LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl |
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.r SOUTH CAROLINA ELECTRIC & GAS COMPANY Post orrica 7e4 COLUMelA, SOUTH CAROUNA 29218 O. W. DixoN, JR.
E susl["o',*,*l"[..
February 7, 1983 c.c (C
Mr. James P. O'Reilly, Director
~~
U.S. Nuclear Regulatory Commission Region II, Suite 3100
- [
101 Marietta Street, N.W.
Atlanta, Georgia 30303
SUBJECT:
Virgil C. Summer Nuclear Station Docket No. 50/395 Operating License No. NPF-12 Thirty Day Written Report LER 83-003
Dear Mr. O'Reilly:
Please find attached Licensee Event Report #83-003 for Virgil C. Summer Nuclear Station.
This Thirty Day Report is required by Technical Specification 6.9.1.13.(b) as a result of entry into Action Statement 6 of Technical Specification 3.3.1,
" Reactor Trip Instrumentation," Item 14, on January 8, 1983, and January 20, 1983.
Should there be any questions, please call us at your convenience.
Very tru y yo rs, O. W.
i xoit,
r.
HCP:OWD:dwf/fjc Attachment cc:
V.
C.
Summer A.
R.
Koon T.
C. Nichols, Jr.
G.
D. Moffatt E.
C.
Roberts Site QA O. W. Dixon, Jr.
C.
L. Ligon (NSRC)
H.
N.
Cyrus G.
J. Braddick H.
T. Babb J.
L.
Skolds D.
A.
Nauman J.
B.
Knotts, Jr.
M. B. Whitaker, Jr.
B.
A.
Bursey W.
A. Williams, Jr.
I&E (Washington)
O.
S. Bradham Document Management Branch R.
B.
Clary INPO Records Center C.
A.
Price NPCF File 8302150613 830207
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O'Reilly i
LER No.83-003 Page Two February 7, 1983 DETAILED DESCRIPTION OF EVENT On January 8, 1983, at 0705 hours0.00816 days <br />0.196 hours <br />0.00117 weeks <br />2.682525e-4 months <br />, the Main Control Board indication for Steam Generator "A"
feedwater flow (IFI-477) failed low.
On January 20, 1983, at 1017 hours0.0118 days <br />0.283 hours <br />0.00168 weeks <br />3.869685e-4 months <br />, IFI-477 indicated approximately 20% below redundant channels.
The i
plant was operating in Mode 1 at 50% power during these occurrences.
The channel was declared inoperable, and its associated bistables were placed in the tripped condition within one (1) hour (during both events) in accordance with Technical Specification 3.3.1, Item 14, Action Statement 6.
PROBABLE CONSEQUENCES There were no adverse consequences as a result of the events since the downscale failure of the instrument channel was in the safe direction.
A reactor trip would still have occurred with a Steam Generator low water level in coincidence with a steam flow /feedwater flow mismatch.
CAUSE(S) OF THE OCCURRENCE The cause of the two (2) events is as follows:
1.
The failure of IFI-477 on January 8, 1983, is attributed to breakdown of the circuit board electronic components when exposed to the internal cabinet temperature.
j 2.
The erroneous readings observed on January 20, 1983, is attributed to instrument drift of the circuit board installed on January 8, 1983.
t
Mr. James P.
O'Reilly LER No.83-003 Page Three February 7, 1983 IMMEDIATE CORRECTIVE ACTIONS TAKEN On January 8, 1983, the channel for Steam Generator "A" feedwater flow (IFI-477) was placed in the tripped condition within one (1) hour.
It was determined that the power supply card (FQY-477) would not function within the temperature parameters present in the instrument cabinet.
The circuit board was replaced, and the channel was returned to operable status af ter the performance of a satisfactory channel calibration with the appropriate surveillance test procedure on January 8, 1983, at 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br />.
Action was initiated to lower instrument cabinet and room temperature to prevent recurrence.
On January 20, 1983, the channel was again placed in the tripped condition within one (1) hour of the observance of the low readings.
The output of the power supply card (FQY-477) was found to be out-of-tolerance low upon performance of a channel calibration.
The output was calibrated, and the channel was returned to operable status on January 20, 1983, at 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br />, upon successful completion of the appropriate surveillance test procedure.
