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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20235X0861987-07-20020 July 1987 Ler:On 870618,in-core Detector Computer Points Inadvertently Removed from Scan.Caused by Personnel Error.Operator Removed Points While Intending to Restore Computer to Normal operation.In-core Detectors Returned to Scan 05000346/LER-1987-001, Errata to LER 87-001-00,correcting Incomplete Sentence on Page 21987-01-21021 January 1987 Errata to LER 87-001-00,correcting Incomplete Sentence on Page 2 ML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 05000346/LER-1984-003, Revised LER 84-003-01:on 840302,MSIV 2 Closed,Isolating Steam Side of Steam Generator 2.Caused by Failed Relay in Safety Instrumentation Channel.Msiv Replaced.Failed Relay Circuit Repaired1984-07-26026 July 1984 Revised LER 84-003-01:on 840302,MSIV 2 Closed,Isolating Steam Side of Steam Generator 2.Caused by Failed Relay in Safety Instrumentation Channel.Msiv Replaced.Failed Relay Circuit Repaired 05000346/LER-1984-001, Revised LER 84-001-01:on 840108,core Imbalanced Positively & Axial Power Shaping Rods Automatically Inserted.Caused by Large Difference in Amount of Xenon in Top of Core & Failed Integrated Circuit Gate,Respectively1984-03-29029 March 1984 Revised LER 84-001-01:on 840108,core Imbalanced Positively & Axial Power Shaping Rods Automatically Inserted.Caused by Large Difference in Amount of Xenon in Top of Core & Failed Integrated Circuit Gate,Respectively 05000346/LER-1982-045, Revised LER 82-045/03X-2:on 820904 & 1203,operator Observed Auxiliary Feedwater (AFW) Pump 1-1 Suction Valve FW786 Closed for No Apparent Reason.Valve Immediately Reopened1983-12-29029 December 1983 Revised LER 82-045/03X-2:on 820904 & 1203,operator Observed Auxiliary Feedwater (AFW) Pump 1-1 Suction Valve FW786 Closed for No Apparent Reason.Valve Immediately Reopened 05000346/LER-1981-061, Revised LER 81-061/03X-2:on 811003 & 20,absolute Position Indication on Group 4,rod 7 Became Erratic,Fluctuating 5-10% of Full Range.Caused by Loss of Electrical Penetration Module Signal.Module Replaced1983-12-29029 December 1983 Revised LER 81-061/03X-2:on 811003 & 20,absolute Position Indication on Group 4,rod 7 Became Erratic,Fluctuating 5-10% of Full Range.Caused by Loss of Electrical Penetration Module Signal.Module Replaced 05000346/LER-1983-036, Revised LER 83-036/03X-1:on 830715 & 21,safety Features Actuation Sys Channel 4 Containment Radiation Monitor RE2007 Failed Low.Caused by Detector failure.RE2007 Replaced1983-10-28028 October 1983 Revised LER 83-036/03X-1:on 830715 & 21,safety Features Actuation Sys Channel 4 Containment Radiation Monitor RE2007 Failed Low.Caused by Detector failure.RE2007 Replaced 05000346/LER-1982-059, Revised LER 82-059/03T-1:on 821108,containment post-accident Radiation Monitor Re 4597AA Channel 2 Discovered Reading Low.On 821116 & 22,equipment Fail Alarm Received on Re 4597AA.Caused by Failed High Voltage Power Supply Boar1982-12-15015 December 1982 Revised LER 82-059/03T-1:on 821108,containment post-accident Radiation Monitor Re 4597AA Channel 2 Discovered Reading Low.On 821116 & 22,equipment Fail Alarm Received on Re 4597AA.Caused by Failed High Voltage Power Supply Board 05000346/LER-1982-060, Revised LER 82-060/03T-1:on 821111,during Steam & Feedwater Sys (SFS) Rupture Control Monthly test,48-volt Dc Power Supply in SFS Channel 2 Failed.Caused by Component Failure. Channel 2 re-energized1982-12-15015 December 1982 Revised LER 82-060/03T-1:on 821111,during Steam & Feedwater Sys (SFS) Rupture Control Monthly test,48-volt Dc Power Supply in SFS Channel 2 Failed.Caused by Component Failure. Channel 2 re-energized ML20063K1681982-08-25025 August 1982 LER 77-ZZZ/01T-3:on 770805,3-inch Pressurizer power-operated Relief Valve Opened & Severe Movement