10-18-2004 | _*On-August 17, 2004; itWas recognized that-the E10 CFR sential-Ser-vice Water ( SX)-flow -terthel A,1B,-5rid-1C Reactor Containment Fan Coolers ( RCFCs) were below the Technical Specification (TS) minimum value. The appropriate Technical Specification Action condition was entered. It was determined the flow rates were inadvertently throttled below the limit on April 20, 2004 due to inaccurate flow indicators used to re-adjust flow rates. The flow instruments are annubar flow measurement devices. On August 19, 2004, flow rates were readjusted using ultrasonic flow instrumentation and TS action condition exited. The root cause of the installed inaccurate flow indicators is currently indeterminate. A troubleshooting plan will be implemented in next refuel outage to determine the cause of the inaccurate flow indication. The findings and corrective actions to prevent recurrence will be reported in a supplement to this report. Interim corrective actions include an adverse monitoring plan to ensure flow rates to the RCFCs remain above the minimum flow and enhancing the SX system monitoring plan for better detection of adverse trends. An engineering evaluation is in progress assessing the safety signifiance of the low flow condition to the Unit 1 1A, 1B, and 1C RCFCs for the 119 day period. The results of the evaluation will also be reported in a supplement to this report. This is reportable to the NRC in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications.
(K:113YRSOCSAERS120031ers454-2003-003-00.doc) |
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LER-2004-001, Exelent
Exelon Generation Company, LLCRwww.exeloncorp.com NuclearByron Station
4450 North German Church Road
Byron, IL 61010-9794
October 17, 2004
LTR: BYRON 2004-0111
File: 2.01.0700
United States Nuclear Regulatory Commission
ATTN: Document Control Desk
Washington, DC 20555-0001
Subject:RLicensee Event Report (LER) 454-2004-001-00, "Reactor Containment Fan
Coolers Flow Rates Below Technical Specification Requirements Due to
Inaccurate Flow Indication"
Byron Station, Unit 1
Facility Operating License No. NPF-37
NRC Docket No. STN 50-454
Enclosed is an LER involving the August 17, 2004, event involving low flow conditions
discovered in Unit 1 Reactor Containment Fan Coolers for a time period longer than allowed by
the Technical Specifications. This event is reportable to the NRC in accordance with 10CFR
50.73 (a)(2)(i)(B), as a condition prohibited by Technical Specifications.
Should you have any questions concerning this matter, please contact Mr. William Grundmann,
Regulatory Assurance. Manager, at (815) 234-5441, extension 2800.
Respectfully,
Stephen E. Kuczynski
Site Vice President
Byron Nuclear Generating Station
Attachment LER 454-2004-001-00
cc:RRegional Administrator, Region III, NRC
NRC Senior Resident Inspector— Byron Station
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004
(7.2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request 50
hours. Reported lessons learned are incorporated into the licensing process and fed back to
industry. Send comments regarding burden estimate to the Records Management Branch (T.6 E6),
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail toLICENSEE EVENT REPORT (LER) *I@ nrc.gov, and to the Desk Officer, Office of Informabon and Regulatory Affairs, NEOB:10202
(3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose
information collection does not display a currently valid OMB control number, the NRC may not
_ conduct or sponsor, and a person is not required to respond to, the information collection.
1 rand ITV NAUP o natuerr An warn q par= .
Byron Station, Unit 1 0500454 1 OF 5
4. Reactor Containment Fan Coolers Flow Rates Below Technical Specifications Requirements Due to
Inaccurate Flow IndicationDocket Number |
Event date: |
08-17-2004 |
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Report date: |
10-18-2004 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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4542004001R00 - NRC Website |
|
LICENSEE EVENT REPORT (LER) estimate to the information and Records Management Branch (t-6133), U.S.
Paperwork Reduction Project (3150-0104), Office Of Management And Budget, Washington, DC 20503. If an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Byron Station, Unit 1 STN 0500454 NUMBER NUMBER (If more space Is required, use additional copies of NRC Form 366A)(17)
A. Plant Conditions Prior to Event:
Event Date/Time: August 17, 2004 / 0855 hours0.0099 days <br />0.238 hours <br />0.00141 weeks <br />3.253275e-4 months <br /> Unit 1 - Mode 1— Power Operations, Reactor Power 100% Reactor Coolant System [AB]: Normal operating temperature and pressure.
No structures, systems or components were inoperable at the start of the event that contributed to the event.
