LER-1998-001, Forwards LER 98-001-00 Re Unit 1 Reactor Trip Resulting from Breaker Failure.Rept Submitted IAW 10CFR50.73(a)(2)(iv) as Event or Condition,Resulted in Automatic Actuation of Esfs, Including Reactor Protection Sys |
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a Tennessee Valley Authority, Post Offce Box 2000. Soddy Daisy, Tennessee 17379-2000 l
Masoud Bajestani Site Vee President Sequoyah Ntclear Plant June 18, 1998 U.S.
Nuclear Regulatory Commission 10 CFR 50.73 ATTN:
Document Control Desk Washington, D.C.
20555 Gentlemen:
TENNESSEE VALLEY AUTHORITY - SEQUOYAH NUCLEAR PLANT (SQN)
UNIT 1 - DOCKET NO. 50-327 - FACILITY OPERATING LICENSE DPR LICENSEE EVENT REPORT (LER) 50-327/1998001 The enclosed report provides details concerning a Unit 1 reactor trip resulting from a breaker failure.
This report is being submitted in accordance with 10 CFR 50.73 (a) (2) (iv) as an event or condition that resulted in an automatic actuation of engineering safety features, including the reactor protection system.
Sincerely, d
/
Masoud B stani /
Enclos rA Se'e page 2 cc:
hh 9806230260 980618
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PDR ADOCK 05000327 S
PDR
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U.S. Nuclear Regulatory Commission Page 2 June 18, 1998 Enclosure cc (Enclosure):
INPO Records Center Institute of Nuclear Power Operations 700 Galleria Parkway Atlanta, Georgia 30339-5957 Mr.
R.
W. Hernan, Project Manager U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 NRC Resident Inspector Sequoyah Nuclear Plant 2600 Igou Ferry Road Soddy-Daisy, Tennessee 37379-3624 Regional Administrator U.S. Nuclear Begulatory Commission Region II Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, Georgia 30303-3415
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| 05000327/LER-1998-001-04, :on 980519,automatic Reactor Trip Occurred. Caused by Failure of Alternate Feedwater to 1A1-A 480-volt Shutdown Board.Normal Feedwater Breaker Placed in Svc & 480- Volt Shutdown Board Returned to Operation |
- on 980519,automatic Reactor Trip Occurred. Caused by Failure of Alternate Feedwater to 1A1-A 480-volt Shutdown Board.Normal Feedwater Breaker Placed in Svc & 480- Volt Shutdown Board Returned to Operation
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000327/LER-1998-001, Forwards LER 98-001-00 Re Unit 1 Reactor Trip Resulting from Breaker Failure.Rept Submitted IAW 10CFR50.73(a)(2)(iv) as Event or Condition,Resulted in Automatic Actuation of Esfs, Including Reactor Protection Sys | Forwards LER 98-001-00 Re Unit 1 Reactor Trip Resulting from Breaker Failure.Rept Submitted IAW 10CFR50.73(a)(2)(iv) as Event or Condition,Resulted in Automatic Actuation of Esfs, Including Reactor Protection Sys | 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000328/LER-1998-001, Forwards LER 98-001-00 Providing Details Re Automatic Turbine & Reactor Trip Due to Failure of Sudden Pressure Relay on B Phase Main Transformer | Forwards LER 98-001-00 Providing Details Re Automatic Turbine & Reactor Trip Due to Failure of Sudden Pressure Relay on B Phase Main Transformer | 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000328/LER-1998-001-05, :on 980827,turbine Trip Occurred Followed by Reactor Trip.Caused by Failure of Sudden Pressure Relay on B Phase Main Transformer.Control Room Operators Responded & Removed,Inspected & Replaced Failed Relays |
- on 980827,turbine Trip Occurred Followed by Reactor Trip.Caused by Failure of Sudden Pressure Relay on B Phase Main Transformer.Control Room Operators Responded & Removed,Inspected & Replaced Failed Relays
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000327/LER-1998-002-03, :on 980716,inadequate Surveillance Testing Was Discovered.Caused by Misinterpretation of ANSI Standard. Revised Appropriate Procedures to Provide Required Guidance |
- on 980716,inadequate Surveillance Testing Was Discovered.Caused by Misinterpretation of ANSI Standard. Revised Appropriate Procedures to Provide Required Guidance
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | | 05000327/LER-1998-002, Forwards LER 98-002-00,providing Details Concerning Inadequate Surveillance Testing of Gas Treatment Ventilation Sys | Forwards LER 98-002-00,providing Details Concerning Inadequate Surveillance Testing of Gas Treatment Ventilation Sys | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000328/LER-1998-002, Forwards LER 98-002-00 Re Automatic Turbine & Reactor Trip, Resulting from Failure of Sudden Pressure Relay on B Phase Main Transformer | Forwards LER 98-002-00 Re Automatic Turbine & Reactor Trip, Resulting from Failure of Sudden Pressure Relay on B Phase Main Transformer | 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000328/LER-1998-002-05, :on 981016,turbine Trip Occurred Followed by Reactor Trip.Caused by Generator Lockout.Mod Being Evaluated to Physically Isolate Relays from Vibration of Transformers & Adding Two of Two Logic for Actuation of Sudden Pressure |
- on 981016,turbine Trip Occurred Followed by Reactor Trip.Caused by Generator Lockout.Mod Being Evaluated to Physically Isolate Relays from Vibration of Transformers & Adding Two of Two Logic for Actuation of Sudden Pressure
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000327/LER-1998-003-04, :on 981109,automatic Reactor Trip Occurred. Caused by Component in Bridge Circuit of Vital Inverter Failed.Inverter Bridge Circuit Replaced |
- on 981109,automatic Reactor Trip Occurred. Caused by Component in Bridge Circuit of Vital Inverter Failed.Inverter Bridge Circuit Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) | | 05000327/LER-1998-003-01, :on 981109,Vital Inverter 1-IV Tripped.Caused by Failed Oscillator Board with Bad Solder Joint,Attributed to Mfg Defect.Replaced Component & Returned Inverter to Operable Status |
- on 981109,Vital Inverter 1-IV Tripped.Caused by Failed Oscillator Board with Bad Solder Joint,Attributed to Mfg Defect.Replaced Component & Returned Inverter to Operable Status
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000327/LER-1998-004-02, :on 981120,failure to Perform Surveillance within Required Time Interval,Was Determined.Caused by Leaking Vent Valve.Engineering Personnel Evaluated Alternative Methods for Performing Channel Check |
- on 981120,failure to Perform Surveillance within Required Time Interval,Was Determined.Caused by Leaking Vent Valve.Engineering Personnel Evaluated Alternative Methods for Performing Channel Check
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000327/LER-1998-004, Forwards LER 98-004-00,providing Details Concerning Inability to Complete Surveillance within Required Time Interval | Forwards LER 98-004-00,providing Details Concerning Inability to Complete Surveillance within Required Time Interval | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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