On June 13 2007, Pilgrim Station was notified that three of the four Target Rock relief valve pilot assemblies exceeded the Technical Specification (TS) tolerance limit of 1115 ±11 psi (± 1%) during routine testing at the Wyle Laboratories test facility. Certified replacement relief valve pilot assemblies were previously installed in the plant.
The cause of the as-found initial popping pressures exceeding the TS tolerance limit for two of the pilot valves was "setpoint variance". The cause of the as-found initial popping pressure exceeding the TS tolerance limit for the third pilot valve was corrosion bonding.
Corrective actions taken include replacing the pilot valves with certified tested replacements.
The conditions posed no threat to public health and safety because an evaluation of the effect of the as-found set pressures concluded that no design or licensing basis limits would have been exceeded had the SRVs been required to operate. |
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
BACKGROUND
The Pilgrim Station Pressure Relief System (PRS) is designed to prevent over-pressurization of the ASME Boiler and Pressure Vessel Code qualified nuclear steam supply system. The PRS consists of two safety valves and four two-stage relief valves. These valves are installed in the main steam system piping upstream of the main steam isolation valves and are located within the Drywell. The safety valves are self-actuating, provide over-pressure protection, and discharge directly to the Drywell atmosphere when actuated. The relief valves augment the safety valves and are sized to prevent unnecessary actuation of the safety valves. The relief valves are self-actuating and discharge into the suppression pool through discharge piping connected to the valves. Each two-stage relief valve consists of a pilot assembly and a main stage. The pilot assembly provides the pressure sensing function and the main stage provides the pressure relieving function. The relief valves are also part of the Automatic Depressurization System (ADS). As part of the ADS, the relief valves are designed to automatically actuate as a result of a depressurization permissive signal, and can also be manually actuated from the Control Room for depressurization.
Technical Specification (TS) 3.6.D.1 specifies that the nominal setpoint of the relief valves shall be selected between 1095 and 1115 psig and that all relief valves shall be set at this nominal setpoint ± 11 psi. The valves' nameplate setpoints are 1115 psig each. Based on the tolerance limit of 11 psi (± 1%), a maximum pressure of 1126 psig and a minimum pressure of 1104 psig are allowed. The established TS limit is stricter that the standard allowable relief valve setpoint drift range of ± 3% given in Section XI of the ASME Boiler and Pressure Vessel Code.
The main steam relief valves were manufactured by Target Rock Corporation, model #7567F.
Since the early 1980s, increased initial lift pressure (or upward setpoint drift) has been an industry concern applicable to the two-stage relief valves found in BWRs. Industry investigations of relief valve reliability problems revealed that one of the primary causes of upward setpoint drift in the two-stage relief valves was corrosion bonding of the pilot valve disk to its seat. Three different design modifications were found to reduce or counteract the corrosion bonding: 1) installation of ion beam implanted platinum pilot valve disks, 2) the installation of Stellite-21 pilot valve disks, and 3) the installation of additional pressure actuation switches. PNPS implemented changes to install the Stellite-21 pilot valve disk design in the mid 1980 timeframe. Another cause of upward setpoint drift was a phenomenon know as "setpoint variance" identified in an EPRI document published in 1996, Technical Report TR-105872, "Safety and Relief Valve Testing and Maintenance Guide." The information contained within the report indicated that most main steam safety valve high lift failures were outside of the ± 1% allowable tolerance but within the ± 3% vendor design tolerance. The report went on to state that these failures were principally driven by the close tolerance between Technical Specification requirements and the actual ability of the valve to perform within the required pressure band. The report identified this phenomenon as "setpoint variance" which occurs when the first lift is between 1% and 3% and the following lifts are within 1%. This is a well recognized occurrence that the National Board of Boiler and Pressure Vessel Inspectors has observed for many years. The cause of this phenomenon has not been identified.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) Additionally, NRC review of upward setpoint drift is documented in NRC Regulatory Issue Summary 2000-12, Resolution of Generic Safety Issue B-55, "Improved Reliability of Target Rock Safety Relief Valves," and Generic Issue 165, "Spring Actuated Safety and Relief Valve Reliability.
