03-29-2016 | On January 30, 2016, with the plant in Mode 3, with the Auxiliary Feedwater System ( AFW) in operation and proceeding with Post Trip recovery actions from the January 29, 2016 Steam Feedwater Rupture Control System (SFRCS) High Level Trip (reference Licensee Event Report (LER) 2016-001) when a SFRCS Steam Generator ( SG) 1 High Reverse Differential Pressure (D/P) Trip was unexpectedly received. The trip was a result of a feedwater isolation valve being opened to align the Motor Driven Feed Pump's (MDFP) discharge to SG 1. The unexpected SFRCS SG 1 Reverse D/P Trip resulted in the closure of the appropriate Main Steam and Main Feedwater ( MFW) valves, as designed. AFW Pumps 1 and 2 remained in operation, as expected and the plant was verified to be stable.
The cause of this event was inadequate procedural guidance contained in the Trip Recovery Procedure with a corrective action to revise the procedure. This report is being submitted as an event that resulted in an automatic actuation of the SFRCS, therefore, reportable in accordance with 10 CFR 50.72(b)(3)(iv)(A). |
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Category:Letter
MONTHYEARML24303A3282024-10-29029 October 2024 Information Request for the Cyber Security Baseline Inspection Identification to Perform Inspection ML24281A0662024-10-0404 October 2024 EN 57363 - MPR Associates, Inc. Report in Accordance with 10 CFR Part 21 on Incomplete Dedication of Contactors Supplied as Basic Components IR 05000346/20244032024-09-27027 September 2024 Security Baseline Inspection Report 05000346/2024403 ML24269A0552024-09-25025 September 2024 Submittal of the Updated Final Safety Analysis Report, Revision 35 05000346/LER-2021-001-01, Emergency Diesel Generator Speed Switch Failure Due to Direct Current System Ground2024-09-19019 September 2024 Emergency Diesel Generator Speed Switch Failure Due to Direct Current System Ground ML24134A1522024-09-17017 September 2024 Exemption from the Requirements of 10 CFR 50.71(e)(4) Final Safety Analysis Report Update Schedule (EPID L-2024-LLE-0005) - Letter ML24260A2382024-09-16016 September 2024 Notification of an NRC Biennial Licensed Operator Requalification Program Inspection and Request for Information ML24255A8032024-09-11011 September 2024 Technical Specification 5.6.6 Steam Generator Tube Inspection 180-Day Report ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24249A1602024-09-0505 September 2024 Information Request to Support Upcoming Material Control and Accounting Inspection at Davis-Besse Nuclear Power Station L-24-188, Submittal of Quality Assurance Program Manual, Revision 302024-08-27027 August 2024 Submittal of Quality Assurance Program Manual, Revision 30 ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 IR 05000346/20240052024-08-22022 August 2024 Updated Inspection Plan for Davis-Besse Nuclear Power Station (Report 05000346/2024005) L-24-186, Response to RAI for Exemption Request from 10 CFR 50.71(e)(4) Final Safety Analysis Update Schedule2024-08-15015 August 2024 Response to RAI for Exemption Request from 10 CFR 50.71(e)(4) Final Safety Analysis Update Schedule IR 05000346/20240022024-08-0101 August 2024 Integrated Inspection Report 05000346/2024002 IR 05000346/20244012024-07-30030 July 2024 Security Baseline Inspection Report 05000346/2024401 ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification L-24-032, Cycle 23 and Refueling Outage 23 Inservice Inspection Summary Report2024-07-15015 July 2024 Cycle 23 and Refueling Outage 23 Inservice Inspection Summary Report L-24-063, License Amendment Request to Remove the Table of Contents from the Technical Specifications2024-07-0808 July 2024 License Amendment Request to Remove the Table of Contents from the Technical Specifications L-24-024, Annual 10 CFR 50.46 Report of Changes to or Errors in Emergency Core