05000346/LER-2005-001

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LER-2005-001, Inadvertent Loss of Essential Bus and Start of Emergency Diesel Generator During Testing
Docket Numbersequential Rev
Event date: 01-13-2005
Report date: 03-14-2005
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
Initial Reporting
ENS 41330 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
3462005001R00 - NRC Website

DESCRIPTION OF OCCURRENCE:

On January 13, 2005, with the Davis-Besse Nuclear Power Station (DBNPS) in Mode 1 operating at approximately 100 percent power, surveillance testing was in progress utilizing procedure DB-ME­ 03046, "D1 Bus Under Voltage Units Monthly Functional Test" (Revision 06 dated May 5, 2004). This procedure performs a monthly functional check of the Safety Features Actuation System (SFAS) [JE] undervoltage units for Essential 4160 Volt Bus D1 [EB] in accordance with Technical Specification Surveillance Requirements 4.3.2.1.1, Table 4.3-2. This procedure functionally checks the Essential Bus Feeder Breaker Trip at 90 percent voltage and the Emergency Diesel Generator [EK-DG] Start and Load Shed at 59 percent voltage.

Power to the two 4160 Volt Essential Buses Cl and D1 is normally supplied from the 4160 V non­ essential Buses C2 and D2 [EA], respectively. The non-essential buses are normally powered from either the Unit Auxiliary Transformer [EL-XFMR] (when the Turbine-Generator is on-line) or from one of two Startup Transformers [FK-XFMR]. Bus tie transformers [EA-XFMR] step down the voltage from 13.8 kV to supply power to the non-essential 4160 V buses (all voltages listed are nominal voltage).

Two redundant Emergency Diesel Generators (EDGs) provide onsite standby sources to supply their respective 4160 Volt Essential Buses. If essential bus voltage is not maintained, the undervoltage relays [EB-27] set at approximately 90 percent of nominal bus voltage automatically initiate isolation of the essential bus following a brief time delay of several seconds. The loss of voltage relays set at approximately 59 percent of nominal bus voltage automatically initiate load shedding and EDG starting after a very short time delay. If an actuation of the SFAS occurs in conjunction with the loss of voltage, the sequencer will automatically load the bus.

During the undervoltage functional test being performed on January 13, 2005, the individual performing the test was inserting a test lead as directed by the procedure terminated with an unshielded male banana plug into an open barrel of a test lug. The opposite end of the test lead was properly connected to a grounded test equipment jack. Due to the location of the equipment (approximately six inches above floor level), the individual was working in a crouched/kneeling position and reaching into a tight space near the floor. To identify the proper test lug, he pointed to the lug with his left hand and received a peer check that the lug was the proper one. At approximately 0849 hours0.00983 days <br />0.236 hours <br />0.0014 weeks <br />3.230445e-4 months <br />, while moving the test lead towards the test lug, the individual inadvertently touched the test lead to an open, energized knife switch that was in close proximity. When the test lead contacted the protruding blade of the knife switch, the energized D1 bus monitoring circuit was shorted to ground, causing the circuit's fuse to clear (blow) due to high current. The blown fuse caused a loss of voltage input to the 59% loss of voltage relays for Essential Bus D1, which then actuated to trip the feeder breakers supplying the bus and fast­ started EDG 2.

Following the start of EDG 2 and the closing of its output breaker to reenergize Essential Bus D1, operators noted that Bus D1 voltage was reading low, Component Cooling Water Pump 2 Motor [CC- MO] current was indicating lower than expected, and Service Water Pump 2 [BI-P] did not start.

Because EDG 2 was operating without its ultimate source of cooling water along with the indications that Bus D1 voltage was approximately 1500 Volts, an emergency shutdown of EDG 2 was performed.

The shutdown of EDG 2 resulted in de-energization of Essential Bus Dl.