In the review the NRC staff found that the industry has significantly improved valve performance and is continuing efforts to evaluate and improve performance as necessary. The staff found no new requirements were necessary and that existing quality assurance, maintenance rule and code testing requirements were adequate to ensure reliable valve performance in the future.
All four pilot assemblies for main steam relief valves RV-203-3A, 3B, 3C and 3D were removed during Refueling Outage 16.
EVENT DESCRIPTION
On June 13, 2007 Pilgrim Station was notified that three of the four pilot valve assemblies previously installed had as-found popping pressures that exceeded the maximum TS tolerance limit of 1126 psig. The as-found popping pressures were 1131 psig (serial number 1207), 1137 psig (serial number 1025), and 1126.7 psig (serial number 1049). The as-found popping pressure of serial number 1054 was 1123 psig.
The condition was identified while operating at 100 percent reactor power with the reactor mode selector switch in the RUN position. The reactor vessel pressure was about 1030 psig with the reactor water temperature at the saturation temperature for that pressure.
CAUSE
The root cause evaluation identified "set point variance" as the most probable cause of initial high as-found popping pressures exceeding the TS tolerance limit for two of the pilots (1207 and 1025) because these two pilots had a step change in set pressures between the first and subsequent lifts during both as-left and as-found testing. Minor corrosion bonding is the cause of the initial high as found popping pressure for the third pilot (1049).
CORRECTIVE ACTION
All four pilots were removed and replaced with spare pilots. The spare pilot valve assemblies that were installed were tested and certified to be within 1% of the normal set point required by Technical Specifications.
An electric lift system which will provide a non-safety backup to the safety-related mechanical lift is scheduled to be installed during the next refueling outage.
Any planned corrective actions will be implemented consistent with the Pilgrim Station corrective action program.
PILGRI
FACILITY NAME (1) M NUCLEAR POWER STATION DOCKET NUMBER (2) LER NUMBER (6) � 004� 00
SAFETY CONSEQUENCES
The condition posed no threat to public health and safety. A review of the applicable accident analysis revealed the following:
Minimum Critical Power Ratio (MCPR) Safety Limit — Fuel Clad Protection:
The limiting pressurization transient for Cycle 16 was the inadvertent HPCI injection followed by a turbine trip. The Operating Limit Minimum Critical Power Ratio (OLMCPR) was established based on the analysis of this event to protect against exceeding the Technical Specification MCPR safety limit of 1.06. This analysis used an assumed SRV set pressure value of 1126 psig. A review of the graphical analysis results provided in the Supplemental Reload Licensing Report shows both the peak neutron and heat flux precede the opening of the relief valves. Therefore, the higher as-found relief valve set pressures do not influence the analysis results with respect to the MCPR operating or safety limit.
Overpressure Protection for Reactor Coolant Pressure Boundary (RCPB):
MSIV Closure Flux Scram is the event used to design/verify adequate overpressure protection to avoid exceeding the ASME Code upset limit of 1375 psig. The valve position anticipatory scram is neglected in this analysis. This analysis used an assumed SRV set pressure value of 1126 psig.
The Cycle 16 analysis for overpressure protection predicted a peak vessel pressure of 1298 psig which results in a margin of 77 psig to the ASME code upset limit. Given the as-found set pressures, the peak vessel pressure will increase slightly (less than 4 psig) but peak vessel pressure will not exceed the acceptance limit of 1375 psig. This conclusion is based on a sensitivity analysis documented in NEDE-30476 "Setpoint Drift Investigation of Target Rock 2- Stage Safety/Relief Valves", dated February 1986. The sensitivity analysis estimated that a 10% increase in set pressure for each of the 4 SRVs would produce a 40 psig increase in peak vessel pressure. The 40 psig peak vessel pressure change translates to a 4 psig increase for each 1°/0 of set pressure increase. The average increase in as-found set pressure of the bank of 4 SRVs was 0.3 % (less than 1%). Therefore, the peak vessel pressure increase would be less than 4 psig and significant margin remains between the predicted peak vessel pressure and the ASME code limit of 1374 psig.
