03-09-2016 | On November 23, 2015, at 0844 Eastern Standard Time, Sequoyah Nuclear Plant ( SQN) Unit 1 reactor was manually tripped due to plant parameters indicating that the Loop 3 Main Steam Isolation Valve ( MSIV) had started drifting in the closed direction. Prior to the reactor trip, the open light indication on the main control board for the Loop 3 MSIV was noted to be extinguished. The light bulb was replaced with no change in indication. At the same time, the Post Accident Monitoring panel indicator for the Loop 3 MSIV displayed full open; however, within two to three minutes, the panel provided dual indication. Subsequently, Operators noted that the reactor coolant system temperature and Loop 3 Steam Generator ( SG) pressure were both rising, and the Loop 3 SG flow was lowering. These indications confirmed the Loop 3 MSIV was drifting closed. Following the reactor trip, all plant safety systems operated as designed, all control rods fully inserted, and auxiliary feedwater automatically initiated from the feedwater isolation signal, as expected. Troubleshooting identified a loose termination associated with the Loop 3 MSIV handswitch that would result in a slow loss of air pressure and cause the MSIV to slowly drift in the closed direction. The direct cause was determined to be a loose electrical connection on the MSIV handswitch. The root cause was determined to be inadequate work practices during replacement of the MSIV handswitch in 1994 that resulted in the loose electrical connection. The corrective action to prevent recurrence is revision of the work control planning procedure to ensure specific connection fastener torque values are utilized during work order planning. SQN Unit 2 was unaffected by this event. |
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Category:Letter
MONTHYEARCNL-24-021, Application to Revise Technical Specification Limiting Condition of Operation 3.5.2, ECCS – Operating, Note 1 to Include Residual Heat Removal Pump Flow Paths (SQN-TS-23-04 and WBN-TS-23-020)2024-11-12012 November 2024 Application to Revise Technical Specification Limiting Condition of Operation 3.5.2, ECCS – Operating, Note 1 to Include Residual Heat Removal Pump Flow Paths (SQN-TS-23-04 and WBN-TS-23-020) ML24312A1552024-11-0606 November 2024 Cycle 27 Core Operating Limits Report, Revision 1 IR 05000327/20240032024-11-0606 November 2024 Integrated Inspection Report 05000327/2024003 and 05000328/2024003 CNL-24-014, License Amendment Request to Revise the Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 Technical Specifications to Use Online Monitoring Methodology (SQN-TS-24-02 and WBN-TS-23-22)2024-11-0404 November 2024 License Amendment Request to Revise the Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 Technical Specifications to Use Online Monitoring Methodology (SQN-TS-24-02 and WBN-TS-23-22) ML24304A8492024-10-31031 October 2024 December 2024 Requalification Inspection Notification Letter IR 05000327/20250102024-10-29029 October 2024 Notification of Sequoyah, Units 1 and 2 - Comprehensive Engineering Team Inspection - U.S. Nuclear Regulatory Commission Inspection Report 05000327/2025010 and 05000328/2025010 ML24298A1172024-10-24024 October 2024 Cycle 26, 180-Day Steam Generator Tube Inspection Report CNL-24-074, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-10-23023 October 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions 05000327/LER-2024-001, Reactor Trip Due to a Turbine Trip2024-10-17017 October 2024 Reactor Trip Due to a Turbine Trip ML24282B0412024-10-15015 October 2024 Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 ML24260A1682024-10-0404 October 2024 Regulatory Audit Summary Related to Request to Add and Revise Notes Related to Technical Specification Table 3.3.2-1, Function 5 ML24284A1072024-09-26026 September 2024 Affidavit for Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2, and Watts Bar Nuclear Plant, Units 1 and 2 05000328/LER-2024-001, Reactor Trip Due to an Electrical Trouble Turbine Trip2024-09-25025 September 2024 Reactor Trip Due to an Electrical Trouble Turbine Trip CNL-24-047, Decommitment of Flood Mode Mitigation Improvement Systems2024-09-24024 September 2024 Decommitment of Flood Mode Mitigation Improvement Systems CNL-24-060, Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description2024-09-24024 September 2024 Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description ML24262A0602024-09-23023 September 2024 Summary of August 19, 2024, Meeting with Tennessee Valley Authority Regarding a Proposed Supplement to the Tennessee Valley Authority Nuclear Quality Assurance Plan ML24267A0402024-09-19019 September 2024 Cycle 27 Core Operating Limits Report Revision 0 CNL-24-065, Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-09-18018 