05000414/LER-1995-001, :on 950221,automatic Reactor/Turbine Trip Occurred.Caused by Degraded Optical Isolator within Control for Msiv.Testing & Replacing Degraded Isolators in Control Cicuitry for MSIV

From kanterella
(Redirected from 05000414/LER-1995-001)
Jump to navigation Jump to search
:on 950221,automatic Reactor/Turbine Trip Occurred.Caused by Degraded Optical Isolator within Control for Msiv.Testing & Replacing Degraded Isolators in Control Cicuitry for MSIV
ML20081J937
Person / Time
Site: Catawba Duke Energy icon.png
Issue date: 03/16/1995
From: Kimball D, Rehn D
DUKE POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-95-001, LER-95-1, NUDOCS 9503280278
Download: ML20081J937 (8)


LER-1995-001, on 950221,automatic Reactor/Turbine Trip Occurred.Caused by Degraded Optical Isolator within Control for Msiv.Testing & Replacing Degraded Isolators in Control Cicuitry for MSIV
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv), System Actuation

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(x)
4141995001R00 - NRC Website

text

a.

O

' DukeIbwer Cornpa:y (C11)8314000 Catawba NuclearStation 4800 ConcordRoad York, SC29745 DUKEPOWER March 16,1995 Document Control Desk U. S. Nuclear Regulatory Commission Washington, D.C. 20555 i

Subject:

Catawba Nuclear Station Docket No. 50-414 j

LER 414/95-001 Gentlemen:

Attached is Licensee Event Report 414/95-001 concerning REACTOR TRIP DUE -TO CLOSURE OF A MAIN STEAM ISOLATION VALVE.

i This event was considered to be of no significance with respect to the health and safety of the public.

Very truly our,

I i

D. L. Rehn xc:

Mr. S. D. Ebneter Marsh & McLennan Nuclear Regional Administrator, Region II 1166 Avenue of the Americas U. S. Nuclear Regulatory Commission New-York, NY 10036-2774 101 Marietta Street, NW, Suite 2900 Atlanta, GA 30323 Mr. R. E. Martin INPO Records Center U. S. Nuclear Regulatory Commission Suite 1500 Office of Nuclear Reactor Regulation 1100 Circle 75 Parkway Washington, D.C. 20555 Atlanta, GA 30339 Mr. R. J. Freudenberger NRC Resident Inspector Catawba Nuclear Station 280033 9503280278 950316 PDR ADOCK 05000414 i

S PDR n.ms w mm ma a

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY oMB NO. 3150-0104 (Sta)

EXPIRES ':/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER) 5 "E*ReGA E'ORDE#SEMO""*i lNrs u Ts F

AND RECORDS MANAGEMENT BRANCH (UNOB 7714). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 205550001. AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF (See reverse for requireo number of digits / characters for each block)

MANAGEMrNT AND BUDGET, WASHINGTON, DC 20503.

FACiUTV NAME (1)

DOCKET NUMBER (2)

PAGE (3)

Catawba Nuclear Station, Unit 2 05000414 10F 7 E t4)

Reactor Trip Due to Closure of a Main Steam Isolation Valve l

EVENT DATE (5)

LER NUMBER (6 REPORT NUMBER (7)

OTHER FACILITIES INVOLVED (8)

F ACLITY NAME DOCKET NUMBEH MONTH DAY YEAR YEA R MONTH DAY YEAR N/A 05000 FACIUTY NAME DOCKET NUMBER 02 21 95 95

~ 001 00 03 16 95 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more) (11)

MODE (9) 1 20.402(td 20 405(c)

X 50.73(a)(2)(iv) 73.71(b)

POWER 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)

LEVEL (10) 100 20 405(a)(1)0i) 50 36(c)(2) 50.73(a)(2)(vil)

OTHER 20.405(a)(1)(ni) 50.73(a)(2)0) 50.73(a)(2)(viii)(A) ppe@n Abwact 20 405(a)(1)0v) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) oI 20 405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER pnctuae Area Code)

D. P. Kimball, Safety Review Group Manager (803)831-3743 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

CAUSE

SYSTE M COMPONENT MANUFACTURER

CAUSE

SYSTEM COMPONENT MANUFACTURER p

p F

SB OB E169 Y

SUPPLEMENTAL REPORT EXPECTED (14)

