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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000395/LER-1993-0041993-08-30030 August 1993 LER 93-004-01:on 930629,missed Surveillance Occurred,Per TS 4.3.2.1,Table 4.3-2.2.b.Caused by Personnel Error in Documenting Test Discrepancy.Operations Personnel Took Part in Discussion of Importance of post-test.W/930830 Ltr 05000395/LER-1993-0031993-07-28028 July 1993 LER 93-003-00:on 930628,purge Sys Discovered Outside Provisions of Ts.Caused by Personnel Error.Operations Mgt Communicated Importance of Proper Procedural Usage & Stressed Usage Level requirements.W/930830 Ltr 05000395/LER-1984-024, Revised LER 84-024-01:on 840422 & 29,reactor Tripped Due to Low Main Turbine Shaft Oil Pump Discharge Pressure.Caused by Conservative Switch Settings & Loss of Suction on Motor Suction Pump.Switch Setpoint Will Be Changed1984-07-0202 July 1984 Revised LER 84-024-01:on 840422 & 29,reactor Tripped Due to Low Main Turbine Shaft Oil Pump Discharge Pressure.Caused by Conservative Switch Settings & Loss of Suction on Motor Suction Pump.Switch Setpoint Will Be Changed 05000395/LER-1984-013, Revised LER 84-013-01:on 840309,mod to Plant Integrated Fire & Security Sys Disabled Control Room Operator Ability to Receive Alarm Upon Actuation of Smoke Detectors in Zones Fff & Mmm of Intermediate Bldg1984-04-19019 April 1984 Revised LER 84-013-01:on 840309,mod to Plant Integrated Fire & Security Sys Disabled Control Room Operator Ability to Receive Alarm Upon Actuation of Smoke Detectors in Zones Fff & Mmm of Intermediate Bldg 05000395/LER-1983-100, Revised LER 83-100-01X-1:on 830831,PORV PCV-445A Declared Inoperable Due to Concern Re Possible Inadvertent Opening of Valve Upon Power Loss to Protective Cabinet 4.Caused by Design Error1984-01-27027 January 1984 Revised LER 83-100-01X-1:on 830831,PORV PCV-445A Declared Inoperable Due to Concern Re Possible Inadvertent Opening of Valve Upon Power Loss to Protective Cabinet 4.Caused by Design Error 05000395/LER-1983-060, /03L-0:on 831117,investigation Into Previously Submitted LER 83-060 Revealed Four Testable Components Not Tested on Quarterly Basis.Caused by Inadequate Procedure.Test Procedures Revised1983-12-16016 December 1983 /03L-0:on 831117,investigation Into Previously Submitted LER 83-060 Revealed Four Testable Components Not Tested on Quarterly Basis.Caused by Inadequate Procedure.Test Procedures Revised 05000395/LER-1983-001, Updated LER 83-001/01T-1:on 830119,three Refueling Water Storage Tank Level Transmitters Failed High.Caused by Transmitter Base Freezing.Transmitters Thawed.Insulated Encls & Addl Permanent Heat Trace Will Be Installed1983-02-22022 February 1983 Updated LER 83-001/01T-1:on 830119,three Refueling Water Storage Tank Level Transmitters Failed High.Caused by Transmitter Base Freezing.Transmitters Thawed.Insulated Encls & Addl Permanent Heat Trace Will Be Installed 1993-08-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D6401999-10-31031 October 1999 Rev 2 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0202, Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for VC Summer Nuclear Station.With ML20216J4191999-09-24024 September 1999 Part 21 Rept Re 990806 Abb K-Line Breaker Defect After Repair.Vendor Notified of Shunt Trip Wiring Problem & Agreed to Modify Procedure for Refurbishment of Breakers RC-99-0180, Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression1999-09-0808 September 1999 Special Rept on 990807,electric Driven Fire Pump XPP0134A Was Declared Inoperable.Caused by Pump Discharge Relief Valve Failing to Open as Normally Expected.Two Temporary Fire Pumps Were Installed to Provide Backup Suppression RC-99-0183, Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Virgil C Summer Nuclear Station,Unit 1.With ML20211K6161999-08-31031 August 1999 Rev 2 to VC Summer Nuclear Station,Colr for Cycle 12, Dtd Aug 1999 RC-99-0168, Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed1999-08-19019 August 1999 Special Rept:On 990804,electric Driven Fire Pump XPP0134A & Diesel Driven Fire Pump XPP0134B,were Removed from Svc to Allow for Plant Mod.Fire Pumps Were Returned to Operable Condition on 990818,after Mod Was Completed ML20210M7071999-07-31031 July 1999 Rev 1 to VC Summer Nuclear Station COLR for Cycle 12 ML20211C2201999-07-31031 July 1999 Rev 1 to