September 2024 Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24185A1742024-09-18018 September 2024 Cover Letter - Issuance of Exemption Related to Non-Destructive Examination Compliance Regarding Sequoyah Nuclear Plant Independent Spent Fuel Storage Installation ML24253A0152024-09-0808 September 2024 Emergency Plan Implementing Procedure Revisions ML24247A2212024-08-29029 August 2024 Notification of Deviation from Pressurized Water Reactor Owners Group (PWROG) Letter OG-21-160, NEI 03-08 Needed Guidance: PWR Lower Radial Support Clevis Insert X-750 Bolt Inspection Requirements, September 1, 2021 ML24247A1802024-08-28028 August 2024 Application to Revise the Fuel Handling Accident Analysis, to Delete Technical Specification 3.9.4, Containment Penetrations, and to Modify Technical Specification 3.3.6, Containment Ventilation Isolation Instrumentation for Sequoyah Nuclea IR 05000327/20240052024-08-26026 August 2024 Updated Inspection Plan for Sequoyah Nuclear Plant, Units 1 and 2 - Report 05000327/2024005 and 05000328/2024005 ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 CNL-24-061, Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08),2024-08-19019 August 2024 Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08), IR 05000327/20240022024-07-31031 July 2024 Integrated Inspection Report 05000327/2024002 and 05000328/2024002 ML24211A0542024-07-29029 July 2024 Operator License Examination Report ML24211A0572024-07-29029 July 2024 Submittal of Emergency Plan Implementing Procedure Revision ML24211A0412024-07-26026 July 2024 Unit 1 Cycle 26 Refueling Outage - 90-Day Inservice Inspection Summary Report ML24199A0012024-07-22022 July 2024 Clarification and Correction to Exemption from Requirement of 10 CFR 37.11(c)(2) ML24172A1342024-07-15015 July 2024 Exemptions from 10 CFR 37.11(C)(2) (EPID L-2023-LLE-0024) - Letter ML24191A4652024-07-0909 July 2024 Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24177A0282024-06-25025 June 2024 Emergency Plan Implementing Procedure Revisions ML24176A0222024-06-24024 June 2024 Retraction of Interim Report of a Deviation or Failure to Comply – Transducer Model 8005N ML24089A1152024-06-21021 June 2024 Transmittal Letter, Environmental Assessments and Findings of No Significant Impact Related to Exemption Requests from 10 CFR 37.11(c)(2) ML24145A0852024-05-30030 May 2024 1B-B Diesel Generator Failure - Final Significance Determination Letter ML24145A1052024-05-29029 May 2024 301 Exam Approval Letter ML24134A1762024-05-13013 May 2024 Submittal of 2023 Annual Radiological Environmental Operating Report CNL-24-040, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-05-0808 May 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24128A0352024-05-0707 May 2024 Providing Supplemental Information to Apparent Violation ML24120A0582024-04-26026 April 2024 10 CFR 50.46 Annual Report for Sequoyah Nuclear Plant Units 1 and 2 ML24116A2612024-04-25025 April 2024 Interim Report of a Deviation or Failure to Comply - Transducer Model 8005N ML24114A0482024-04-23023 April 2024 Annual Radioactive Effluent Release Report for 2023 Monitoring Period CNL-24-037, Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Unit 1 and 2, Nuclear Quality Assurance Plan, TVA-NQA-PLN89-A, Revision 422024-04-22022 April 2024 Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Unit 1 and 2, Nuclear Quality Assurance Plan, TVA-NQA-PLN89-A, Revision 42 ML24144A2362024-04-20020 April 2024 Discharge Monitoring Report (Dmr), March 2024 ML24144A2322024-04-20020 April 2024 Tennessee Multi-Sector Permit (Tmsp), 2024 Annual Discharge Monitoring Report for Outfalls SW-3, SW-3, and SW-9 ML24102A1212024-04-18018 April 2024 Summary of Conference Call with Tennessee Valley Authority Regarding Sequoyah Nuclear Plant, Unit 1 Spring 2024 Steam Generator Tube Inspections ML24089A0882024-04-18018 April 2024 – Exemption from Select Requirements of 10 CFR Part 73; Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting IR 05000327/20240012024-04-17017 April 2024 Integrated Inspection Report 05000327/2024001 and 05000328/2024001 CNL-24-033, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-04-17017 April 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions 2024-09-08
