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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000395/LER-1993-0041993-08-30030 August 1993 LER 93-004-01:on 930629,missed Surveillance Occurred,Per TS 4.3.2.1,Table 4.3-2.2.b.Caused by Personnel Error in Documenting Test Discrepancy.Operations Personnel Took Part in Discussion of Importance of post-test.W/930830 Ltr 05000395/LER-1993-0031993-07-28028 July 1993 LER 93-003-00:on 930628,purge Sys Discovered Outside Provisions of Ts.Caused by Personnel Error.Operations Mgt Communicated Importance of Proper Procedural Usage & Stressed Usage Level requirements.W/930830 Ltr 05000395/LER-1984-024, Revised LER 84-024-01:on 840422 & 29,reactor Tripped Due to Low Main Turbine Shaft Oil Pump Discharge Pressure.Caused by Conservative Switch Settings & Loss of Suction on Motor Suction Pump.Switch Setpoint Will Be Changed1984-07-0202 July 1984 Revised LER 84-024-01:on 840422 & 29,reactor Tripped Due to Low Main Turbine Shaft Oil Pump Discharge Pressure.Caused by Conservative Switch Settings & Loss of Suction on Motor Suction Pump.Switch Setpoint Will Be Changed 05000395/LER-1984-013, Revised LER 84-013-01:on 840309,mod to Plant Integrated Fire & Security Sys Disabled Control Room Operator Ability to Receive Alarm Upon Actuation of Smoke Detectors in Zones Fff & Mmm of Intermediate Bldg1984-04-19019 April 1984 Revised LER 84-013-01:on 840309,mod to Plant Integrated Fire & Security Sys Disabled Control Room Operator Ability to Receive Alarm Upon Actuation of Smoke Detectors in Zones Fff & Mmm of Intermediate Bldg 05000395/LER-1983-100, Revised LER 83-100-01X-1:on 830831,PORV PCV-445A Declared Inoperable Due to Concern Re Possible Inadvertent Opening of Valve Upon Power Loss to Protective Cabinet 4.Caused by Design Error1984-01-27027 January 1984 Revised LER 83-100-01X-1:on 830831,PORV PCV-445A Declared Inoperable Due to Concern Re Possible Inadvertent Opening of Valve Upon Power Loss to Protective Cabinet 4.Caused by Design Error 05000395/LER-1983-060, /03L-0:on 831117,investigation Into Previously Submitted LER 83-060 Revealed Four Testable Components Not Tested on Quarterly Basis.Caused by Inadequate Procedure.Test Procedures Revised1983-12-16016 December 1983 /03L-0:on 831117,investigation Into Previously Submitted LER 83-060 Revealed Four Testable Components Not Tested on Quarterly Basis.Caused by Inadequate Procedure.Test Procedures Revised 05000395/LER-1983-001, Updated LER 83-001/01T-1:on 830119,three Refueling Water Storage Tank Level Transmitters Failed High.Caused by Transmitter Base Freezing.Transmitters Thawed.Insulated Encls & Addl Permanent Heat Trace Will Be Installed1983-02-22022 February 1983 Updated LER 83-001/01T-1:on 830119,three Refueling Water Storage Tank Level Transmitters Failed High.Caused by Transmitter Base Freezing.Transmitters Thawed.Insulated Encls & Addl Permanent Heat Trace Will Be Installed 1993-08-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D6401999-10-31031 October 1999 Rev 2 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0202, Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With ML20216J4191999-09-24024 September 1999 Part 21 Rept Re 990806 Abb K-Line Breaker Defect After Repair.Vendor Notified of Shunt Trip Wiring Problem & Agreed to Modify Procedure for Refurbishment of Breakers RC-99-0180, Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression1999-09-0808 September 1999 Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression RC-99-0183, Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With ML20211K6161999-08-31031 August 1999 Rev 2 to VC Summer Nuclear Station,Colr for Cycle 12, Dtd Aug 1999 RC-99-0168, Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed1999-08-19019 August 1999 Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed ML20210M7071999-07-31031 July 1999 Rev 1 to VC Summer Nuclear Station COLR for Cycle 12 ML20211C2201999-07-31031 July 1999 Rev 1 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0163, Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0137, Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0122, Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With ML20206H2971999-05-0505 May 1999 Part 21 Rept Re Common Mode Failure for magne-blast Breakers.Vc Summer Nuclear Station Utilizes These Breakers in Many Applications,Including 7.2-kV