|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000327/LER-1999-002-03, :on 990916,EDG Started as Result of Cable Being Damaged During Installation of Thermo-Lag for Kaowool Upgrade Project.Caused by Inadequate pre-job Briefing. Involved Individuals Were Counseled on Event1999-10-15015 October 1999
- on 990916,EDG Started as Result of Cable Being Damaged During Installation of Thermo-Lag for Kaowool Upgrade Project.Caused by Inadequate pre-job Briefing. Involved Individuals Were Counseled on Event
05000327/LER-1998-003-01, :on 981109,Vital Inverter 1-IV Tripped.Caused by Failed Oscillator Board with Bad Solder Joint,Attributed to Mfg Defect.Replaced Component & Returned Inverter to Operable Status1999-05-27027 May 1999
- on 981109,Vital Inverter 1-IV Tripped.Caused by Failed Oscillator Board with Bad Solder Joint,Attributed to Mfg Defect.Replaced Component & Returned Inverter to Operable Status
05000327/LER-1999-001-04, :on 990415,exceedance of AOT Occurred Due to Failure of Centrifugal Charging Pump.Rotating Element Was Replaced,Testing Was Completed & Pump Was Returned to Svc1999-05-11011 May 1999
- on 990415,exceedance of AOT Occurred Due to Failure of Centrifugal Charging Pump.Rotating Element Was Replaced,Testing Was Completed & Pump Was Returned to Svc
05000327/LER-1998-004-02, :on 981120,failure to Perform Surveillance within Required Time Interval,Was Determined.Caused by Leaking Vent Valve.Engineering Personnel Evaluated Alternative Methods for Performing Channel Check1998-12-21021 December 1998
- on 981120,failure to Perform Surveillance within Required Time Interval,Was Determined.Caused by Leaking Vent Valve.Engineering Personnel Evaluated Alternative Methods for Performing Channel Check
05000327/LER-1998-003-04, :on 981109,automatic Reactor Trip Occurred. Caused by Component in Bridge Circuit of Vital Inverter Failed.Inverter Bridge Circuit Replaced1998-12-0909 December 1998
- on 981109,automatic Reactor Trip Occurred. Caused by Component in Bridge Circuit of Vital Inverter Failed.Inverter Bridge Circuit Replaced
05000328/LER-1998-002-05, :on 981016,turbine Trip Occurred Followed by Reactor Trip.Caused by Generator Lockout.Mod Being Evaluated to Physically Isolate Relays from Vibration of Transformers & Adding Two of Two Logic for Actuation of Sudden Pressure1998-11-10010 November 1998
- on 981016,turbine Trip Occurred Followed by Reactor Trip.Caused by Generator Lockout.Mod Being Evaluated to Physically Isolate Relays from Vibration of Transformers & Adding Two of Two Logic for Actuation of Sudden Pressure
05000328/LER-1998-001-05, :on 980827,turbine Trip Occurred Followed by Reactor Trip.Caused by Failure of Sudden Pressure Relay on B Phase Main Transformer.Control Room Operators Responded & Removed,Inspected & Replaced Failed Relays1998-09-28028 September 1998
- on 980827,turbine Trip Occurred Followed by Reactor Trip.Caused by Failure of Sudden Pressure Relay on B Phase Main Transformer.Control Room Operators Responded & Removed,Inspected & Replaced Failed Relays
05000327/LER-1998-002-03, :on 980716,inadequate Surveillance Testing Was Discovered.Caused by Misinterpretation of ANSI Standard. Revised Appropriate Procedures to Provide Required Guidance1998-08-14014 August 1998
- on 980716,inadequate Surveillance Testing Was Discovered.Caused by Misinterpretation of ANSI Standard. Revised Appropriate Procedures to Provide Required Guidance
ML20236P6441998-07-10010 July 1998 LER 98-S01-00:on 980610,failure of Safeguard Sys Occurred for Which Compensatory Measures Were Not Satisfied within Required Time Period.Caused by Inadequate Security Procedure.Licensee Revised Procedure MI-134 05000327/LER-1998-001-04, :on 980519,automatic Reactor Trip Occurred. Caused by Failure of Alternate Feedwater to 1A1-A 480-volt Shutdown Board.Normal Feedwater Breaker Placed in Svc & 480- Volt Shutdown Board Returned to Operation1998-06-18018 June 1998
- on 980519,automatic Reactor Trip Occurred. Caused by Failure of Alternate Feedwater to 1A1-A 480-volt Shutdown Board.Normal Feedwater Breaker Placed in Svc & 480- Volt Shutdown Board Returned to Operation
05000327/LER-1997-014-01, :on 971101,discovered That RCS PORVs Were Not Cycled in Mode 4 as Required by Ts.Caused by Inadequate Procedures.Procedure Revised & Unit Cooled Down to Mode 41997-12-0101 December 1997
- on 971101,discovered That RCS PORVs Were Not Cycled in Mode 4 as Required by Ts.Caused by Inadequate Procedures.Procedure Revised & Unit Cooled Down to Mode 4
ML20199C2951997-11-13013 November 1997 LER 97-S01-00:on 971017,vandalism of Electrical Cables Was Observed.Caused by Vandalism.Repaired Damaged Cables, Interviewed Personnel Having Potential for Being in Area at Time Damage Occurred & Walkdowns 05000328/LER-1997-001, :on 970117,missed Surveillance on Auxiliary Contacts of Reactor Trip Breakers Discovered.Caused by Adequate PMT for Reactor Trip Breaker Was Not Performed. Multi-disciplinary Team Formed to Perform Investigation1997-10-0606 October 1997
- on 970117,missed Surveillance on Auxiliary Contacts of Reactor Trip Breakers Discovered.Caused by Adequate PMT for Reactor Trip Breaker Was Not Performed. Multi-disciplinary Team Formed to Perform Investigation
05000327/LER-1997-011-01, :on 970725,operations Training Personnel Found 125 Vdc Vital Battery Board 4 Improperly Aligned.Caused by Personnel Error.Provided Appropriate Disciplinary Action for Individuals Involved in Event1997-09-17017 September 1997
- on 970725,operations Training Personnel Found 125 Vdc Vital Battery Board 4 Improperly Aligned.Caused by Personnel Error.Provided Appropriate Disciplinary Action for Individuals Involved in Event
05000327/LER-1997-012-01, :on 970801,manual Reactor Tripped Due to Loss of Control Air.Caused by Corrosion Products (Rust Debris) Inhibiting Full Closure of One of six-inch Gate Valves. Isolated Breached Control & Svc Air Sys Header1997-09-0202 September 1997
- on 970801,manual Reactor Tripped Due to Loss of Control Air.Caused by Corrosion Products (Rust Debris) Inhibiting Full Closure of One of six-inch Gate Valves. Isolated Breached Control & Svc Air Sys Header
05000327/LER-1997-011-01, :on 970725,vital Battery Board 4 Was Operating W/O Battery Source.Caused by Personnel Error.Revised Appropriate Instructions to Caution of Possibility of Breaker Misalignment1997-08-25025 August 1997
- on 970725,vital Battery Board 4 Was Operating W/O Battery Source.Caused by Personnel Error.Revised Appropriate Instructions to Caution of Possibility of Breaker Misalignment
05000327/LER-1997-010-01, :on 970626,failure to Properly Return Portion of Fire Protection Sys to Svc Following Mod Activities Was Noted.Caused by Failure to Follow Procedures.Manual Isolation Valve Was Opened1997-07-31031 July 1997
- on 970626,failure to Properly Return Portion of Fire Protection Sys to Svc Following Mod Activities Was Noted.Caused by Failure to Follow Procedures.Manual Isolation Valve Was Opened
05000327/LER-1997-009-02, :on 970521,failed to Perform Response Time Testing of Containment Radiation Monitor Following Maint Activities.Caused by Misinterpretation of Surveillance Requirements.Tested Radiation Monitor1997-06-20020 June 1997
- on 970521,failed to Perform Response Time Testing of Containment Radiation Monitor Following Maint Activities.Caused by Misinterpretation of Surveillance Requirements.Tested Radiation Monitor
05000328/LER-1997-009, :on 970401,licensed Failed to Maintain 2 Offsite Power Sources as Required by Ts.Caused Because Main Contact Compression Was Out of Tolerance.Start Bus 1A Was Transfered to Normal Feed Breaker1997-05-0606 May 1997
- on 970401,licensed Failed to Maintain 2 Offsite Power Sources as Required by Ts.Caused Because Main Contact Compression Was Out of Tolerance.Start Bus 1A Was Transfered to Normal Feed Breaker
05000327/LER-1997-007-01, :on 970404,DG Started When Drill Bit Being Used to Drill Into Electrical Panel in Main Control Room,Cut Into Cable.Caused by Drill Bit Penetrating Energized Wire Bundle Causing Short.Work Stopped on All Electrical Mods for S1997-05-0101 May 1997
- on 970404,DG Started When Drill Bit Being Used to Drill Into Electrical Panel in Main Control Room,Cut Into Cable.Caused by Drill Bit Penetrating Energized Wire Bundle Causing Short.Work Stopped on All Electrical Mods for Shift
05000327/LER-1997-004-01, :on 970320,failure to Properly Perform Surveillance Testing on Circuit Breakers Was Identified,Due to Inadequate Review of Surveillance Instruction Revs.Lcos Were Entered1997-04-21021 April 1997
