12-15-2004 | ■ ,., , , 20.2203(2)(2)(1v) 50.73(aX2)(i)(A) 50.73(aX2)(v)(D) . I , 20.2203(aX2Xv) 50.73(aX2XiXB) 50.73(a)(2Xvii)
- ' , 20.2203(aX2)(vi) 50.73(aX2)(1XC) 50.73(a)(2XviiiXA) 20.2203(a)(3Xi) 50.73(aX2)(ii)(A) 50.73(aX2Xviii)(B) 4.. ” i
- ,, , 3 , ,,,,,, i'
|
---|
LER-2004-002, Manual Reactor Trip Initiated Due to Control Rods from Shutdown Bank D Dropping into the CoreDocket Number |
Event date: |
10-28-2004 |
---|
Report date: |
12-15-2004 |
---|
4142004002R00 - NRC Website |
|
12. LICENSEE CONTACT FOR THIS LER
NAME TELEPHONE NUMBER (Include Area Code) A. Jones-Young, Regulatory Compliance (803)831-3051
13. COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT
MANU- REPORTABLE j MANU- REPORTABLE CAUSE SYSTEM COMPONENT FACTURER TO EPIX i. CAUSE SYSTEM COMPONENT FA CTURER TO EPIX X6 IRE 2IRECM0046 WEST YES 14. SUPPLEMENTAL REPORT EXPECTED 15. EXPECTED MONTH DAY YEARSUBMISSIONIYES (If yes, complete EXPECTED SUBMISSION DATE). I X NO DATE 16. ABSTRACT (Umit to 1400 spaces, I.e., approximately 15 single-spaced typewritten lines) On October 28, 2004, at 0052 hours6.018519e-4 days <br />0.0144 hours <br />8.597884e-5 weeks <br />1.9786e-5 months <br />,' with Catawba Unit 2 operating in Mode 1 at 100% power, all four control rods from Shutdown Bank D inserted into the core.C Consequently, the Operators responded by manually tripping the reactor.
The plant response to the reactor trip remained within the limits of the Updated Final Safety Analysis Report.C All plant equipment operated as expected.
The most probable cause of this event was an intermittent failure of a circuit card in the rod control system.C Corrective actions for this event included replacing the suspect circuit card and sending the card to the vendor for further analysis.
This event was of no significance with respect to the health and safety of the public.
BACKGROUND
This event is being reported under 10 CFR 50.73 (a)(2)(iv)(A), Any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature including the Reactor Protection System.
Catawba Nuclear Station (CNS) Unit 2 is a Westinghouse four-loop pressurized water reactor [EIIS: RCT]. Unit 2 was operating in Mode 1 (Power Operation) at 100% power prior to this event.
The CNS Unit 2 core contains 53 control rods [EIIS: ROD]. The control rods [EIIS: ROD] are grouped into four control banks and five shutdown banks. During Mode 1 operation, the shutdown banks are fully withdrawn. The shutdown banks are held in position by energizing the stationary gripper coils from the control rod power supply cabinets.
Manual movement of the shutdown banks are based on input signals from the rod control logic cabinet.
There were no systems, structures or components out of service during this event that contributed to this event.
EVENT DESCRIPTION
(Dates and times are approximate) 10/28/04/0052:22�The Operator 'at the Controls (OATC) simultaneously received the following Annunciator alarms, "Pressurizer Low Pressure Control"; "Rod Control Urgent Failure"; "RPI at Rod Bottom Drop"; and "RPI Two or more Rods at Bottom".
10/28/04/0052 The OATC announced that all four rods of Shutdown Bank D had dropped and that he was manually tripping the reactor.
10/28/04/0052:38� The reactor was manually tripped per procedure.
10/28/04/0122 All plant control systems functioned as designed. Plant conditions stabilized at no load conditions.
10/28/04/0312 Required four hour notification to the NRC completed.
10/29/04/2037 Unit 2 Turbine Generator placed on line.
10/31/04/1447 Unit 2 returned to 100% power.
CAUSAL FACTORS
The reactor was manually tripped because all four control rods from Shutdown Bank D unexpectedly inserted into the core. The most probable cause of this event was an intermittent failure of a circuit card in the rod control system. Extensive testing of the circuit card was performed and the failure mode could not be duplicated. Technology is not currently available to detect intermittent failures. The consensus of Westinghouse and the failure investigation process (FIP) team was that the testing was inconclusive as far as ruling out the card as the cause of the failure because the card could be exhibiting a sporadic problem. Industry operating experience for Westinghouse Rod Control indicates that intermittent failures do occur. Based on the extensive testing that was performed on the card and the industry operating experience, the FIP team had reasonable assurance that the circuit card was the most likely cause and agreed to accept the Westinghouse recommendation to replace the circuit card prior to restart. The suspect circuit card was sent to Westinghouse for further analysis of the failure. Investigations into the failure of the rod control system with respect to the circuit card are inconclusive.
