On March 30, 2004, while at power, VCSNS personnel were performing a reactor building inspection to identify the source of reactor coolant system unidentified leakage that was within Technical Specification (TS) limits. At 1129 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.295845e-4 months <br />, a pressure boundary leak was identified at the seal injection line nozzle weld to reactor coolant pump "C" ( RCP C).
Pursuant to TS 3.4.6.2, Action a., VCSNS commenced a controlled reactor shutdown at 1410 on March 30, 2004.
During the shutdown, the main turbine experienced higher than normal vibration. At 1517, the turbine was manually tripped at approximately 43% reactor power. Subsequent to the manual turbine trip, feedwater regulating valve IFV-498 failed in the closed position while in automatic with a full open demand signal. The reactor automatically tripped at 1521 due to lo-lo level in the "C" steam generator.
All control rods fully inserted and all safety systems responded normally. Both motor driven emergency feedwater pumps started as required. The plant stabilized in mode 3.
The cause of failure for IFV-498 is attributed to service induced fretting on the positioner pilot valve stem. All positioners on the feedwater regulating valves have been replaced and will be scheduled for future periodic replacement at appropriate intervals. The leakage for RCP C seal injection nozzle has been determined to be a weld failure caused by low-amplitude high cycle fatigue. A modification replaced the line with a new nozzle design with enhanced pipe supports. |
LER-2004-001, Reactor Trip Due to Valve Failure During Forced ShutdownDocket Number |
Event date: |
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Report date: |
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Reporting criterion: |
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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Initial Reporting |
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ENS 40628 |
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded |
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3952004001R00 - NRC Website |
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PLANT IDENTIFICATION
Westinghouse - Pressurized Water Reactor
EQUIPMENT IDENTIFICATION
Reactor Coolant Pump "C" Seal Injection Nozzle Feedwater Regulating Valve IFV-498
IDENTIFICATION OF EVENT
On March 30, 2004, while at power, VCSNS personnel were performing a reactor building inspection to identify the source of reactor coolant system unidentified leakage that was within Technical Specification (TS) limits. At 1129 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.295845e-4 months <br />, a pressure boundary leak was identified at the seal injection line nozzle weld to reactor coolant pump "C". Pursuant to TS 3.4.6.2, Action a., VCSNS commenced a controlled reactor shutdown at 1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br /> on March 30, 2004.
During the shutdown, the main turbine experienced higher than normal vibration. At 1517 hours0.0176 days <br />0.421 hours <br />0.00251 weeks <br />5.772185e-4 months <br />, the turbine was manually tripped at approximately 43% reactor power. Subsequent to the manual turbine trip, feedwater regulating valve IFV-498 failed in the closed position while in automatic with a full open demand signal. The reactor automatically tripped at 1521 hours0.0176 days <br />0.423 hours <br />0.00251 weeks <br />5.787405e-4 months <br /> due to lo-lo level in the "C" steam generator with reactor power at approximately 9%.
This event was reported under Event Notification EN#40628 at 1738 hours0.0201 days <br />0.483 hours <br />0.00287 weeks <br />6.61309e-4 months <br /> on March 30, 2004 in accordance with 10CFR50.72(b)(2)(i), 50.72(b)(2)(iv)(B), 50.72(b)(3)(ii)(A), and 50.72(b)(3)(iv)(A).