Background
Byron Station Unit 1 has two trains of containment cooling each of sufficient capacity to supply 100% of the design basis containment cooling requirement. Each train consists of two Reactor Containment Fan Coolers (RCFCs) [IK]. The RCFCs are supplied cooling water from the Essential Service Water System (SX) [BI], which is throttled to each cooler to keep the SX flow rate above the minimum Technical Specification (TS) required flow rate of 2260 gpm.
B. Description of Event:
During performance of a lA SX pump surveillance on August 17, 2004, the SX System Engineer (non licensed) observed an unexpectedly low flow rate in the lA train SX supply header. The flow rate of 4560 gpm was measured using an ultrasonic flow meter where as a nominal flow of greater than 5320 gpm would be expected. This supply header provides flow to various IA SX train components; including the two RCFCs of the A train of containment cooling (i.e., the 1A and 1C RCFCs). Realizing that the Technical Specifications require a minimum SX flow rate of 2660 gpm for each of the two RCFCs, the SX System Engineer recognized that the observed lA SX header flow rate could not support the required minimum flow to the two RCFCs. The Ul Operations Shift Supervisor (licensed) was immediately notified. The lA SX supply header flow rate was re-checked using different ultra-sonic flow instrumentation and the same low flow condition was confirmed. At this time the lA and 1C RCFC were declared inoperable and TS Limiting Condition for Operation (LCO) 3.6.6, "Two containment Spray trains and two containment cooling trains shall be operable," Action C was entered for one train of containment cooling inoperable. The entry time was retroactive to the first shift notification by the SX System Engineer.
(KABYR_DOCSAJERS120031ers1454-2CO3-003-00.doc) LICENSEE EVENT REPORT (LER) estimate to the information and Records Management Branch (t-6 f33), U.S.
Paperwork Reduction Project (3150-0104), Office Of Management And Budget Washington, DC 20503. If an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Byron Station, Unit 1 STN 0500454 NUMBER NUMBER (If more space is required, use additional copies of NRC Form 366A)(17) A troubleshooting plan was immediately developed to resolve this discrepancy. The local installed flow indicators inside containment, which are used to throttle flow to the RCFCs, were checked and all indicated a flow rate of griater than 2660 gpm to each RCFC. These instruments are Annubar flow measuring devices. These flow rates were then checked to all four RCFCs using an ultrasonic flow instrumentation. Flow to the 1A, 1C and 1B RCFCs were found to be below the TS minimum value of 2660 gpm. Since TS 3.6.6 LCO, Action C, also covers two trains of containment cooling inoperable, additional TS actions were not necessary. It was apparent at this time the installed flow rate indicators to the RCFCs were reading inaccurately.
Historical surveillance data were reviewed of the lA Supply header flow rates from the quarterly 1A SX and 1B SX pump surveillances and the monthly RCFC flow rates verification. The RCFC flow rates were consistent with the lA SX header flow and above the TS limit until the April 20, 2004 RCFC flow verification surveillance. In this surveillance, the flow to the 1D RCFC was found to be below 2660 gpm. In order to adjust flow of one RCFC it is necessary adjust and re-balance flow to the other three RCFCs. The throttle valves were repositioned to achieve a flow rate of greater than 2660 gpm on each RCFC based on the installed flow instrumentation. At this time it is believed that the flow rates were inadvertently adjusted below the TS minimum flow for the 1A, 1B, and 1C RCFCs due to the installed flow rate indicators reading inaccurately.
On August 19,2004, the flow rates to all four RCFCs were adjusted to greater than 2660 gpm using the ultrasonic flow instrumentation. In addition, a successful thermal performance test on the Unit lA �RCFC was completed on August 19 2004.
The lA, 1B, and 1C RCFCs had SX flow rates below the TS value of 2660 gpm from April 20, 2004 until August 18, 2004 (i.e., 119 days). This is a period longer than the allowed 7 days by Technical Specifications. Consequently, this is a reportable to the NRC in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications.
C.�Cause of Event:
The cause for this event was inaccurate indication of SX flow rate through the RCFC's. The root cause of the inaccurate indication is currently indeterminate. The installed Annubar flow measurement device is a multiple tubed probe that has holes on both the upstream and downstream sides to measure differential pressure.
(KABYR_DOCS\_LERS2003Iers1454-2003-003-00.doc) .
ti LICENSEE EVENT REPORT (LER) estimate to the information and Records Management Branch (1-6 f33), U.S.