Cooling System Evaluation Models2024-06-19019 June 2024 Annual 10 CFR 50.46 Report of Changes to or Errors in Emergency Core Cooling System Evaluation Models L-23-214, Submittal of Relief Request for Impractical American Society of Mechanical Engineers Boiler and Pressure Vessel Code Section XI Examination Requirements2024-06-0505 June 2024 Submittal of Relief Request for Impractical American Society of Mechanical Engineers Boiler and Pressure Vessel Code Section XI Examination Requirements L-24-019, Unit No.1 - Report of Facility Changes, Tests, and Experiments2024-05-22022 May 2024 Unit No.1 - Report of Facility Changes, Tests, and Experiments ML24142A3532024-05-21021 May 2024 Station—Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes Inspection L-24-072, Combined Annual Radiological Environmental Operating Report and Radioactive Effluent Release Report - 20232024-05-15015 May 2024 Combined Annual Radiological Environmental Operating Report and Radioactive Effluent Release Report - 2023 L-24-111, Response to Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-05-15015 May 2024 Response to Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations L-24-031, Unit No.1 - Steam Generator Tube Circumferential Crack Report - Spring 2024 Refueling Outage2024-05-14014 May 2024 Unit No.1 - Steam Generator Tube Circumferential Crack Report - Spring 2024 Refueling Outage IR 05000346/20240012024-05-0303 May 2024 Integrated Inspection Report 05000346/2024001 L-24-069, Occupational Radiation Exposure Report for Year 20232024-04-30030 April 2024 Occupational Radiation Exposure Report for Year 2023 L-24-018, Submittal of Core Operating Limits Report, Cycle 24, Revision 02024-04-16016 April 2024 Submittal of Core Operating Limits Report, Cycle 24, Revision 0 ML24089A2582024-04-0101 April 2024 Request for Information for the NRC Quuadrennial Comprehensive Engineering Team Inspection: Inspection Report 05000346/2024010 L-24-013, Annual Notification of Property Insurance Coverage2024-03-26026 March 2024 Annual Notification of Property Insurance Coverage ML24036A3472024-03-0707 March 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0076 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML24057A0752024-03-0101 March 2024 The Associated Independent Spent Fuel Storage Installations ML24057A3362024-02-28028 February 2024 Annual Assessment Letter for Davis-Besse Nuclear Power Station (Report 05000346/2023006) IR 05000346/20230062024-02-28028 February 2024 Re-Issue Annual Assessment Letter for Davis-Besse Nuclear Power Station (Report 05000346/2023006) L-23-264, Request for Exemption from 10 CFR 50.71(e)(4) Final Safety Analysis Report Update Schedule2024-02-23023 February 2024 Request for Exemption from 10 CFR 50.71(e)(4) Final Safety Analysis Report Update Schedule CP-202300502, Notice of Planned Closing of Transaction and Provision of Documents to Satisfy Order Conditions2024-02-23023 February 2024 Notice of Planned Closing of Transaction and Provision of Documents to Satisfy Order Conditions L-24-050, Retrospective Premium Guarantee2024-02-22022 February 2024 Retrospective Premium Guarantee IR 05000346/20243012024-02-0202 February 2024 NRC Initial License Examination Report 05000346/2024301 IR 05000346/20230042024-01-31031 January 2024 Integrated Inspection Report 05000346/2023004 ML23313A1352024-01-17017 January 2024 Authorization and Safety Evaluation for Alternative Request RP 5 for the Fifth 10 Year Interval Inservice Testing Program ML23353A1192023-12-19019 December 2023 Operator Licensing Examination Approval Davis Besse Nuclear Power Station, January 2024 L-23-260, Corrections to the 2022 Combined Annual Radiological Environmental Operating Report and Radioactive Effluent Release Report for the Davis-Besse Nuclear Power Station2023-12-0707 December 2023 Corrections to the 2022 Combined