DESCRIPTION OF OCCURRENCE (continued):

The de-energization of Essential Bus D1 resulted in the following Technical Specification (TS) equipment being rendered inoperable because neither normal or emergency power was available:

  • Emergency Core Cooling Subsystem Train 2, including High Pressure Injection Pump 2 and Decay Heat/Low Pressure Injection Pump 2 (TS 3.5.2)
  • Containment Isolation Motor-Operated Valves (TS 3.6.3.1)

The de-energization of Essential Bus D1 caused the de-energization of 480 V Bus Fl [EC-BU] that, in turn, resulted in a loss of power to Station Batteries 2N and 2P battery chargers [EJ-BYC]. While DC loads remained energized from the Station Batteries 2N and 2P [EJ-BTRY], the loss of power to both battery chargers resulted in the plant being outside the Limiting Condition for Operation of TS 3.8.2.3, therefore TS 3.0.3 was entered at 0849 hours0.00983 days <br />0.236 hours <br />0.0014 weeks <br />3.230445e-4 months <br />, which required initiation of a plant shutdown within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of occurrence. At 0949 hours0.011 days <br />0.264 hours <br />0.00157 weeks <br />3.610945e-4 months <br />, a plant shutdown was initiated as required by Technical Specification 3.0.3.

A problem solving and decision making team was formed to investigate the event. The investigation discovered the blown secondary side Potential Transformer (PT) fuse. The fuse was replaced and Essential Bus D1 was reenergized at 1049 hours0.0121 days <br />0.291 hours <br />0.00173 weeks <br />3.991445e-4 months <br />. With power restored to the Station Battery Chargers, TS 3.0.3 was exited at 1051 hours0.0122 days <br />0.292 hours <br />0.00174 weeks <br />3.999055e-4 months <br />, and the plant shutdown was terminated at approximately 96 percent power. Service Water Pump 2 was then restarted.

With the restoration of power to the battery chargers, Station Batteries 2N and 2P were placed on equalizing charge at 1208 hours0.014 days <br />0.336 hours <br />0.002 weeks <br />4.59644e-4 months <br />. After approximately an hour on equalizing charge, Batteries 2N and 2P were placed on a float charge and verified that the charging current was less than 2 amperes. The batteries were then declared operable and TS 3.8.2.3 was exited at 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br />.

Follow-on review of this event determined that TS 3.0.3 should not have been exited when power was restored to the Station Battery Chargers at 1051 hours0.0122 days <br />0.292 hours <br />0.00174 weeks <br />3.999055e-4 months <br />. At this time Batteries 2N and 2P had a less than full charge, and therefore the requirements of TS 3.8.2.3 Action b, which requires no more than one battery to be inoperable, were still not met. However, had the plant remained in TS 3.0.3, the next required action was for the plant to be in Mode 3 within six hours of initiating the plant shutdown, or at 1549 hours0.0179 days <br />0.43 hours <br />0.00256 weeks <br />5.893945e-4 months <br />. Because Station Batteries 2N and 2P were returned to Operable status at 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br />, TS 3.0.3 would have been exited prior to the plant being required to be in Mode 3 (1549 hours0.0179 days <br />0.43 hours <br />0.00256 weeks <br />5.893945e-4 months <br />), therefore no violation of TS 3.0.3 occurred.

DESCRIPTION OF OCCURRENCE (continued):

Initial notification of this initiation of a plant shutdown required by the Technical Specifications was made to the NRC at 1332 hours0.0154 days <br />0.37 hours <br />0.0022 weeks <br />5.06826e-4 months <br /> on January 13, 2005, in accordance with the four-hour reporting requirement of 10CFR50.72(b)(2)(i) (Event Number 41330). Notification of the valid actuation of an Emergency Diesel Generator was also made at this time in accordance with the eight-hour reporting requirement of 10CFR50.72(b)(3)(iv)(A). This report is being submitted in accordance with the 10CFR50.73(a)(2)(iv)(A) as an event that resulted in automatic actuation of an Emergency Diesel Generator.

APPARENT CAUSE OF OCCURRENCE:

The cause of Essential Bus D1 de-energizing was the clearing of a potential transformer fuse when the test lead contacted the potential transformer circuit, grounding the circuit. Clearing the potential transformer fuse caused the Essential Bus D1 undervoltage relays to actuate, causing the opening of the Essential Bus D1 Supply Breaker, de-powering the Bus, and starting EDG 2.

The plant was relying on a single human action (being careful) to prevent the event from occurring.

Changes had not been made to remove the potential for de-powering the Essential 4160 V Buses by grounding the potential transformers during testing. Improvements in test leads were made in the past by recommending the use of test plugs and jacks instead of using test leads with alligator-style clip or mini-grabber connectors. However, due to the unavailability of shielded test plugs that would connect with the installed jacks on Essential Buses Cl and D1, shielded test plugs were not being used for routine tests.