Paperwork Reduction Project (3150-0104), Office Of Management And Budget, Washington, DC 20503. If an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the Information collection.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Byron Station, Unit 1 STN 0500454 NUMBER NUMBER (If more space Is required, use additional copies of NRC Form 366A)(17) Failure mechanisms for the Annubar device are: plugging or fouling of the probe holes, air entrainment inside theprobeor instrument sensing lines, failure of the weld that divides the high pressure side from the low pressure side, failuFF5f the flow iridicator and flow anomalies-due to-improper design implementation. Further actions will attempt to determine the actual cause of the failure.
Three potential contributing causes were identified:
Failure to fully review lesson learned documents from similar issues at Braidwood Station involving their RCFCs flow measurement devices.
The SX supply header flow was not identified as a parameter that could be trended in the system monitoring plan to identify degraded flow conditions in the RCFC's.
Lack of guidance in monthly RCFC flow verification surveillance procedure to document as-left throttle valve positions resulted in a missed opportunity to identify the instrumentation problem.
D. Safety Analysis:
Two containment cooling trains, in addition to two containment spray trains, provide containment atmosphere cooling to limit post accident pressure and temperature in containment to less than design values.
An engineering evaluation is in progress assessing the safety significance of the low flow condition to � the 1A,1B,.andJC RCFCs for..the119day_period. _Preliminary results indicate that both trains of containment cooling could have performed their design function with the as-found low flow condition.
The final results of the evaluation will be reported in a supplement to this report due April 15, 2005.
E. Corrective Actions:
A troubleshooting plan will be implemented during the Unit 1 Spring 2005 refuel outage to determine the cause of the inaccurate flow rate indications. The results of the troubleshooting plan and additional corrective actions based on the findings will be reported in a supplement to this report.
Pending the identification of a corrective action to prevent recurrence, an Adverse Condition Monitoring and Contingency Plan was developed to measure the Unit 1 individual RCFC flow with ultrasonic flow instrumentation during the monthly surveillance and to monitor the total containment cooling trains RCFC flow on a weekly basis for one month.
(KABYR_DOCS J.ERS120031ers1454-2003-033-00.doe) NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (7-2001) EXPIRES 07/31/2004 collection request 50 hrs. Reported lessons learned are incorporated into the licensing process and fed back to industry. Forward comments regarding burden LICENSEE EVENT REPORT (LER) estimate to the information and Records Management Branch (t-6 f33), U.S.
Paperwork Reduction Project (3150-0104), Office Of Management And Budget, Washington, DC 20503. If an Information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Byron Station, Unit 1 STN 0500454 (If more space Is required, use additional copies of NRC Form 366A)(17) The Unit 2 RCFC SX flow indicators were verified to be reading-a-ccurately-Usifig ultrasonic flow instrumentation and will continue to be verified with ultrasonic flow instrumentation until the root cause is determined.
The interim adverse condition monitoring plan will ensure proper flow rates to the RCFC's pending the following permanent procedure changes and root cause determination:
The monthly RCFC flow surveillance will be revised to record throttle valve as found and as left valve positions and to require notification of the system engineer when re-throttling is necessary.
The quarterly SX ASME surveillance will be revised to provide criteria for the minimum allowed train SX flow rate value.
The system monitoring plan for the SX system will be revised to monitor and trend SX supply header flow data recorded during the quarterly ASME surveillances.
F. Previous Occurrences:
None
G. Component Failure Data:
Manufacturer Nomenclature Model Dieterich Standard Corp. Annubar Flow Measuring Device FTM-75 (KBYR_DOCSLLER
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05000348/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2004-001 | Inadvertent Actuation of ECCS and EDGs While in Refueling Mode | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2004-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2004-001 | Failure To Comply With Technical Specification 3 .7 .5 .1, Control Room Emergency Ventilation System | | 05000301/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000313/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000285/LER-2004-001 | Failure To Perform A Leakage Test Due To Lack Of Understanding of Penetration Design | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000271/LER-2004-001 | Main Steam Isolation Valve Leakage Exceeds a Technical Specification Leakage Rate Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2004-001 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000318/LER-2004-001 | . Reactor Trip Due to Low Steam Generator Water Level After Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000289/LER-2004-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-001 | | | 05000247/LER-2004-001 | Manual Reactor Trip Due to Oscillating Feedwater Flow and Steam Generator Level with Flow Perturbations Caused by a Degraded Feed Water Regulating Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000244/LER-2004-001 | Gaps in the Control Room Emergency Zone Boundary | | 05000255/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000461/LER-2004-001 | Clinton Power Station 05000461 1 OF 4 | | 05000414/LER-2004-001 | relPowere Vice President A Duke Energy Company Duke Power Catawba Nuclear Station 4800 Concord Rd. / CNO1VP York, SC 29745-9635 803 831 4251 803 831 3221 fax November 9, 2004
U. S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, DC 20555-0001
SUBJECT: Duke Energy Corporation
Catawba Nuclear Station Unit 2
Docket No. 50-414
Licensee Event Report 414/04-001 Revision 0
Reactor Coolant System Pressure Boundary Leakage
Due to Small Cracks Found in Steam Generator
Channel Head Bowl Drain Line on 2C & 2D Steam
Generators
Attached please find Licensee Event Report 414/04-001
Revision 0, entitled "Reactor Coolant System Pressure
Boundary Leakage Due to Small Cracks Found in.Steam
Generator Channel Head Bowl Drain Line on 2C & 2D Steam
Generators."