EXPECTED MONTH DAY YEAR vEs SUDMISSION E

pf yes, compwe E KPECTED SUHM SSION DATEl DATE (15)

ABSTRACT (Umit to 1400 spaces, i e., approximately 15 single spaced typewntten lines) (16)

On February 21,1995, at 2153 hours0.0249 days <br />0.598 hours <br />0.00356 weeks <br />8.192165e-4 months <br />, Unit 2 was in Mode 1, Power Operation at 100%, when an automatic Reactor /rurbine Trip occurmd on Over Power Differential Temperature after the Main Steam Isolation Valve (MSIV) for "B" Steam Generator (S/G) closed unexpectedly. Following the trip, a Main Feedwater System isolation occurred as a result of a reactor trip with low Reactor Coolant (NC) System average temperature (T-ave).

i Auxiliary Feedwater (CA) System motor driven and turbine driven pumps autostarted as expected due to 10-10 l

steam generator levels. Following reset of the CA System, NC T-ave increased above no-load setpoint allowing the Steam Dump System to actuate which resulted in S/G level decreasing below 10-10 level setpoint causing a second CA System turbine driven pump autostart. Engineering is evaluating transient data and will provide Operations with recommendations concerning maintaining S/G levels following transients. The MSIV closure was caused by a degraded optical isolator within the control circuitry for the MSIV. Corrective Actions included testing and replacing degraded isolators in the control circuitry for all MSIVs and in critical applications in other systems for both units. The degraded optical isolators were returned to the vendor for testing. Engineering is evaluating reliability improvements of optical isolators, and developing a trending program for optical isolators.

All safety systems responded as designed to shutdown the Reactor and maintain it in a safe shutdown condition.

NnC rORM = (s-923

=

REQUIRED NUMBER OF DIGITS / CHARACTERS FOR EACN BLOCK BLOCK NUMBER OF E

NUMBER DIGITS / CHARACTERS 1

UP TO 46 FACILITY NAME 8 TOTAL DOCKET NUMBER 3 IN ADDITION TO 05000 3

VARIES PAGE NUMBER 4

UP TO 76 TITLE 6 TOTAL EVENT DATE 2 PER BLOCK 7 TOTAL

~

OR W R LER NUMBER 6

3 FOR SEQUENTIAL NUMBER 2 FOR REVISION NUMBER 6 TOTAL REPORT DATE 7

2 PER BLOCK UP TO 18 - FACILITY NAME OmER FACILmES MOWED 0

8 TOTAL - DOCKET NUMBER 3 IN ADDITION TO 05000 9

1 OPERATING MODE 10 3

POWER LEVEL REQUIREMENTS OF 10 CFR II CHECK BOX THAT APPLIES UP TO 50 FOR NAME LICENSEE CONTACT I2 14 FOR TELEPHONE CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARIES SUPPLEMENTAL REPORT EXPECTED I#

CHECK BOX THAT APPLIES 6 TOTAL EXPECTED SUBMISSION DATE 15 2 PER BLOCK l

IdlO FORM 366A U.S. NUCLEAR REGULATORY COMMISSIChi APPROVED BY OMB NO. 3150-0104 e e2)

EXPIRES 5/31/95 ESTtMATED BURDEN PER RESPONSE TO COMPLY WITH THIS i.lCENSEE EVENT REPORT (LER)

Z T^

EG % 'f EROE,f E S O Z8 d % E M'

TEXT CONTINUATION ME8"gu^$"gCC"aT84'A*,iS8 "Z c

o7 TKI PAPERWORK REDUCTION PROJECT (3150 0104). OFFICE OF i

M ANAGEMENT AND BUDGET, WASHINGTON. DC 20503 j

FACIUTY NAME (1)

DOCKET NUMBER (2)

LER NUMBER (t)

PAGE (3)

SEQUENhA.

REv40N

{

YEAR l Catawba Nuclear Station, Unit 2 05000 414 2OF7 l

95

- 001 00 rw w,,.-.

o.. 7-.mn v,,

Main Steam Isolation Valves [ Ells:V) (MSIV) provide steam isolation for the Steam Generators [EIIS:HX] (S/Gs) during shutdown and accident conditions.