The circuit card has been installed since Unit 2 Startup and has not experienced any major problems. The card was last tested in the year 2000; however, checks are made on the rod control logic cabinet each refueling outage.
CORRECTIVE ACTIONS
Immediate:
1. Operations entered the reactor trip response procedure and plant conditions were stabilized at no-load conditions.
Subsequent:
1.The circuit card was replaced and the unit was returned to service.
2.The suspect circuit card was sent to Westinghouse for further analysis.
Planned:
1.Complete the root cause evaluation of the suspect circuit card.
2.Based on the results of the evaluation, Engineering will evaluate and initiate corrective actions, as appropriate, for the rod control circuit cards.
The planned corrective actions are being addressed via the Catawba Corrective Action Program. There are no NRC commitments contained in this LER.
SAFETY ANALYSIS
Safety Analysis Overview The Solid State Protection System functioned as designed upon receipt of the manual reactor trip signal. The reactor trip breakers opened and all control rods and shutdown rods inserted as designed. Main turbine trip was initiated by a reactor trip signal as designed.
Nuclear instrumentation response was normal following the trip.
Reactor coolant system pressure control functioned as expected.
Pressurizer power operated relief valves and code safety valves were not challenged and did not lift during the event. The pressurizer spray valves and pressurizer heaters controlled primary system pressure as designed. Pressurizer level control functioned as expected.
Reactor coolant temperature control was by the condenser dump valves.
Steam generator power operated relief valves and code safety valves were not challenged and did not lift during the event. The plant cooldown rate was less than the Technical Specification limit of 100 degrees F per hour.
Steam generator level control functioned as expected with makeup being provided by the motor driven auxiliary feedwater pumps. The Main Feedwater isolation system operated as designed.
In summary, the transient remained within the bounds of the Updated Final Safety Analysis Report and the post trip transient response was as expected.
The core damage significance of this event has been evaluated quantitatively by considering the following:
- Diesel Generator 1A in maintenance on the opposite unit at the time of the trip The conditional core damage probability for the event is estimated to be 3E-7, which is less than the accident sequence precursor threshold of 1E-6.
The dominant base case Large Early Release Frequency (LERF) sequences for Catawba involve steam generator tube rupture, inter-system Loss of Coolant Accident (ISLOCA) and seismic-initiated sequences. In addition, the reliability of the important containment safeguards systems (containment spray and hydrogen mitigation) was not impacted by the reactor trip. Therefore, this event is not significant with respect to the LERF for'Catawba.
This event was of no significance with respect to the health and safety of the public.
ADDITIONAL INFORMATION
Within the last three years, four other reactor trip events occurred from power operation at Catawba. They were as follows:
low reactor coolant flow when the 2D reactor coolant pump 6900 VAC feeder breaker opened in response to a protective relay actuation caused by an electrical fault internal to the pump motor.
a turbine trip. The turbine trip was due to steam generator high level. The root cause of this event was determined to be an inadequate understanding of the digital feedwater control system response to a common impulse line hydraulic interaction.
out of four trip logic for OTdT was satisfied. One channel of OTdT was previously tripped because of a reactor coolant system hot leg temperature detector failure. The second channel trip was caused by the failure of the pressurizer pressure loop power supply card.
resulted when the hydraulic system for the actuator on 1B Steam Generator Main Feedwater Isolation valve (1CF-42) failed and the valve closed.
The specific causes of the four events were unrelated. Therefore, this event was determined to be non-recurring in nature.
Energy Industry Identification System (EIIS) codes are identified in the text as [EIIS: XX]. The rod control system circuit card failure is an EPIX program reportable equipment failure.
This event does not reflect a manual reactor trip with a loss of secondary heat removal capability as monitored by the NRC performance indicator. Main Feedwater and Auxiliary Feedwater systems remained available. Condenser vacuum was maintained and condenser steam dump valves controlled reactor coolant system temperature throughout the event.
This event did not involve a Safety System Functional Failure.