EDG Electrical Buses RC-99-0103, Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With ML20206K2421999-04-30030 April 1999 Rev 0 to COLR for Cycle 12 for Summer Nuclear Station RC-99-0087, Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory1999-04-15015 April 1999 Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory RC-99-0083, Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0063, Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced1999-03-26026 March 1999 Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced ML20196K5421999-03-22022 March 1999 Rev 2 to VC Summer Nuclear Station,Training Simulator Quadrennial Certification Rept,1996-99, Books 1 & 2. Page 2 of 2 Section 2.4.4 (Rev 2) of Incoming Submittal Were Not Included RC-99-0055, Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 9903121999-03-16016 March 1999 Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 990312 RC-99-0050, Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML20203F4511999-02-12012 February 1999 SER Finding Licensee Adequately Addressed GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves, for Virgil C Summer Nuclear Station ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20206R5241998-12-31031 December 1998 Santee Cooper 1998 Annual Rept RC-99-0052, Vsns 1998 Annual Operating Rept. with1998-12-31031 December 1998 Vsns 1998 Annual Operating Rept. with RC-99-0004, Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With ML20206R5191998-12-31031 December 1998 Scana Corp 1998 Annual Rept ML20198F4241998-12-18018 December 1998 Safety Evaluation Granting Relief Request for Approval to Repair ASME Code Class 3 Service Water Piping Flaws in Accordance with GL 90-05 for VC Summer Nuclear Station RC-98-0223, Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method1998-12-16016 December 1998 Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method RC-98-0222, Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With ML20155G4551998-11-0404 November 1998 Safety Evaluation Accepting Licensee Proposed Alternative to Use Code Case N-416-1 with Licensee Proposed Addl Exams RC-98-0208, Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With ML20207J5701998-10-31031 October 1998 Non-proprietary Rev 1 to WCAP-14955, Probabilistic & Economic Evaluation of Rv Closure Head Penetration Integrity for VC Summer Nuclear Plant ML20154Q9571998-10-21021 October 1998 SER Accepting Request Seeking Approval to Use Alternative Rules of ASME Code Case N-498-1 for Class 1,2 or 3 Sys ML20154K7901998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15101, Analysis of Capsule W from Sceg VC Summer Unit 1 Rv Radiation Surveillance Program RC-98-0184, Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With ML20154K8041998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15103, Evaluation of Pressurized Thermal Shock for VC Summer Unit 1 RC-98-0166, Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With ML20237A7181998-08-13013 August 1998 SER Accepting Util Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves RC-98-0153, Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0131, Monthly Operating Rept for June 1998 for VC Summer Nuclear Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for VC Summer Nuclear Station ML20248J0191998-06-0404 June 1998 Safety Evaluation Accepting Licensee Inservice Testing Program Interim Pump Relief Request Per 10CFR50.55a(a)(3) (II) RC-98-0113, Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0100, Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 1 ML20217G7411998-04-22022 April 1998 Rev 1 to VC Summer Nuclear Station COLR for Cycle 11 RC-98-0076, Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure1998-04-17017 April 1998 Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure RC-98-0084, Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 1 ML20212H1421998-03-0202 March 1998 Interim Part 21 Rept SSH 98-002 Re EG-B Unit That Was Sent to Power Control Svcs for Determination of Instability & Refurbishment of a Dg.Cause of Speed Oscillations Unknown. Completed Hot Bore Checks on Power Case 1999-09-08
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LER-2084-024, Revised LER 84-024-01:on 840422 & 29,reactor Tripped Due to Low Main Turbine Shaft Oil Pump Discharge Pressure.Caused by Conservative Switch Settings & Loss of Suction on Motor Suction Pump.Switch Setpoint Will Be Changed |