- on 970320,failure to Properly Perform Surveillance Testing on Circuit Breakers Was Identified,Due to Inadequate Review of Surveillance Instruction Revs.Lcos Were Entered
05000327/LER-1997-006-01, :on 970322,failed to Perform Surveillance Requirement During Containment Entry Due to Personnel Error. RWP Was Closed to Prevent Further Use1997-04-21021 April 1997
- on 970322,failed to Perform Surveillance Requirement During Containment Entry Due to Personnel Error. RWP Was Closed to Prevent Further Use
05000327/LER-1997-005-01, :on 970319,two of Six Tested Main Steam Safety Relief Valves Not within TS Setpoint Tolerance.Appropriate LCOs Entered & Valves Found Outside TS Setpoint Tolerance Adjusted to within TS Tolerance & Retested1997-04-17017 April 1997
- on 970319,two of Six Tested Main Steam Safety Relief Valves Not within TS Setpoint Tolerance.Appropriate LCOs Entered & Valves Found Outside TS Setpoint Tolerance Adjusted to within TS Tolerance & Retested
05000327/LER-1997-003-02, :on 970305,failed to Properly Perform Surveillance Testing on Centrifugal Charging Pump Inlet Isolation Valve Logic.Caused by Inadequate Surveillance Instruction.Prepared Special Test Procedure1997-04-0404 April 1997
- on 970305,failed to Properly Perform Surveillance Testing on Centrifugal Charging Pump Inlet Isolation Valve Logic.Caused by Inadequate Surveillance Instruction.Prepared Special Test Procedure
05000328/LER-1996-004-02, :on 960919,reactor Trip Breaker Was Removed After It Was Found to Have Inoperable Auxiliary Contacts. Caused by Inadequate Procedure.Revised Breaker Procedure & Reemphasized Requirements for Working Steps Out of Sequence1997-03-28028 March 1997
- on 960919,reactor Trip Breaker Was Removed After It Was Found to Have Inoperable Auxiliary Contacts. Caused by Inadequate Procedure.Revised Breaker Procedure & Reemphasized Requirements for Working Steps Out of Sequence
05000327/LER-1997-002-01, :on 970214,TS AOT Exceeded for DG 2A-A.Caused by Mechanical Failure of DG 2A-A Governor Actuator on Engine 2.DG 2A-A Governor Actuators on Both Engines Replaced, Functional Tested & PMT Performed1997-03-13013 March 1997
- on 970214,TS AOT Exceeded for DG 2A-A.Caused by Mechanical Failure of DG 2A-A Governor Actuator on Engine 2.DG 2A-A Governor Actuators on Both Engines Replaced, Functional Tested & PMT Performed
05000327/LER-1997-001-02, :on 970125,failed to Perform Surveillance Testing on EDG Start Timer Relays Contained in Start Logic Circuitry.Caused by Inadequate Surveillance Procedures. Revised Procedures & Performed Testing1997-02-24024 February 1997
- on 970125,failed to Perform Surveillance Testing on EDG Start Timer Relays Contained in Start Logic Circuitry.Caused by Inadequate Surveillance Procedures. Revised Procedures & Performed Testing
05000328/LER-1997-001-01, :on 970117,failed to Perform Surveillance on Turbine Trip Contacts of Reactor Trip Breakers.Caused by Inadequate Procedure.Performed Test on Turbine Trip Contacts & Declared Rtb a Operable1997-02-18018 February 1997
- on 970117,failed to Perform Surveillance on Turbine Trip Contacts of Reactor Trip Breakers.Caused by Inadequate Procedure.Performed Test on Turbine Trip Contacts & Declared Rtb a Operable
05000327/LER-1995-001-01, :on 950118,accumulation of Gas in Residual Heat Removal Sys.Caused by Normal Leakage from Cold Leg Accumulators.Performed Monitoring & Venting of Gas Accumulation & Revised Quarterly Pump Tests1997-02-0606 February 1997
- on 950118,accumulation of Gas in Residual Heat Removal Sys.Caused by Normal Leakage from Cold Leg Accumulators.Performed Monitoring & Venting of Gas Accumulation & Revised Quarterly Pump Tests
05000328/LER-1996-007-03, :on 961207,ESF Actuation,Start of Feedwater Sys,Occurred as Result of Inadequate Return of Equipment to Svc.Refresher Training on Filling & Venting Fundamentals Will Be Conducted in Yrs Training Cycle1997-01-0606 January 1997
- on 961207,ESF Actuation,Start of Feedwater Sys,Occurred as Result of Inadequate Return of Equipment to Svc.Refresher Training on Filling & Venting Fundamentals Will Be Conducted in Yrs Training Cycle
05000327/LER-1996-012-01, :on 960330,two Cold Leg Accumulator Sample Isolation Valves & Missing Data Sheet in Surveillance Package Were Inoperable.Caused by LCO Not Being Entered. Isolation Valves Were Tested1997-01-0202 January 1997
- on 960330,two Cold Leg Accumulator Sample Isolation Valves & Missing Data Sheet in Surveillance Package Were Inoperable.Caused by LCO Not Being Entered. Isolation Valves Were Tested
05000328/LER-1996-006-04, :on 961206,automatic Reactor Trip Occurred. Caused by Loss of Power to Start Bus 2A,start of Four EDG & Loading of EDG 2B-B.Refurbished Breaker Installed in 2A Start Bus & Breaker Tested Acceptable1997-01-0202 January 1997
- on 961206,automatic Reactor Trip Occurred. Caused by Loss of Power to Start Bus 2A,start of Four EDG & Loading of EDG 2B-B.Refurbished Breaker Installed in 2A Start Bus & Breaker Tested Acceptable
05000327/LER-1996-011-01, :on 961118,discovered Rod Position Indication Sys Was Out of Step W/Demand Position Indication Sys.Caused by Incorrect Position Indication on Analog Rod Position. Began Dilution of Reactor Coolant Sys1996-12-18018 December 1996
- on 961118,discovered Rod Position Indication Sys Was Out of Step W/Demand Position Indication Sys.Caused by Incorrect Position Indication on Analog Rod Position. Began Dilution of Reactor Coolant Sys
05000327/LER-1996-010-01, :on 961116,manual Reactor Trip Occurred.Caused by Unexpected Feedwater Heater Isolation.Informed Personnel of Effects Changing Proportional Band on Operating Range of Associated Valve Controllers1996-12-16016 December 1996
- on 961116,manual Reactor Trip Occurred.Caused by Unexpected Feedwater Heater Isolation.Informed Personnel of Effects Changing Proportional Band on Operating Range of Associated Valve Controllers
05000328/LER-1996-005-04, :on 961011,manual Trip Occurred.Caused by Unexpected Loss of Load.Stabilized Unit,Replaced Turbine Impulse Pressure Switches & Replaced Failed Feedwater Isolation Valve Motor & Brake Assembly1996-11-12012 November 1996
- on 961011,manual Trip Occurred.Caused by Unexpected Loss of Load.Stabilized Unit,Replaced Turbine Impulse Pressure Switches & Replaced Failed Feedwater Isolation Valve Motor & Brake Assembly
05000328/LER-1996-004-04, :on 960919,after Reactor Trip Breaker Was Removed Breaker Found to Have Inoperable Auxiliary Contacts. Caused by Inadequate Evaluation of Procedural Change. Procedures Revised1996-10-23023 October 1996
- on 960919,after Reactor Trip Breaker Was Removed Breaker Found to Have Inoperable Auxiliary Contacts. Caused by Inadequate Evaluation of Procedural Change. Procedures Revised
05000327/LER-1996-009-01, :on 960718,auxiliary Building Secondary Containment Boundary/Fire Barrier Not Maintained as Required by Design.Caused by Failure to Follow Design Control Process1996-08-19019 August 1996
- on 960718,auxiliary Building Secondary Containment Boundary/Fire Barrier Not Maintained as Required by Design.Caused by Failure to Follow Design Control Process
05000327/LER-1996-008-01, :on 960709,failed to Perform Quarterly Backseat/Closure Test on Five Check Valves.Caused by Personnel Error.Test Procedure Written & Performed on Subject Check Valves1996-08-0808 August 1996
- on 960709,failed to Perform Quarterly Backseat/Closure Test on Five Check Valves.Caused by Personnel Error.Test Procedure Written & Performed on Subject Check Valves
05000327/LER-1996-006-02, :on 960623,failed Coupled Capacitor Potential Device Caused Actuation of Generator Backup/Transfomer Feeder Relay Tripping Turbine & Reactor.Removed & Replaced Ccpd1996-07-18018 July 1996
- on 960623,failed Coupled Capacitor Potential Device Caused Actuation of Generator Backup/Transfomer Feeder Relay Tripping Turbine & Reactor.Removed & Replaced Ccpd
05000327/LER-1996-007-01, :on 960614,rod Position Indicators for Control Bank D Rods M4 & M12 More than Required 12 Steps Out from Respective Demand Position Indicators.Caused by Incorrect Position Indication on Rod.Response Reduced1996-07-15015 July 1996
- on 960614,rod Position Indicators for Control Bank D Rods M4 & M12 More than Required 12 Steps Out from Respective Demand Position Indicators.Caused by Incorrect Position Indication on Rod.Response Reduced
05000328/LER-1996-003-05, :on 960605,reactor Trip Breakers Manually Opened Because Shutdown Bank D Dropped Into Reactor Core.On 960607 Manual Reactor Trip Initiated Due to Dropped Rod. Added Caution Statement to Apropriate Operations Prcedure1996-07-0505 July 1996