Annual Radiological Environmental Operating Report and Radioactive Effluent Release Report for the Davis-Besse Nuclear Power Station L-23-243, Independent Spent Fuel Storage Installation - Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-12-0606 December 2023 Independent Spent Fuel Storage Installation - Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23338A3172023-12-0606 December 2023 Notification of NRC Baseline Inspection and Request for Information; Inspection Report 05000346/2024001 IR 05000346/20234032023-11-0202 November 2023 Security Baseline Inspection Report 05000346/2023403 ML23293A0612023-11-0101 November 2023 Letter to the Honorable Marcy Kaptur, from Chair Hanson Responds to Letter Regarding Follow Up on Concerns Raised by Union Representatives During the June Visit to the Davis-Besse Nuclear Power Plant ML24045A0322023-10-26026 October 2023 L-23-221 Proposed Exam Submittal Cover Letter L-23-215, Changes to Emergency Plan2023-10-19019 October 2023 Changes to Emergency Plan ML23237B4222023-09-28028 September 2023 Energy Harbor Nuclear Corp. - Vistra Operations Company LLC - Letter Regarding Order Approving Transfer of Licenses and Draft Conforming License Amendments 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000346/LER-2021-001-01, Emergency Diesel Generator Speed Switch Failure Due to Direct Current System Ground2024-09-19019 September 2024 Emergency Diesel Generator Speed Switch Failure Due to Direct Current System Ground 05000346/LER-2022-002, Strong Winds Result in Ultimate Heat Sink Low Water Level2023-02-20020 February 2023 Strong Winds Result in Ultimate Heat Sink Low Water Level 05000346/LER-2022-001, Plant Heatup with Inoperable Decay Heat Pump Due to Oil Leak Induced by Constant Level Oiler2022-08-16016 August 2022 Plant Heatup with Inoperable Decay Heat Pump Due to Oil Leak Induced by Constant Level Oiler 05000346/LER-2021-003, Reactor Trip Due to Failed Uninterruptible Power Supply and Steam Feedwater Rupture Control System Actuations2021-09-0707 September 2021 Reactor Trip Due to Failed Uninterruptible Power Supply and Steam Feedwater Rupture Control System Actuations 05000346/LER-2017-0022017-11-27027 November 2017 Auxiliary Feed Water Pump Turbine Bearing Damaged due to Improperly Marked Lubricating Oil Sight Glass, LER 17-002-00 For Davis-Besse Nuclear Power Station, Unit 1, Regarding Auxiliary Feed Water Pump Turbine Bearing Damaged due to Improperly Marked Lubricating Oil Sight Glass 05000346/LER-2017-0012017-09-18018 September 2017 Emergency Diesel Generator Fuel Oil Storage Tank Vents Not Adequately Protected from Tornado-Generated Missiles, LER 17-001-00 for Davis-Besse, Unit 1, Regarding Emergency Diesel Generator Fuel Oil Storage Tank Vents Not Adequately Protected from Tornado-Generated Missiles 05000346/LER-2016-0082017-02-27027 February 2017 Application of Technical Specification for the Safety Features Actuation System Instrumentation, LER 16-008-01 for Davis-Besse Nuclear Power Station Unit 1 Regarding Application of Technical Specification for the Safety Features Actuation System Instrumentation 05000346/LER-2016-0092016-11-0909 November 2016 Reactor Trip due to Rainwater Intrusion and Auxiliary Feedwater Actuation on High Steam Generator Level, LER 16-009-00 for Davis-Besse Nuclear Power Station, Unit 1 Regarding Reactor Trip due to Rainwater Intrusion and Auxiliary Feedwater Actuation on High Steam Generator Level 05000346/LER-2016-0072016-08-22022 August 2016 Pressurizer Code Safety Valve Setpoint Test Failures, LER 16-007-00 for Davis-Besse, Unit 1 Regarding Pressurizer Code Safety Valve Setpoint Test Failures 05000346/LER-2016-0062016-08-15015 August 2016 Potential to Trip Emergency Diesel Generator on High Crankcase Pressure, LER 16-006-00 for Davis-Besse Nuclear Power Station Unit 1 RE: Potential to Trip Emergency Diesel