The Main Steam Vent to Atmosphere System [EIIS:VL] (SV) S/G safety valves provide over pressure protection for Main Steam System [EIIS:SB] (SM). There are five valves per steam line and provide 100% steam relief capacity.

The Main Feedwater [EIIS:SJ) (CF) system consists of two steam driven feedwater pumps [EIIS:PJ, two stages of high pressure feedwater heaters [EIIS:HTR] (A and B), piping [ Ells: PSP], valves, and instrumentation. Normally, both feedwater pumps will be operating with each pump handling half the feedwater flow. Downstream of the feedwater pumps, the feedwater passes through two stages of high pressure heaters to a final header where the temperature is equalized. The feedwater is then admitted to the steam generators through four steam generator i

feedwater lines, each of which contains a control valve and a flow nozzle [EIIS:NZL].

The purpose of the feedwater isolation signal is to initiate isolation of each steam generator and rapidly terminate j

feedwater flow and steam blowdown inside containment [EIIS:NH] following a main steam or feedwater line

)

break in containment, and to prevent overfilling the steam generators if for some reason the normal means of controlling steam generator level malfunctions. Feedwater isolation is activated by any one of the followir.g signals: safety injection, reactor trip plus low average reactor coolant temperature (T-ave less than 564 degrees F),

or Hi-Hi Steam Generator level. A feedwater isolation signal closes the Feedwater Isolation Valves, Feedwater Purge Valves, Feedwater Control Valves, Feedwater Control Bypass Valves, Feedwater Preheater Bypass Valves, and Feedwater Bypass Tempering Flow Valves.

The Auxiliary Feedwater [EIIS:BA] (CA) System assures sufficient feedwater supply to the steam generators in the event ofloss of the CF System, to remove primary coolant stored and residual core energy. The system is designed to start automatically in the event of loss of offsite electrical power, trip of both CF pumps, safety injection signal, or 10-10 steam generator water level; any of which may result in, coincide with, or be caused by a Reactor trip. In addition, the CA System will supply sufficient feedwater flow to maintain the Reactor [EIIS:RCT] at hot standby for two hours followed by cooldown of the Reactor Coolant [EIIS:AB] (NC) System to the temperature at which the Residual Heat Removal [EIIS:BP] (ND) System may be operated.

The Over Power Differential Temperature (OPDT) trip setpoint protects against excessive fuel centerline temperature. The OPDT is continuously calculated by analog circuitry for each loop and depends on the temperature in the loop and the neutron flux distribution in the Reactor.

The Reactor Protection System [ Ells:JC] (IPX) is (* signed to trip the Reactor or actuate appropriate safeguards equipment in time to prevent violating any plant safety limits. A Reactor Trip signal is generated when 2/4 NC system loops have exceeded their calculated OPDT setpoint.

NRC FORM 366415 92;

MC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 N

EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH TH:S

' LICENSEE EVENT REPORT (LER)

EMT*JMEGTSE*nDE"'*'EE "o %*,dRTTl TEXT CONTINUATION

^$uS*c5'"M $*oESENGT57E"5AYx*n7ED $

u THE PAPERWORK REDUCTION PROJECT (3150-0104J. OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC POS03-FACluTV NAME (1)

DOCKET NUMBER (2l L.ER NUMBER (4)

PAGE (3) d "lj SEQUENTiA;.

REvtSiON yggg NUMBER NUMBER Catawba Nuclear Station, Unit 2 05000 414 3 OF7 95

- 001 00 l

ten tu moa.aou.

r.w.a,a.. mow cap eunc nr.w; on

EVENT DESCRIPTION

February 21,1995 Unit 2 was in Mode i. Power Operation at 100% power.

i 2153:47 S/G "B" MSIV began going closed.

2153:49 S/G "B" MSIV was completely closed.

2153:55 Safety relief valves on "B" Main Steam Line opened to control pressure.

2153:59 An Automatic Reactor Trip occurred on Unit 2 due to two out of four NC System Loops exceeding OPDT setpoint. Main Turbine tripped as a result of the Reactor Trip.

2154:10 Safety relief valves on "B" Main Steam Line closed.