- on 960605,reactor Trip Breakers Manually Opened Because Shutdown Bank D Dropped Into Reactor Core.On 960607 Manual Reactor Trip Initiated Due to Dropped Rod. Added Caution Statement to Apropriate Operations Prcedure
05000327/LER-1995-010, :on 950717,turbine & Reactor Trips Occurred. Caused by Bellows Being Deformed When Sudden Pressure Relay Is Isolated & Heated.New Qualitrol Relays Installed & Placed in Service1996-07-0303 July 1996
- on 950717,turbine & Reactor Trips Occurred. Caused by Bellows Being Deformed When Sudden Pressure Relay Is Isolated & Heated.New Qualitrol Relays Installed & Placed in Service
05000327/LER-1996-005-02, :on 960526,ESF Actuation Occurred Resulting in DG Start.Cause Unknown.Diagnosed Condition,Reset Start Signal & Secured Actuated Equipment1996-06-21021 June 1996
- on 960526,ESF Actuation Occurred Resulting in DG Start.Cause Unknown.Diagnosed Condition,Reset Start Signal & Secured Actuated Equipment
05000328/LER-1996-002-05, :on 960822,discovered Failure to Properly Identify Steam Generator Tube May Have Exceeded Tech Spec Plugging Criteria.Caused by Misjudgement by Two Independent Analysts.Evaluation Performed1996-06-13013 June 1996
- on 960822,discovered Failure to Properly Identify Steam Generator Tube May Have Exceeded Tech Spec Plugging Criteria.Caused by Misjudgement by Two Independent Analysts.Evaluation Performed
05000327/LER-1996-004-02, :on 960509,normal Feeder Breaker Unexpectedly Tripped,Resulting in Loss of Power Signal & Start of Four Dgs.Caused by Failure of Breaker Mechanism.Spare Breaker Operating Mechanism Refurbished & Installed1996-06-0505 June 1996
- on 960509,normal Feeder Breaker Unexpectedly Tripped,Resulting in Loss of Power Signal & Start of Four Dgs.Caused by Failure of Breaker Mechanism.Spare Breaker Operating Mechanism Refurbished & Installed
05000328/LER-1996-001-05, :on 960418,inadvertent ESF Actuation & Loss of Power Signal & Load Sequencing Occurred During Maint. Caused by Personnel Error.Individual Involved in Event Was Counseled & Lessons Were Discussed1996-05-17017 May 1996
- on 960418,inadvertent ESF Actuation & Loss of Power Signal & Load Sequencing Occurred During Maint. Caused by Personnel Error.Individual Involved in Event Was Counseled & Lessons Were Discussed
05000327/LER-1996-003-01, :on 960325,failure to Perform Surveillance Requirements for Penetration Fire Barrier Insps as Required by Tech Specs Occurred.Caused by Personnel Error.Appropriate Disciplinary Action Taken W/Individuals1996-04-24024 April 1996
- on 960325,failure to Perform Surveillance Requirements for Penetration Fire Barrier Insps as Required by Tech Specs Occurred.Caused by Personnel Error.Appropriate Disciplinary Action Taken W/Individuals
05000327/LER-1996-002-01, :on 960215,SRs Associated W/Fire Protection Hose Stations Not Performed as Required by Ts.Caused by Inadequate Procedure Rev.Entered Action of LCO & Established Measures to Address Issue1996-03-15015 March 1996
- on 960215,SRs Associated W/Fire Protection Hose Stations Not Performed as Required by Ts.Caused by Inadequate Procedure Rev.Entered Action of LCO & Established Measures to Address Issue
05000327/LER-1996-001-02, :on 960121,discovered Fire Watch Patrol Did Not Patrol Some Assigned Areas in Control Bldg & on 960126,fire Watch Patrol Not Performed within Timeframe Required by Ts. Appropriate Disciplinary Action Taken1996-02-20020 February 1996
- on 960121,discovered Fire Watch Patrol Did Not Patrol Some Assigned Areas in Control Bldg & on 960126,fire Watch Patrol Not Performed within Timeframe Required by Ts. Appropriate Disciplinary Action Taken
05000328/LER-1992-008, :on 920627,reactor Tripped.Caused by Varying Resistance Readings Substandard Workmanship.Plant Instruction Written to Provide Guidance1996-02-0808 February 1996
- on 920627,reactor Tripped.Caused by Varying Resistance Readings Substandard Workmanship.Plant Instruction Written to Provide Guidance
1999-05-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000327/LER-1999-002-03, :on 990916,EDG Started as Result of Cable Being Damaged During Installation of Thermo-Lag for Kaowool Upgrade Project.Caused by Inadequate pre-job Briefing. Involved Individuals Were Counseled on Event1999-10-15015 October 1999
- on 990916,EDG Started as Result of Cable Being Damaged During Installation of Thermo-Lag for Kaowool Upgrade Project.Caused by Inadequate pre-job Briefing. Involved Individuals Were Counseled on Event
ML20217D2721999-10-12012 October 1999 Safety Evaluation Supporting Amends 248 & 239 to Licenses DPR-77 & DPR-79,respectively ML20217B3651999-10-0606 October 1999 Safety Evaluation Supporting Amends 247 & 238 to Licenses DPR-77 & DPR-79,respectively ML20212J6311999-10-0101 October 1999 SER Accepting Request for Relief from ASME Boiler & Pressure Vessel Code,Section Xi,Requirements for Certain Inservice Insp at Plant,Unit 1 ML20217G3721999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Sequoyah Nuclear Plant.With ML20212F0831999-09-23023 September 1999 Safety Evaluation Granting Relief from Certain Weld Insp at Sequoyah Nuclear Plant,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(ii) for Second 10-year ISI Interval ML20212F4761999-09-23023 September 1999 Safety Evaluation Supporting Amends 246 & 237 to Licenses DPR-77 & DPR-79,respectively ML20212C4761999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Sequoyah Nuclear Plant.With ML20212A1841999-08-25025 August 1999 Errata Pages for Rev 0 of WCAP-15224, Analysis of Capsule Y from TVA Sequoyah Unit 1 Reactor Vessel Radiation Surveillance Program ML20210L4361999-08-0202 August 1999 Cycle 9 12-Month SG Insp Rept ML20210L4451999-07-31031 July 1999 Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20216E3781999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20210G6631999-07-28028 July 1999 Cycle 9 90-Day ISI Summary Rept ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209H3831999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Sequoyah Nuclear Plant.With ML20211F9031999-06-30030 June 1999 Cycle 9 Refueling Outage ML20196J8521999-06-28028 June 1999 Safety Evaluation Authorizing Proposed Alternative to Use Iqis for Radiography Examinations as Provided for in ASME Section III,1992 Edition with 1993 Addenda,Pursuant to 10CFR50.55a(a)(3)(i) ML20195K2951999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With 05000327/LER-1998-003-01, :on 981109,Vital Inverter 1-IV Tripped.Caused by Failed Oscillator Board with Bad Solder Joint,Attributed to Mfg Defect.Replaced Component & Returned Inverter to Operable Status1999-05-27027 May 1999
- on 981109,Vital Inverter 1-IV Tripped.Caused by Failed Oscillator Board with Bad Solder Joint,Attributed to Mfg Defect.Replaced Component & Returned Inverter to Operable Status
05000327/LER-1999-001-04, :on 990415,exceedance of AOT Occurred Due to Failure of Centrifugal Charging Pump.Rotating Element Was Replaced,Testing Was Completed & Pump Was Returned to Svc1999-05-11011 May 1999
- on 990415,exceedance of AOT Occurred Due to Failure of Centrifugal Charging Pump.Rotating Element Was Replaced,Testing Was Completed & Pump Was Returned to Svc
ML20206Q8951999-05-0505 May 1999 Rev 0 to L36 990415 802, COLR for Sequoyah Unit 2 Cycle 10 ML20206G3751999-05-0404 May 1999 Safety Evaluation Supporting Amends 244 & 235 to Licenses DPR-77 & DPR-79,respectively ML20206R5031999-04-30030 April 1999 Monthly Operating Repts for April 1999 for Sequoyah Units 1 & 2.With ML20205N0361999-04-12012 April 1999 Safety Evaluation Supporting Amend 234 to License DPR-79 ML20205P9811999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20204E8211999-03-16016 March 1999 Safety Evaluation Supporting Amends 243 & 233 to Licenses DPR-77 & DPR-79,respectively ML20204C3111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20205B6631999-02-28028 February 1999 Underground Storage Tank (Ust) Permanent Closure Rept, Sequoyah Nuclear Plant Security Backup DG Ust Sys ML20203H7381999-02-18018 February 1999 Safety Evaluation of Topical Rept BAW-2328, Blended U Lead Test Assembly Design Rept. Rept Acceptable Subj to Listed Conditions ML20206U4331999-02-0909 February 1999 Safety Evaluation Supporting Amends 242 & 232 to Licenses DPR-77 & DPR-79,respectively ML20211A2021999-01-31031 January 1999 Non-proprietary TR WCAP-15129, Depth-Based SG Tube Repair Criteria for Axial PWSCC Dented TSP Intersections ML20198S7301998-12-31031 December 1998 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20199G3641998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With 05000327/LER-1998-004-02, :on 981120,failure to Perform Surveillance within Required Time Interval,Was Determined.Caused by Leaking Vent Valve.Engineering Personnel Evaluated Alternative Methods for Performing Channel Check1998-12-21021 December 1998