Generator on High Crankcase Pressure 05000346/LER-2016-0052016-07-11011 July 2016 - , Plant Startup with Anticipatory Reactor Trip System in Main Turbine Bypass, LER 16-005-00 for Davis-Besse, Unit 1, Regarding Plant Startup with Anticipatory Reactor Trip System in Main Turbine Bypass 05000346/LER-2016-0042016-06-0606 June 2016 Reactor Coolant System Hot Leg Resistance Temperature Detector Wire Insulation Degradation, LER 16-004-00 for Davis-Besse Nuclear Power Station, Unit 1 Regarding Reactor Coolant System Hot Leg Resistance Temperature Detector Wire Insulation Degradation 05000346/LER-2016-0032016-05-31031 May 2016 Leak from Reactor Coolant Pump Seal Piping Flexible Hose due to Undetected Manufacture Weld Defect, LER 16-003-00 for Davis-Besse Nuclear Power Station, Unit 1 Regarding Leak from Reactor Coolant Pump Seal Piping Flexible Hose due to Undetected Manufacture Weld Defect 05000346/LER-2016-0022016-03-29029 March 2016 Unanticipated Steam and Feedwater Rupture Control System Actuation, LER 16-002-00 for Davis-Besse Nuclear Power Station, Unit 1, Regarding Unanticipated Steam and Feedwater Rupture Control System Actuation 05000346/LER-2016-0012016-03-29029 March 2016 1 OF 7, LER 16-001-00 for Davis-Besse Nuclear Power Station Unit 1 Regarding Reactor Trip During Nuclear Instrumentation Calibrations and Steam Feedwater Rupture Control System Actuation on High Steam Generator Level ML0409003422004-03-26026 March 2004 LER 97-004-01 for Davis-Besse, Unit 1 Regarding Reactor Coolant Pump Motor Oil Piping Not Protected from Leakage as Required Per 10CFR50, Appendix R ML0404901932004-02-13013 February 2004 LER 99-003-01 for Davis-Besse, Unit 1 Regarding Failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding Technical Specification Limit ML0331701982003-11-0707 November 2003 LER 98-002-01 for Davis-Besse Unit 1 Regarding Plant Trip Due to High Pressurizer Level as a Result of Loss of Letdown Capability 2024-09-19
[Table view] |
Reported lessons learned are incorporated into the licensing process and fed back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
System Description:
The Davis-Besse Nuclear Power Station (DBNPS) Steam and Feedwater Line Rupture Control System (SFRCS) [JB] is a protection system that initiates the Auxiliary Feedwater System (AFW) [BA] and isolates the affected Steam Generator (SG) [AB-SG] on a steam or feedwater line rupture. The SFRCS is required to ensure an adequate feedwater supply to the steam generators to, remove reactor decay heat during periods when the normal feedwater supply and/or the electric power supply to essential auxiliaries has been lost. The design of the SFRCS is to mitigate release of high energy steam, to automatically start the AFW System in the event of a main steam line or Main Feedwater (MFW) line rupture, or on the loss of both main feed pumps [SJ-P] or the loss of all four Reactor Coolant Pumps (RCPs) [AB-P], and to prevent steam generator overfill and subsequent spillover into the main steam lines. The SFRCS also provides a trip signal to the Anticipatory Reactor Trip System (ARTS). In the event of a main steam line rupture, the SFRCS will close both Main Steam Isolation Valves (MSIVs) [SB-ISV] and all MFW control [SJ-LCV] and stop valves [SJ-ISV] and trip the main turbine [TA-TRB].
A loss of normal feedwater is sensed by monitoring the differential pressure across the main feedwater check valves. On a high reverse differential pressure, the SFRCS opens the steam supply from either steam generator to either auxiliary feedwater pump turbine and aligns the auxiliary feedwater pump to its associated steam generator. SFRCS also isolates MFW, main steam, and trips the reactor and the main turbine. On a reduced steam generator(s) inventory, the SFRCS responds similarly, with the exception that MFW and main steam will not be isolated.