EVENT DATE
03/30/04
REPORT DATE
05/27/04
CONDITIONS PRIOR TO EVENT
Mode 1 , 100% Power - 1129 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.295845e-4 months <br /> through 1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br /> - Pressure Boundary LeakfTS Shutdown Initiation Mode 1, 9% Power - 1521 hours0.0176 days <br />0.423 hours <br />0.00251 weeks <br />5.787405e-4 months <br /> - Reactor Trip
DESCRIPTION OF EVENT
On March 30, 2004, while at power, VCSNS personnel were performing a reactor building inspection to identify the source of reactor coolant system unidentified leakage that was within Technical Specification (TS) limits. At 1129 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.295845e-4 months <br />, a pressure boundary leak was identified at the seal injection line nozzle weld to reactor coolant pump "C" (RCP C). This nozzle weld was part of the repair performed for a previous leak at this location during refueling outage 14 (RF14) [Reference LER 2003-004]. Pursuant to TS 3.4.6.2, Action a., VCSNS commenced a controlled reactor shutdown at 1410 hours0.0163 days <br />0.392 hours <br />0.00233 weeks <br />5.36505e-4 months <br /> on March 30, 2004. The average rate of the shutdown was 1% per minute.
Main Turbine Bearing 5 vibration started to increase at approximately 70% reactor power and continued to rise as the shutdown progressed. At 40% reactor power, Bearing 5 vibration had increased to 10 mils, and the operators manually tripped the Main Turbine from the control room. A reactor trip was not required since reactor power was below the P-9 setpoint of 50%. The manual turbine trip occurred at 1517.
Because of the turbine trip, Steam Dump Banks 1 and 2 opened to the condenser and Control Bank D was automatically inserted from 120 steps to 60 steps. The Steam Generator Water Level Control System modulated the Feedwater Regulating Valves to maintain Steam Generator water level. Feedwater response was normal after the turbine trip, but IFV-498 appeared to go closed at 1518 as indicated by decreasing Feedwater flow to Steam Generator C. The lower limit switch for IFV-498 gave a closed indication to the plant computer shortly after 1519. Steam Generator C level decreased to the Low-Low Level Reactor Trip setpoint of 35%, and an automatic reactor trip occurred at 1521.
All control rods fully inserted and all safety systems responded normally. Both motor driven emergency feedwater pumps started as required. The plant stabilized in mode 3.
Condition Evaluation Report C-04-0879 was generated to address the RCP C seal injection line leakage, evaluate the cause, and develop effective corrective actions. This report was reclassified as a non-conforming condition and transferred to Non-Conformance Notice NCN 04-0879.
Condition Evaluation Report C-04-0884 was generated to address the failure of IFV-498 and provide the corrective actions necessary to preclude reoccurrence.
CAUSE OF EVENT
RCP C nozzle weld failure was caused by high-cycle, low amplitude vibration induced fatigue. The weld repair performed on the RCP C seal injection line during RF14 created a hot tear starter crack, which significantly reduced the time required for crack initiation, resulting in a rapid tearing of the weld once fatigue loading was applied. Fatigue loading on "C" seal injection nozzle was more severe than on the eight other RCP nozzles based on measurements of line vibratory displacements and natural frequencies. A RF 15 modification was planned to reduce the high cycle, low amplitude vibration induced fatigue loadings on the C RCP.
CAUSE OF EVENT (Cont'd) The cause of the failure of IFV-498 to operate properly is attributed to the pilot valve stem of the Bailey AV-1 positioner sticking due to fretting. The sticking of the stem prevented control air from opening the valve upon demand.
ANALYSIS OF EVENT
The "C" RCP seal injection nozzle exhibited a through wall leak on March 30, 2004 which resulted in a forced shutdown of the plant. This same nozzle had previously leaked in 1987 and again in 1994. These leaks were resolved by local weld repairs as allowed by the ASME Code to restore the welds. A third leak occurred in October of 2003 during RF 14 that resulted in the complete replacement of this nozzle and weldment.
SCE&G performed detailed inspections of the existing nozzle to support root cause evaluation. After all visual examinations, measurements and vibration testing had been completed, a metallurgical sample of the complete weld was removed for testing. The sample was transported to the hot cell metallurgical laboratory of BWXT Services, Inc. of Lynchburg, Virginia for analysis. The purpose of this testing was to determine the nature and physical characteristics of the failure.
The test results clearly indicate that the failure of the nozzle weld was entirely low-amplitude high cycle fatigue.