- on 981120,failure to Perform Surveillance within Required Time Interval,Was Determined.Caused by Leaking Vent Valve.Engineering Personnel Evaluated Alternative Methods for Performing Channel Check
05000327/LER-1998-003-04, :on 981109,automatic Reactor Trip Occurred. Caused by Component in Bridge Circuit of Vital Inverter Failed.Inverter Bridge Circuit Replaced1998-12-0909 December 1998
- on 981109,automatic Reactor Trip Occurred. Caused by Component in Bridge Circuit of Vital Inverter Failed.Inverter Bridge Circuit Replaced
ML20197J5621998-12-0303 December 1998 Unit 1 Cycle 9 90-Day ISI Summary Rept ML20197K1161998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20196B0231998-11-19019 November 1998 Safety Evaluation Supporting Amends 239 & 229 to Licenses DPR-77 & DPR-79,respectively 05000328/LER-1998-002-05, :on 981016,turbine Trip Occurred Followed by Reactor Trip.Caused by Generator Lockout.Mod Being Evaluated to Physically Isolate Relays from Vibration of Transformers & Adding Two of Two Logic for Actuation of Sudden Pressure1998-11-10010 November 1998
- on 981016,turbine Trip Occurred Followed by Reactor Trip.Caused by Generator Lockout.Mod Being Evaluated to Physically Isolate Relays from Vibration of Transformers & Adding Two of Two Logic for Actuation of Sudden Pressure
ML20195F8061998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Sequoyah Nuclear Plant.With ML20154H6091998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With 05000328/LER-1998-001-05, :on 980827,turbine Trip Occurred Followed by Reactor Trip.Caused by Failure of Sudden Pressure Relay on B Phase Main Transformer.Control Room Operators Responded & Removed,Inspected & Replaced Failed Relays1998-09-28028 September 1998
- on 980827,turbine Trip Occurred Followed by Reactor Trip.Caused by Failure of Sudden Pressure Relay on B Phase Main Transformer.Control Room Operators Responded & Removed,Inspected & Replaced Failed Relays
ML20154H6251998-09-17017 September 1998 Rev 0 to Sequoyah Nuclear Plant Unit 1 Cycle 10 Colr ML20153B0881998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Sequoyah Nuclear Plant.With ML20238F2961998-08-28028 August 1998 Safety Evaluation Supporting Amends 235 & 225 to Licenses DPR-77 & DPR-79,respectively ML20239A0631998-08-27027 August 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Sequoyah Nuclear Plant,Units 1 & 2 05000327/LER-1998-002-03, :on 980716,inadequate Surveillance Testing Was Discovered.Caused by Misinterpretation of ANSI Standard. Revised Appropriate Procedures to Provide Required Guidance1998-08-14014 August 1998
- on 980716,inadequate Surveillance Testing Was Discovered.Caused by Misinterpretation of ANSI Standard. Revised Appropriate Procedures to Provide Required Guidance
ML20236Y2091998-08-0707 August 1998 Safety Evaluation Accepting Relief Requests RP-03,RP-05, RP-07,RV-05 & RV-06 & Denying RV-07 & RV-08 ML20237B5221998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Snp ML20237A4411998-07-31031 July 1998 Blended Uranium Lead Test Assembly Design Rept 1999-09-30
[Table view] |
text
,
3
%.c.. m o e i,vetim. evutoav ca au i
swaovnvaneno va mn l
LICENSEE IVENT REPORT ILER) m'*" ' " "
,acSit, %a. n i ovc a,.,,va e i,,
ran m l
_Sequoyah. Unit 1 o is i n l o l 0 l312 I ?
t lor 0 [6 l
'itf'fnaccurate Computer Database Causes Technical Specification Surveillance Intervals Xo l
SS Exceeded Resulting In Inoperable Diesel Generators And Boron Injection Flow Paths evt%f Datt i6i tem esvenee n isi espont cats m ofus a pacitities,sivoLvec sei wo%fa Da, tsaa igan
Day team eac+vemawes cccatt % weal Sequoyah, IJnit 2 0 f t l91010 l 3 218 1
0l1 1h 88 818 0l0 l 1 0k 0l2 1l 8 d8
~
~
0 is to to, o g l t
'"'s ateos?.8 s.tesittsp avatva%, to eat asoviasug%tt De to ca n i scane ce en meg e. sae s -ewse 01, e
o.s a atswa "O
- M ael ti H eel d M ttwaMal f a tt el n m.m u w w.nu u n+an.i vine y
n..
0,0 io
.... n m.,
...i.,
. nvou.
g, =,;. ;,.g n o.~
g_
u n.,2.
w no.
a, m e.
l n a #n n,.<
se n.n m
%,,4, - +
l n m.u 4.,
e n, a.o gg
.m..
Liet%444 contact see twis 6 i+0 gave 186s. c% %sveer sagaCyg K. W. Fenn. Plant Orserations Review Staff 61 LM B l7101 - 16 i $111) co Lets o%: 6i%: een e,. m con o%s%t saituas eenemieso % v e espont nr
- l[
1
.'e f b
C (a ll
- 8. gtgy cpyeegggt
' t,'g AP/
Castl 8.l't v c?v"0%t%'
w
~..
! ! I I I I i
i i f f I 1 g
I i 1 l I I I I
l l !
I l I Sv htwt% tat stroet IaptctID Ha-hoo%ta Cav
l.tv 46 0%
],sim.
,.-,,,s..<.,
s.,wn e eor 2u l
l l
au, a e v +-.,. ax
.,,4.
..,.. -... n. -
This report is beint revised to include an additional deficiency found and to provide additional corrective actions.
On January ll, 1988, with units 1 and 2 in mode 5 (cold shutdown) all four emergency l
diesel r,enerators (D/Gs) were (;ociared inoperable becaase the interval for Technical l
Specification (TS) Surveillance Requirement (SR) 4.8.1.2 (chemical analysis of D/G fuel oil) was exceeded.
In addition, because the high pressure fire pumps use the D/Gs as an emergency power source, the plant fire suppression system was also declared inoperable, and a backup fire suppression system was established. Because of an oversight during the recent conversion to a new computer program used to schedule surveillance instructions (sis). SI-116, "Quarterly Chemistry Requirements on Diesel Generator Fuel Oil," was not performed within the time interval required
,L by the TS.
Immediately upon discovery of the event, a special SI-116 package was A
issued and performed, and all D/Gs and fire suppression pumps were returned to I (
operable status on January 12, 1988.
In addition, an immediate review of all sis was initiated to ensure that the mode requirements in the scheduling program were consistent with the applicability section in the sis.
Four additional deficiencies were found; however, only one of these caused a TS SR to be escoeded (SR 4.0.5) and involved SI-166.17. "CVCS and SI iSafety Injection) Cheet Valve Test During Cold Shutdown," not being performed in the required time interval. A special SI performance putage was subsequently issued and successfully perforped. To prevent recurrence of this event TVA is upgrading the overall Sequoyah Nuclear Plant surveillance program by implementint. recommendations derived from an independent assessment of the SI pror, ram. These actions will ensure the technical adequacy of completed SI packsges, decrease the potential for scheduling errors, and improve the overall efficiency of the SI program. These actions are espected to be completed by June 1. 1988.
0802240270 800010 PDR ADOCK 05000327 4:e S
DCD
i tRC Form 384A U S NUCLE 1A [EEULATORY COh8M18880N LICENSEE EVENT REPORT (LER) TEXT CONTINUATION amoveo ous ~o mo-oio.
exesRE: ni as s &CILIT Y hA'at (11 OOCatt hutsSER LU LER huns 0ER14 PA00 (31
" 0 01.
Of *.72 Seauovah. Unic 1 o l5 lo j o j o l3 l 217 8 18 01 d 1
-- 0l1 Ol 2 0' 0l6 rixT w u.u.a
=ac i mm r, This LER is being revised to include a unit I surveillance instruction (SI) that was not performed within the time interval required by the technical specifications (TSs) and to provide additional information relating to the l
corrective actions TVA is iraplementing to prevent the recurrence of this event.
i
DESCRIPTION OF EVENT
On January 11, 1988, units I and 2 of the Sequoyah Nuclear Plant (SQN) were in mode 5 (0 percent power, 4 psig, 128 degrees F and 0 percent power, 140 psig, 125 degrees F, respectively) when at approximately 1330 EST, all four emergency diesel generators (D/Gs) (EIIS Code KP), servicing both units 1 and 2, were j
declared inoperable. The D/Gs were declared inoperable because the interval for i
TS Surveillance Requirement (SR) 4.8.1.2 (92 days) plus extension was exceeded, TS SR 4.8.1.2 requires each D/G set (a D/G set consists of D/Gs IA-A and 2A-A or D/Gs IB-B and 2B-B) to be demonstrated operable at least once ever'y 92 days or before the addition of new fuel oil to the 7-day fuel oil tanks, by verifying that a fuel oil sample obtained in accordance with ASTM-D270-1975 has a water and sadiment content -T less than or equal to 0.05 volume percent and a kinematic viscosity a? 100 degrees F of greater than or equal to 3.8 but less than or equal to 5.8 contistokes when tested in accordance with ASTM-D975-77.
