Withheld1999-09-15015 September 1999 Forwards Proprietary Rev 1 to Topical Rept BAW-10235P, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs, in Response to 990831 Rai.Proprietary Encl Withheld 2CAN099905, Informs That Jk Caery,License OP-42589 & as Bates,License OP-42506,no Longer Need to Maintain Operating License at Ano,Unit 2.Withdrawal of Licenses Is Requested1999-09-0909 September 1999 Informs That Jk Caery,License OP-42589 & as Bates,License OP-42506,no Longer Need to Maintain Operating License at Ano,Unit 2.Withdrawal of Licenses Is Requested ML20211P4121999-09-0707 September 1999 Requests NRC Staff Review & Approval of Integrated Nuclear Security Plan (Insp) & Integrated Security Training & Qualification Plan (Ist&Q), for Use by All Entergy Operations,Inc.Encl Withheld,Per 10CFR2.790(d) 1CAN099901, Forwards Responses to 990831 RAI Containing follow-up Questions Discussed on 990823-26,in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria. Revs to Proposed TSs Included in Attachments1999-09-0707 September 1999 Forwards Responses to 990831 RAI Containing follow-up Questions Discussed on 990823-26,in Support of SG Outer Diameter Intergranular Attack Alternate Repair Criteria. Revs to Proposed TSs Included in Attachments 0CAN099906, Forwards Comments on Ano,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid,Version 2,in Response to NRC 990708 & 0715 Ltrs1999-09-0101 September 1999 Forwards Comments on Ano,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid,Version 2,in Response to NRC 990708 & 0715 Ltrs ML20211E6161999-08-25025 August 1999 Forwards Amend 15 to ANO Unit 2,USAR,per 10CFR50.71(e) & 10CFR50.4(b)(6).Summary of 10CFR50.59 Evaluations Associated with Amend 15 of ANO Unit 2 SAR Will Be Provided Under Separate Cover Ltr with 30 Days 0CAN089905, Forwards Arkansas Nuclear One Units 1 & 2 FFD Program Performance Data for Period Jan-June 19991999-08-25025 August 1999 Forwards Arkansas Nuclear One Units 1 & 2 FFD Program Performance Data for Period Jan-June 1999 ML20211G0731999-08-19019 August 1999 Forwards Applications for Renewal of Operating License for Kw Canitz & Aj South.Without Encls 1CAN089904, Forwards Addl Info in Support of SG Tube End Cracking Alternate Repair Criteria,In Response to NRC 990728 Rai. Proposed TS Changes Encl1999-08-19019 August 1999 Forwards Addl Info in Support of SG Tube End Cracking Alternate Repair Criteria,In Response to NRC 990728 Rai. Proposed TS Changes Encl ML20211C5101999-08-19019 August 1999 Forwards Certified Copies of Liability Insurance Policy Endorsements Issued in First Half of 1999 for Each Entergy Operations,Inc Nuclear Unit,Per 10CFR140.15 0CAN089903, Submits Addl Response to NRC Second RAI Re GL 95-07, Pressure Locking & Thermal Binding of Gate Valves1999-08-12012 August 1999 Submits Addl Response to NRC Second RAI Re GL 95-07, Pressure Locking & Thermal Binding of Gate Valves 2CAN089901, Forwards Description of Planned Scope & Expansion Criteria for Special SG Tube Insp,In Support of Proposed ANO-2 TS Amend for 2P99 Special SG Insp Submitted on 9907291999-08-0606 August 1999 Forwards Description of Planned Scope & Expansion Criteria for Special SG Tube Insp,In Support of Proposed ANO-2 TS Amend for 2P99 Special SG Insp Submitted on 990729 1CAN089902, Requests NRC Input on Encl Proposed Draft Format for ANO-1 License Renewal Application,Which Will Provide Option to Continue Operating Plant for Addl