of 8-inch Discharge Piping Observed.Caused by Failure to Maintain Relief Inlet Loop Seal Temp to Ensure Complete Water to Steam Flashing 05000289/LER-1977-016, Supplemental LER 77-016/01T:on 770924,emergency Core Cooling Actuation Occurred.Caused by Full Open Pressurizer Power Relief Valve.Valve Closed1977-02-14014 February 1977 Supplemental LER 77-016/01T:on 770924,emergency Core Cooling Actuation Occurred.Caused by Full Open Pressurizer Power Relief Valve.Valve Closed 1987-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML20249A4121998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20196B5221998-05-23023 May 1998 10CFR50.59 Summary Rept of Facility Changes,Tests & Experiments Dbnps,Unit 1 for 960602-980523 ML20236E7581998-05-19019 May 1998 Rev 0 to Davis-Besse Unit 1 Cycle 12 Colr ML20236N7501998-04-30030 April 1998 Rev 2 to Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit ML20247F6721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Davis-Bess Nuclear Power Station,Unit 1 ML20249A4141998-04-30030 April 1998 Revised Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20217P8041998-04-0707 April 1998 11RFO OTSG ECT Insp Scope ML20216B4041998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216C5131998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20202D3721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20199G6321998-01-26026 January 1998 Rev 1 to Davis-Besse Unit 1,Cycle 11,COLR ML20198R4771998-01-13013 January 1998 SER Approving Second 10-year Interval Inservice Inspection Program Plan Requests for Relief for Davis-Besse Nuclear Power Station,Unit 1 ML20198K7931997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20217K6401997-12-31031 December 1997 1997 Annual Rept First Energy ML20203A3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Davis-Besse Nuclear Power Plant,Unit 1 ML20198S5371997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Davis-Besse Nuclear Power Station ML20217H7701997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20216H3261997-08-31031 August 1997 Monthly Operating Rept for August 1997 for DBNPS ML20217K0241997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Davis Besse Nuclear Power Station,Unit 1 1999-09-30
[Table view] |
LER-2084-001, Revised LER 84-001-01:on 840108,core Imbalanced Positively & Axial Power Shaping Rods Automatically Inserted.Caused by Large Difference in Amount of Xenon in Top of Core & Failed Integrated Circuit Gate,Respectively |
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3462084001R00 - NRC Website |
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i MNIC Foren 384 U S. NELEAR KEGULATORY COMMES$60N
"" APPROVED Oue NO 3150-4104 5""* 5 84' '85 LICENSEE EVENT REFORT (LER)
FACILITY NAME (Il DOCKET NUMBER (28 PAGE43)
Davis-Besse Unit 1 o 15 l 0 l0 l 0 l 3l4 16 1 l0Fl O! 3 14 fliNeactor trip caused by autcmatic insertion of Axial Power Shaping Rods AYENT DATE (51 LE R NUMBE R 161 REPORT DATE 17) OTHER F ACILITIES INVOLVED (4#
MONTH DAY YEAR YEAR IE '
- 8 MONTH DAY YEAR F ACILIT V N AwfS DOCKET NUMeERis) 0 15101010 1 1 I 0 lt 0l8 8 4 8 l4 0l0l1 0l1 0 l3 2l9 8 l4 o isto l0 tol l l OPE R ATING TH18 REPORT IS SUSMITTED PURSUANT TO THE REOUIREMENTS OP 10 CPR {. (Chere one or more of rae renewest 1118 MOOE m 1 20 402M 20 406(el SX 00.73'eH2Het 73 71141 POWER 20 406teH111d 60 3eleH1) 50.738eH2Het 73.7118)
SEOP O 14 i 6 20 0steH1H., so3si. m s0.73.H2H,ei
_ guEgsggAg 20 406falt1H6hl 50 73tel(2ibt 50.73taH2HendHAl JudA1 20 406teH1Hivl 50.734s H2 H W) 80 731sH2Hvii6H01 20 4064eH1Het 60.73teH2 Heel to.73(all2Hal LICENSEE CONTACT FOR TMit LER (12)
NAME TELEPHONE NUMBER ARE A CODE John D. Swartz 4 ;1,9 2i 5i 9l g5l0g0l0 COMPLETE ONii LINE FOR EACH COMPONENT F AILURE DESCR' SED IN TH18 REPORT (13i i
"A "A% E CAUSE SYSTEM COMPONENT R' O NPROg CAUSE $YSTEM COMPONENT .