The weldment was found to be sound. Three factors appeared to dominate the fatigue process as follows:
1. The geometry at the weld root creates an inherent stress riser that intensifies the cyclic vibrational loads at the weld root.
2. The end of the nozzle impacted the bottom of the socket over a portion of the circumference. Also at this location the inner surface of the pipe was displaced inward towards the pipe axis. This action likely was a result of the shrinkage forces during welding coupled with the forces generated by the bottomed-out condition. This produces residual tensile forces at the root notch that opens the root notch and produces a crack starter (hot tear).
3. The crack starter effectively eliminated the crack initiation portion of fatigue life.
These three factors concurrent with the pump vibration produced sufficient stress to drive the crack completely through wall over a distance of about 0.44 inches in only 3 months. Fatigue propagation was entirely transgranular and there was no evidence of corrosion processes having influenced the fatigue propagation.
During a controlled shut down to repair the seal injection leakage on "C" Reactor Coolant Pump (RCP), the "C" Feed Water (FW) Regulating Valve, IFV-498, closed after a manual turbine trip and resulted in a reactor trip on Lo-Lo Steam Generator (SG) level. Initial troubleshooting by VCSNS Instrumentation & Control personnel did not reveal any failed components that lead to the FW Regulating Valve closure.
ANALYSIS OF EVENT (Cont'd) A Failure Modes Analysis (FMA) was initiated to determine the potential valve failure mechanisms, to obtain the necessary evidence to support/refute each potential mechanism and to provide the corrective actions necessary to preclude reoccurrence. The FMA narrowed the potential failure mechanisms to the Bailey AV-1 positioner.
A recent external Operating Experience (OE) Report 0E17276 identified industry issues with the pilot valves in these positioners. Quality issues in the manufacturing of the pilot valve were found to produce service induced fretting on the pilot valve stem. The fretting between the stem guides and the body can cause the stem to stick, which in turn can cause erratic valve operation including oscillations, valve failure to respond to demand and/or uncontrolled movement of the valve.
Inspection of the VCSNS pilot valve stem guides showed service induced fretting on the guides removed from the IFV-498 positioner. The cause of the failure is attributed to the pilot valve stem sticking due to fretting, thus preventing control air from opening the valve upon demand.
CORRECTIVE ACTIONS
The Station has taken the following corrective actions:
This section summarizes the corrective actions performed on the RCP C seal injection line under NCN 04-0879 and ECR 50547 to address the failure mechanisms identified and ensure safe restart.
Completed Corrective Actions
- Removed and replaced nozzle and weld, including all fillet, partial penetration, build-up, and heat affected zone weld material.
- Installed new nozzle design on "C" RCP seal injection nozzle using SCH160 pipe and a larger weld.
- Use of 1/8" pullback on new nozzle fit-up, followed by verification of pullback during and after welding using boroscope.
- PT of each weld pass (which exceeds the ASME code requirements) and an informational post-weld ultrasonic ID examination of the weld.
- Installed a new rigid pipe support on "C" seal injection line just upstream of nozzle flange that is supported by the RCP main flange. Pipe stress analysis predicts that the additional support will increase the resonant frequency and reduce vibration loading on the nozzle.
- Installed a new spring can pipe support on "C" seal injection line.
Post-modification measurement of "C" seal injection line natural frequency and vibration performed at Mode 3 during startup verified that displacements had been significantly reduced and natural frequency shifted away from pump driving frequency.
CORRECTIVE ACTIONS (Coned) Corrective Actions identified from the FMA for I FV-498 are as follows:
Completed Corrective Actions
- Installed new positioners on IFV-478, 488, 498 that include the quality improvements made at Bailey after January 30, 2004. Note these improvements are only in inspection/assembly not actual hardware improvements or changes.