2154:13 CA System Motor Driven Pumps autostaned due to 10-10 level in two out of four l

channels on "B" S/G.

i 2154:15 Main Feedwater System isolation occurred due to Reactor Trip with low T-ave (below 564 degrees Fahrenheit).

2154:19 CA System Turbine Driven Pump autostarted due to 10-10 level in two out of four channels on "B" and "D" S/Gs.

2158:30 CA System was reset.

2210:48 Lo-Lo S/G signal for "A", "C", and "D" S/G cleared. CA Turbine Driven Pump was armed due to only one S/G being below S/G 10-10 setpoint.

2211 Steam Dump System actuated due to NC System T-ave increasing above no-load temperature setpoint. Steam Dump System actuation caused S/G levels to decrease.

2211:13 Second CA System Turbine Driven Pump autostart occurred due to 10-10 level in two out of four channels on "A" and "B" S/G.

t lliG WRC FORM ma pe2;

,U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES 5/31/95 ESTMATED BURDEN PER RESPONSE TO COMPLY WTH THis

' LICENSEE EVENT REPORT (LER)

$*MTEt5$'SEno"EN$$AT O

INF ION TEXT CONTINUATION

@M" S "o^EZ"' CNo"g*S'E8,"fgi" C

cM w

3 L*Me"Fa".'u=."2%.a72 "" '

raciurv nAue m oocuT avusta m un nuween m Pace <>>

p 6EQUENTIAL FLEVSON l

NUMBER NUMBER 05000 414 4OF7 Catawba Nuclear Station, Unit 2 tex, in aw, n c.,, r.e,.a. m..aaga, cop,.nr mc um, am o n 2212:30 CA System was reset.

2216 All S/G levels stable with Unit 2 in mode 3.

CONCLUSION The Reactor Trip was due to OPDT setpoints being exceeded as a result of the unexpected closure of MSIV for "B" S/G. The MSIV closure was caused by a degraded optical isolator within the control circuitry for the MSIV.

Engineering replaced the faulty optical isolator (E-max model number 175C156) and elected to conservatively replace all the relays and an additional optical isolator, of the same type, that could have caused the failure in the MSIV control cin'uit for "B" S/G. The remaining MSIV control circuits for Unit 2 were inspected to evaluate whether any of circuits contained degraded components. The inspection revealed that four additional optical isolators (E-max model number 175C156) were degraded. All of the degraded optical isolators were replaced and the new optical isolators were successfully tested. The degraded optical isolators were returned to the vendor for testing.

Engineering reviewed other critical circuits for Unit 2 systems [ Main Steam System [ Ells:SB] (SM), Main Feedwater System [ Ells:SJ) (CF), Condensate System [EIIS:KA] (CM), Nuclear Service Water System [EIIS:BI]

(RN), Auxiliary Feedwater System [EIIS:BA) (CA), Reactor Coolr.nt System [EIIS:AB] (NC), Chemical and Volume Control System [ElIS:CB] (NV), and Safety Injection System [EIIS:BQ] (NI)] that may utilize optical isolators in a control application that would result in a plant trip or a transient that would likely cause a trip. In the circuits reviewed, there were a total of 23 optical isolators identified in critical applications. The twenty-three isolators were tested and all were within the manufacturer speciications.

Engineering reviewed the failure history of E-max optical isolators model number 175C155,175C156, and 175C157. All of the degraded isolators that failed in the Unit 2 MSIV circuitry were model number 175C156. A search of optical isolators revealed model numbers 175C156 and 175C157 had a higher replacement rate when compared to other optical isolators at Catawba Nucleac Station (CNS), particularly in the Main Steam System and Main Feedwater System. Supplier of optical isolator mocid numbers 175C156 and 175C157 could not provide CNS with a predicted replacement rate. Both of these isolator models are digital isolators with AC inputs and DC outputs. Model number 175C155 is a digital isolator with a DC input with AC sutput. This model isolator showed a very low replacement rate.

Planned Corrective Actions include testing optical isolators in Unit 1 MSIV circuits, testing isolators in critical applications for critical circuits on Unit I systems (SM, CF, CM, RN, CA, NC, NV, NI), replacing degraded isolators, developing a Periodic Maintenance program for energized isolators (E-max model number 175C156 and 175C157) in critical applications, evaluating reliability improvements of optical isolators, and develop a trending program for optical isolators. The optical isolator failure is NPRDS reportable.