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000327/LER-2024-001, Reactor Trip Due to a Turbine Trip2024-10-17017 October 2024 Reactor Trip Due to a Turbine Trip 05000328/LER-2024-001, Reactor Trip Due to an Electrical Trouble Turbine Trip2024-09-25025 September 2024 Reactor Trip Due to an Electrical Trouble Turbine Trip 05000328/LER-2023-001, Inoperable Ice Condenser Intermediate Deck Doors Results in Condition Prohibited by Technical Specifications2023-06-0707 June 2023 Inoperable Ice Condenser Intermediate Deck Doors Results in Condition Prohibited by Technical Specifications 05000327/LER-2022-002, Turbine Trip Function Inoperable Due to Slow to Close Turbine Throttle Valve2022-12-15015 December 2022 Turbine Trip Function Inoperable Due to Slow to Close Turbine Throttle Valve 05000327/LER-2022-001, Regarding Failure of 1B-B Centrifugal Charging Pump Results in Condition Prohibited by Technical Specifications2022-09-15015 September 2022 Regarding Failure of 1B-B Centrifugal Charging Pump Results in Condition Prohibited by Technical Specifications 05000328/LER-2021-002, Turbine Trio Function Inoperable Due to Slow to Close Turbine Throttle Valve2022-01-0606 January 2022 Turbine Trio Function Inoperable Due to Slow to Close Turbine Throttle Valve 05000327/LER-2021-003, Exceeded Breach Margin Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable2021-10-19019 October 2021 Exceeded Breach Margin Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable 05000328/LER-2021-001, Ice Bed Inoperable Due to Exceeding Surveillance Requirement Frequency2021-09-22022 September 2021 Ice Bed Inoperable Due to Exceeding Surveillance Requirement Frequency 05000327/LER-2021-001, Sequoya Nuclear Plant, Unit 1, Reactor Trip on High Neutron Flux Rate Due to Dropped Control Rods2021-07-21021 July 2021 Sequoya Nuclear Plant, Unit 1, Reactor Trip on High Neutron Flux Rate Due to Dropped Control Rods 05000328/LER-2020-001, Ice Bed Inoperable Due to Exceeding Maximum Allowed Ice Bed Temperature2020-09-16016 September 2020 Ice Bed Inoperable Due to Exceeding Maximum Allowed Ice Bed Temperature 05000327/LER-2020-002, Safety Injection Signal with Reactor Trip Caused by a Failure with the Main Turbine Control System2020-07-0101 July 2020 Safety Injection Signal with Reactor Trip Caused by a Failure with the Main Turbine Control System 05000327/LER-2019-003-01, 1 for Sequoyah Nuclear Plant, Unit 1, Automatic Reactor Trio Due to Negative Rate Trip as a Result of a Dropped Control Rod2020-04-25025 April 2020 1 for Sequoyah Nuclear Plant, Unit 1, Automatic Reactor Trio Due to Negative Rate Trip as a Result of a Dropped Control Rod 05000327/LER-2020-001-01, 1 for Sequoyah Nuclear Plant, Unit 1, Containment Vacuum Relief Lines Found Isolated2020-03-20020 March 2020 1 for Sequoyah Nuclear Plant, Unit 1, Containment Vacuum Relief Lines Found Isolated 05000327/LER-2019-004, Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board2020-02-13013 February 2020 Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board 05000328/LER-2019-002, Loss of Heater Drain Tank Flow Causes Turbine Runback and Manual Reactor Trip2020-02-0707 February 2020 Loss of Heater Drain Tank Flow Causes Turbine Runback and Manual Reactor Trip 05000327/LER-2017-0022017-07-14014 July 2017 Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board, LER 17-002-00 for Sequoyah, Unit 1, Regarding Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board 05000327/LER-2017-0012017-04-26026 April 2017 Breached Door Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable, LER 17-001-00 for Sequoyah, Unit 1, Regarding Breached Door Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable 05000327/LER-2016-0012016-04-11011 April 2016 Automatic Safety Injection due to Low Steam Line Pressure on Loop 2 Main Steam, LER 16-001-00 for Sequoyah, Unit 1, Regarding Automatic Safety Injection due to Low Steam Line Pressure on Loop 2 Main Steam 05000327/LER-2015-0042016-01-22022 January 2016 Manual Reactor Trip due to Main Steam Isolation Valve Drifting in the Closed Direction, LER 15-004-00 for Sequoyah, Unit 1, Regarding Manual Reactor Trip Due to Main Steam Isolation Valve Drifting in the Closed Direction 05000328/LER-2015-0022016-01-0606 January 2016 Unanalyzed Condition Due To Inoperable Containment Recirculation Drains, LER 15-002-00 for Sequoyah, Unit 2, Regarding Unanalyzed Condition Due to Inoperable Containment Recirculation Drains ML11276A1492011-09-30030 September 2011 Revised Submittal Schedule for Supplemental Report for License Event Report 327/2011-003, Unit I Reactor Trip as a Result of Turbine Control Card Failure ML11256A0162011-09-0606 September 2011 Withdrawal of License Event Report 327/2011-002, Feedwater Regulator Valve Inoperable ML0516403152005-06-0707 June 2005 LER 50-001-00 for Sequoyah, Unit 1 Re Automatic Reactor Trip Following Loss of Turbine Auto Stop Oil (ASO) Pressure ML0325804392003-09-0202 September 2003 LER 03-S01-00, Sequoyah Units 1 & 2, 30-Day Report Re Uncontrolled Security Weapon in the Protected Area 2024-09-25
[Table view] |
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I. Plant Operating Conditions Before the Event
At the time of the event, Sequoyah Nuclear Plant (SQN) Unit 1 reactor was operating at 100 percent rated thermal power (RTP). The condition described in this LER did not impact SQN Unit 2.