ACTION TAKEN TO PREVENT RECURRENCE The licensee is implementing a modification to alter the relay room ventilation flow path for the purpose of providing more effective cooling to the instrument cabinets.
Testing performed by the licensee indicated that air stagnation existed in the relay room from inadequate HVAC air distribution.
A temporary modification has been installed with acceptable results to date.
The permanent modification is expected to be complete by April 15, 1983.
This action negates the need to add air conditioning in the Relay Room as discussed in LER 82-016, Revision 2 (January 13, 1983, letter from O.
W.
Dixon, Jr. to J.
P.
O'Reilly).
Additionally, for the January 20, 1983 event, the licensee plans to initiate a follow-up investigation to determine the cause of the instrument drift.
This is expected to be complete by April 15, 1983.
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| 05000395/LER-1983-001-01, /01T-0:on 830119,w/plant in Mode 1,three Refueling Water Storage Tank Level Transmitters Failed High. Caused by Frozen Instrument Lines.Transmitters Thawed. Insulated Encls Will Be Installed | /01T-0:on 830119,w/plant in Mode 1,three Refueling Water Storage Tank Level Transmitters Failed High. Caused by Frozen Instrument Lines.Transmitters Thawed. Insulated Encls Will Be Installed | | | 05000395/LER-1983-001, Updated LER 83-001/01T-1:on 830119,three Refueling Water Storage Tank Level Transmitters Failed High.Caused by Transmitter Base Freezing.Transmitters Thawed.Insulated Encls & Addl Permanent Heat Trace Will Be Installed | Updated LER 83-001/01T-1:on 830119,three Refueling Water Storage Tank Level Transmitters Failed High.Caused by Transmitter Base Freezing.Transmitters Thawed.Insulated Encls & Addl Permanent Heat Trace Will Be Installed | | | 05000395/LER-1983-003, Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | Forwards LER 83-003/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-003-03, /03L-0:on 830108 & 20,main Control Board Indication for Steam Generator a Feedwater Flow IFI-477 Failed Low.Caused by High Instrument Cabinet Temp.Power Supply Card Replaced & Recalibr | /03L-0:on 830108 & 20,main Control Board Indication for Steam Generator a Feedwater Flow IFI-477 Failed Low.Caused by High Instrument Cabinet Temp.Power Supply Card Replaced & Recalibr | | | 05000395/LER-1983-008-03, W/Plant in Mode 1,main Control Board Indication for Steam Generator B Steam Pressure Decreased Approx 100 Psig.Caused by Plugged Transmitter Sensing Line.Sensing Line Back Flushed | W/Plant in Mode 1,main Control Board Indication for Steam Generator B Steam Pressure Decreased Approx 100 Psig.Caused by Plugged Transmitter Sensing Line.Sensing Line Back Flushed | | | 05000395/LER-1983-008, Forwards Updated LER 83-008/03L-1.Detailed Event Analysis Encl | Forwards Updated LER 83-008/03L-1.Detailed Event Analysis Encl | | | 05000395/LER-1983-009, Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-009-03, /03L-0:on 830203,main Control Board Indicator (PI-950) for Reactor Bldg Pressure Failed Low.Caused by Intermittent Pressure Transmitter Failure.Transmitter Output Returned to Normal | /03L-0:on 830203,main Control Board Indicator (PI-950) for Reactor Bldg Pressure Failed Low.Caused by Intermittent Pressure Transmitter Failure.Transmitter Output Returned to Normal | | | 05000395/LER-1983-010, Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | Forwards LER 83-010/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-010-03, /03L-0:on 830206,only One Isotopic Iodine Analysis Performed During Power Reduction from 50% to 5%.Caused by Personnel Misinterpreting Power Changes.Chemistry Lab Policy Issued Re Need for Analysis | /03L-0:on 830206,only One Isotopic Iodine Analysis Performed During Power Reduction from 50% to 5%.Caused by Personnel