WCAP-15102, VC Summer Unit 1 Heatup & Cooldown Limit Curves for Normal Operation RC-99-0163, Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0137, Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0122, Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for VC Summer Nuclear Station.With ML20206H2971999-05-0505 May 1999 Part 21 Rept Re Common Mode Failure for magne-blast Breakers.Vc Summer Nuclear Station Utilizes These Breakers in Many Applications,Including 7.2-kV EDG Electrical Buses RC-99-0103, Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for VC Summer Nuclear Station.With ML20206K2421999-04-30030 April 1999 Rev 0 to COLR for Cycle 12 for Summer Nuclear Station RC-99-0087, Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory1999-04-15015 April 1999 Part 21 Interim Rept (SSH 99-0001) Re 990218 Failure of Circuit Breaker Located in Cubicle 14 of XSW1DB to Close During Surveillance Testing.Caused by Positive Interlock Angle Was Incorrect.Breaker Was Returned to GE Factory RC-99-0083, Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for VC Summer Nuclear Station,Unit 1.With RC-99-0063, Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced1999-03-26026 March 1999 Special Rept:On 990302 & 16,meteorological Site Number One 10 Meter Temp Element Was Declared Inoperable.Caused by Erratic Operation.Cabling & 10 Meter Electrical Connectors Were Replaced ML20196K5421999-03-22022 March 1999 Rev 2 to VC Summer Nuclear Station,Training Simulator Quadrennial Certification Rept,1996-99, Books 1 & 2. Page 2 of 2 Section 2.4.4 (Rev 2) of Incoming Submittal Were Not Included RC-99-0055, Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 9903121999-03-16016 March 1999 Special Rept:On 990302,Meteorological Site Number One 10 Meter Temp Element (RTD) Was Declared Inoperable Due to Erratic Operation.Cause of Original RTD Failure Is Unknown. Equipment Was Declared Operable on 990312 RC-99-0050, Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for VC Summer Nuclear Station,Units 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML20203F4511999-02-12012 February 1999 SER Finding Licensee Adequately Addressed GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves, for Virgil C Summer Nuclear Station ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20206R5241998-12-31031 December 1998 Santee Cooper 1998 Annual Rept RC-99-0052, Vsns 1998 Annual Operating Rept. with1998-12-31031 December 1998 Vsns 1998 Annual Operating Rept. with RC-99-0004, Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for VC Summer Nuclear Station,Unit 1.With ML20206R5191998-12-31031 December 1998 Scana Corp 1998 Annual Rept ML20198F4241998-12-18018 December 1998 Safety Evaluation Granting Relief Request for Approval to Repair ASME Code Class 3 Service Water Piping Flaws in Accordance with GL 90-05 for VC Summer Nuclear Station RC-98-0223, Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method1998-12-16016 December 1998 Special Rept 98-001:on 981130,steam Line High Range Gamma Monitor (RMG-19C) Was Declared Inoperable Due to Indeterminate Alarm.Caused by Failures in Detector & Meter Reset Circuitry.Established Preplanned Alternate Method RC-98-0222, Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for VC Summer Nuclear Station,Unit 1.With ML20155G4551998-11-0404 November 1998 Safety Evaluation Accepting Licensee Proposed Alternative to Use Code Case N-416-1 with Licensee Proposed Addl Exams RC-98-0208, Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for VC Summer Nuclear Station,Unit 1.With ML20207J5701998-10-31031 October 1998 Non-proprietary Rev 1 to WCAP-14955, Probabilistic & Economic Evaluation of Rv Closure Head Penetration Integrity for VC Summer Nuclear Plant ML20154Q9571998-10-21021 October 1998 SER Accepting Request Seeking Approval to Use Alternative Rules of ASME Code Case N-498-1 for Class 1,2 or 3 Sys ML20154K7901998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15101, Analysis of Capsule W from Sceg VC Summer Unit 1 Rv Radiation Surveillance Program RC-98-0184, Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for VC Summer Nuclear Station.With ML20154K8041998-09-30030 September 1998 Non-proprietary Rev 0 to WCAP-15103, Evaluation of Pressurized Thermal Shock for VC Summer Unit 1 RC-98-0166, Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for VC