There were no releases of radioactive materials, radiation exposures, or personnel injuries associated with this event.
|
---|
|
|
| | Reporting criterion |
---|
05000348/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2004-001 | Inadvertent Actuation of ECCS and EDGs While in Refueling Mode | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2004-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2004-001 | Failure To Comply With Technical Specification 3 .7 .5 .1, Control Room Emergency Ventilation System | | 05000301/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000313/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000285/LER-2004-001 | Failure To Perform A Leakage Test Due To Lack Of Understanding of Penetration Design | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000271/LER-2004-001 | Main Steam Isolation Valve Leakage Exceeds a Technical Specification Leakage Rate Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2004-001 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000318/LER-2004-001 | . Reactor Trip Due to Low Steam Generator Water Level After Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000289/LER-2004-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-001 | | | 05000247/LER-2004-001 | Manual Reactor Trip Due to Oscillating Feedwater Flow and Steam Generator Level with Flow Perturbations Caused by a Degraded Feed Water Regulating Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000244/LER-2004-001 | Gaps in the Control Room Emergency Zone Boundary | | 05000255/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000461/LER-2004-001 | Clinton Power Station 05000461 1 OF 4 | | 05000414/LER-2004-001 | relPowere Vice President A Duke Energy Company Duke Power Catawba Nuclear Station 4800 Concord Rd. / CNO1VP York, SC 29745-9635 803 831 4251 803 831 3221 fax November 9, 2004
U. S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, DC 20555-0001
SUBJECT: Duke Energy Corporation
Catawba Nuclear Station Unit 2
Docket No. 50-414
Licensee Event Report 414/04-001 Revision 0
Reactor Coolant System Pressure Boundary Leakage
Due to Small Cracks Found in Steam Generator
Channel Head Bowl Drain Line on 2C & 2D Steam
Generators
Attached please find Licensee Event Report 414/04-001
Revision 0, entitled "Reactor Coolant System Pressure
Boundary Leakage Due to Small Cracks Found in.Steam
Generator Channel Head Bowl Drain Line on 2C & 2D Steam
Generators."
This Licensee Event Report does not contain any regulatory
commitments. Questions regarding this Licensee Event Report
should be directed to R. D. Hart at (803) 831-3622.
Sincerely,
Dhiaa Jamil
Attachment
www.dukepower.corn 00- U.S. Nuclear Reguldhory Commission
November 9, 2004
Page 2
XC: W.D. Travers
U.S. Nuclear Regulatory Commission
Regional Administrator, Region II
Atlanta Federal Center
61 Forsyth St., SW, Suite 23T85
Atlanta, GA 30303
E.F. Guthrie
Senior Resident Inspector (CNS)
U.S. Nuclear Regulatory Commission
Catawba Nuclear Station
S.E. Peters (addressee only)
NRC Project Manager (CNS)
U.S. Nuclear Regulatory Commission
One White Flint North, Mail Stop 10-B3
11555 Rockville Pike
Rockville, MD 20852-2738
NRC FORM 366� U.S. NUCLEAR REGULATORY APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004)� COMMISSION Estimated burden per response to comply with this mandatory collection request 50
hours. Reported lessons learned are Incorporated Into the licensing process and fed back
to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy
Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, WashinMon, DC 2055
LICENSEE EN/ENT REPORT (LER) 0001, or by Internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104). Office of Management(See reverse for required number of and Budget, Washington, DC 20503. If a means used to impose an Information col ectiond( inverse �for each block) does not display a currently valid OMB control number, the NRC may not conduct or sponsor. and a person Is not required to respond o. the Information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 050- 00414 1 OF�6 4. TITLE Reactor Coolant System Pressure Boundary Leakage Due to Small Cracks Found in
Steam Generator Channel Head Bowl Drain Line on 2C & 2D Steam Generators | | 05000368/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2004-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2004-001 | Gas Accumulation in Centrifugal Charging Pump Suction Piping | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000395/LER-2004-001 | Reactor Trip Due to Valve Failure During Forced Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000390/LER-2004-001 | Automatic Reactor Trip Due to a Invalid Turbine Trip Signal (P-4) | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2004-001 | Auxiliary Feedwater System in prohibited condition due to inadequate procedure. | | 05000454/LER-2004-001 | Exelent
Exelon Generation Company, LLCRwww.exeloncorp.com NuclearByron Station 4450 North German Church Road Byron, IL 61010-9794 October 17, 2004 LTR: BYRON 2004-0111 File: 2.01.0700 United States Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Subject:RLicensee Event Report (LER) 454-2004-001-00, "Reactor Containment Fan Coolers Flow Rates Below Technical Specification Requirements Due to Inaccurate Flow Indication" Byron Station, Unit 1
Facility Operating License No. NPF-37
NRC Docket No. STN 50-454
