02-25-2004 | On January 16, 2004, with Watts Bar Nuclear Plant Unit 1 at 100 percent power, an automatic turbine trip occurred in response to a invalid trip signal (P-4), which then caused an automatic reactor trip because reactor power was above 50 percent power (P-9). The auxiliary feedwater system started as designed.
Surveillance Instruction 1-SI-99-10-B, "31 Day Functional Test of SSPS Train B and Reactor Trip Breaker B," Revision 22, was in progress when an instrument mechanic inserted test leads to take a voltage reading across the P-4 contacts without realizing that the multi-test meter was in the ohms reading position.
The result of the volt-ohm meter being in the ohm position was to create a current path equivalent to P-4 contact closure which energized Train B turbine trip bus.
The root cause of this event was determined to be a failure of the involved individuals to follow expectations to "stop" when unexpected conditions occurred. A contributor to the event was improper use of test leads for connection to multi-test meters.
Corrective actions included: 1) appropriate personnel action, 2) requiring an additional management observer to be present during the future test performances, 3) providing lessons learned and reinforcing expectations to site personnel on the use of human performance error reduction tools and appropriate test equipment, 4) and placing affected procedures on administrative hold until precautions are added. |
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FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3) 05000 390 2004 2 -� � 001 -�� 000 � of 6
I. PLANT CONDITION(S)
On January 16, 2004, at approximately 1138 Eastern Standard Time, Unit 1 was in Mode 1, steady state operation at 100 percent power. The Reactor Coolant System (RCS) (Energy Industry Identification System (EDS) Code AB) pressure was 2235 psig and RCS Tavg was 588 degrees F.
II. DESCRIPTION OF EVENT
A. Event
On January 16, 2004, with Watts Bar Nuclear Plant Unit 1 at 100 percent power, an automatic turbine (ENS Code TRB) trip occurred in response to a invalid turbine trip signal (P-4), which then caused an automatic reactor (EllS Code RCT) trip because reactor power was above 50 percent power (P-9). The auxiliary feedwater system (EIIS Code BA) started as designed. The invalid trip signal resulted from the introduction of a external circuit which created a current path equivalent to P-4 contact closure.
Surveillance Instruction 1-SI-99-10-B, "31 Day Functional Test of SSPS Train B and Reactor Trip Breaker B," Revision 22, was in progress. The test had progressed through Section 7.0, "Post Performance Activities," Step 24. The test director instructed the Instrument Mechanics (IMs) located in the Reactor Protection System (RPS) (EIIS Code JC) motor generator (MG) Set (EIIS Code MG) Room to perform Steps 24a and 24b, then call him back. The IMs proceeded at Step 24a which is to verify the position of the RPS Trip Breaker 8, P.4 contact, using DC voltage measurements. One IM held the volt ohm meter (Triplett) while the second IM plugged the test leads into test points TB4, Terminals 1 and 2. The IMs did not obtain the expected 240 to 290 volts DC. At that point, they changed the volt-ohm meter to ohms. The IM using the test leads then realized one of the test leads had fallen out of the volt-ohm meter. The IM reinserted the test lead and again attempted to take a voltage reading. The volt-ohm meter was most probably in ohms since neither IM recalls switching the volt-ohm meter to volts prior to inserting the test lead. The result of the volt-ohm meter being in the ohm position was to create a current path equivalent to P-4 contact closure which energized Train B turbine trip bus.
B. Inoperable Structures, Components, or Systems that Contributed to the Event There were no inoperable systems that contributed to this event.
C. Dates and Approximate Times of Major Occurrences:
Time� Event 0903� Authorized performance of 1-SI-99-10-B, "31 Day Functional Test SSPS Train B and Reactor Trip Breaker (RTB) B.
0954� Entered the following Limiting Conditions for Operations (LCOs): LCO 3.3.1, Condition P; LCO 3.3.2, Condition C; LCO 3.3.6, Condition B; LCO 3.3.7, Condition A; LCO 3.3.8, Condition A.
1004� Entered LCO 3.3.1, Condition 0 - one RTB maybe bypassed for 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.
1138� Reactor Trip/Turbine Trip.
1140� Transition from E0-0, "Reactor Trip or Safety Injection," to ES-0.1, "Reactor Trip Response.
FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3) 05000 YEAR SEQUENTIAL Watts Bar Nuclear Plant, Unit 1 390 2004 -�� 001 -�� 000 i
D. Other Systems or Secondary Functions Affected:
There were no other systems affected other than equipment required for plant shutdown.