- Inspected and replaced the pilot assemblies on the remaining valves that are equipped with a Bailey AV-1 positioner. Affected valves are as follows:
I FV02006-0-MB �I PV02000-0-MS HCV00936-0-SI I FV02016-0-MB I PV02010-0-MS LCV01003-0-WL I FV02106-0-MB �I PV02020-0-MS
- Inspected warehouse stock for all Bailey AV-1 model positioners for quality. Two problems were identified. The roller bearing in one positioner was found seized and one positioner had a leaky diaphragm.
- Established a PM to periodically inspect and/or replace the in service pilot valve assemblies.
Long Term Corrective Actions
- Develop a receiving and inspection procedure to inspect the Bailey AV-1 positioner to insure quality.
- Evaluate the need to replace the AV-1 positioner with a different brand.
- Establish a link between OE and the PM Program in the Equipment Reliability Improvement Program (ERIP) and evaluate component level assignments within Engineering.
VCS Engineering has concluded that the corrective actions to replace the Bailey AV-1 Positioners on the Feed Water Regulating Valves combined with the inspection and replacement of all other installed Bailey AV 1 pilot valve assemblies is adequate to operate the plant safely and reliably until RF-15.
PRIOR OCCURRENCES
There are no prior occurrences of failure for the feedwater regulating valves and/or their positioners.
This is a repetitive failure of the RCP seal injection nozzle. There were events in 1987 (LER 1987-013, June 25, 1987), 1994 (LER 1994-006, January 3, 1995), and 2003 (LER 2003-004, December 17, 2003) where the plant experienced pressure boundary leakage from the reactor coolant system from this same weld area.
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05000348/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2004-001 | Inadvertent Actuation of ECCS and EDGs While in Refueling Mode | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2004-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2004-001 | Failure To Comply With Technical Specification 3 .7 .5 .1, Control Room Emergency Ventilation System | | 05000301/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000313/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000285/LER-2004-001 | Failure To Perform A Leakage Test Due To Lack Of Understanding of Penetration Design | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000271/LER-2004-001 | Main Steam Isolation Valve Leakage Exceeds a Technical Specification Leakage Rate Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2004-001 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000318/LER-2004-001 | . Reactor Trip Due to Low Steam Generator Water Level After Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000289/LER-2004-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-001 | | | 05000247/LER-2004-001 | Manual Reactor Trip Due to Oscillating Feedwater Flow and Steam Generator Level with Flow Perturbations Caused by a Degraded Feed Water Regulating Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000244/LER-2004-001 | Gaps in the Control Room Emergency Zone Boundary | | 05000255/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000461/LER-2004-001 | Clinton Power Station 05000461 1 OF 4 | | 05000414/LER-2004-001 | relPowere Vice President A Duke Energy Company Duke Power Catawba Nuclear Station 4800 Concord Rd. / CNO1VP York, SC 29745-9635 803 831 4251 803 831 3221 fax November 9, 2004
U. S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, DC 20555-0001
SUBJECT: Duke Energy Corporation
Catawba Nuclear Station Unit 2
Docket No. 50-414
Licensee Event Report 414/04-001 Revision 0
Reactor Coolant System Pressure Boundary Leakage
Due to Small Cracks Found in Steam Generator
Channel Head Bowl Drain Line on 2C & 2D Steam
Generators
Attached please find Licensee Event Report 414/04-001
Revision 0, entitled "Reactor Coolant System Pressure
Boundary Leakage Due to Small Cracks Found in.Steam
Generator Channel Head Bowl Drain Line on 2C & 2D Steam
Generators."
This Licensee Event Report does not contain any regulatory
commitments. Questions regarding this Licensee Event Report
should be directed to R. D. Hart at (803) 831-3622.