Further, the fuel oil sample is required to have an impurity level of less than 2 milligrams of insolubles per 100 milliliters when tested in accordance with ASTM-D2274-70. Since the above described TS SR had not been performed since September 10, 1981, ard the due date including the allowable TS extension was December 30, 1987, both D/G sets were declared inoperable.
j The following systems use the D/Gs as an emergency power 6.1rce and are required in mode 5; therefore, these systems were also declarva inoperable, and the appropriate TS Limiting Condition for Operation (LCC: o tions were complied with.
- - All four motor-driven high pressure fire pumps (EIIS Code KP), LCO 3.7.11.1.
- - Both trains (common to units 1 and 2) of the Auxiliary Building gas treatment system (EIIS Code BH), LCO 3.9.12.
- - All four (2 per unit) centrifugal charging pumps (EIIS Code BQ),
LCOs 3.1.2.1 and 3.1.2.3.
The actions for the above described equipment required (1) the establishment of a backup fire suppression system within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, (2) the suspension of all operations involving core alterations or positive reactivity changes, and (3) the suspension of all operations involving movement of fuel within the spent fuel pit or crane operations with loads over the spent fuel pit.
The control room emergency ventilation system (EIIS Code VI) also uses the D/Gs as an emergency power source; however, both trains of this system were already inoperable because of previous deficiencies.
.g.o.
x..
.u wo i.e.me u 4n
7 Inc For4 3844 U S huCLEAA K11ULATOAY COMMstslose LICENSEE EVENY REPORT 'LER) TEXT CON 11NUATICN An*aono ove %o me.oio.
(AmAES 8 31'88 raclLIT T MAW 4 m DOCE ST NUMS(R QI L$R hUhetR 191 PAQt (31 "t',0.
tlJ,f:
"a 0 l0 l 1 Q1 013 0F 0l6 Seouovar Unit 1 0151010 l o 13 l2 l 7 8 18 rm,,
w.
- - we i me,m On January 23, 1988, following a generic review of all SQN sis to determine if the mode requirements listed in the SI scheduling program were consistent with the applicability section listed in the specific sis, an additional performance deficiency was identified that resulted in a unit 1 TS SR being exceeded.
SI-166.17 "CVCS and SI iSafety Injection) Check Valve Test During Cold Shutdown," was not performed within the time interval required by TSs. This SI verifies the operability of check valves62-504 and 63-502 by ensuring that 62-504 will open when pressure is applied to open it, and that 63-502 will close when pressure is applied to close it.
Check valve 63-502 is in the residual heat removal (RHR) pump suction line from the refueling water storage tank (RWST) and is required to be operable only when the RHR loops are used as emergency core cooling system (ECCS) subsystems (i.e.,
modes 1, 2, 3, and 4).
Therefore, the missed performance of the SI-166.17 did not cause an operation prohibited by TSs for the 63-502 valve. However, check valve 62-504 is required to be operable during all modes of plant operation since it is in the centrifugal charging pumps (CCPs) suction line from the RWST (modes 1 through 4 for ECCS path modes 1 through 6 for boron injection path).
Since SQN unit I was crediting the boration flow path from the RWST through the CCPs at the time (mode 5) of this event, the action statement to TS 3.1.2.1 was entered. This action statement required the suspension of all operations involving core alterations or positive reactivity changes.
CAUSE OF EVENT
The failure to perform SI-116 "Quarterly Chemistry Requirements on Diesel Generator Fuel Oil," vithin the required time interval was caused by an oversight during a recent revision of the computer program that is used by the SQN Maintenance and Surveillance Scheduling (M&S) department to schedule sis.
In this case, SI-116 was incorrectly classified "HA" (i.e., SI on hold until applicable mode is reached) in the scheduling program. As a result, M&S did not issue an SI package to the responsible section (Chemistry), and the SI was not performed within the required TS time interval. The oversight which caused the event occurred during the recent (November 1987) conversion to a new M&S computer program.
During this conversion, the mode requirements for the performance of SI-116 were incorrectly changed from "all modes" to "modes 1-4."
The failure to perform SI-166.17 within the required time interval was caused by Operations personnel not realizing that the subject SI was partially applicable (i.e., applicable to one of the two valves) during all modes of operation. As a result, Operations returned SI packages stating that performance was not required until mode 4.
Also during the conversion to the new M&S computer program as noted above, the applicability of this SI was inadvertently changed from "all modes" to "modes I through 4."
A contributing caust to both events was the failure of the M&S department to perform an adequate review of the new computer program before implementation.
- .g.e.. m.
. U wo........ e
a L AC 7.rm 364A U S =VCLE AR EEtULATORY COpursgeon LICENSEE EVENT REPORT (LER) TEXT CONTINUATION amovio ove w siso_eie.
ixmais si se
,*cun
..n,
.0c..,,,vu.. u,
"t u;.
'JJJ:
"*a Seonovah. Unit 1 015 l o j o l o l 3 2l 7 8i8
-- 0l d 1
-- 0l1 d4 0F 0 l6 rm a,
.w
..c w ass.u nn
ANALYSIS OF EVENT
This event is being reported in accordance with 10 CFR 50.73, paragraph a.2.1.B.
as an operation that is prohibited by the plant's TS.
This report also satisfies the special report requirement of action st2tement (b) to LCO 3.7.11.1.
Although the D/Gs were declared inoperable, they were not "tagged out" or isolated from their respective emergency power busses because there was no evidence that the D/Gs would not be able to perform their designed safety function. The ability of the D/Gs to operate following the expiration of the required surveillance interval was confirmed when the results of the fuel oil analysis were acceptable for all four 7-day fuel oil tanks, and the D/Gs were returned to operable status.
Thus, the D/Gs could have supplied emergency AC power, if required, despite the fact that they were administrative 1y declared inoperable.
The ability of unit I check valve 62-504 to open is required to ensure the availability of a boration flow path from the RWST to the reactor coolant system (RCS). During mode 5 operation, sufficient boration capability must be available to ensure that the reactivity excursion associated with an uncontrolled cooldown from 200 degrees F to 140 degrees F will not result in the loss of required shutdown margin. Since SQN unit I has typically been operating j
with RCS boron concentrations of approximately 2000 ppm, adequate shutdown i
margin is available to withstand the reactivity excursion described above even without additional boration from the RWST.
In addition, if the boration flow path through valve 62-504 could not be established, plant operators could line up an alternative boration flow path from the boric acid tants to the suction of the CCPs. Thus, there were no significant consequences associated with the failure to test check valve 62-504.
Since the 63-502 check valve is only required in modes 1 through 4, the missed performance of SI-166.17 did not cause an operation prohibited by TS for the RHR system and did not affect the operability of the RHR system for mode 5.
CORRECTIVE ACTION
In compliance with action statement (b) to TS 3.7.11.1, a backup fire suppression system was established within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of declaring the D/Gs inoperable. The backup system was on site and connected to the SQN fire suppression header by 1100 EST on January 12, 1988.
- . gee x..
.u s c.ao ino o er. su is
s
\\
l v s = vets Aa s stutafoRv couwission lixac,. seea LICENSEE EVENT REPORT (LER) TEXT CONTINUATION A m oviooWeao vio-o
, Acnktiv Naut ill ooCh t? WVMBE R (21 gg R hWMet a 164 PAGE135
" t!,0.
3*e3
- saa 0101 1 0 11 01 5 0F 0 l6 Seauovah, Unit 1 0]5lojo[cl312l7 818 TIXT (F mere apose e sosised. se, assumpiW 44C Aego Mt 11M Immediately upon discovery of the failure to perform SI-116, M&S personnel issued a special performance package for the subject SI and revised the computer program used for SI scheduling to ensure SI-116 was appilcable in all modes.
In addition, M&S personnel immediately reviewed all sis currently classified as "HA" and verified that no other sis w're incorrectly placed in that category.
Similarly, following the discovery of the f ailitre to perform SI-166.17. M&S personnel issued a special performance package of the subject SI and revised the computer program to ensure SI-166.17 was applicable in all modes. The subject SI was successfully completed on January 24, 1988.
M&S personnel also initiated an immediate review of all TS sis to ensure all applicable mode requirements listed in the scheduling program were consistent with the applicability section in the sis. All SI procedures that are common to units 1 and 2 or applicable to unit 2 only, have been reviewed. Three other instances, as listed below, were discovered where the mode appilcability was incorrect; however, a review by M&S has shown that none of these instances had resulted in any TS SR being exceeded.