E. Method of Discovery:
The operators were first alerted of the event by the annunciation in the control room.
F.Operator Actions:
Operations crew performance for this Reactor/Turbine Trip was satisfactory. At the time of the trip, the Shift Manager, Unit Supervisor, and three Board Operators were in the control room. The operating crew commenced implementation of E-0, "Reactor Trip or Safety Injection." Progress through E-0 and transition to ES-0.1, "Reactor Trip Response" was as expected.
Progress through ES-0.1 was as expected.� Auxiliary feedwater system throttling was required to limit RCS cooldown and low pressurizer level. AUOs in the field implemented A01-17, "Turbine Trip," in a timely manner.
G.Safety System Responses:
Plant safety systems operated as designed.
Ill. CAUSE OF THE EVENT
A. Immediate Cause:
The immediate cause of the trip was the placement of multi-meter test leads across the P-4 contacts with the meter set to read ohms instead of volts.
B. Root Cause:
The root cause of this event was determined to be a failure of the involved individuals to follow expectations to "stop" when unexpected conditions occurred. Without realizing the test lead had pulled loose, the IMs immediately went into the "troubleshooting mode" when the expected voltage was not obtained, by repositioning the meter to read ohms in a effort to determine if the contact was closed. When they discovered that the lead was disconnected, one of the IMs reinserted the test lead and again attempted to take a voltage reading apparently without repositioning the meter back to read voltage. The result of the meter being in the ohms position was to create a current path equivalent to P-4 contact closure which energized Train B turbine trip bus.
FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3) 05000 390 2004 4 -00 001 -00 000
C. Contributing Factors
Contributing factor was an accepted improper use of test leads for connection to multi-test meters.
IV. ANALYSIS OF THE EVENT
The principal plant safety systems operated as designed. The investigation of the cause of the trip focused on the performance of the SSPS Reactor Trip Breaker Surveillance Testing and the voltmeter application. With WBN Unit 1 at 100 percent power, the monthly functional test of the B-train Solid State Protection System (SSPS) (EIIS Code JE) and Reactor Trip Breaker B (RTB) was in progress when an automatic plant trip occurred due to an invalid turbine trip signal. At the time of the trip, two instrument mechanics (IMs) were attempting to verify that RTB's P-4 auxiliary contacts were open, as indicated by 240-290 VDC across the contacts. The P-4 contacts of each reactor trip (scram) breaker are closed when the breaker is closed to generate a turbine trip signal.
To accomplish this task, IM-A held the multi-meter (Triplett), while IM-B plugged the test leads into the specified test points in the back of RTB's cubicle. Based on interview, when the multi-meter indicated 0.0 VDC, the IMs Instinctively" went into the troubleshooting mode, wherein they changed the multi-meter to measure ohms to see if the 0.0 VDC was due to the P-4 contacts actually being closed. After changing the multi-meter to read ohms, IM-B then noticed one of the test leads had fallen out of the multi-meter. The test lead was reinserted, and IM-B again attempted to take a voltage reading. At this time, the multi-meter was most probably selected for measuring ohms, since neither IM recalls switching the multi-meter to volts prior to reinserting the test lead. The result of the multi-meter being in the ohm position would be to create a current path equivalent to P-4 contact closure, thereby energizing the B-train turbine trip bus and tripping the turbine. An automatic reactor trip occurred since power was above 50 percent (P-9). This is supported by the absence of "first out" alarms other than those indicating turbine and reactor trips had occurred, and there were no other alarms or indications of any equipment problems.
This event is compared to the LOSS OF EXTERNAL ELECTRICAL LOAD AND/OR TURBINE TRIP as described in Final Safety Analysis Report (FSAR) Section 15.2.7. The complete loss of load/turbine trip from full power is examined to show the adequacy of the pressure relieving devices and also to demonstrate protection from the departure from nucleate boiling (DNB). This plant trip was less challenging than and bounded by the event described in the FSAR. The following plant conditions were bounded by the event described in the FSAR:
1. Reactor power was at 100% and less than the analysis value of 100.6%.
2. The anticipatory reactor trip occurred on turbine trip versus the reactor protection system trip setpoints.
3.Reactor control was in automaticversus manual assumed in the FSAR.
4. Steam dumps operated as designed. The FSAR design basis does not credit the operation of the steam dump system or steam generator power operated relief valves (SG-PORVs) (EIIS Code SGN).