NAC FORM asaA 15 62;

NhC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB No. 3150-0104 rna)

EXPIRES 5/31/95 1

ESTIMATED BURDEN PER RESPONSE TO COMPLY Wf7H THIS I

' LICENSEE EVENT REPORT (LER)

C$uT J* OEG %'f 7j "'N E ATUo O idR%^2 TEXT CONTINUATION guRECgSuggsyTs e nssIS"E Eu eH e

w gor a

THE PAPERWORK REDUCTION PRCUECT (3150-0104). OFFICE OF i

MANAGEMENT AND BUDGET, WASHINGTON. DC 20503 F ACILITY NAME (1)

DOCKET NUMBER (2) tER NUMBER (4)

PAGE (3) j bEQUENitA; REVISION NUMBER NUMBER 05000 M '

Catawba Nuclear Station, Unit 2 95

- 001 00 TtxT or me

.w.

,.na.a m..aa.r.o,w ev., or mc io.m wi <m Following the Unit 2 trip, Operators reset the CA System and were maintaining S/G level at approximately forty percent by throttling flow to S/Gs. When NC T-ave increased above no-load setpoint, the Steam Dump System actuated bringing T-ave back to no-load setpoint. The Steam Dump System actuation caused S/G levels to decrease below lo-lo setpoints resulting in a second CA System Turbine Driven Pump autostart. The autostart occurred due to level in "A' and "D" S/G decreasing below lo-lo setpoint of 36.8 percent. Engineering is evaluating transient data and will provide Operations with recommendations concerning maintaining S/G levels following transients. Operations Management discussed the incident with operators and reviewed data conceming S/G levels that were being maintained during the transient. Management concluded that the difference in Unit 1 (17 percent) and Unit 2 (36.8 percent) S/G 10-10 level setpoints could have attributed to S/G levels being maintained close to Unit 2 lo-lo S/G setpoint. Operations training will develop training that will focus more attention on the difference in S/G 10-10 setpoints between Unit I and Unit 2. Engineering recommendations and Operator training will help reduce CA System autostarts due to lo-lo S/G levels after CA System is reset.

During this event, Control Room Operators (CROs) entered the conect emergency response procedures and performed the required steps to maintain the plant in a safe shutdown condition. All safety systems responded as designed.

A review of the Operating Experience Program for the twenty-four months prior to this event revealed a previous Unit 2 Reactor Trip due to closure of a MSIV. LER 414/94-006 involved a Unit 2 Reactor Trip when MSIV for "C" S/G closed unexpectedly due to a short circuit in a normally energized coil in a D26 Cutler Hammer relay.

Since these two 1 rips involved failure of different components, and the Corrective Actions for LER 414/94/-006 would not have prevented this trip, this event is considered not to be recurring.

CORRECTIVE ACTIONS

IMMEDIATE 1.)

CROs entered procedure EP/2/A/5000/E-0, Reactor Trip or Safety injection to verify the plant responded properly and to assess plant conditions.

2.)

CROs entered procedure EP/2/A/5000/ES-0.1, Reactor Trip Response, per EP/2/A/5000/E-0.

NRC FORV 366A ($ 92)

,u.S. NUCt. EAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 i

f5-92)

EXPlRES 5/31/95 ESTiMA4D BURDEN PER RESPONSE TO COMPLY WfTH THfS 1.lCENSEE EVENT REPORT (LER)

E$M7 5NEa %'S ERo"E E r7M d io O w E r'5" TEXT CONTINUATION Eu"E*CEuE"' "$", o"ro$"*E'$i S*> "N" w

L"in"*A"00luid? "J5L%"JO "" '

FACluTV NAME (1)

DOCKET NUMBER (2)

LIR NUMBER (s)

PAGE (3)

EEQUENT A, HEVISION ygg NUMBER NUMBER Catawba Nuclear Station, Unit 2 05000 414 6oF7 95

- 001 00 nm m.

.c.,,

w.a..- ~ n..,ac - m on SUBSEQUENT 1)

IAE and Engineering investigated why the MSIV unexpectedly closed. A degraded optical isolator was discovered and replaced. The relays and an additional optical isolator (model number 175C156) in the circuit were conservatively replaced even though they met manufacturers' specifications when tested. The replacement optical isolators and relays were successfully tested.