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- Apf*OVED Oase seO.3100-410s LICENSEE dVENT REPORT (LER) ;
00CEET soutWGR Q) PA4BE m PACILITY 80AAAE 14 ,
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71TLE 448 Main Turbine Trip - Reactor Trip EVENT DATE 151 LOR NURGER ($1 RSPORT DATE 17) OTMER PACILITIE9 INVOLVEO ISI MONTM OAY YEAR YEAR
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@O ; ; l A TRACT <v,,,R,,Am - ,.. nei On April 22, 1984, with reactor power at 12%, and on April 29, 1984, with reactor power at 11%, the reactor tripped due to a main turbine trip. Both main turbine trips occurred as a result of main turbine ,
l shaft oil pump low discharge pressure while rolling the main turbine up to 1800 rpm. The Reactor Protection System functioned properly on both events, and Engineering Safety Feature actuated as designed (i.e., ,
Emergency Feedwater Pump start on Low-Low Steam Generator Level). The l causes of these events were attributed to conservative switch settings ;
and loss of suction on the motor suction pump. l t
I Inspection of the motor suction pump and' check valve will be performed during the First Refueling outage. The procedure has been changed to delete the head correction on the pressure switch, and the pressure ,
switch setpoint will be changed during the First Refueling Outage.
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i NAC Ferse 3esA U S. NUCLEAR KEGULATO7Y COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTlWUATION mRovEo oMe No 3 iso-w f MPIRE5 8/31115 F ACILITY NAmet tu OOCKET NUMSER (21 LER NUMgER d6) PAGE(31
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0l1 0l 2 oF 0 l3 TEXT f# more ausse de escused was seMasant NAC Form JM4's)(17)
At approximately 0903, April 22, 1984, the reactor tripped fran 12% power due to a main turbine trip. While rolling the main turbine to 1800 rpu, the main turbine shaft oil pump discharge low pressure switch actuated causing the main turbine to trip. NCffE: First Out Annunciator was Turbine Trip and P-7 Fermissive. The Reactor Protection System functioned properly, and there was nc actuation of any safety or Power Operated Relief valves. he Steam Dump Valves functioned properly and no Safety Limits nor Limiting Safety Setting were exceeded.
Subsequent investigation revealed actual lube oil pressure to be normal when checked locally with the turbine rolling between 1600 and 1700 rpm. Maintenance personnel manually actuated the switch several times, verified calibration, and found it to be satisfactory. Inadvertent switch operation was attributed to the cause of the reactor trip.
The unit was placed in a stable condition after the trip; the cause of the reactor ,
trip was adequately evaluated, ard a restart was autlurized in accorcance with Emergency Operating Procedure (EOP) 5, " Recovery fran Reactor Trip."
On April 29, 1984, at approximately 0855 hours0.0099 days <br />0.238 hours <br />0.00141 weeks <br />3.253275e-4 months <br />, the reactor tripped from 11% power due to a main turbine trip. The main turbine tripped while rolling up to 1800 rpm on main turbine shaft pump discharge low pressure. 'lhis aggin was verified by First Out Annunciator. Local readings taken immediately following the c'eactor trip showed the discharge pressure of the main turbine motor suction pump arri the shaft driven lube oil pump to be zero. 'Ihe Reactor Protection System functioned properly, and there was no actuation of arly safety or Power Operated Relief Valves.
Steam Dump Valves functioned properly, and there were no Safety Limits nor Limiting Safety Setting exceeded. Steam Generator "B" Feedwater Isolation Valve XVG-1611B failed to auto close on reactor trip; however, the Feedwater Control Valve gcVided Feedwater Isolation. Valve XVG-1611B wes manually closed anormiste.y seven (7) minutes into the event. The operator also received an urgent failure alann on rod control, and NI-31, Source Range Detector "B", developad excessive spikirg before failing low. Maintenance work requests were initiated to investigate and repair XVG-1611B, NI-31, ard the urgent failure alann in rof. control. The air motor on the hydraulic pump for the operation of XVG-1611B was found to be defective and was replaced. The valve was tested satisfactorily ard declared operable April 30.