Twenty Years Beyond End of Current Operating License1999-08-0505 August 1999 Requests NRC Input on Encl Proposed Draft Format for ANO-1 License Renewal Application,Which Will Provide Option to Continue Operating Plant for Addl Twenty Years Beyond End of Current Operating License 2CAN089902, Informs That Tl Russell,License SOP-43587-1 & Jk Fancher, License OP-42300-1,no Longer Have Need to Maintain Operating License at ANO-2.Withdrawal of Licenses Requested1999-08-0404 August 1999 Informs That Tl Russell,License SOP-43587-1 & Jk Fancher, License OP-42300-1,no Longer Have Need to Maintain Operating License at ANO-2.Withdrawal of Licenses Requested 0CAN089901, Forwards Info Re Estimate of licensee-originated Licensing Actions for ANO-1 & ANO-2,in Response to Administrative Ltr 99-02,dtd 9906031999-08-0202 August 1999 Forwards Info Re Estimate of licensee-originated Licensing Actions for ANO-1 & ANO-2,in Response to Administrative Ltr 99-02,dtd 990603 0CAN089902, Submits 60 Day Response to GL 99-02, Laboratory Testing of Nuclear Grade Activated Charcoal. Proposed Actions That Will Be Taken on ANO Unit 1 RB Purge Filtration Sys & Unit 2 Containment Purge & Exhaust Sys,Clarified1999-08-0202 August 1999 Submits 60 Day Response to GL 99-02, Laboratory Testing of Nuclear Grade Activated Charcoal. Proposed Actions That Will Be Taken on ANO Unit 1 RB Purge Filtration Sys & Unit 2 Containment Purge & Exhaust Sys,Clarified 1CAN079903, Forwards non-proprietary Addendum to Rev 0 of Topical Rept BAW-2346P,in Support of Proposed TS Changes Revising SG Tubing Surveillance Requirements to Provide Alternate Repair Criteria for Tube End Cracks1999-07-29029 July 1999 Forwards non-proprietary Addendum to Rev 0 of Topical Rept BAW-2346P,in Support of Proposed TS Changes Revising SG Tubing Surveillance Requirements to Provide Alternate Repair Criteria for Tube End Cracks ML20216D3561999-07-23023 July 1999 Discusses non-cited Violation Identified in Insp Rept 50-313/98-21,involving Failure to Have Acceptable Alternative Shutdown Capability for ANO-1 1CAN079901, Forwards Proposed Changes to Current Util 990409 Submittal Re Rev to RB Structural Integrity Requirements Contained in Plant Ts.Proposed Revs Affect ACs & Applicable Bases Re ISI Reporting for Containment Structures,Tendons & Anchorages1999-07-14014 July 1999 Forwards Proposed Changes to Current Util 990409 Submittal Re Rev to RB Structural Integrity Requirements Contained in Plant Ts.Proposed Revs Affect ACs & Applicable Bases Re ISI Reporting for Containment Structures,Tendons & Anchorages 0CAN079902, Responds to NRC Telcon RAI Re Proposed Administrative Controls TS Changes.Revised TS Pages Which Replaces Pages Previously Provided in 981124 Submittal,Encl1999-07-14014 July 1999 Responds to NRC Telcon RAI Re Proposed Administrative Controls TS Changes.Revised TS Pages Which Replaces Pages Previously Provided in 981124 Submittal,Encl ML20210K1621999-07-0707 July 1999 Informs That Licensee in Process of Preparing Scope of Service Delineation for Environ Assessment to Be Performed for New Airport Located Near Russellville,Ar,To Identify Anticipated Environ Impacts from Various Agencies 1CAN079902, Documents ANO-1 Position Discussed on 990705,with Members of NRC Staff & Formally Requests Enforcement Discretion from Requirements of TS 3.7.2.C to Allow Continued Power of Operation1999-07-0606 July 1999 Documents ANO-1 Position Discussed on 