DESCRIPTION OF EVENT:
On January 29, 2016, at 1322 hours0.0153 days <br />0.367 hours <br />0.00219 weeks <br />5.03021e-4 months <br />, the DBNPS experienced a reactor trip and subsequent SFRCS actuation on SG 1 High Level. This resulted in various automatic actions, including the isolation of MFW to the SGs and starting both trains of AFW. The Plant was stable in Mode 3 with the AFW System providing AFW to the SGs, as designed. Refer to LER 2016-001 for more information on the January 29, 2016 events.
On January 30, 2016, with the plant remaining in Mode 3, Operations personnel were proceeding with Post Trip recovery actions using procedure DB-OP-06910, Trip Recovery, to transition from AFW to MFW supplying feedwater to the SGs. The Motor Driven Feedwater Pump (MDFP) was started and operated on minimum recirculation flow back to the Deaerator. The MDFP discharge flowpath was then aligned to the MFW system to refill and pressurize the downstream MFW header through the individual Minimum Bypass Throttle Valves (FW139, FW44) up to the closed MFW Isolation Valves (FW612, FW601). The MDFP continued to deliver feedwater to the MFW header establishing a stable FW pressure upstream of the Minimum Bypass Throttle Valves (FW139, FW44). The MDFP flow remained steady at approximately 12-15 gallons per minute for approximately 5 minutes. In accordance with procedure DB-OP-06910, Operations personnel verified MFW pressure upstream of the Minimum Bypass Throttle Valves (FW139 and FW44) was greater than SG pressure. MFW to SG 2 Isolation Valve (FW601) was opened and in approximately 1 minute, MFW to SG 1 Isolation Valve (FW612) was opened. This resulted in a reverse delta pressure indication across the MFW check valve at 0123 hours0.00142 days <br />0.0342 hours <br />2.03373e-4 weeks <br />4.68015e-5 months <br /> as MFW to SG 1 Isolation Valve (FW612) was opened, resulting in an automatic actuation of the SFRCS Reported lessons learned are incorporated into the licensing process and fed back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB,10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
on High Reverse Differential Pressure and realignment of several valves in the Main Steam Feedwater System as designed. AFW continued to operate throughout the event and the Plant was verified to be stable.
CAUSE OF EVENT
The direct cause of the event was insufficient pressure in the piping upstream of the MFW to SG 1 Check valve (FW147), resulting in the SFRCS Actuation. When MFW to SG 1 Isolation Valve (FW612) was opening, the downstream SG pressure of approximately 870 pounds per square inch gauge (psig) was immediately applied to the downstream side of MFW to SG 1 Check Valve (FW147), developing greater than 125 pounds per square inch differential (psid) reverse DP, thus causing the SFRCS SG 1 High Reverse DP trip. The unexpected SFRCS SG 1 High Reverse D/P trip resulted in the reclosure of affected valves, including the MFW Isolation Valves, as designed. The AFW Pumps remained in operation, as expected. The MDFP remained operating aligned to the MFW Header and continued to pressurize the piping between the FW Heaters up to the MFW Isolation Valves.
The apparent cause of the event is that less than adequate procedural guidance is contained in procedure DB-OP-06910, Trip Recovery. The guidance in this procedure was inadequate to ensure that the MFW piping segment between MFW Bypass Throttle Valve (FW139) and MFW to SG 1 Isolation Valve (FW612) was sufficiently pressurized prior to opening MFW to SG 1 Isolation Valve (FW612)..
ANALYSIS OF EVENT
The SFRCS is a protection system required to actuate AFW to the SG's to remove reactor decay heat during periods when normal feedwater supply has been lost and/or upon loss of power to the RCP motors. Crossover piping exists that may be used to direct feedwater from either AFW source to either SG. The SFRCS also functions to isolate steam and main feedwater lines to mitigate overcooling events caused by steam depressurization:
At the time of the event, the AFW System was operating and feeding the Steam Generators. The unit remained in Mode 3 and stable. This actuation did not have any negative impact to the AFW system and the ability to feed the steam generators.
A bounding quantitative evaluation of risk impact was performed, using best available information, which estimated the delta Core Damage Frequency (CDF) to be 4.9E-07/yr. Based on this analysis, this event is considered to have a very low safety significance.