Enclosed is an LER involving the August 17, 2004, event involving low flow conditions discovered in Unit 1 Reactor Containment Fan Coolers for a time period longer than allowed by the Technical Specifications. This event is reportable to the NRC in accordance with 10CFR 50.73 (a)(2)(i)(B), as a condition prohibited by Technical Specifications. Should you have any questions concerning this matter, please contact Mr. William Grundmann, Regulatory Assurance. Manager, at (815) 234-5441, extension 2800. Respectfully, Stephen E. Kuczynski Site Vice President Byron Nuclear Generating Station Attachment LER 454-2004-001-00 cc:RRegional Administrator, Region III, NRC NRC Senior Resident Inspector— Byron Station NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7.2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T.6 E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail toLICENSEE EVENT REPORT (LER) *I@ nrc.gov, and to the Desk Officer, Office of Informabon and Regulatory Affairs, NEOB:10202 (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose information collection does not display a currently valid OMB control number, the NRC may not _ conduct or sponsor, and a person is not required to respond to, the information collection. 1 rand ITV NAUP o natuerr An warn q par= . Byron Station, Unit 1 0500454 1 OF 5 4. Reactor Containment Fan Coolers Flow Rates Below Technical Specifications Requirements Due to Inaccurate Flow Indication | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2004-001 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000336/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2004-002 | Dresden Nuclear Power Station Unit 2 05000237 1 of 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000244/LER-2004-002 | Consolidated Rod Storage Canister Placed in Incorrect Storage Location | | 05000530/LER-2004-002 | Main Turbine Control System Malfunction Results in Automatic Reactor Trip on Low DNBR | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000305/LER-2004-002 | | | 05000247/LER-2004-002 | Manual Reactor Trip Due to Decreasing 23 Steam Generator Level Caused by Feedwater Regulating Valve Closure Due to a De-energized Solenoid Operated Valve from Wiring Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000414/LER-2004-002 | Manual Reactor Trip Initiated Due to Control Rods from Shutdown Bank D Dropping into the Core | | 05000251/LER-2004-002 | AAA | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv)(b) | 05000397/LER-2004-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000346/LER-2004-002 | Reactor Trip During Reactor Trip Breaker Testing Due To Fuse Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2004-002 | Emergency Diesel Generator Start and Load Due to Momentary Fault on Incoming Feed | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000269/LER-2004-002 | eif Powere RON A. JONES Vice President A Duke Energy Company Oconee Nuclear Site Duke Power ONO1VP / 7800 Rochester Highway Seneca, SC 29672 864 885 3158 864 885 3564 fax September 9, 2004
U.S. Nuclear Regulatory Commission
Document Control Desk
Washington, D.C. 20555
Subject: Oconee Nuclear Station
Docket Nos. 50-269,-270, -287
Licensee Event Report 269/2004-02, Revision 1
Problem Investigation Process No.: 0-04-2808
Gentlemen:
Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached
is Licensee Event Report 269/2004-02, Revision 1, regarding
a Main Steam Line Break mitigation design/analysis
deficiency which could result in the main and startup
feedwater control valves being technically inoperable for
mitigation of some steam line break scenarios.
This report is being submitted to supplement Revision 0
submitted July 6, 2004. At that time the root cause
investigation and an analysis of the consequences of
potentially exceeding the Environment Qualification (EQ)
envelope curve were still in progress.
This event is being reported in accordance with 10 CFR
50.73 (a)(2)(i)(B) as a condition prohibited by Technical
Specifications, 50.73(a)(2)(ii)(B) as an Unanalyzed
Condition, and 50.73(a)(2)(V)(D) as a potential loss of
safety function for Accident Mitigation. This event is
considered to be of no significance with respect to the
health and safety of the public.
www.dukepower.corn Document Control Desk
Date: September 9, 2004
Page 2
Attachment: Licensee Event Report 269/2004-02, Revision 1
cc: Mr. William D. Travers
Administrator, Region II
U.S. Nuclear Regulatory Commission
61 Forsyth Street, S. W., Suite 23T85
Atlanta, GA 30303
Mr. L. N. Olshan
Project Manager
U.S. Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Washington, D.C. 20555
Mr. M. C. Shannon
NRC Senior Resident Inspector
Oconee Nuclear Station
INPO (via E-mail)
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7-2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T-6 E6), U.S. Nuclear Regulatory Commission, Washington. DCLICENSEE EVENT REPORT (LER) 20555-0001, or by Internet e-mail to bpi @nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management and(See reverse for required number of Budget, Washington, DC 20503. If a means used to impose information collection doesdigits/characters for each block) not display a currently valid OMB control number, the NRC may not conduct or sponsor, and,1 nnmnn lc not rent Owl to tocnnni-I to the intnrmatinn rntlentinn 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Oconee Nuclear Station, Unit 1 050-81 OF 0269 11 4. TITLE Main Steam Line Break Mitigation Design/Analysis Deficiency | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000313/LER-2004-002 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000271/LER-2004-002 | Special Nuclear Material Inventory Location Discrepancy | | 05000285/LER-2004-002 | Inoperable Diesel Generator for 28 Days Due to Blown Fuse During Shutdown | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2004-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000311/LER-2004-002 | Failure To Comply With Technical Specifications During Reactor Protection Instrument Calibration . | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2004-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-002 | | | 05000302/LER-2004-002 | Emergency Diesel Generator Inoperable Due To Fuel Oil Header Outlet Check Valve Leaking Past Seat | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
|