5. Station Power was not lost during the event.
FACILITY NAME (1)� _ DOCKET LER NUMBER (6) PAGE (3) 05000 YEAR SEQUENTIAL Watts Bar Nuclear Plant, Unit 1 390 2004 5 -�� 001 -�� 000 � of 6 The reactor trip occurred as designed from a turbine trip. The plant response remained within the FSAR boundary analysis. The main condenser steam dump valves opened per design and as a result it was not necessary for the SG-PORVs to operate. Pressurizer level and pressure did not increase to challenge the pressurizer PORVs and safeties to limit RCS pressure. RCS pressure and loop average temperatures decreased during the transient rather than increasing as predicted by the conservative FSAR assumptions and the DNBR was not challenged. The differences between the FSAR and the plant event are associated with the conservatism assumed in the FSAR analysis and the benign nature of the actual plant event which was quickly brought to a stable condition.
Therefore, there was no safety significance to this event. The plant responded as designed to the initiating condition.
V. ASSESSMENT OF SAFETY CONSEQUENCES
Based on the discussion in Section IV above, there was no safety significance to this event.
VI. CORRECTIVE ACTIONS
A Immediate Corrective Actions The following actions and those being evaluated in Item B below are tracked under TVA's Corrective Action Program and therefore are not considered to be regulatory commitments. The immediate corrective measures developed to address the above cause of the trip included:
1.Appropriate personnel action was taken for the individuals involved.
2. Standdown meetings were conducted with the appropriate plant personnel on the use of correct Measuring and Testing Equipment (M&TE) leads and self checking practices.
3. Lessons learned from the event were provided to site personnel describing the use of appropriate test equipment, self checking and peer checking expectations.
4. Management observers were required to be present when using volt ohmmeters during the performance of 1-51-99-10A, "31 Day functional Test of SSPS Train A and Reactor Trip Breaker A," and 1-SI-99-10-B, "31 Day Functional Test of SSPS Train B and Reactor Trip breaker B," and 1-SI-99-4-A, "Trip Actuating Device Operation Test of Reactor Trip P4 ESFAS Interlock Train A," and 1-SI-99-4-B, "Trip Actuating Device Operation Test of Reactor Trip P-4 ESFAS Interlock Train B.
5. Procedures, 1-SI-99-10-A&B were placed on Administrative Hold until the revisions can be made to provide additional guidance/precautions.
FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3) 05000 YEAR SEQUENTIAL REVISION 6�of 6 Watts Bar Nuclear Plant, Unit 1 390 2004 -��001 -��000
B. Corrective Actions to Prevent Recurrence
Long term items that are being evaluated include:
1. Revising 1-SI-99-10A and -10B to place appropriate precautions at the affected steps.
2. Inspecting shops, toolrooms, and training center to identify and correct similar tool/equipment issues.
3. Developing and conducting training on management observer expectations.
4. Reviewing lessons learned from this event with all WBN Curriculum Review Committees.
VII. ADDITIONAL INFORMATION
A Failed Components:
There were no failed components which caused this event.
B. Previous LERs on Similar Events:
A review of previous WBN LERs indicated that there had been a number of plant trips but none attributed to the placement of test leads across P.4 contacts that caused a plant trip.
C. Additional Information:
None.
D.Safety System Functional Failure Consideration:
- This event is not considered a safety system functional failure in accordance with NEI 99-02 in that the principal plant safety systems operated as designed. Therefore, the functional capability of the overall system was not jeopardized.
- E. Loss Of Normal Heat Removal Consideration:
- This event is not considered a scram with loss of normal heat removal.
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05000348/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2004-001 | Inadvertent Actuation of ECCS and EDGs While in Refueling Mode | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2004-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2004-001 | Failure To Comply With Technical Specification 3 .7 .5 .1, Control Room Emergency Ventilation System | | 05000301/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000313/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000285/LER-2004-001 | Failure To Perform A Leakage Test Due To Lack Of Understanding of Penetration Design | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000271/LER-2004-001 | Main Steam Isolation Valve Leakage Exceeds a Technical Specification Leakage Rate Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2004-001 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000318/LER-2004-001 | . Reactor Trip Due to Low Steam Generator Water Level After Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000289/LER-2004-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-001 | | | 05000247/LER-2004-001 | Manual Reactor Trip Due to Oscillating Feedwater Flow and Steam Generator Level with Flow Perturbations Caused by a Degraded Feed Water Regulating Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000244/LER-2004-001 | Gaps in the Control Room Emergency Zone Boundary | | 05000255/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000461/LER-2004-001 | Clinton Power Station 05000461 1 OF 4 | | 05000414/LER-2004-001 | relPowere Vice President A Duke Energy Company Duke Power Catawba Nuclear Station 4800 Concord Rd. / CNO1VP York, SC 29745-9635 803 831 4251 803 831 3221 fax November 9, 2004
U. S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, DC 20555-0001
SUBJECT: Duke Energy Corporation
Catawba Nuclear Station Unit 2
Docket No. 50-414
Licensee Event Report 414/04-001 Revision 0
Reactor Coolant System Pressure Boundary Leakage
Due to Small Cracks Found in Steam Generator
Channel Head Bowl Drain Line on 2C & 2D Steam
Generators
Attached please find Licensee Event Report 414/04-001
Revision 0, entitled "Reactor Coolant System Pressure
Boundary Leakage Due to Small Cracks Found in.Steam
Generator Channel Head Bowl Drain Line on 2C & 2D Steam
Generators."