The work was performed under Work Order (W/O 95016298-01).

2.)

The remaining MSIV control circuits for Unit 2 were inspected for degraded components.

Degraded optical isolators were replaced and the replacements were successfully tested. The work was performed under Work Orders (95016755-01,95016759-01,95016976-01).

3.)

Testing was conducted on the degraded optical isolators that were removed from the Unit 2 MSIV circuits. Testing revealed a failure within the intemal circuit of the optical isolators.

4.)

Testing was performed on twenty-three optical isolators that were identified by Engineering to be in critical applications on Unit 2 systems (SM, CF, CM, RN, CA, NC, NV, NI). All of the optical isolators were within the manufacturers' specifications. The work was performed under Work Request (95011132).

5.)

Engineering reviewed failure history of E-max model number 175C155,175C156, and 175C157.

Model numbers 175C156 and 175C157 indicated a high replacement rate when compared to other optical isolators at CNS. Model number 175C155 indicated a low replacement rate.

6.)

Degraded optical isolators were retumed to the vendor for testing.

PLANNED 1.)

Test optical isolators in Unit 1 MSIV control circuits and in critical circuits for critical applications on Unit I systems (SM, CF, CM, RN, CA, NC, NV, NI). Replace degraded optical isolators and test the replacements.

2.)

Develop a PM program to periodically monitor E-max model number 175C156 and 175C157 energized optical isolators in critical applications.

3.)

Evaluate reliability improvements for critical control circuits that have E-max model numbers 175C156 and 175C157 optical isolators.

NRC FORM 3n6A (5 421

NiC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES 5/31/95 ESTeMATED BURDEN PER RESPONSE TO COMPLY W'TH THIS

' LICENSEE EVENT REPORT (LER) 5 "uMUeG8$'SERDE, E'uATE OT*E MOT 7 TEXT CONTINUATION

^$uMS "**%$8%Q*8 'A's'; Q,N E

C0uy o

THE PAPERWORK REDUCTION PRCUECT (3150-0104), OFFCE OF MANAGEMENT AND BJDGET. WASHINGTON. DC 20503.

F ACILITY NAME (1)

DOCKET NUMBER (2)

LEH NUMBER (6)

PAGE (3)

SLQUENTIA;.

REVISION YUR NUMBER NUMBER Catawba Nuclear Station, Unit 2 05000 414 7OF7 95

- 001 00 Tm w ma. n.c. a a.v,.a. a..aa,ma em, or u8C Fen my v r; 4.)

Develop a trending program to monitor the performance of optical isolators using the recent testing and measurements as the baseline data.

5.)

Engineering will evaluate transient data concerning S/G levels and will provide recommendations to Operations concerning maintaining S/G level following transients.

6.)

Operations training will develop training that will focus more attention on the difference in S/G 10-lo level setpoints between Unit I and Unit 2.

SAFETY ANALYSIS

1 1

This event was initiated due to an unexpected closure of a main steam isolation valve 2SM5 which resulted in a Reactos/ Turbine Trip on Overpower Differential Temperature. These events are bounded by the Safety Analysis documented in the FSAR Sections 15.2.4, Inadvertent Closure of Main Steam Isolation Valves, and 15.2.3, Turbine Trip.

Safety relief valves on Main Steam Line for "B" S/G opened to control pressure. CA system motor driven and turbine driven pumps autostarted due to 10-10 levels in "B" and "D" S/Gs. CF Isolation occurred due to Reactor trip with low NC system T-ave. Following reset of CA System, NC T-ave increased above no-load setpoint allowing Steam Dump System to actuate which resulted in S/G level decreasing below 10-10 level setpoint causing a second CA System turbine driven pump auto start. S/G levels returned to normal. NC System cooldown experienced during this event is bounded by the Safety Analysis in Section 15.1.5, Steam System Piping Failure.

During this event, all systems responded as designed to shutdown the reactor and maintain it in a safe shutdown condition. There y ere no unusual releases of radioactive material.

The health and safety of the public were not affected by this event.

NRC FORY 366A ($ 90