Reportability Discussion:
The Auxiliary Feedwater System by the SFRCS on a valid reverse differential pressure is reportable within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> of the event in accordance with 10 CFR 50.72(b)(3)(iv)(A). This notification was completed at 07:32 on January 30, 2016 (Event Number 51702). The receipt of an actuation signal of the Auxiliary Feedwater System and the actuation/closure of several main steam system valves is reportable as a Licensee Event Report per 10 CFR 50.73(a)(2)(iv)(A). All safety systems performed as required in response to the event, and no loss of safety function occurred.
Reported lessons learned are incorporated into the licensing process and fed back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
SEQUENTIA
- 002 00
CORRECTIVE ACTIONS
Procedure, DB-OP-06910, Trip Recovery, will be revised to add the requirement to verify that the, pressure in SG 1 (2) Feedwater piping segment between valves MFW to SG 1 Check Valves (FW139 and FW147) and MFW to SG 2 Check Valves (FW44 and FW156) exceeds SG 1 (2) steam pressure prior to opening MFW to SG 2 (SG 1) Isolation Valve FW612 (FW601). This verification will require the installation of a temporary pressure indicator(s).
PREVIOUS SIMILAR EVENTS
Licensee Event Report (LER) 2015-002 documents the manual actuation of SFRCS in May 2015 to isolate a steam leak in the turbine building. LER 2016-001 documents the automatic actuation of SFRCS on January 29, 2016, in response to high SG levels following a reactor trip. There have been no LERs at the DBNPS involving an SFRCS reverse differential pressure trip in the past three years.
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05000346/LER-2016-001 | 1 OF 7 LER 16-001-00 for Davis-Besse Nuclear Power Station Unit 1 Regarding Reactor Trip During Nuclear Instrumentation Calibrations and Steam Feedwater Rupture Control System Actuation on High Steam Generator Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000346/LER-2016-002 | Unanticipated Steam and Feedwater Rupture Control System Actuation LER 16-002-00 for Davis-Besse Nuclear Power Station, Unit 1, Regarding Unanticipated Steam and Feedwater Rupture Control System Actuation | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000346/LER-2016-003 | Leak from Reactor Coolant Pump Seal Piping Flexible Hose due to Undetected Manufacture Weld Defect LER 16-003-00 for Davis-Besse Nuclear Power Station, Unit 1 Regarding Leak from Reactor Coolant Pump Seal Piping Flexible Hose due to Undetected Manufacture Weld Defect | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000346/LER-2016-004 | Reactor Coolant System Hot Leg Resistance Temperature Detector Wire Insulation Degradation LER 16-004-00 for Davis-Besse Nuclear Power Station, Unit 1 Regarding Reactor Coolant System Hot Leg Resistance Temperature Detector Wire Insulation Degradation | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2016-005 | - , Plant Startup with Anticipatory Reactor Trip System in Main Turbine Bypass LER 16-005-00 for Davis-Besse, Unit 1, Regarding Plant Startup with Anticipatory Reactor Trip System in Main Turbine Bypass | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2016-006 | Potential to Trip Emergency Diesel Generator on High Crankcase Pressure LER 16-006-00 for Davis-Besse Nuclear Power Station Unit 1 RE: Potential to Trip Emergency Diesel Generator on High Crankcase Pressure | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2016-007 | Pressurizer Code Safety Valve Setpoint Test Failures LER 16-007-00 for Davis-Besse, Unit 1 Regarding Pressurizer Code Safety Valve Setpoint Test Failures | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2016-008 | Application of Technical Specification for the Safety Features Actuation System Instrumentation LER 16-008-01 for Davis-Besse Nuclear Power Station Unit 1 Regarding Application of Technical Specification for the Safety Features Actuation System Instrumentation | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2016-009 | Reactor Trip due to Rainwater Intrusion and Auxiliary Feedwater Actuation on High Steam Generator Level LER 16-009-00 for Davis-Besse Nuclear Power Station, Unit 1 Regarding Reactor Trip due to Rainwater Intrusion and Auxiliary Feedwater Actuation on High Steam Generator Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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