II. Description of Events
A. Event:
On November 23, 2015, at 0844 Eastern Standard Time (EST), SQN Unit 1 reactor was manually tripped due to plant parameters indicating that Loop 3 Main Steam Isolation Valve (MSIV) [EIIS Code SB] [EIIS Code ISV] had started drifting in the closed direction. Prior to the reactor trip, the open light indication [EIIS Code IL], on the main control room (MCR) panel for the MSIV was noted to be extinguished. The light bulb was replaced with no change in indication. At the same time, the Post Accident Monitoring (PAM) indicator for the MSIV displayed full open; however, within two to three minutes dual indication (mid-position) was provided. Subsequently, operators noted that the reactor coolant system (RCS) [EIIS Code AB] temperature and Loop 3 Steam Generator (SG) [EIIS Code SG] pressure were both slowly rising, and the Loop 3 SG flow was slowly lowering. These indications confirmed the Loop 3 MSIV was slowly drifting closed. Operators placed the handswitch [EIIS Code HS] for the MSIV in the open position for approximately 5 seconds. This resulted in no apparent affect. Operators manually tripped the reactor per procedure.
After the reactor trip, it was noted that all three lights on the MCR panel for the MSIV (closed, 10 percent closed, and open) illuminated followed by an immediate return to full open indication.
Additionally, PAM indication confirmed the MSIV was full open.
Troubleshooting identified a loose nut on a termination for the handswitch associated with the Loop 3 MSIV. The loose nut on the terminal could cause intermittent power through the circuit, which could cause flickering indicator lights and intermittent power to the solenoid. The loss of a single source of power to the solenoid could cut off the air supply to the MSIV, but not completely open the vent. This could result in a slow loss of air pressure and cause the Loop 3 MSIV to slowly drift in the closed position.
All plant safety related equipment operated as designed, all control rods fully inserted, and auxiliary feedwater (AFVV) [EIIS Code BA] automatically initiated from the feedwater isolation signal, as expected. No complications were experienced during the reactor trip.
This event is' reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A), as an event that resulted in a manual or automatic actuation of the Reactor Protection System and the Auxiliary Feedwater System.
B. Status of structures, components, or systems that were inoperable at the start of the event and contributed to the event:
There were no inoperable structures, components, or systems that contributed to this event.
C. Dates and approximate times of occurrences:
On November 23, 2015, at 0815 EST, operators noted the open light indicator on the MCR panel for the Loop 3 MSIV was extinguished while the PAM panel indicator for the MSIV indicated the valve was full open. Within minutes, the PAM panel indicated the MSIV was in mid-position. Operators noted the RCS temperature and Loop 3 SG pressure were both slowly rising, and the Loop 3 SG flow was slowly lowering. These indications confirmed the Loop 3 MSIV was slowly drifting closed. At 0844, the Unit 1 reactor was manually tripped.
November 23, 2015 at I All three light indicators for the MSIV on the MCR panel were 10845 EST illuminated followed by an immediate return to only full open indication. Coincidently, the indicator for the MSIV on the PAM panel indicated the valve was full open.
D. Manufacturer and model number of each component that failed during the event:
There were no components that failed during this event.
E. Other systems or secondary functions affected:
There were no other systems or functions affected by this event.