Summer Nuclear Station,Unit 1.With ML20237A7181998-08-13013 August 1998 SER Accepting Util Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves RC-98-0153, Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0131, Monthly Operating Rept for June 1998 for VC Summer Nuclear Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for VC Summer Nuclear Station ML20248J0191998-06-0404 June 1998 Safety Evaluation Accepting Licensee Inservice Testing Program Interim Pump Relief Request Per 10CFR50.55a(a)(3) (II) RC-98-0113, Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for VC Summer Nuclear Station,Unit 1 RC-98-0100, Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for VC Summer Nuclear Station,Unit 1 ML20217G7411998-04-22022 April 1998 Rev 1 to VC Summer Nuclear Station COLR for Cycle 11 RC-98-0076, Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure1998-04-17017 April 1998 Final Part 21 Rept Re a DG EG-B for Vsns,As Followup to .Power Control Svcs of Engine Sys,Inc Provided Response on 980318.Evaluation Concludes That Failure of EG-B Is one-time non-repeatable Failure RC-98-0084, Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Virgil C Summer Nuclear Station,Unit 1 ML20212H1421998-03-0202 March 1998 Interim Part 21 Rept SSH 98-002 Re EG-B Unit That Was Sent to Power Control Svcs for Determination of Instability & Refurbishment of a Dg.Cause of Speed Oscillations Unknown. Completed Hot Bore Checks on Power Case 1999-09-08
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,
- y. .
John A.
&_ 2A Couth Carolma Dettlic & Gas Company gglggsCmes 3 ko s Nuc
August 30, 1993 L Refer to: RC-93-0233 l
Document Control Desk U. S. Nuclear Regulatory Commission ;
Washington, DC 20555 Gentlemen:
Subject:
VIRGIL C. SUMMER NUCLEAR STATION (VCSNS)
DOCKET NO. 50/395 OPERATING LICENSE NO. NPF-12 i RESPONSE TO NOTICE OF VIOLATION NRC INSPECTION REPORT 93-19 Attached is the South Carolina Electric & Gas Company (SCE&G) Licensee Event Report No.93-003 which responds to the violation addressed in Enclosure 1 of NRC Inspection Report 50-395/93-19. SCE&G is in agreement with the alleged i violation, and the enclosed response addresses the reason for the violation and corrr:ctive actions being taken to prevent recurrence. Additional corrective action items 1 and 2 have been completed.
If you should have any questions, please call at your convenience.
Very truly yours, M
John L. Skolds DCH:lcd Attachment c: 0. W. Dixon (w/o attachment)
R. R. Mahan (w/o attachment)
R. J. White S. D. Ebneter i NRC Resident Inspector 1 J. B. Knotts Jr. '
J. I. Byrd !
NSRC '
Central File System RTS (IE 931901)
File (815.01) 070003 93o909o2e4 93033o 8" NME - A NR NNM gl~ih y
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'"" M u~n M ," 19"#3, aI0l 65 To*urs, approval was granted by the control room to remove At e spheric Radiation Monitor RMA-2 from service to allow the performance of pn entive maintenance. A Removal and Restoration Checklist (R&R) was entered and logged in the control room documenting that RMA-2 was out of service. The status of RMA-2 was discussed and included as part of turnover to the oncoming shift which was completed at approximately 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />.
Soon after turnover was completed, the Reactor Building pressure alarm annunciated indicating the pressure was approaching the low pressure limit allowed by Technical Specifications. At 0745, the control building operator c .!ned purge supply valves PVG-6056 and 6057 and started purge supply fan XFN-95 to increase reactor building pressure without consulting System Operating Procedure (SOP) 114, Reactor Building Ventilation System. Shortly after the valves were opened, another control room operator noticed the valves were open and pointed out that the valves should be closed due to RMA-2 being out of service. The fan was stopped and the valves were closed at 0748. Action 17 of Table 3.3-3 states that plant operation may continue provided the containment purge and exhaust valves are maintained closed. Opening the valves with RMA-2 out of service constitutes operation outside the provisions of Technical Specifications.
Radiation levels inside containment were normal and remained steady during the three minutes the valves were opened. Therefore, this event resulted ir: no safety consequences.