Sincerely,
Dhiaa Jamil
Attachment
www.dukepower.corn 00- U.S. Nuclear Reguldhory Commission
November 9, 2004
Page 2
XC: W.D. Travers
U.S. Nuclear Regulatory Commission
Regional Administrator, Region II
Atlanta Federal Center
61 Forsyth St., SW, Suite 23T85
Atlanta, GA 30303
E.F. Guthrie
Senior Resident Inspector (CNS)
U.S. Nuclear Regulatory Commission
Catawba Nuclear Station
S.E. Peters (addressee only)
NRC Project Manager (CNS)
U.S. Nuclear Regulatory Commission
One White Flint North, Mail Stop 10-B3
11555 Rockville Pike
Rockville, MD 20852-2738
NRC FORM 366� U.S. NUCLEAR REGULATORY APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004)� COMMISSION Estimated burden per response to comply with this mandatory collection request 50
hours. Reported lessons learned are Incorporated Into the licensing process and fed back
to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy
Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, WashinMon, DC 2055
LICENSEE EN/ENT REPORT (LER) 0001, or by Internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104). Office of Management(See reverse for required number of and Budget, Washington, DC 20503. If a means used to impose an Information col ectiond( inverse �for each block) does not display a currently valid OMB control number, the NRC may not conduct or sponsor. and a person Is not required to respond o. the Information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 050- 00414 1 OF�6 4. TITLE Reactor Coolant System Pressure Boundary Leakage Due to Small Cracks Found in
Steam Generator Channel Head Bowl Drain Line on 2C & 2D Steam Generators | | 05000368/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2004-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2004-001 | Gas Accumulation in Centrifugal Charging Pump Suction Piping | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000395/LER-2004-001 | Reactor Trip Due to Valve Failure During Forced Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000390/LER-2004-001 | Automatic Reactor Trip Due to a Invalid Turbine Trip Signal (P-4) | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2004-001 | Auxiliary Feedwater System in prohibited condition due to inadequate procedure. | | 05000454/LER-2004-001 | Exelent
Exelon Generation Company, LLCRwww.exeloncorp.com NuclearByron Station 4450 North German Church Road Byron, IL 61010-9794 October 17, 2004 LTR: BYRON 2004-0111 File: 2.01.0700 United States Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Subject:RLicensee Event Report (LER) 454-2004-001-00, "Reactor Containment Fan Coolers Flow Rates Below Technical Specification Requirements Due to Inaccurate Flow Indication" Byron Station, Unit 1
Facility Operating License No. NPF-37
NRC Docket No. STN 50-454
Enclosed is an LER involving the August 17, 2004, event involving low flow conditions discovered in Unit 1 Reactor Containment Fan Coolers for a time period longer than allowed by the Technical Specifications. This event is reportable to the NRC in accordance with 10CFR 50.73 (a)(2)(i)(B), as a condition prohibited by Technical Specifications. Should you have any questions concerning this matter, please contact Mr. William Grundmann, Regulatory Assurance. Manager, at (815) 234-5441, extension 2800. Respectfully, Stephen E. Kuczynski Site Vice President Byron Nuclear Generating Station Attachment LER 454-2004-001-00 cc:RRegional Administrator, Region III, NRC NRC Senior Resident Inspector— Byron Station NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7.2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T.6 E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail toLICENSEE EVENT REPORT (LER) *I@ nrc.gov, and to the Desk Officer, Office of Informabon and Regulatory Affairs, NEOB:10202 (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose information collection does not display a currently valid OMB control number, the NRC may not _ conduct or sponsor, and a person is not required to respond to, the information collection. 