F. Method of discovery of each component or system failure or procedural error:
Operators observed open light indication for the Loop 3 MSIV on the MCR panel was extinguished while PAM indication initially showed full open. Approximately two to three minutes later, the PAM panel displayed dual indication. Subsequently, operators noted that the RCS temperature and Loop 3 SG pressure were both slowly rising, and the Loop 3 SG flow was slowly lowering. These indications confirmed the Loop 3 MSIV was slowly drifting closed.
G. The failure mode, mechanism, and effect of each failed component, if known:
There were no failed components associated with this event.
H. Operator actions:
After the Loop 3 MSIV was verified to be drifting closed by diverse indications, the operators established trigger values for Loop 3 SG pressure and RCS Tave-Tref mismatch. Once the Loop 3 MSIV showed dual indication on the PAM instrumentation, operators briefed for a potential manual reactor trip. After it was apparent that the Loop 3 MSIV was continuing to close, the operators made the decision to manually trip the reactor. Following the reactor trip, operators entered Emergency Procedure E-0, "Reactor Trip or Safety Injection," and then transitioned from E-0 to Emergency Subprocedure ES-0.1, "Reactor Trip Response." No human performance issues were identified.
I. Automatically and manually initiated safety system responses:
All plant safety related equipment operated as designed, all control rods fully inserted, and AFW automatically initiated from the feedwater isolation signal, as expected.
III. Cause of the event
A. The cause of each component or system failure or personnel error, if known:
The direct cause of the MSIV drifting in the closed direction was a loose connection (terminal lug and nut assembly) on the MSIV handswitch located in the MCR.
B. The cause(s) and circumstances for each human performance related root cause:
The root cause for this event was determined to be inadequate work practices during MSIV handswitch replacement in 1994. In 1994 during replacement of the handswitch, technicians utilized less than adequate work practices and human performance tools (i.e., fastener tightness, situational awareness, self-check, verification and procedure use) resulting in the assembly of the handswitch with a loose connection.
The root cause analysis is documented in Condition Report 1107656.
IV. Analysis of the event:
Prior to the event, SQN Unit 1 was operating at approximately 100 percent RTP with the RCS pressure and temperature near the nominal value of approximately 2235 pounds per square inch gauge (psig) and approximately 578 degrees Fahrenheit. Both the motor driven and the turbine driven AFW pumps and steam dump valves and the atmospheric relief valves were available.
The plant transient response including reactor power, RCS pressure, RCS temperature, pressurizer level, RCS secondary side pressure, and AFW flow remained within technical specification limits and were bounded by the Updated Final Safety Analysis Report (UFSAR) analysis. Containment pressure, temperature, and radiation levels were unaffected by this transient. SG level changes experienced during this event were bounded by UFSAR analysis. The plant responded as expected for the conditions of the trip.
V. Assessment of Safety Consequences
There were no safety consequences as a result of the event. All safety systems functioned as designed and no complications were experienced. Subsequent investigation determined that the Loop 3 MSIV remained capable of closing during the event and able to perform its safety function.
A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event:
There were no components that failed during this event. There were no other components that could have performed the same function as the Loop 3 MSIV.
B. For events that occurred when the reactor was shut down, availability of systems or components needed to shutdown the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident:
This event did not occur when the reactor was shut down. Safety-related systems that were needed to shut down the reactor, maintain safe shutdown conditions, remove residual heat or mitigate the consequences of an accident remained available throughout the event.
C. For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from discovery of the failure until the train was returned to service:
There was no failure that rendered a train of a safety system inoperable during this event.
VI. Corrective Actions
Corrective Actions are being managed by TVA's corrective action program under Condition Report 1107656.
A. Immediate Corrective Actions:
Troubleshooting of the Loop 3 MSIV handswitch was conducted. The cause of the intermittent electrical signal to the MSIV handswitch was identified and corrected.
B. Corrective Actions to Prevent Recurrence or to reduce probability of similar events occurring in the future:
The corrective action to prevent recurrence is revision of the work control planning procedure to ensure specific connection fastener torque values are utilized during work order planning.
VII. Additional Information
A. Previous similar events at the same plant:
A review of previous reportable events for the past three years at SQN identified standards for multi-wire terminations and verifications associated with work performed in the mid-1990s.
B. Additional Information:
None.
C. Safety System Functional Failure Consideration:
This event did not result in a safety system functional failure.
D. Scrams with Complications Consideration:
This event did not result in an unplanned scram with complications.
VIII. Commitments:
None.