990705,with Members of NRC Staff & Formally Requests Enforcement Discretion from Requirements of TS 3.7.2.C to Allow Continued Power of Operation ML20209B6081999-06-30030 June 1999 Submits Response to NRC GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Disclosure Encl 0CAN069906, Forwards Corrected Pages to 1997 & 1998 Annual Radiological Environ Operating Repts, Issued 980430 (0CAN049804) & 990506 (0CAN059902).Ltr Number & Page Number Are at Top of of Corrected Pages to Replace Originally Pages1999-06-30030 June 1999 Forwards Corrected Pages to 1997 & 1998 Annual Radiological Environ Operating Repts, Issued 980430 (0CAN049804) & 990506 (0CAN059902).Ltr Number & Page Number Are at Top of of Corrected Pages to Replace Originally Pages 1CAN069905, Forwards non-proprietary Version of Rev 0 to TR BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs1999-06-17017 June 1999 Forwards non-proprietary Version of Rev 0 to TR BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs 0CAN069903, Submits Rept of Each Change to or Error Discovered in Acceptable Evaluation Model or in Application of Such Model for ECCS That Affects Peak Cladding Temp,Iaw 10CFR50.46(a) (3)(ii)1999-06-10010 June 1999 Submits Rept of Each Change to or Error Discovered in Acceptable Evaluation Model or in Application of Such Model for ECCS That Affects Peak Cladding Temp,Iaw 10CFR50.46(a) (3)(ii) 2CAN069901, Forwards Probabilistic Operational Assessment of ANO-2 SG Tubing for Cycle 14. Replacement of SGs Planned for Next Refueling Outage (2R14) Scheduled for Fall of 20001999-06-0202 June 1999 Forwards Probabilistic Operational Assessment of ANO-2 SG Tubing for Cycle 14. Replacement of SGs Planned for Next Refueling Outage (2R14) Scheduled for Fall of 2000 1CAN069901, Submits 10CFR50.46 Rept Re Inconsistent Input in SBLOCA Analysis.Rept Submitted in Accordance with Recommendations Stated in Notice1999-06-0202 June 1999 Submits 10CFR50.46 Rept Re Inconsistent Input in SBLOCA Analysis.Rept Submitted in Accordance with Recommendations Stated in Notice 0CAN059906, Forwards Response to NRC 990402 RAI Re GL 96-05, Periodic Verification of Design Basis Capability of Safety-Related Movs1999-05-28028 May 1999 Forwards Response to NRC 990402 RAI Re GL 96-05, Periodic Verification of Design Basis Capability of Safety-Related Movs ML20207E4341999-05-25025 May 1999 Submits 30-day Written Rept on Significant PCT Changes in ECCS Analysis for ANO-1.CRAFT2 Limiting PCT for ANO-1 Was Bounded by 1859 F PCT Calculated at 2568 Mwt for Crystal River 3 Cold Leg Pump Discharge Break Size of 0.125 Ft 1CAN059904, Informs NRC That Wl Franklin No Longer Has Need to Maintain Operating License on Ano,Unit 1.Requests License for Wl Franklin Be Withdrawn1999-05-20020 May 1999 Informs NRC That Wl Franklin No Longer Has Need to Maintain Operating License on Ano,Unit 1.Requests License for Wl Franklin Be Withdrawn 2CAN059906, Informs That ANO-2 UFSAR Will Be Revised to Include Comprehensive Discussions of Each Category of Containment Penetration Overcurrent Protective Devices,Per NRC Review of 980806 TS Change Request Re Relocation of TS Table 3.8-11999-05-18018 May 1999 Informs That ANO-2 UFSAR Will Be Revised to Include Comprehensive Discussions of Each Category of Containment Penetration Overcurrent Protective Devices,Per NRC Review of 980806 TS Change Request Re Relocation of TS Table 3.8-1 1CAN059902, Responds to NRC 990406 RAI Re