SI Title SR 162.1 Snubber Visual Inspection (Hydraulic and Mechanical) ()
4.7.9 162.2 Snubber Functional Testing (Hydraulic and Mechanical) 4.7.9 26.2B Loss of Offsite Power with Safety Injection D/G 2B-B Test 4.8.1.1.2 All three of these instances involved the scheduling program indicating applicable modes "1-4" but the SRs required applicable modes of "1-6," and all of these errors were made during the conversion to the new scheduling program.
All three of these instances have now been corrected on the scheduling program.
Immediately upon receiving the special performance package for SI-116, Chemistry personnel sampled and analyzed the fuel oil in the 7-day fuel oil tanks.
Chemistry personnel also performed an immediate and comprehensive review of all other sis under their cognizance and verified that there were no other discrepancies in the M&S database for Chemistry sis. On January 12, 1988, following the successful completion of the D/G fuel oil analysis in accordance j
with SI-116, the D/Gs were returned to operable status (D/G 1A-A at 1205 EST, l
D/G IB-B at 1330 EST, and D/Gs 14-A and 2B-B at 1415 EST), and all D/G-related 9
LCO action statements were exited.
1; b
1
. mo...... u. o.
g...o
G mc per-3esa u s neucLat.a KEtutATos v couwissios:
LICENSEE EVENT REPORT (LER) TEXT COf!TINUATION
sxemis s.stes
oOCa t T stVesS S R 431 ggg p,yngegn gap PAgg (3i "ti,R.
"'a*J:
vs.a Sequovah, Unit 1 ol5tojojo 131217 d 8i - 010l1 0 11 0 l6 0F 0 l6 TEXT M meure ausse a sugierast one assumewW MC pom W W I1M To prevent recurrence of these events and to improve SQN's overall surveillance program, TVA is implementing the following measures:
1.
A review to evaluate all aspects of the acquisition and utilization of data used to schedule sis. This review will include an evaluation of the methods used to update the SI scheduling computer program as well as the current performance of the computer program itself.
2.
SQN Quality Assurance (QA) personnel will revise their regularly scheduled audits of the surveillance program to include expanded reviews which will verify the accuracy of the computer program's data base and ensure that established change control measures are being followed.
3.
An "SI Coordinator" will be established within each SI performance organization. This individual will be technically qualified with that organization and will be responsible for interacting with M&S personnel for scheduling or updating SI packages, as well as ensuring SI test packages are adequately reviewed and returned to M&S in a timely manner.
4.
For TS implementing sis, approval to postpone, delete, or reschedule a scheduled performance must be obtained by the SQN plant manager or his designee.
The above described actions will ensure the technical adequacy of completed SI packages, decrease the scheduling errors, aad improve the overall efficiency of the SQN surveillance program. These actions are expected to be implemented by June 1, 1988.
ADDITIONAL INFORMATION
There have been 5 previous occurrences of TS surveillance intervals that were exceeded due to scheduling errors - SQRO-327/85001, 85003, 85004, 85049, and 86013.
0835Q l
- .g.......
.u. x 1.
..... n...
w TENNESSEE VALLEY AUTHORITY Sequoyah Nuclear Plant Post Office Box 2000 Soddy-Daisy, Tennessee 37379 U. S. Nuclear Regulatory Commission I
Document Control Desk Washington, DC 20555 Gentlemen; i
TENNESSEE VALLEY AUTHORITY - SEQUOYAH NUCLEAR PIANT UNIT 1 - DOCKET NO.
50-327 - FACILITY OPERATING LICENSE DPR REPORTABLE OCCURRENCE REPORT SQRO-50-327/88001 REVISION 1 The enclosed licensee event report is being revised to include an additional deficiency found in the surveillance instruction scheduling computer program
)
and to provide additional corrective actions. This event was previously reported in accordance with 10 CFR 50.73, paragraph a.2.1.B. on January 23, 1988.
Very truly yours, TENNESSEE VALLEY AUTHORITY i
S. J. Smith Plant Manager Enclosure cc (Enclosure):
J. Nelson Grace, Regional Administrator U. S. Nuclear Regulatory Connission Suite 2900 101 Marietta Street, noncompliance Atlanta, Georgia 30323 Records Center Institute of Nuclear Power Operations Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 NRC Inspector, Sequoyah Nuclear Plant f l An Equal Opportunity Employer
|
---|
|
|
| | Reporting criterion |
---|
05000327/LER-1988-001, :on 880111,four Emergency Diesel Generators Declared Inoperable Due to Interval for Tech Spec Surveillance Requirement 4.8.1.2 Exceeded.Caused by Oversight During Rev of Computer Program.W/Undated Ltr |
- on 880111,four Emergency Diesel Generators Declared Inoperable Due to Interval for Tech Spec Surveillance Requirement 4.8.1.2 Exceeded.Caused by Oversight During Rev of Computer Program.W/Undated Ltr
| | 05000328/LER-1988-001-01, :on 880111,ltr Received from S&W Revealing That Lower Support Frame of Containment Spray HXs 2A & 2B Could Be Overstressed During Design Basis Seismic Event.Caused by Design Deficiency.Frames Modified |
- on 880111,ltr Received from S&W Revealing That Lower Support Frame of Containment Spray HXs 2A & 2B Could Be Overstressed During Design Basis Seismic Event.Caused by Design Deficiency.Frames Modified
| | 05000328/LER-1988-002-01, :on 880118,instrument Maint Instruction Incorrectly Measured Response Time of Two Valves.Caused by Inadequate Review of ECN-L5591.Permanent Procedure Changes 88-105 & 88-106 Issued |
- on 880118,instrument Maint Instruction Incorrectly Measured Response Time of Two Valves.Caused by Inadequate Review of ECN-L5591.Permanent Procedure Changes 88-105 & 88-106 Issued
| | 05000327/LER-1988-003, :on 880114,both Trains of Auxiliary Bldg Isolation Inadvertently Actuated.Cause Undetermined.Operator Notified Mechanics Working on RM-90-101A Channel & Output Signal Reduced Below High Radiation Setpoint |
- on 880114,both Trains of Auxiliary Bldg Isolation Inadvertently Actuated.Cause Undetermined.Operator Notified Mechanics Working on RM-90-101A Channel & Output Signal Reduced Below High Radiation Setpoint
| | 05000328/LER-1988-003-02, :on 880119,discovered Ice Buildup in Flow Passages of Ice Condenser Due to Sublimation.Cause Not Determined.Ice Condenser Defrosted & Special Maint Instruction Performed |
- on 880119,discovered Ice Buildup in Flow Passages of Ice Condenser Due to Sublimation.Cause Not Determined.Ice Condenser Defrosted & Special Maint Instruction Performed
| | 05000328/LER-1988-003, :on 880119,discovered Ice Buildup in Flow Passage of Ice Condenser.Caused by Failure to Convert Original Design Requirements Into Verifiable,Repeatable Surveillance Requirements.Condenser Defrosted |
- on 880119,discovered Ice Buildup in Flow Passage of Ice Condenser.Caused by Failure to Convert Original Design Requirements Into Verifiable,Repeatable Surveillance Requirements.Condenser Defrosted
| | 05000327/LER-1988-004, :on 880111,discovered That 24 Breakers Did Not Adequately Protect 8 Awg & 10 Awg Cables from auto-ignition Temps.Caused by Programmatic Failure to Verify Proper Breaker Characteristic Curve.Breakers Replaced |
- on 880111,discovered That 24 Breakers Did Not Adequately Protect 8 Awg & 10 Awg Cables from auto-ignition Temps.Caused by Programmatic Failure to Verify Proper Breaker Characteristic Curve.Breakers Replaced
| | 05000328/LER-1988-004-01, :on 880127,during Surveillance Testing, Emergency Start of Four Diesel Generators Occurred.Caused by Shutdown Board Deenergizing Due to Normal Feeder Breaker Failing to Close.Lockout Relay Tested |
- on 880127,during Surveillance Testing, Emergency Start of Four Diesel Generators Occurred.Caused by Shutdown Board Deenergizing Due to Normal Feeder Breaker Failing to Close.Lockout Relay Tested
| | 05000327/LER-1988-005, :on 880116,turbine Bldg Sump Release Line Radiation Monitor Inappropriately Declared Operable on 880115 Resulting in Failure to Take Grab Samples for 25.5 H. Caused by Operator Error.Grab Samples Resumed |
- on 880116,turbine Bldg Sump Release Line Radiation Monitor Inappropriately Declared Operable on 880115 Resulting in Failure to Take Grab Samples for 25.5 H. Caused by Operator Error.Grab Samples Resumed
| | 05000328/LER-1988-005, :on 880212,smoke Discovered Coming from Speed Increaser Unit for Centrifugal Charging Pump 2A-A.Caused by Bolts Backing Out Due to Lack of Periodic Adjustments.Speed Increaser Lube Oil Pump 2A-A CCP Replaced |
- on 880212,smoke Discovered Coming from Speed Increaser Unit for Centrifugal Charging Pump 2A-A.Caused by Bolts Backing Out Due to Lack of Periodic Adjustments.Speed Increaser Lube Oil Pump 2A-A CCP Replaced