Misinterpreting Power Changes.Chemistry Lab Policy Issued Re Need for Analysis | | | 05000395/LER-1983-011, Forwards LER 83-011/03L-0.Detailed Event Analyis Encl | Forwards LER 83-011/03L-0.Detailed Event Analyis Encl | | | 05000395/LER-1983-011-03, /03L-0:on 830208 & 17,during Mode 1 Operation, Nuclear Sampling Sys Valves 9398 A,B & C Failed to Close. Caused by Limit Switch Failure on One Valve & Crud Buildup on Other Valve Seats.Crud Dislodged.Limit Switches Repaired | /03L-0:on 830208 & 17,during Mode 1 Operation, Nuclear Sampling Sys Valves 9398 A,B & C Failed to Close. Caused by Limit Switch Failure on One Valve & Crud Buildup on Other Valve Seats.Crud Dislodged.Limit Switches Repaired | | | 05000395/LER-1983-012, Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | Forwards LER 83-012/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-012-03, /03L-0:on 830210,flow Indicator for Steam Generator a Feedwater Flow FI-477 Failed Low.Caused by Failure of Power Supply FQY-477.Circuit Board Replaced | /03L-0:on 830210,flow Indicator for Steam Generator a Feedwater Flow FI-477 Failed Low.Caused by Failure of Power Supply FQY-477.Circuit Board Replaced | | | 05000395/LER-1983-013, Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-013-03, /03L-0:on 830113 & 19,condensate Storage Tank Level Transmitters LT-3631 & LT-3631A Failed Due to Frozen Instrument Lines.Caused by Temp Sensing Element Not Being Located Per Design Specs.Element Relocated | /03L-0:on 830113 & 19,condensate Storage Tank Level Transmitters LT-3631 & LT-3631A Failed Due to Frozen Instrument Lines.Caused by Temp Sensing Element Not Being Located Per Design Specs.Element Relocated | | | 05000395/LER-1983-014-03, /03L-0:on 830217 & 0303,pressurizer PORV PCV-445B Found Leaking.Events Discovered by High Temp Indication in PORV Discharge Piping.Cause Unknown.Valve Will Remain Closed & Be Disassembled During 830317 Outage | /03L-0:on 830217 & 0303,pressurizer PORV PCV-445B Found Leaking.Events Discovered by High Temp Indication in PORV Discharge Piping.Cause Unknown.Valve Will Remain Closed & Be Disassembled During 830317 Outage | | | 05000395/LER-1983-014, Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | Forwards LER 83-014/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-015-03, /03L-0:on 830219,while in Mode 1,5% Discrepancy Observed Between Main Control Board & Control Room Evacuation Panel Indication for Pressurizer Relief Tank Level.Caused by Design Error.New Transmitter Installed | /03L-0:on 830219,while in Mode 1,5% Discrepancy Observed Between Main Control Board & Control Room Evacuation Panel Indication for Pressurizer Relief Tank Level.Caused by Design Error.New Transmitter Installed | | | 05000395/LER-1983-015, Forwards LER 83-015/03L-0.Detailed Event Analysis Encl | Forwards LER 83-015/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-016, Forwards LER 83-016/03L-0.Detailed Event Analysis Encl | Forwards LER 83-016/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-016-03, /03L-0:on 830216,w/plant in Mode 1,discrepancy of 6% Observed Between Main Control Board Indicators for Sodium Hydroxide Storage Tank Level.Caused by Loose Fitting on High Side Sensing Line of Level Transmitter | /03L-0:on 830216,w/plant in Mode 1,discrepancy of 6% Observed Between Main Control Board Indicators for Sodium Hydroxide Storage Tank Level.Caused by Loose Fitting on High Side Sensing Line of Level Transmitter | | | 05000395/LER-1983-017, Forwards LER 83-017/03L-0.Detailed Event Analysis Encl | Forwards LER 83-017/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-017-03, /03L-0:on 830305,remote Info Acquisition Cabinet Experienced Electronic Problems Rendering Four Reactor Bldg Zone 3 Smoke Detectors Inoperable.Caused by Printed Circuit Card Failure.Card Replaced | /03L-0:on 830305,remote