risk-informed Inservice Insp Pilot Application,Submitted 980603.Approval of Alternative Is Requested Prior to End of July 1999,to Allow Sufficient Time for Util to Revise ANO-1 ISI Program1999-05-17017 May 1999 Responds to NRC 990406 RAI Re risk-informed Inservice Insp Pilot Application,Submitted 980603.Approval of Alternative Is Requested Prior to End of July 1999,to Allow Sufficient Time for Util to Revise ANO-1 ISI Program 2CAN059905, Expresses Appreciation for Staff & Mgt Team Efforts in Aggressively Pursuing Risk Informed ISI Initiative1999-05-14014 May 1999 Expresses Appreciation for Staff & Mgt Team Efforts in Aggressively Pursuing Risk Informed ISI Initiative ML20206P7681999-05-10010 May 1999 Forwards Applications for Renewal of Operating License (Form 398) for MW Little & F Uptagrafft.Without Encl 2CAN059903, Forwards Rev to Footnote Submitted to Provide Clarity to Aforementioned Guidance1999-05-10010 May 1999 Forwards Rev to Footnote Submitted to Provide Clarity to Aforementioned Guidance ML20206N1921999-05-10010 May 1999 Provides Revised Attachment 2 for Alternative Request IWE-02,originally Submitted 990429 Re Bolt Torque or Tension Testing of Class Mc pressure-retaining Bolting as Specified in Item 8.20 of Article IWE-2500,Table IWE-2500-1 ML20206H7121999-05-0606 May 1999 Forwards 1998 Annual Radiological Environ Operating Rept, for Ano.All Radionuclides Detected by Radiological Environ Monitoring Program During 1998 Were Significantly Below Regulatory Limits 1999-09-09
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Text
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- e Entergy Operations, Inc.
1448 SR 333 -
= ENTERGY %*J" J!s" ' .
l
. - Jerry W. Yelverton Vcc Presdent . ;
Operakns 40
~ August 16,1995 ,
OCAN089502 ,
U. S. Nuclear Regulatory Commission Document Control Desk Mail Station Pi-137 :
Washington, DC 20555
Subject:
Arkansas Nuclear One - Units 1 and 2 Docket Nos. 50-313 and 50-368 4 License Nos. DPR-51 and NPF-6 Response To Inspection Report i 50-313/95-12;50-368/95-12 EA 95-085
References:
(1) Letter, Mr. A. Bill Beach to Mr. J. W. Yelverton, dated May 22, .
1995, (Inspection Report 50-313/95-12; 50-368/95-12) l (2) Letter, Mr. A. Bill Beach to Mr. J. W. Yelverton, dated June 23, 1995, (Enforcement Conference Presentation)
(3) Letter, Mr. L.' J. Callan to Mr. J.W. Yelverton, dated July 17,1995 (Inspection Report 50-313/95-12; 50-368/95-12, Notice of ,
Violation)
Gentlemen:
- Pursuant to the provisions of 10CFR2.201, attached is the response to the Notice of Violation identified during the inspection of activities associated with the circumstances surrounding the higher than expected radiation dose rates and accumulated exposure received during the installation of the core support assembly (CSA) in the Arkansas Nuclear One (ANO) Unit 1 ,
reactor vessel on March 9,1995.
Entergy Operations ' acknowledges the significnnce of. the CSA higher than anticipated-exposure event and is concerned with the diversity of the inappropriate actions that occurred prior to and during the event. Following the higher than anticipated exposure event, Entergy Operations performed a thorough investigation and ident!'*.i the inappropriate actions' and associated causes of the event. Additionally, Entergy Operations has developed' a comprehensive corrective action plan that addresses each inappropriate action and associated cause, ,
^
95082302h8 50815 l PDR Q.