This Licensee Event Report does not contain any regulatory
commitments. Questions regarding this Licensee Event Report
should be directed to R. D. Hart at (803) 831-3622.
Sincerely,
Dhiaa Jamil
Attachment
www.dukepower.corn 00- U.S. Nuclear Reguldhory Commission
November 9, 2004
Page 2
XC: W.D. Travers
U.S. Nuclear Regulatory Commission
Regional Administrator, Region II
Atlanta Federal Center
61 Forsyth St., SW, Suite 23T85
Atlanta, GA 30303
E.F. Guthrie
Senior Resident Inspector (CNS)
U.S. Nuclear Regulatory Commission
Catawba Nuclear Station
S.E. Peters (addressee only)
NRC Project Manager (CNS)
U.S. Nuclear Regulatory Commission
One White Flint North, Mail Stop 10-B3
11555 Rockville Pike
Rockville, MD 20852-2738
NRC FORM 366� U.S. NUCLEAR REGULATORY APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004)� COMMISSION Estimated burden per response to comply with this mandatory collection request 50
hours. Reported lessons learned are Incorporated Into the licensing process and fed back
to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy
Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, WashinMon, DC 2055
LICENSEE EN/ENT REPORT (LER) 0001, or by Internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104). Office of Management(See reverse for required number of and Budget, Washington, DC 20503. If a means used to impose an Information col ectiond( inverse �for each block) does not display a currently valid OMB control number, the NRC may not conduct or sponsor. and a person Is not required to respond o. the Information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 050- 00414 1 OF�6 4. TITLE Reactor Coolant System Pressure Boundary Leakage Due to Small Cracks Found in
Steam Generator Channel Head Bowl Drain Line on 2C & 2D Steam Generators | | 05000368/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2004-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2004-001 | Gas Accumulation in Centrifugal Charging Pump Suction Piping | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000395/LER-2004-001 | Reactor Trip Due to Valve Failure During Forced Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000390/LER-2004-001 | Automatic Reactor Trip Due to a Invalid Turbine Trip Signal (P-4) | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2004-001 | Auxiliary Feedwater System in prohibited condition due to inadequate procedure. | | 05000454/LER-2004-001 | Exelent
Exelon Generation Company, LLCRwww.exeloncorp.com NuclearByron Station 4450 North German Church Road Byron, IL 61010-9794 October 17, 2004 LTR: BYRON 2004-0111 File: 2.01.0700 United States Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Subject:RLicensee Event Report (LER) 454-2004-001-00, "Reactor Containment Fan Coolers Flow Rates Below Technical Specification Requirements Due to Inaccurate Flow Indication" Byron Station, Unit 1
Facility Operating License No. NPF-37
NRC Docket No. STN 50-454
Enclosed is an LER involving the August 17, 2004, event involving low flow conditions discovered in Unit 1 Reactor Containment Fan Coolers for a time period longer than allowed by the Technical Specifications. This event is reportable to the NRC in accordance with 10CFR 50.73 (a)(2)(i)(B), as a condition prohibited by Technical Specifications. Should you have any questions concerning this matter, please contact Mr. William Grundmann, Regulatory Assurance. Manager, at (815) 234-5441, extension 2800. Respectfully, Stephen E. Kuczynski Site Vice President Byron Nuclear Generating Station Attachment LER 454-2004-001-00 cc:RRegional Administrator, Region III, NRC NRC Senior Resident Inspector— Byron Station NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7.2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T.6 E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail toLICENSEE EVENT REPORT (LER) *I@ nrc.gov, and to the Desk Officer, Office of Informabon and Regulatory Affairs, NEOB:10202 (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose information collection does not display a currently valid OMB control number, the NRC may not _ conduct or sponsor, and a person is not required to respond to, the information collection. 