In addition, when a trip of the Fuel Handling Ventilation System [VG] occurred in 2001 due to the use of inadequate test leads (i.e., use of alligator-style clips), the resultant recommendation was to use only shielded connectors during activities where systems needed to be maintained for nuclear or personnel safety. However, this recommendation was not fully implemented for Essential Buses Cl and D1 because the shielded type of connectors could not be acceptably configured.

ANALYSIS OF OCCURRENCE:

There were no safety concerns identified during or as a result of this event. In accordance with the DBNPS policy of allowing work activities on only one train of safety equipment, equipment designated as train 1 was not affected from the de-energization of Essential Bus Dl. All off-site to on-site power sources remained energized during this event. With the exception of Service Water Pump 2, all train 2 equipment responded appropriately to the de-energization of Essential Bus Dl.

The failure of Service Water Pump 2 to start was a direct result of the event, in that the undervoltage relays were still tripped due to the cleared fuse when the pump received a signal to automatically start.

Following replacement of the cleared fuse, the Service Water Pump was started successfully.

A review of the associated circuits showed that the clearing of the potential transformer fuse would cause abnormal voltage readings for Essential Bus D1.

ANALYSIS OF OCCURRENCE (continued):

Investigation into the lower than expected current readings of Component Cooling Water Pump 2 Motor determined these to be the result of the motor ammeter sticking at the lower end of the indicating band.

No problems were encountered with the operation of the pump after power was restored to Essential Bus D1, and a notification to repair or replace this ammeter was generated. Because Component Cooling Water Pump 2 started and was operating after EDG 2 started, it provided cooling to EDG 2 during the approximately five minutes EDG 2 operated. Therefore, even though EDG 2 was shutdown because Service Water Pump 2 did not start to provide cooling water to the Component Cooling Water System that in turn would provide cooling water to EDG 2, based on a review of plant computer data no EDG operating temperature limits were exceeded. Performance of the EDG 2 Monthly Test later in the day on January 13, 2005 showed no problems with EDG 2.

Based upon the proper response of the affected equipment to the de-energization of Essential Bus D1, the short duration of time that train 2 equipment was unavailable until the cleared fuse was replaced, and the availability of train 1 equipment to respond to any actual event during this time frame, the de- energization of Essential Bus D1 had minimal safety significance.

CORRECTIVE ACTIONS:

The cleared Essential Bus D1 potential transformer fuse was replaced and Essential Bus D1 was re- energized at 1049 hours0.0121 days <br />0.291 hours <br />0.00173 weeks <br />3.991445e-4 months <br />. Equipment affected by the de-energization of Bus D1 was returned to service in accordance with plant procedures and Technical Specification requirements.

The station administrative procedure governing the conduct of maintenance will be revised to direct that test leads and jumpers that could affect a critical system function or have a significant plant impact should be protected from inadvertent contact by a combination of shielded plugs and/or two-part test leads/jumpers and/or insulated material. In applications where these types of test leads and jumpers cannot be used, the procedure will direct that a Condition Report be generated to determine appropriate compensatory measures or evaluation of acceptable risk. This action will eliminate the potential for inadvertent contact while establishing standards for the types of test leads and jumpers allowed to be used during testing activities.

Since the application of shielded plugs has not been successful for the test connection used during undervoltage relay testing, panel mounted shielded connections will be designed and installed to eliminate the potential for inadvertent contact for the test connections on the Essential Buses Cl and Dl. These connections will be installed during the next scheduled Essential Bus outages.

FAILURE DATA:

There have been no Licensee Event Reports at the DBNPS involving a de-energization of an Essential documented a loss of offsite power at the DBNPS due to degraded regional grid voltage where both EDGs started to re-energize the Essential 4160 V Buses). Three similar events occurred at the DBNPS involving de-energization of Essential 4160 V Buses during undervoltage relay testing in 1988, 1989, and 1990. Following these three events, plant equipment was modified to add a test block to allow better access to connection points and better connection points for.undervoltage relay testing.

However, these previously modified connections were not the connections involved in the January 13, 2005, test of the undervoltage relays.

Energy Industry Identification System (EDS) codes are identified in the text as [XX].

NP-33-05-001-00� CRs 2005-00219, 2005-00260