f TU g 'h'O NPR X RlB 16 l9 Ml4 i5 i 5 Y i t i l i t l I I I I I I I I I I I I I SUPPLEMENTAL REPORT E RPECTED (148 MONTM DAY YEAR
$U8 MISSION
\ ES {!r yn como.re EXPTCTEn SUBVI55 TON DA TEI NC l l l AanR ACT ,t.m., ,,1ax roa. . . ..m.r.o.,r . .a. n , a. i o e, Due to a condenser tube leak, reactor power was reduced to 46%. Operators borated the Reactor Coolant System to minimize the normal negative imbalance caused by the rod insertion during the power reduction. When core imbalance turned around and became positive due to rod withdrawal and Xeron, operators added deminerclized water i to the RCS to allow rods to insert. Due to a failure in the Control Rod Drive Control System, the operators could not operate the Axial Power Shaping Rods to help reduce the positive core imbalance, and the Axial Power Shaping Rods inserted without command. The imbalance as read by the out-of-core detectors was much greater tha 1 the imbalance as read by the incore detectors. The apparent reason for g the out-of-core detectors reading rusch greater than the more accurate incore detectors is because the out-of-corcs are calibrated to irnbalance caused by an Axial Power Shaping Rod movement. The positive core irrbalance increased to the Reactor Protec-tion System flux /de lta flux / flow setpoint, and the reactor tripped about 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after reducing power to 46%. The Control Rod Drive Control System problem was due to a faulty logic card which was later repaired.
8404120334 840329 DRADOCK05000g Q_h h h N~C Peres Joe 19 8U
' NRC Fem 3640 0 S. NUCLEOR REGULOTORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO Ove NO 3150-0104 E APtRES 8'31 BS E U3 DOCKET NUM8ER L21 g gg YEA" w [a v, a Davis-Besse Unit 1 015101010l3l4l6 8I4 --
0 l 0l1 --
011 0l2 oF 0 13 "Te~TcEf*p"tTE"of"ffEcIfrEEnTe?"On January 8 , 1984, the unit was operating at approxi-mately 100% power. At 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br />, high c.nductivity alarms of the condensate discharging from the polishers were received by Control Room operators, and a i reduction in power to 50% was commenced at a rate of 1/3% per minute, eventually reaching 46%.
As the Integrated Control System (ICS) reduced reactor power, regulating Group 7 rods inserted into the core, and the core imbalance went from -2% to a maximum negative imbalance of -10% as measured by the out-of-core detectors. The more accurate incore detector system read -8%. The imbalance remained at approximately
-8% for approximately one hour.
I
- In response to the Xenon buildup, the control rods withdrew to a maximum value of 91% withdrawn at 2115 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.047575e-4 months <br />. During the 1.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period of rod withdrawal, the core imbalance increased to +20% by out-of-cores (+10% by incores) due to both rod withdrawal and the relative burnout of Xenon in the top of the core as compared to the bottom. To limit rod withdrawal, the operator began adding demineralized water at 1955 hours0.0226 days <br />0.543 hours <br />0.00323 weeks <br />7.438775e-4 months <br />. The control rod insertion (due to the water added) was not enough to completely stop the increase on imbalance.
1 Approximately eight minutes prior to the trip, the Axial Power Shaping Rods (APSR) were selected to be withdrawn, however, the rods automatically started inserting.
The Reactor Operator stopped the insertion by selecting a different group of regulat-ing rods.
The reactor tripped at 2318 hours0.0268 days <br />0.644 hours <br />0.00383 weeks <br />8.81999e-4 months <br /> on Reactor Protection System (RPS) flux / delta flux / flow. At this time, the out-of-core detectors, which the RPS looks at, were indicating an imbalance of approximately +24%. The incore detectors were indicating an imbalance of approximately +12%. This event is reportable under 10CFR50.73(a)(2)
(iv), Automatic Actuation of RPS.