| | 05000328/LER-1988-006, :on 880207,main Steam Isolation Occurred & Reactor Trip Signal Generated by ESF Actuation Sys.Caused by Improper Compliance W/Procedures & Nuance Between Operating Procedures.Procedures Changed & Recategorized |
- on 880207,main Steam Isolation Occurred & Reactor Trip Signal Generated by ESF Actuation Sys.Caused by Improper Compliance W/Procedures & Nuance Between Operating Procedures.Procedures Changed & Recategorized
| | 05000327/LER-1988-006, :on 880127,containment Ventilation Isolation Occurred.Caused by Instrument Maint Technician Inadvertently Removing Incorrect Radiation Monitor Module.Technician Counseled |
- on 880127,containment Ventilation Isolation Occurred.Caused by Instrument Maint Technician Inadvertently Removing Incorrect Radiation Monitor Module.Technician Counseled
| | 05000328/LER-1988-006-01, :on 880207,main Steam Isolation Occurred & Reactor Trip Signal Generated by ESF Actuation Sys.Caused by Improper Compliance W/Procedures & Nuance Between Operating Procedures.Procedure Changed & Recategorized |
- on 880207,main Steam Isolation Occurred & Reactor Trip Signal Generated by ESF Actuation Sys.Caused by Improper Compliance W/Procedures & Nuance Between Operating Procedures.Procedure Changed & Recategorized
| | 05000327/LER-1988-007, :on 880124,discovered That Auxiliary Bldg Secondary Containment Encl Not Maintained within TS Set Configuration.Caused by Use of Improper Design Assumptions.Aop Instruction Enhanced |
- on 880124,discovered That Auxiliary Bldg Secondary Containment Encl Not Maintained within TS Set Configuration.Caused by Use of Improper Design Assumptions.Aop Instruction Enhanced
| | 05000328/LER-1988-007-02, :on 880210,main Steam Isolation Occurred During Calibr of Channel I Turbine Impulse Pressure Transmitter. Caused by Inadequate Calibr Procedure & Weak Communication. Calibr Procedure Revised |
- on 880210,main Steam Isolation Occurred During Calibr of Channel I Turbine Impulse Pressure Transmitter. Caused by Inadequate Calibr Procedure & Weak Communication. Calibr Procedure Revised
| | 05000328/LER-1988-008, :on 880209,failure to Initiate Performance of Required Surveillance Instruction in Timely Manner Resulted in Tech Spec 3/4.4.6.2 Being Exceeded.Caused by Personnel Error.Operations Personnel Instructed |
- on 880209,failure to Initiate Performance of Required Surveillance Instruction in Timely Manner Resulted in Tech Spec 3/4.4.6.2 Being Exceeded.Caused by Personnel Error.Operations Personnel Instructed
| | 05000327/LER-1988-008-01, :on 880130,discovered Essential Raw Cooling Water Sys Effluent Line Radiation Monitor Inappropriately Declared Operable & Tech Spec Action Statement Exited Prematurely.Caused by Personnel Error |
- on 880130,discovered Essential Raw Cooling Water Sys Effluent Line Radiation Monitor Inappropriately Declared Operable & Tech Spec Action Statement Exited Prematurely.Caused by Personnel Error
| | 05000328/LER-1988-008-02, :on 880209,Surveillance Instruction (SI)-137.2 Not Completed within Time Interval Required by Tech Spec 3/4.4.6.2.Caused by Personnel Error.Part C of SI-137.2 Completed & Operations Personnel Instructed |
- on 880209,Surveillance Instruction (SI)-137.2 Not Completed within Time Interval Required by Tech Spec 3/4.4.6.2.Caused by Personnel Error.Part C of SI-137.2 Completed & Operations Personnel Instructed
| | 05000328/LER-1988-009-02, :on 880207 & 28,ESF Main Steam Line Isolation Actuation Occurred During Maint Activities.Caused by Improper Verification of Required Logic That Generates Signal.Operators Provided W/Addl Training |
- on 880207 & 28,ESF Main Steam Line Isolation Actuation Occurred During Maint Activities.Caused by Improper Verification of Required Logic That Generates Signal.Operators Provided W/Addl Training
| | 05000328/LER-1988-009, :on 871205,electromagnetic Interference Caused Spurious High Radiation Spikes Resulting in Two Containment Ventilation Isolations.Sample Gas Prefilter Replacement Increased from Once Every 24 H to Every 4 H |
- on 871205,electromagnetic Interference Caused Spurious High Radiation Spikes Resulting in Two Containment Ventilation Isolations.Sample Gas Prefilter Replacement Increased from Once Every 24 H to Every 4 H
| | 05000327/LER-1988-009, :on 880204,discovered That Inaccurate Primary to Secondary Leak Rates Measurements Resulted in Potential Noncompliance W/Limiting Condition for Operation.Caused by Inadequate Procedure.Procedure Revised |
- on 880204,discovered That Inaccurate Primary to Secondary Leak Rates Measurements Resulted in Potential Noncompliance W/Limiting Condition for Operation.Caused by Inadequate Procedure.Procedure Revised
| | 05000328/LER-1988-010-02, :on 880309,centrifugal Charging Pump Placed in pull-to-lock Position While Second Pump Inoperable.Caused by Personnel Error.Procedure Changes Initiated & Tech Specs Being Reviewed |
- on 880309,centrifugal Charging Pump Placed in pull-to-lock Position While Second Pump Inoperable.Caused by Personnel Error.Procedure Changes Initiated & Tech Specs Being Reviewed
| | 05000327/LER-1988-010, :on 880205,procedure Governing Stroke Time Testing for motor-operated Valves Determined Inconsistent W/ Design Criteria for ESF Actuated Valves.Max Allowable Stroke Time Corrected as Specified by SI-166 |
- on 880205,procedure Governing Stroke Time Testing for motor-operated Valves Determined Inconsistent W/ Design Criteria for ESF Actuated Valves.Max Allowable Stroke Time Corrected as Specified by SI-166
| | 05000328/LER-1988-010, :on 871221,electromagnetic Interference Caused Spurious High Radiation Spikes Resulting in Two Containment Ventilation Isolations.Caused by Electromagnetic Interference in Radiation Monitor Cables |
- on 871221,electromagnetic Interference Caused Spurious High Radiation Spikes Resulting in Two Containment Ventilation Isolations.Caused by Electromagnetic Interference in Radiation Monitor Cables
| | 05000328/LER-1988-011-01, :on 880306,cold Leg Accumulator 3 Declared Inoperable Due to Failure to Perform Surveillance Requirement Used to Verify Boron Concentration.Caused by Personnel Error.Procedure Revised |
- on 880306,cold Leg Accumulator 3 Declared Inoperable Due to Failure to Perform Surveillance Requirement Used to Verify Boron Concentration.Caused by Personnel Error.Procedure Revised
| | 05000327/LER-1988-011, :on 880216,both Trains of Control Room Emergency Ventilation Sys Inoperable.Caused by Inadequate Review of Applicable Tech Specs Before Removing Generator from Svc.Diesel Generator Returned to Svc |
- on 880216,both Trains of Control Room Emergency Ventilation Sys Inoperable.Caused by Inadequate Review of Applicable Tech Specs Before Removing Generator from Svc.Diesel Generator Returned to Svc
| | 05000328/LER-1988-012-01, :on 880305,level Control Valve 2-LCV-3-175 Could Not Be Opened from Main Control Room.Caused by Crew Not Immediately Entering Limiting Condition for Operation 3.0.5.Late Entry of Condition Made |
- on 880305,level Control Valve 2-LCV-3-175 Could Not Be Opened from Main Control Room.Caused by Crew Not Immediately Entering Limiting Condition for Operation 3.0.5.Late Entry of Condition Made
| | 05000327/LER-1988-012, :on 880301,ESF Actuation Containment Ventilation Isolation Occurred.Caused by Prefilters Clogging Due to Suspended Particulate Near Radiation Monitor. Prefilter Change Frequency Increased |
- on 880301,ESF Actuation Containment Ventilation Isolation Occurred.Caused by Prefilters Clogging Due to Suspended Particulate Near Radiation Monitor. Prefilter Change Frequency Increased
| | 05000327/LER-1988-013, :on 880314,four Steam Generator Blowdown Sys Radiation Monitors Discovered Inadequately Tested.Caused by Oversight During Implementation of Surveillance Instruction Review Program.Tests Satisfactorily Completed |
- on 880314,four Steam Generator Blowdown Sys Radiation Monitors Discovered Inadequately Tested.Caused by Oversight During Implementation of Surveillance Instruction Review Program.Tests Satisfactorily Completed
| | 05000328/LER-1988-013, :on 880316,rod Control Sys Position Indication Not within 2 Steps of Actual Demand Position Per Tech Spec 3.1.3.3.Caused by Inaccuracy in Group 2 Demand Step Counter. Personnel Replaced Supervisory & Data Logging |
- on 880316,rod Control Sys Position Indication Not within 2 Steps of Actual Demand Position Per Tech Spec 3.1.3.3.Caused by Inaccuracy in Group 2 Demand Step Counter. Personnel Replaced Supervisory & Data Logging