ADOCK 05000313 PDR 8h' 6
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V U. S. NRC August 16,1995 Page 2 The. chronology of the CSA event is detailed in references I and 2. The root causes of the
. event and those corrective actions that were immediate, cor.ipleted and "to be completed" were presented to the Nuclear Regulatory Commission (NRC) during the June 15, 1995, enforcement conference and are detailed in reference 2. The presented corrective action plan consisted of approximately 35 actions to be completed prior to either the upcoming ANO Units 1 or 2 refueling outages and those proposed by Babcock and Wilcox Nuclear Technologies (BWNT). It is Entergy Operations' intent to complete each identified corrective action in accordance with our corrective action program; however, only those corrective actions outlined in this NOV response are considered NRC commitments.
Should you have any comments or questions, please call Mr. Dwight Mims at 501-858-4601.
Very truly yours,
/s W
JWY/RMC
~
Attachments
U. S. NRC August 16,1995 Page 3 To the best of my knowledge and belief, the statements contained in this submittal are
" true.
SUBSCRIBED AND SWORN TO before me, a Notary Public in and for Johnson County and the State of Arkansas, this 16th day of August 1995.
n 5 c0DDO l Notary $blic #0 My Commission Empires //-8 -$d90 --
JUANA M.TAPP "w*sfem x
cc: Mr. Leonard J. Callan w c - .= n = u...sooo :
Regional Administrator U. S. Nuclear Regulatory Commission Region IV 611 Ryan Plaza Drive, Suite 400 Arlington, TX 76011-8064 NRC Senior Resident Inspector Arkansas Nuclear One P. O. Box 310 '
London, AR 72847 Mr. George Kalman NRR Project Manager Region IV/ANO-1 & 2 U. S. Nuclear Regulatory Commission NRR Mail Stop 13-II-3 One White Flint North 11555 Rockville Pike Rockville, MD 20852
'-y ,
- Attachment ts OCAN089502 Page 1 of 6 A. . , Resp _onse to violation:
(1) Reason for the violation:
' The root cause for the' NOV associated with the failure to terminate the entry after alarming ' dosimeters alarmed on accumulated dose and unexpected job difficulties is detailed in reference 2 and is outlined below.
Additionally, the root cause for the NOV associated with the as low as reasonably achievable (ALARA) worksheet is also outlined below:
A.1 Failure to route a pre-job ALARA work sheet for Radiation Work Permit (RWP) 1995-1093 to the appropriate craft for completion.
Root Cause: The reason the pre-job ALARA work sheet was not routed for craft review was an error injudgment which resulted in a procedure violation. The BWNT supplied ALARA plan was judged to contain sufficient information to satisfy the intent of the pre-job ALARA work sheet; therefore, a determination was made that a contractor work force review was unnecessary.
A.2 During the removal and replacement of the Unit 1 CSA, four individuals involved in this task did not terminate the entry despite dosimeters alarming on accumulated dose and unegected job difficulties.
Root Cause: Job termination expectations were inadequate. This included the failure to establish an adequate control authority and appropriate communications; contingency considerations were not adequately addressed; termination criteria specifics were not established; competing elements (HP instructions to leave the area and training to never leave a heavy load suspended) created conflicting considerations relative to determining safe conditions; and some HP instructions were ineffective.
(2) Corrective steps taken and results achieved: '
A.1 Procedure 1012.019, Radiation Work Permits, was revised to ensure that ALARA plan requirements are included in the appropriate field document.
I A memorandum was issued to the ALARA staff re-enforcing expectations for the proper use of the pre-job ALARA worksheet.
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Attachment ti
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1 1 J .0CAN089502
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,-- 'A.2 Implemented an HP pre-jobichecklist to ensure that key elements?
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such as.the following are considered; job termination criteria are j" clearly defined; how to terminate the job;-designation of HP and -
'W
~
craft - leads;.- contingency actions;' and ' establislunent- of --
F-;.:- [ Communications.
Hes!th Physics, HP Contractor' and General Employee Training .
(GET) programs were revised to increase emphasis on role and1 authority of HP personnel to'"Stop Work" during radiological events.
The CSA event, including stop work' expectations, was discussed with BWNT field service employees.