Blown fuses were found in the rod control power cabilets. 'Ihe fuses were replaced ard the rod control returned to service April 29 Investigation into the spiking of NI-31 attributed the cause to a defective detecto'. The detector was replaced, calibrated, and declared operable May 3, 1984.
As noted previously, local reading on the nnin turbire notor suction pump discharge pressure indicated zero. When the motor suction pump was manually stopped ard restarted, oil pressure indications were obtained. D_scussion with General Electric Corporation (G.E.) revealed that other planti had experienced similar problems because of the notor suction pump discharge check valve sticking closed.
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NRC Form 3ssa U S NUOLE&2 REGULATOXY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AreROvEo cus NO atso-oio4 empires 8/3115 P ACILIM NAME (M DOCKET NUMeER (2) LER NUMSER 161 PAGE(31 l
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Virnil C. Summer Nuclear Station 0 l5 l0 l0 l0 l3 l 9l5 814 -
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Ol1 01 3 OF 0l3 l TEXT IJF mee space e recured, use adseenaf hMC Fomo JIM'sJ tlh Preventive Test Procedure (PTP) 102.006, " Main Turbine Lube Oil Suction Pressure Monitoring," was written to be implemented on the next turbine roll up. The PTP was initiated to gather information to help determine the root cause of the trips because of low lube oil pressure. The PTP was conducted on May 3 and May 7,1984.
Fran the test data results, the turbine would have tripped in both roll ups because of low shaft driven pump discharge pressure at 1300 rpm. The main turbine mctor suction pump, on occasions appeared to lose prime causing the discharge pressure to decrease. The dischargp pressure of the shaft driven pump did not increase linear with pump speed, but there appeared to be a droop in the discharge pressure. l G.E. was also questioned concernirs the set points of the pressure switch. The schematics show the pressure setpoints in relation to the centerline of the turbine. The Licensee, therefore, applied a " head correction" of 23.5 psig due to the location of the switch in respect to the centerline of the turbine.
Confirmation was received fran G.E. on May 16, 1984, that the value shown at centerline should be the value at the pressure switch. As such, the setting has been conservative. A procedure change has been issued to delete the head correction from the setpoint.
Inspection of the pump and check valve has been scheduled during the First Refueling Outage.
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SOUTH CAROLINA ELECTRIC & GAS COMPANY post OFFICE 784 CotuusiA. South CAROLINA 29218 O W. Druom. Ja.
Vict PatsDENT NuCLEan Optmatio~S July 2, 1984 i
U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
SUBJECT:
Virgil C. Summer Nuclear Station .
Docket No. 50/395 I Operating License No. NPF-12 LER 84-024, Revision 1
Dear Sir:
Please find attached Revision 1 to Licensee Event Report #84-024 for the Virgil C. Summer Nuclear Station. The changes are denoted by the bar lines in the right hand margin on pages 1, 2 and 3.
This Report was previously submitted on May 22, 1984, in accordance with the requirements of 10 CFR 50.73(a)(2)(iv).
Should there be any questions, please call us at your convenience.
Very truly yours, y- m O. W. , ixon, Jr.
ARK:RJB:OWD/dwf Attachment cc: V. C. Summer J. F. Heilman T. C. Nichols, Jr./O. W. Dixon, Jr. C. L. Ligon (NSRC)
E. H. Crews, Jr. K. E. Nodland E. C. Roberts R. A. Stough W. A. Williams, Jr. G. Percival D. A. Nauman C. W. Hehl J. B. Knotts, Jr.
J. P. O'Reilly Group Managers INPO Records Center ANI Library O. S. Bradham NPCF C. A. Price ;
D. A. Lavigne File h,,
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