1 rand ITV NAUP o natuerr An warn q par= . Byron Station, Unit 1 0500454 1 OF 5 4. Reactor Containment Fan Coolers Flow Rates Below Technical Specifications Requirements Due to Inaccurate Flow Indication | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2004-001 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000336/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2004-002 | Dresden Nuclear Power Station Unit 2 05000237 1 of 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000244/LER-2004-002 | Consolidated Rod Storage Canister Placed in Incorrect Storage Location | | 05000530/LER-2004-002 | Main Turbine Control System Malfunction Results in Automatic Reactor Trip on Low DNBR | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000305/LER-2004-002 | | | 05000247/LER-2004-002 | Manual Reactor Trip Due to Decreasing 23 Steam Generator Level Caused by Feedwater Regulating Valve Closure Due to a De-energized Solenoid Operated Valve from Wiring Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000414/LER-2004-002 | Manual Reactor Trip Initiated Due to Control Rods from Shutdown Bank D Dropping into the Core | | 05000251/LER-2004-002 | AAA | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv)(b) | 05000397/LER-2004-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000346/LER-2004-002 | Reactor Trip During Reactor Trip Breaker Testing Due To Fuse Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2004-002 | Emergency Diesel Generator Start and Load Due to Momentary Fault on Incoming Feed | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000269/LER-2004-002 | eif Powere RON A. JONES Vice President A Duke Energy Company Oconee Nuclear Site Duke Power ONO1VP / 7800 Rochester Highway Seneca, SC 29672 864 885 3158 864 885 3564 fax September 9, 2004
U.S. Nuclear Regulatory Commission
Document Control Desk
Washington, D.C. 20555
Subject: Oconee Nuclear Station
Docket Nos. 50-269,-270, -287
Licensee Event Report 269/2004-02, Revision 1
Problem Investigation Process No.: 0-04-2808
Gentlemen:
Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached
is Licensee Event Report 269/2004-02, Revision 1, regarding
a Main Steam Line Break mitigation design/analysis
deficiency which could result in the main and startup
feedwater control valves being technically inoperable for
mitigation of some steam line break scenarios.
This report is being submitted to supplement Revision 0
submitted July 6, 2004. At that time the root cause
investigation and an analysis of the consequences of
potentially exceeding the Environment Qualification (EQ)
envelope curve were still in progress.
This event is being reported in accordance with 10 CFR
50.73 (a)(2)(i)(B) as a condition prohibited by Technical
Specifications, 50.73(a)(2)(ii)(B) as an Unanalyzed
Condition, and 50.73(a)(2)(V)(D) as a potential loss of
safety function for Accident Mitigation. This event is
considered to be of no significance with respect to the
health and safety of the public.
www.dukepower.corn Document Control Desk
Date: September 9, 2004
Page 2
Attachment: Licensee Event Report 269/2004-02, Revision 1
cc: Mr. William D. Travers
Administrator, Region II
U.S. Nuclear Regulatory Commission
61 Forsyth Street, S. W., Suite 23T85
Atlanta, GA 30303
Mr. L. N. Olshan
Project Manager
U.S. Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Washington, D.C. 20555
Mr. M. C. Shannon
NRC Senior Resident Inspector
Oconee Nuclear Station
INPO (via E-mail)
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7-2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T-6 E6), U.S. Nuclear Regulatory Commission, Washington. DCLICENSEE EVENT REPORT (LER) 20555-0001, or by Internet e-mail to bpi @nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management and(See reverse for required number of Budget, Washington, DC 20503. If a means used to impose information collection doesdigits/characters for each block) not display a currently valid OMB control number, the NRC may not conduct or sponsor, and,1 nnmnn lc not rent Owl to tocnnni-I to the intnrmatinn rntlentinn 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Oconee Nuclear Station, Unit 1 050-81 OF 0269 11 4. TITLE Main Steam Line Break Mitigation Design/Analysis Deficiency | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000313/LER-2004-002 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000271/LER-2004-002 | Special Nuclear Material Inventory Location Discrepancy | | 05000285/LER-2004-002 | Inoperable Diesel Generator for 28 Days Due to Blown Fuse During Shutdown | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2004-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000311/LER-2004-002 | Failure To Comply With Technical Specifications During Reactor Protection Instrument Calibration . | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2004-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-002 | | | 05000302/LER-2004-002 | Emergency Diesel Generator Inoperable Due To Fuel Oil Header Outlet Check Valve Leaking Past Seat | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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