- (3) .- Corrective steps that will be taken to prevent funher violations
A.1 The ALARA pre-job checklist will be revised prior to the Unit 2 refueling outage currently scheduled for the Fall of 1995, to ensure review of the pre-job AL' ARA worksheet by.the appropriate craft and ALARA staff.
An assessment of the pre-job ALARA worksheet for h0 man factors considerations and effectiveness will be performed during the ANO Units I and Unit 2 refueling outages which are currently scheduled-
- for the Fall of 1996 and the Fall of 1995, respectively. -i
~
.A.2 Corrective actions have bien completed.' 1 (4). . Date when full compliance will be achievedi
- A.1 - Full compliance will.be achieved when procedure 1012.019 is -
revised prior to the Unit 2 refueling outage currently scheduled for the Fall of 1995, to enhance the pre-job ALARA checklist' l
A.2 Full compliance was achieved on June 14,1995, when the HP pre- 1 job checklist was implemented. >
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s - Page 3 of 6 -
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, c U .B; ,jResponse to violation: ;
- l(1)' ; Reason for the violation
a M -
The root causes for the NOV associated with the infrequently performed ;
test or evolution (IPTE), Pre-Job: Briefings, and refueling transfer canal ;
r water level are detailed in reference 2 and are outlined below:-
L .
Y " B.1 Procedure 1402.055, Removal and: Replacement of the Core . .;
Support Assembly, was not identified as an IPTE in accordance , -!
with Procedure 1000.143, Control ofInfrequently Performed Tests or Evolutions".
Root Cause: The root cause of this condition was determined to be
. personnel error. L The procedure writer did not recognize .that .
Procedure 1402.055 should have been classified as an IPTE.
B.2 Prior to the removal and replacement of the Unit 1 CSA, a-complete briefing including all. personnel involved with the . l replacement of the CSA was not conducted.- .j 1
Root Cause: The individuals involved in the replacement of the CSA were provided an ALARA briefing. Since this evolution was not considered to be an IPTE, the ALARA briefing was acceptable; ,
for that situation. If the evolution had been classified as an IPTE, j then a pre-job briefing with involved personnel would have been required. .
B.3(1) Failure to establish the required fuel canal water level prior to !
moving the CSA which resulted in a highly irradiated section of the core support assembly being lifted above the surface of the water ' ;
and higher than expected dose rates and accumulated doses for: '!
personnel involved in'the activity. i
~
Root Cause: A' CSA installation procedural pre-requisite step l' required that the fuel transfer canal (FTC) water level be verified at .
the " normal . water level" for refueling activities. ;The normal '
refueling water level elevation value was not specified in the CSA installation procedure. Additionally, the responsibility for !
verification of the CSA installation pre-requisites was delegated to ,
a contractor who .was not appropriately sensitive to' procedural' ,
requirements for FTC water level elevation. 1
-l a
.' Attachment to E OCAN089502 Page'4 of 6 4
, B.3(2) Procedure 1402.055 was inadequate in that it did not incorporate radiation dose reduction provisions to prohibit raising the hold-down bolt area of the CSA above an established normal fuel
- transfer canal waterlevel.
Root' Cause: There was no established method in place to
}; incorporate ALARA plan information into field documents. The v ALARA plan format implied that the contractor was responsible for controlling this portion of the evolution. The ANO ALARA plan reviewers did not recognize the need to incorporate this aspect into the ANO process.
(2) Corrective stens taken and results achieved:
B.1 Procedure 1402.055 was classified as an IPTE and revised to include critical CSA movement attributes, i.e. minimum and maximum lift heights, cautionary statements concerning bolt region exposure, FTC water level elevation limits.
A Quality Assurance (QA) audit of ANO procedures for IPTE applicability was performed.
Unit I and Unit 2 Maintenance procedures and refueling path procedures assigned to Maintenance, Outage Management, and Design Engineering were reviewed by a multi-discipline team to assure proper IPTE classifications.