| | 05000328/LER-1988-013-01, :on 880316 & 17,rod Control Sys Deficiencies Caused Inaccuracies in Rod Group Demand Position Indication Resulting in Manual Reactor Trips.Caused by Demand Step Counter Circuitry Failure & Internal Binding |
- on 880316 & 17,rod Control Sys Deficiencies Caused Inaccuracies in Rod Group Demand Position Indication Resulting in Manual Reactor Trips.Caused by Demand Step Counter Circuitry Failure & Internal Binding
| | 05000328/LER-1988-013, :on 880316 & 17,rod Group Demand Position Indication Not within Plus/Minus 2 Steps of Actual Demand Position,Resulting in Three Manual Reactor Trips.Caused by Rod Control Sys Deficiencies |
- on 880316 & 17,rod Group Demand Position Indication Not within Plus/Minus 2 Steps of Actual Demand Position,Resulting in Three Manual Reactor Trips.Caused by Rod Control Sys Deficiencies
| | 05000328/LER-1988-014, :on 880320,pressure Changes in balance-of-plant Condensate Sys Caused Main Feedwater Pumps to Trip.Procedure Revised to de-energize Main Feedwater Pump Trip Bus While Filling & Deaerating Condensate Sys |
- on 880320,pressure Changes in balance-of-plant Condensate Sys Caused Main Feedwater Pumps to Trip.Procedure Revised to de-energize Main Feedwater Pump Trip Bus While Filling & Deaerating Condensate Sys
| | 05000327/LER-1988-014-01, :on 880314,noncompliance W/Configuration Control Requirements Following post-mod Test of Radiation Monitor Resulted in Containment Ventilation Isolation.Caused by Personnel Error.Personnel Counseled |
- on 880314,noncompliance W/Configuration Control Requirements Following post-mod Test of Radiation Monitor Resulted in Containment Ventilation Isolation.Caused by Personnel Error.Personnel Counseled
| | 05000328/LER-1988-015-01, :on 880324,inadvertent Train a Main Feedwater (EIIS Code Sj) Isolation Occurred.Caused by MI-10.9.2 Inadequacy.Maint Instructions MI-10.9.1 & MI-10.9.2 Revised |
- on 880324,inadvertent Train a Main Feedwater (EIIS Code Sj) Isolation Occurred.Caused by MI-10.9.2 Inadequacy.Maint Instructions MI-10.9.1 & MI-10.9.2 Revised
| | 05000327/LER-1988-015, :on 880317,Tech Spec Surveillance Requirement Not Completely Incorporated Into Implementing Procedure. Caused by Incomplete Procedure Review.Surveillance Instruction 410.2 Revised |
- on 880317,Tech Spec Surveillance Requirement Not Completely Incorporated Into Implementing Procedure. Caused by Incomplete Procedure Review.Surveillance Instruction 410.2 Revised
| | 05000328/LER-1988-016-01, :on 880402,found That Three Relief Valves Exceeded Tech Spec Lift Setting.Caused by Using Different Methodologies to Determine Valve Lift Setting Between Bench & Inservice Tests.Consistent Method to Be Used |
- on 880402,found That Three Relief Valves Exceeded Tech Spec Lift Setting.Caused by Using Different Methodologies to Determine Valve Lift Setting Between Bench & Inservice Tests.Consistent Method to Be Used
| | 05000327/LER-1988-016, :on 880324,unplanned Main Steam Line Isolation Signal Occurred.Caused by Inadequate Review of Work Package Issued to Replace Flexible Sense Lines on Transmitter. Content of LER Will Be Reviewed W/Personnel |
- on 880324,unplanned Main Steam Line Isolation Signal Occurred.Caused by Inadequate Review of Work Package Issued to Replace Flexible Sense Lines on Transmitter. Content of LER Will Be Reviewed W/Personnel
| | 05000327/LER-1988-017, :on 880331,Train a Containment Ventilation Isolation Occurred.Caused by Improperly Controlling Operation of Sample Pump Local Switch.Local Sample Pump Switch Will Be Replaced Prior to Mode 4 |
- on 880331,Train a Containment Ventilation Isolation Occurred.Caused by Improperly Controlling Operation of Sample Pump Local Switch.Local Sample Pump Switch Will Be Replaced Prior to Mode 4
| | 05000328/LER-1988-017-01, :on 880401,inadvertent Reactor Trip Signal Generated.Caused by Lack of Work Document Initiated Before Manipulating Fuse & Misunderstanding of Fuse Connector Const.Reactor Trip Signal Reset |
- on 880401,inadvertent Reactor Trip Signal Generated.Caused by Lack of Work Document Initiated Before Manipulating Fuse & Misunderstanding of Fuse Connector Const.Reactor Trip Signal Reset
| | 05000327/LER-1988-018, :on 880411,incomplete Posting of Signs Resulted in Radio Transmission Interference & Reactor Trip Signal. Caused by Use of Portable Radio in Accumulator Room 4. Reduction of Radio Power Under Review |
- on 880411,incomplete Posting of Signs Resulted in Radio Transmission Interference & Reactor Trip Signal. Caused by Use of Portable Radio in Accumulator Room 4. Reduction of Radio Power Under Review
| | 05000328/LER-1988-018, :on 880330,improper Maint of Containment Integrity Resulted in Noncompliance W/Tech Spec.Caused by Lack of Available Regulatory Guidance Re Use of Threaded Caps During Const of Plant.Cap Design Changed |
- on 880330,improper Maint of Containment Integrity Resulted in Noncompliance W/Tech Spec.Caused by Lack of Available Regulatory Guidance Re Use of Threaded Caps During Const of Plant.Cap Design Changed
| | 05000327/LER-1988-018-01, :on 880411,first Out Reactor Trip Annunciator Received Twice But No Reactor Trips Occurred.Caused by Inadequate Posting of Signs Prohibiting Use of Portable Radios in Accumulator Rooms.Addl Signs Posted |
- on 880411,first Out Reactor Trip Annunciator Received Twice But No Reactor Trips Occurred.Caused by Inadequate Posting of Signs Prohibiting Use of Portable Radios in Accumulator Rooms.Addl Signs Posted
| | 05000328/LER-1988-019-02, :on 880407,discovered That Two ECCS Pumps to Be Inoperable,Resulting in Inadvertent Entry Into Tech Spec 3.0.3.Caused by Inadequate Work Control.Plant Procedure for Work Control Revised |
- on 880407,discovered That Two ECCS Pumps to Be Inoperable,Resulting in Inadvertent Entry Into Tech Spec 3.0.3.Caused by Inadequate Work Control.Plant Procedure for Work Control Revised
| | 05000327/LER-1988-019-01, :on 880424 & 0502,reactor Trip Signals Generated from Source Range Nuclear Instrument Channel Spike.Caused by Noise Induced Operation of Welding Machine at High Frequency |
- on 880424 & 0502,reactor Trip Signals Generated from Source Range Nuclear Instrument Channel Spike.Caused by Noise Induced Operation of Welding Machine at High Frequency
| | 05000328/LER-1988-019, :on 880407,inadequate Work Control Caused ECCS Pumps to Be Inoperable Resulting in Inadvertent Entry Into Tech Spec 3.0.3.Plant Procedure Revised to Ensure Activities Controlled During Work Impact Evaluation |
- on 880407,inadequate Work Control Caused ECCS Pumps to Be Inoperable Resulting in Inadvertent Entry Into Tech Spec 3.0.3.Plant Procedure Revised to Ensure Activities Controlled During Work Impact Evaluation
| | 05000327/LER-1988-019, :on 880424,reactor Trip Signal Generated from Electromagnetic Interference.Caused by Welding Machine Operating at High Frequency Near Source Range Nuclear Instrument Cabling.Signals Can Be Bypassed |
- on 880424,reactor Trip Signal Generated from Electromagnetic Interference.Caused by Welding Machine Operating at High Frequency Near Source Range Nuclear Instrument Cabling.Signals Can Be Bypassed
| | 05000328/LER-1988-020, :on 880422,ERCW Containment Isolation Valves Did Not Pass Leak Rate Test.Caused by Improper Application of Valve Usage.Work Requests Initiated to Repair Valves & Components Cleaned |
- on 880422,ERCW Containment Isolation Valves Did Not Pass Leak Rate Test.Caused by Improper Application of Valve Usage.Work Requests Initiated to Repair Valves & Components Cleaned
| | 05000327/LER-1988-020-01, :on 880512,potential Operation Outside Design Basis Noted.Caused by Unanalyzed Single Failure That Could Cause Inadvertent Actuation of Cold Overpressure Protection Sys During Postulated Main Steamline Break |
- on 880512,potential Operation Outside Design Basis Noted.Caused by Unanalyzed Single Failure That Could Cause Inadvertent Actuation of Cold Overpressure Protection Sys During Postulated Main Steamline Break
| | 05000328/LER-1988-021, :on 880504,containment Penetration Circuit Breakers Test Did Not Completely Satisfy Tech Spec.Caused by Incorrect Interpretation of Bases for Tech Spec 3.8.3.1. Scheduling Program Will Be Revised |
- on 880504,containment Penetration Circuit Breakers Test Did Not Completely Satisfy Tech Spec.Caused by Incorrect Interpretation of Bases for Tech Spec 3.8.3.1. Scheduling Program Will Be Revised
| |
|