This Licensee Event Report does not contain any regulatory
commitments. Questions regarding this Licensee Event Report
should be directed to R. D. Hart at (803) 831-3622.
Sincerely,
Dhiaa Jamil
Attachment
www.dukepower.corn 00- U.S. Nuclear Reguldhory Commission
November 9, 2004
Page 2
XC: W.D. Travers
U.S. Nuclear Regulatory Commission
Regional Administrator, Region II
Atlanta Federal Center
61 Forsyth St., SW, Suite 23T85
Atlanta, GA 30303
E.F. Guthrie
Senior Resident Inspector (CNS)
U.S. Nuclear Regulatory Commission
Catawba Nuclear Station
S.E. Peters (addressee only)
NRC Project Manager (CNS)
U.S. Nuclear Regulatory Commission
One White Flint North, Mail Stop 10-B3
11555 Rockville Pike
Rockville, MD 20852-2738
NRC FORM 366� U.S. NUCLEAR REGULATORY APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004)� COMMISSION Estimated burden per response to comply with this mandatory collection request 50
hours. Reported lessons learned are Incorporated Into the licensing process and fed back
to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy
Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, WashinMon, DC 2055
LICENSEE EN/ENT REPORT (LER) 0001, or by Internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104). Office of Management(See reverse for required number of and Budget, Washington, DC 20503. If a means used to impose an Information col ectiond( inverse �for each block) does not display a currently valid OMB control number, the NRC may not conduct or sponsor. and a person Is not required to respond o. the Information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 050- 00414 1 OF�6 4. TITLE Reactor Coolant System Pressure Boundary Leakage Due to Small Cracks Found in
Steam Generator Channel Head Bowl Drain Line on 2C & 2D Steam Generators | | 05000368/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2004-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2004-001 | Gas Accumulation in Centrifugal Charging Pump Suction Piping | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000395/LER-2004-001 | Reactor Trip Due to Valve Failure During Forced Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000390/LER-2004-001 | Automatic Reactor Trip Due to a Invalid Turbine Trip Signal (P-4) | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2004-001 | Auxiliary Feedwater System in prohibited condition due to inadequate procedure. | | 05000454/LER-2004-001 | Exelent
Exelon Generation Company, LLCRwww.exeloncorp.com NuclearByron Station 4450 North German Church Road Byron, IL 61010-9794 October 17, 2004 LTR: BYRON 2004-0111 File: 2.01.0700 United States Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Subject:RLicensee Event Report (LER) 454-2004-001-00, "Reactor Containment Fan Coolers Flow Rates Below Technical Specification Requirements Due to Inaccurate Flow Indication" Byron Station, Unit 1
Facility Operating License No. NPF-37
NRC Docket No. STN 50-454
Enclosed is an LER involving the August 17, 2004, event involving low flow conditions discovered in Unit 1 Reactor Containment Fan Coolers for a time period longer than allowed by the Technical Specifications. This event is reportable to the NRC in accordance with 10CFR 50.73 (a)(2)(i)(B), as a condition prohibited by Technical Specifications. Should you have any questions concerning this matter, please contact Mr. William Grundmann, Regulatory Assurance. Manager, at (815) 234-5441, extension 2800. Respectfully, Stephen E. Kuczynski Site Vice President Byron Nuclear Generating Station Attachment LER 454-2004-001-00 cc:RRegional Administrator, Region III, NRC NRC Senior Resident Inspector— Byron Station NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7.2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T.6 E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail toLICENSEE EVENT REPORT (LER) *I@ nrc.gov, and to the Desk Officer, Office of Informabon and Regulatory Affairs, NEOB:10202 (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose information collection does not display a currently valid OMB control number, the NRC may not _ conduct or sponsor, and a person is not required to respond to, the information collection. 