Procedure 1000.143, Control ofInfrequently Performed Tests or Evolutions was revised to emphasize communication and job termination criteria. ;
l Refresher training was provided to applicable procedure writers on !
the IPTE process. j i
}
B.2 No corrective actions were identified for this area.
i B.3 A process to incorporate ALARA plan requirements into field documents was implemented.
The Unit 1 CSA removal and installation refueling. task was designated as an IPTE and was revised to include cautionary statements regarding CSA bolt ring region exposure.
The responsibility for Unit I refueling path procedures was shifted to Outage Management.
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3 g,, i~Atischment to' M F OCAN089502 i ,
(Page'5of6: .
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f , _ ;(3) ; Corrective steps that will be taken to prevent further violations: f i
f ,
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- B.1 A' databaseto -identify IPTE procedures! will; be developed lby '
October 16,1995.
B.2 . A meth_od to flag IPTE and other critical briefings in the outage j
. schedule will be developed by May 3,1996. -
Periodic -assessments will- be . performed to' determine the i effectiveness of IPTE briefs 'during lR13 and 2R11,' currently; '
u e
. scheduled for the Fall 'of 19% and the Fall of 1995, respectivelyl l B.3 : The appropriate Unit 2 refueling path procedures will be revised ' <
- . prior. to the ANO Unit 2 refueling outage 2R11, currently .!
scheduled for the Fall of 1995, to include:
e ProperIPTE designation ;
- Specific fuel transfer canal water level , l e ANO sign off ofinitial conditions / prerequisites _
The Unit I and 2 refueling procedures will be evaluated for lessons learned from the CSA event prior to refueling outages IR13.and ;
2R11 currently scheduled for the Fall of 1996 and the Fall of 1995,~ ;
respectively.
In future outages, Unit 1 ANO refueling supervisors will be utilized . e
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during the entire refueling path verses fuel movement only.
l !
' The Unit 1 and Unit 2 Operations, Outage Management, and HP
'depanments will evaluate existing fuel transfer canal water level controls prior to' refueling outages- 1R13 Land 2R11 currently -
scheduled for the Fall of 1996'and the Fall ~of 1995, respectively.-
Consideration will be given to the necessary level for non-fuel.
components such as CSA, plenum, and incore detectors.
(4) Date when full comoliance will be achievedi i
Full compliance will be achieved prior to refueling outages 1R13 and 2R11, ,
currently scheduled for the Fall of 1996 and the Fall of 1995, respectively.
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Attachment to OCAN089502 l Page 6 of 6 C., , , Essp2Dse to violation:
(1) Reason for the violttion:
The root cause for the NOV associated with the failure to approve an overtime extension is detailed in reference 2 and outlined below:
C. Personnel directly involved in the replacement of the core support assembly worked between 19 and 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> straight without the approval of the Unit 1 Plant Manager.
Root Cause: The root cause of this condition was personnel error.
The requester did not ensure that approval to exceed ovenime limits had been given. One contributing cause was determined to be miscommunication, in that the BWNT workers were notified ,
that they had approval to exceed the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> ovenime limit. The j other contributing cause was that the ovenime extension request form lacked human factor elements for ease of use and understanding. 1 (2) Corrective steps taken and results achieved.
1 C. A memorandum was issued designating approval authority for I overtime extensions.
A multi-discipline team reviewed the overtime policy and' recommended enhancements. As a result, the ovenime policy, and associated forms were revised based on the recommended i enhancements. This new policy was communicated to supervisors and above.
GET training was revised to include a discussion on the ovenime--
policy and approval process.
(3) Corrective steps that will be taken to prevent further violations: ;
1 C. QA will assess the effectiveness of selected corrective actions during refueling outages IR13 and 2Rll scheduled for the Fall of 1996 and the Fall of 1995, respectively.
(4) p_ ate when full comoliance will be achieved:
C. ANO is currently in compliance with ANO Unit 1 Technical Specification 6.2.2.1.
I .:.,