Operations management has communicated to all operations personnel the importance of proper procedural usage and stressed the usage level requirements defined in Station Administrative Procedure (SAP) 123, Procedural Use and Adherence (Revision - 1).
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Virgil C. Summer Nuclear Jtation o is Io lo 10 t 31915 91 3 _ - 01013 -
010 012 or O! 3 j vw - ~ _ c o , w., m, PLANT IDENTIFICATION: ;
L Westinghouse - Pressurized Water Reactor j i
EQUIPMENT IDENTIFICATION:
Contaicment Isolation Valve EIIS - JM i
IDENTIFICATION OF EVENT: -
A personnel error in performing a plant evolution without proper procedural adherence I led to operations outside the provisions of Technical Specifications (T.S.). l 1
i EVENT TIME AND DATE* t June 28, 1993, at 0745 hours0.00862 days <br />0.207 hours <br />0.00123 weeks <br />2.834725e-4 months <br />. l REPORT DATE: i July 28, 1993 ;
I' This report was initiated by Off-Normal Occurrence report 93-046.
CCNDITIONS PRIOR TO EVENT: i Mode 1, 100% power DESCRIPTION OF EVENT:
On June 28, 1993, at 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> approval was granted by the control room to remove ;
Atmospheric Radiation Monitor RMA-2 from service to allow the performance of preventive j maintenance. 'A Removal and Restoration Checklist (R&R) was entered and logged in the j control room documenting that RMA-2 was out of service. (The R&R logs are part of the configuration control process used to aid operations personnel in tracking the status of out-of-service' equipment and any associated alternate actions.) The status of RMA-2 was discussed and included as part of turnover to the oncoming _ shift which was completed at approximately 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />.
Soon after turnover was completed, the Reactor Building pressure alarm annunciated indicating the pressure was approaching the low pressure limit allowed by Technical Specifications. At 0745, the control building' operator opened purge supply valves PVG-6056 and 6057 and started purge supply fan XFN-95 to increase reactor building pressure without consulting System Operating Procedure (SOP) 114, Reactor Building Ventilation System. Shortly after the valves were opened, another control room operator noticed
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001 013 or 0l3 the valves were open and pointed out that the valves should be closed due to RMA-2 being out of service. The fan was stopped and the valves were closed at 0748. Action 17 of Table 3.3-3 states that plant operation may continue provided the containment purge and exhaust valves are maintained closed. 50P-114, Section-N, Reactor Building Normal Pressure Control, lists the following statement; "RMA-2 Atmosphere Gaseous Iodine - RB sample line is in service," as an initial condition to procedure performance. Opening the valves with RMA-2 out of service constitutes operation outside the provisions of Technical Specifications.
CAUSE OF EVENT:
A non-licensed, control building operator made a personnel error by performing an evolution without consulting the governing procedure which contained the control to prevent the opening of the purge supply valves if RMA-2 is out of service.
2 ANALYSIS OF EVENT:
Radiation levels inside containment were normal and remained steady during the three
- j. minutes the valves were open. Also, due to this event involving only the Reactor l Building supply portion of the system, no release of Reactor Building Atmosphere occurred. Therefore, this event resulted in no safety consequences.
4 IMMEDIATE CORRECTIVE ACTION:
1
- The Reactor Building purge supply valves were closed as required by Technical
- Specification 3.3.2.
ADDITIONAL CORRECTIVE ACTIONS:
- (1) Operations management has communicated to all operations personnel the importance t
of proper procedural usage and stressed the usage level requirements defined in l Station Administrative Procedure (SAP) 123, Procedural Use and Adherence (Rev-1).
j (2) This event was included in a meeting of the Management Review Board on July 13, 1 1993, and again on July 20, 1993, to insure adequate management attention was
)
given to this matter.
l PRIOR EVENTS:
J None.
l 4
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05000395/LER-1993-003 | LER 93-003-00:on 930628,purge Sys Discovered Outside Provisions of Ts.Caused by Personnel Error.Operations Mgt Communicated Importance of Proper Procedural Usage & Stressed Usage Level requirements.W/930830 Ltr | | 05000395/LER-1993-004 | LER 93-004-01:on 930629,missed Surveillance Occurred,Per TS 4.3.2.1,Table 4.3-2.2.b.Caused by Personnel Error in Documenting Test Discrepancy.Operations Personnel Took Part in Discussion of Importance of post-test.W/930830 Ltr | |
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