1 rand ITV NAUP o natuerr An warn q par= . Byron Station, Unit 1 0500454 1 OF 5 4. Reactor Containment Fan Coolers Flow Rates Below Technical Specifications Requirements Due to Inaccurate Flow Indication | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2004-001 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000336/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2004-002 | Dresden Nuclear Power Station Unit 2 05000237 1 of 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000244/LER-2004-002 | Consolidated Rod Storage Canister Placed in Incorrect Storage Location | | 05000530/LER-2004-002 | Main Turbine Control System Malfunction Results in Automatic Reactor Trip on Low DNBR | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000305/LER-2004-002 | | | 05000247/LER-2004-002 | Manual Reactor Trip Due to Decreasing 23 Steam Generator Level Caused by Feedwater Regulating Valve Closure Due to a De-energized Solenoid Operated Valve from Wiring Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000414/LER-2004-002 | Manual Reactor Trip Initiated Due to Control Rods from Shutdown Bank D Dropping into the Core | | 05000251/LER-2004-002 | AAA | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv)(b) | 05000397/LER-2004-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000346/LER-2004-002 | Reactor Trip During Reactor Trip Breaker Testing Due To Fuse Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2004-002 | Emergency Diesel Generator Start and Load Due to Momentary Fault on Incoming Feed | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000269/LER-2004-002 | eif Powere RON A. JONES Vice President A Duke Energy Company Oconee Nuclear Site Duke Power ONO1VP / 7800 Rochester Highway Seneca, SC 29672 864 885 3158 864 885 3564 fax September 9, 2004
U.S. Nuclear Regulatory Commission
Document Control Desk
Washington, D.C. 20555
Subject: Oconee Nuclear Station
Docket Nos. 50-269,-270, -287
Licensee Event Report 269/2004-02, Revision 1
Problem Investigation Process No.: 0-04-2808
Gentlemen:
Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached
is Licensee Event Report 269/2004-02, Revision 1, regarding
a Main Steam Line Break mitigation design/analysis
deficiency which could result in the main and startup
feedwater control valves being technically inoperable for
mitigation of some steam line break scenarios.
This report is being submitted to supplement Revision 0
submitted July 6, 2004. At that time the root cause
investigation and an analysis of the consequences of
potentially exceeding the Environment Qualification (EQ)
envelope curve were still in progress.
This event is being reported in accordance with 10 CFR
50.73 (a)(2)(i)(B) as a condition prohibited by Technical
Specifications, 50.73(a)(2)(ii)(B) as an Unanalyzed
Condition, and 50.73(a)(2)(V)(D) as a potential loss of
safety function for Accident Mitigation. This event is
considered to be of no significance with respect to the
health and safety of the public.
www.dukepower.corn Document Control Desk
Date: September 9, 2004
Page 2
Attachment: Licensee Event Report 269/2004-02, Revision 1
cc: Mr. William D. Travers
Administrator, Region II
U.S. Nuclear Regulatory Commission
61 Forsyth Street, S. W., Suite 23T85
Atlanta, GA 30303
Mr. L. N. Olshan
Project Manager
U.S. Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Washington, D.C. 20555
Mr. M. C. Shannon
NRC Senior Resident Inspector
Oconee Nuclear Station
INPO (via E-mail)
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7-2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T-6 E6), U.S. Nuclear Regulatory Commission, Washington. DCLICENSEE EVENT REPORT (LER) 20555-0001, or by Internet e-mail to bpi @nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management and(See reverse for required number of Budget, Washington, DC 20503. If a means used to impose information collection doesdigits/characters for each block) not display a currently valid OMB control number, the NRC may not conduct or sponsor, and,1 nnmnn lc not rent Owl to tocnnni-I to the intnrmatinn rntlentinn 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Oconee Nuclear Station, Unit 1 050-81 OF 0269 11 4. TITLE Main Steam Line Break Mitigation Design/Analysis Deficiency | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000313/LER-2004-002 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000271/LER-2004-002 | Special Nuclear Material Inventory Location Discrepancy | | 05000285/LER-2004-002 | Inoperable Diesel Generator for 28 Days Due to Blown Fuse During Shutdown | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2004-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000311/LER-2004-002 | Failure To Comply With Technical Specifications During Reactor Protection Instrument Calibration . | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2004-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-002 | | | 05000302/LER-2004-002 | Emergency Diesel Generator Inoperable Due To Fuel Oil Header Outlet Check Valve Leaking Past Seat | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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