Designation of Apparent Cause of Occurrence: The cause of the positive imbalance was due to the large difference in the amount of Xenon in the top of the core as compartd to the bottom. The apparent reason for the out-of-core detectors reading much greater than the more accurate incore detectors is because the out-of-cores are calibrated to imbalance caused by an APSR movement. The imbalance caused by APSR movement is more conservative than any combination of Xenon, Group 7, or APSRs.
Therefore, the reactor trip imbalance setpoint is always conservative.
The cause of the APSR in motion, without a manual command, was found to be a failed integrated circuit gate on system logic module C6 (IC2). The fault caused a con-stant manual "in" command, which when Group 8 was selected, resulted in the APSR group run in.
Analysis of Occurrence: The RPS acted as designed, tripping the reactor when the flux / delta flux / flow setpoint was reached on the out-of-core detectors. A reactor g trip would have occurred earlier in the event if the plant would have been at a higher power during the imbalance swing due to a tighter RPS operating envelope on flux / delta flux / flow.
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MRC Form 3000 U S NUCLEGR REGULOTORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION arraoveo ove No. siso-cio.
EXPIRES 8131 1 5 FOCILITY NAME III DOCK E T FwuM8 E R GI ggggg pg g YIA" '
v 6m
~
V6
- Davis-Besse Unit 1 01510 l0 l0 l3 l 4l 6 8 l4 -
0 l Ol 1 -
0 l1 0 l3 OF 0 l3
"EEclTiEratToTTY$756Ei"of-core detector imbalance to an imbalance caused by APSR I movement is more conservative than any combination of Xenon, Group 7, or APSRs.
Therefore, the reactor trip imbalance setpoint is always conservative.
Corrective Action: On January 9, 1984 at 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br />, Instrument and Control Mechan-ics repaired the faulty system logic card under Maintenance Work Order 1-84-0102-00.
The group was tested satisfactorily and declared operable at 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br /> on January 9, 1984. Toledo Edison personnel will work with Babcock & Wilcox to investigate the
, possibility of reducing some of the excess conservatism in out-of-core imbalance 1
indication.
I Failure Data: This is the first failure of this type system logic module.
1 Report No: NP-33-84-01 DVR No(s): 84-001 1
i geo.wa..
d TOLEOO
%m EDISON March 29, 1984 Log No. K84-355 File: RR 2 (NP-33-84-01)
Docket No. 50-346 License No. NPF-3 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555 Gentlemen:
Enclosed is Revision 1 to Licensee Event Report 84-001, which is being submitted in accordance with 10CFR50.73. The revisions to the report are indicated by a "1" in the left margin of each page.
The system code for component failures was taken from the old LER instruc-tion book since the new IEEE-805 is not yet available.
Yours truly, 4h Terry D. Murray Station Superintendent Davis-Besse Nuclear Power Station TDM/lj k Enclosure cc: Mr. James G. Keppler, Regional Administrator, USNRC Region III Mr. Walt Rogers DB-1 NRC Renident Inspector JCS/001 %
THE TOLEDO EDISON COMPANY EDISON PLAZA 300 MADISON AVENL'E TOLEDO, OHIO 43052 i
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05000346/LER-1984-001, Revised LER 84-001-01:on 840108,core Imbalanced Positively & Axial Power Shaping Rods Automatically Inserted.Caused by Large Difference in Amount of Xenon in Top of Core & Failed Integrated Circuit Gate,Respectively | Revised LER 84-001-01:on 840108,core Imbalanced Positively & Axial Power Shaping Rods Automatically Inserted.Caused by Large Difference in Amount of Xenon in Top of Core & Failed Integrated Circuit Gate,Respectively | | 05000346/LER-1984-003, Revised LER 84-003-01:on 840302,MSIV 2 Closed,Isolating Steam Side of Steam Generator 2.Caused by Failed Relay in Safety Instrumentation Channel.Msiv Replaced.Failed Relay Circuit Repaired | Revised LER 84-003-01:on 840302,MSIV 2 Closed,Isolating Steam Side of Steam Generator 2.Caused by Failed Relay in Safety Instrumentation Channel.Msiv Replaced.Failed Relay Circuit Repaired | |
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