Info Acquisition Cabinet Experienced Electronic Problems Rendering Four Reactor Bldg Zone 3 Smoke Detectors Inoperable.Caused by Printed Circuit Card Failure.Card Replaced | | | 05000395/LER-1983-018-03, /03L-0:on 830306,while in Mode 1,nuclear Sampling Sys Valves 9398 A,B & C Failed to Close During Initial Performance of Accelerated Test Program.Caused by Crud Buildup on Valve Seats.Crud Dislodged & Switch Repaired | /03L-0:on 830306,while in Mode 1,nuclear Sampling Sys Valves 9398 A,B & C Failed to Close During Initial Performance of Accelerated Test Program.Caused by Crud Buildup on Valve Seats.Crud Dislodged & Switch Repaired | | | 05000395/LER-1983-018, Forwards LER 83-018/03L-0.Detailed Event Analysis Encl | Forwards LER 83-018/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-019-01, /01L-0:on 830317,trains of RHR & High Head Safety Injection Train a Inoperable for Approx 45 Minutes.Caused by Switching Problems W/Starting Circuitry of Chiller Unit XHX0001C.Switch Apparatus Modified | /01L-0:on 830317,trains of RHR & High Head Safety Injection Train a Inoperable for Approx 45 Minutes.Caused by Switching Problems W/Starting Circuitry of Chiller Unit XHX0001C.Switch Apparatus Modified | | | 05000395/LER-1983-019, Forwards LER 83-019/01L-0.Detailed Event Analysis Encl | Forwards LER 83-019/01L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-020-03, /03L-0:on 830305,fire Detector Sys Control Room Alarm Capability Lost for Intermediate Bldg Zones Aa,Bb & CC & for Diesel Generator Bldg Zones DG (427) & DG (436).Caused by Blown Fuse.Fuse Replaced | /03L-0:on 830305,fire Detector Sys Control Room Alarm Capability Lost for Intermediate Bldg Zones Aa,Bb & CC & for Diesel Generator Bldg Zones DG (427) & DG (436).Caused by Blown Fuse.Fuse Replaced | | | 05000395/LER-1983-020, Forwards LER 83-020/03L-0.Detailed Event Analysis Encl | Forwards LER 83-020/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-021, Forwards LER 83-021/03L-0.Detailed Event Analysis Encl | Forwards LER 83-021/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-021-03, /03L-0:on 830307,steam Generator Blowdown Monitor RM-L3 Failed Low,Reducing Number of Operable Channels. Caused by Moisture in Monitor Detector Due to Overhead Sample Valve O-ring Rupture.Detector Replaced | /03L-0:on 830307,steam Generator Blowdown Monitor RM-L3 Failed Low,Reducing Number of Operable Channels. Caused by Moisture in Monitor Detector Due to Overhead Sample Valve O-ring Rupture.Detector Replaced | | | 05000395/LER-1983-022-03, /03L-0:on 830308,conduit Containing Smoke Detector Circuits Cut During Core Drilling for Plant Mod.Fire Watch Posted.Caused by Failure to See Conduit Embedded in Fireproofing Matl.Conduit & Cable Replaced | /03L-0:on 830308,conduit Containing Smoke Detector Circuits Cut During Core Drilling for Plant Mod.Fire Watch Posted.Caused by Failure to See Conduit Embedded in Fireproofing Matl.Conduit & Cable Replaced | | | 05000395/LER-1983-022, Forwards LER 83-022/03L-0.Detailed Event Analysis Encl | Forwards LER 83-022/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-023, Forwards LER 83-023/03L-0.Detailed Event Analysis Encl | Forwards LER 83-023/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-023-03, /03L-0:on 830309,main Control Board Pressure Indicator for Reactor Bldg Pressure Channel 950 Failed Low. Caused by Intermittent Electronic Failure of Transmitter. Transmitter Replaced | /03L-0:on 830309,main Control Board Pressure Indicator for Reactor Bldg Pressure Channel 950 Failed Low. Caused by Intermittent Electronic Failure of Transmitter. Transmitter Replaced | | | 05000395/LER-1983-024, Forwards LER 83-024/03L-0.Detailed Event Analysis Encl | Forwards LER 83-024/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-024-03, /03L-0:on 830311,main Steam Line C Radiation