1 rand ITV NAUP o natuerr An warn q par= . Byron Station, Unit 1 0500454 1 OF 5 4. Reactor Containment Fan Coolers Flow Rates Below Technical Specifications Requirements Due to Inaccurate Flow Indication | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2004-001 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000336/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2004-002 | Dresden Nuclear Power Station Unit 2 05000237 1 of 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000244/LER-2004-002 | Consolidated Rod Storage Canister Placed in Incorrect Storage Location | | 05000530/LER-2004-002 | Main Turbine Control System Malfunction Results in Automatic Reactor Trip on Low DNBR | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000305/LER-2004-002 | | | 05000247/LER-2004-002 | Manual Reactor Trip Due to Decreasing 23 Steam Generator Level Caused by Feedwater Regulating Valve Closure Due to a De-energized Solenoid Operated Valve from Wiring Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000414/LER-2004-002 | Manual Reactor Trip Initiated Due to Control Rods from Shutdown Bank D Dropping into the Core | | 05000251/LER-2004-002 | AAA | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv)(b) | 05000397/LER-2004-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000346/LER-2004-002 | Reactor Trip During Reactor Trip Breaker Testing Due To Fuse Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2004-002 | Emergency Diesel Generator Start and Load Due to Momentary Fault on Incoming Feed | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000269/LER-2004-002 | eif Powere RON A. JONES Vice President A Duke Energy Company Oconee Nuclear Site Duke Power ONO1VP / 7800 Rochester Highway Seneca, SC 29672 864 885 3158 864 885 3564 fax September 9, 2004
U.S. Nuclear Regulatory Commission
Document Control Desk
Washington, D.C. 20555
Subject: Oconee Nuclear Station
Docket Nos. 50-269,-270, -287
Licensee Event Report 269/2004-02, Revision 1
Problem Investigation Process No.: 0-04-2808
Gentlemen:
Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached
is Licensee Event Report 269/2004-02, Revision 1, regarding
a Main Steam Line Break mitigation design/analysis
deficiency which could result in the main and startup
feedwater control valves being technically inoperable for
mitigation of some steam line break scenarios.
This report is being submitted to supplement Revision 0
submitted July 6, 2004. At that time the root cause
investigation and an analysis of the consequences of
potentially exceeding the Environment Qualification (EQ)
envelope curve were still in progress.
This event is being reported in accordance with 10 CFR
50.73 (a)(2)(i)(B) as a condition prohibited by Technical
Specifications, 50.73(a)(2)(ii)(B) as an Unanalyzed
Condition, and 50.73(a)(2)(V)(D) as a potential loss of
safety function for Accident Mitigation. This event is
considered to be of no significance with respect to the
health and safety of the public.
www.dukepower.corn Document Control Desk
Date: September 9, 2004
Page 2
Attachment: Licensee Event Report 269/2004-02, Revision 1
cc: Mr. William D. Travers
Administrator, Region II
U.S. Nuclear Regulatory Commission
61 Forsyth Street, S. W., Suite 23T85
Atlanta, GA 30303
Mr. L. N. Olshan
Project Manager
U.S. Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Washington, D.C. 20555
Mr. M. C. Shannon
NRC Senior Resident Inspector
Oconee Nuclear Station
INPO (via E-mail)
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7-2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T-6 E6), U.S. Nuclear Regulatory Commission, Washington. DCLICENSEE EVENT REPORT (LER) 20555-0001, or by Internet e-mail to bpi @nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management and(See reverse for required number of Budget, Washington, DC 20503. If a means used to impose information collection doesdigits/characters for each block) not display a currently valid OMB control number, the NRC may not conduct or sponsor, and,1 nnmnn lc not rent Owl to tocnnni-I to the intnrmatinn rntlentinn 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Oconee Nuclear Station, Unit 1 050-81 OF 0269 11 4. TITLE Main Steam Line Break Mitigation Design/Analysis Deficiency | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000313/LER-2004-002 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000271/LER-2004-002 | Special Nuclear Material Inventory Location Discrepancy | | 05000285/LER-2004-002 | Inoperable Diesel Generator for 28 Days Due to Blown Fuse During Shutdown | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2004-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000311/LER-2004-002 | Failure To Comply With Technical Specifications During Reactor Protection Instrument Calibration . | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2004-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-002 | | | 05000302/LER-2004-002 | Emergency Diesel Generator Inoperable Due To Fuel Oil Header Outlet Check Valve Leaking Past Seat | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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