Monitor Experienced Spurious Alarms.Caused by Slack Detector Cable Allowing Signal Oscillations.Detector Cable Will Be More Adequately Secured by 830501 | /03L-0:on 830311,main Steam Line C Radiation Monitor Experienced Spurious Alarms.Caused by Slack Detector Cable Allowing Signal Oscillations.Detector Cable Will Be More Adequately Secured by 830501 | | | 05000395/LER-1983-025, Forwards LER 83-025/03L-0.Detailed Event Analysis Encl | Forwards LER 83-025/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-025-03, /03L-0:on 830313,containment Bulkhead Door Seal on Personnel Access Air Lock Found W/Excessive Seal Leakage. Caused by Dirt on Door Seal.Seal Cleaned.Air Lock Tested | /03L-0:on 830313,containment Bulkhead Door Seal on Personnel Access Air Lock Found W/Excessive Seal Leakage. Caused by Dirt on Door Seal.Seal Cleaned.Air Lock Tested | | | 05000395/LER-1983-026, Forwards LER 83-026/03L-0 | Forwards LER 83-026/03L-0 | | | 05000395/LER-1983-026-03, /03L-0:on 830318,reactor Bldg Cooling Unit Svc Water Flow Indicators Failed Low & Accident Monitoring Instrumentation Channel 4496 Declared Inoperable.Caused by Internal Failure of Indicator FI-4496.Indicator Replaced | /03L-0:on 830318,reactor Bldg Cooling Unit Svc Water Flow Indicators Failed Low & Accident Monitoring Instrumentation Channel 4496 Declared Inoperable.Caused by Internal Failure of Indicator FI-4496.Indicator Replaced | | | 05000395/LER-1983-027, Forwards LER 83-027/03L-0.Detailed Event Analysis Encl | Forwards LER 83-027/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-027-03, /03L-0:on 830318,main Control Board Temp Indication TE-413 for Reactor Coolant Outlet Temp Exhibited Erratic Indications.Caused by Varying Resistance Between Compensated Lead & Low Side Resistance Leg of TE-413 | /03L-0:on 830318,main Control Board Temp Indication TE-413 for Reactor Coolant Outlet Temp Exhibited Erratic Indications.Caused by Varying Resistance Between Compensated Lead & Low Side Resistance Leg of TE-413 | | | 05000395/LER-1983-028-01, /01T-0:on 830406,out-of-tolerance Measurement Found on Undervoltage (UV) Trip Device Between Moving Core & Rolling Bracket.Caused by Mfg Variation of UV Trip Devices. Devices Will Be Replaced | /01T-0:on 830406,out-of-tolerance Measurement Found on Undervoltage (UV) Trip Device Between Moving Core & Rolling Bracket.Caused by Mfg Variation of UV Trip Devices. Devices Will Be Replaced | | | 05000395/LER-1983-028, Forwards LER 83-028/01T-0.Detailed Event Analysis Encl | Forwards LER 83-028/01T-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-029, Forwards LER 83-029/03L-0.Detailed Event Analysis Encl | Forwards LER 83-029/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-029-03, /03L-0:on 830320,w/reactor Bldg Purge Initiated, Radiation Monitor RM-A4 Read Higher than Normal Pump RM-A4 & Detector Secured to Change Filter,Leaving Purge Unmonitored for 5 Minutes.No Activity Released During Event | /03L-0:on 830320,w/reactor Bldg Purge Initiated, Radiation Monitor RM-A4 Read Higher than Normal Pump RM-A4 & Detector Secured to Change Filter,Leaving Purge Unmonitored for 5 Minutes.No Activity Released During Event | | | 05000395/LER-1983-030, Forwards LER 83-030/03L-0.Detailed Event Analysis Encl | Forwards LER 83-030/03L-0.Detailed Event Analysis Encl | | | 05000395/LER-1983-030-03, /03L-0:on 830324,reactor Bldg Fire Detection Zones Ooo & Ppp Declared Inoperable When Power Supply Breaker Opened.Caused by Faulty Power Supply Transformer in Smoke Detector IXA-4964E in Zone Ppp.Transformer Replaced | /03L-0:on 830324,reactor Bldg Fire Detection Zones Ooo & Ppp Declared Inoperable When Power Supply Breaker Opened.Caused by Faulty Power Supply Transformer in Smoke Detector IXA-4964E in Zone Ppp.Transformer Replaced | |
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