Anticipated Transient Without a Scram (ATWS) Beginning in Cycle 15, the licensed thermal power level for PNPS was increased from 1998 MWth to 2028 MWth. During the licensing phase of the power uprate, a revised ATWS analysis was performed that evaluated the MSIV closure and pressure regulator failed open (PRFO) events. The PRFO ATWS event resulted in a higher peak vessel pressure (1495 psig) than the MSIV closure ATWS pressure (1464 psig).
This analysis used the General Electric computer code ODYN. The analytical set pressures used were 1126 for three SRVs and 1136 for one SRV. The average set pressure for the bank of four SRV was 1128.5 psig.
Given the 0.9 psig difference between the average as-found set pressure of 1129.4 and the ATWS analysis value of 1128.5 psig, the peak vessel pressure increase would be small.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) Anticipated Transient Without a Scram (ATWS) con't Using the same method as used for the over pressure protection evaluation, the increase would be less than 4 psig and the calculated peak vessel pressure was expected to be below the emergency limit of 1500 psig.
Therefore given an ATWS event considering the as-found relief valve opening pressures, the estimated peak vessel pressure did not increase significantly based on engineering judgment, and system integrity would not have been impaired.
Loss of Feedwater — Core Coverage In the event of a loss of all Feedwater with reactor vessel isolation, the Reactor Core Isolation Cooling (RCIC) system or its backup, the High Pressure Coolant Injection (HPIC) system is required to maintain reactor water level above the top of active fuel. After the initial discharge of stored energy from the reactor vessel to the suppression pool, a single SRV is capable of removing decay heat. Reactor pressure will be controlled at the lowest set pressure of the four SRVs (i.e. 1123 psig for pilot assembly serial number 1054). A pilot assembly typically exhibits a higher setpoint during the initial opening and a slightly lower setpoint during subsequent lifts. The RCIC system is capable of maintaining rated flow of 400 gpm with reactor pressure between the 150 psig and 1126 psig while the HPCI system is capable of much greater flow rates over the same pressure range. Therefore the analysis that evaluated the capability to maintain reactor level was unaffected by the pilot assemblies with as-found popping pressures exceeding the TS limits.
Loss of Coolant Accident (LOCA) — Peak Clad Temperature Following a small break LOCA and vessel isolation, reactor pressure will remain high and is controlled by cycling the SRVs. The small break analysis for Pilgrim Station assumed that both HPCI and RCIC were unavailable. Core cooling is provided by the Alternate Depressurization System (ADS) in combination with low-pressure Core Standby Cooling Systems (CSCS). Until ADS initiation, the loss of inventory from the vessel is a function of break area and the reactor pressure is controlled by the SRVs. After the initial discharge of stored energy from the reactor vessel to the suppression pool by multiple SRVs, a single SRV is capable of removing decay heat. Since the lowest as-found popping pressure of the four relief valve pilot assemblies was 1123 psig (serial number 1054), the analysis on record is bounding with respect to reactor pressure and inventory loss from the vessel prior to depressurizations by ADS. Therefore the existing LOCA analysis provides a bounding prediction of core uncovery time, fuel clad heat-up and peak clad temperatures.
REPORTABILITY
This report is submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) because it was conservatively assumed that the as-found popping pressures could have been the pressure at which the relief valves would have operated if a high reactor pressure condition had occurred while the pilot assemblies were installed. The condition is assumed to have existed for a period greater than the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> limiting condition of operations specified in Technical Specification 3.6.D.2 for the relief valves.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
SIMILARITY TO PREVIOUS EVENTS
A review was conducted of Pilgrim Station LERs. The review focused on LERs related to relief valve tests submitted since 2001. The review identified LER 2001-004-000, LER 2004-001-00, and LER 2005-003-00.
ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for this report are as follows:
COMPONENTS� CODES Valve, Relief � RV SYSTEMS� CODES Main Steam� SB Licensing Correspondence Control Sheet Letter Number: 2.07.057 Licensing Engineer (LE):
MJ Gatslick Letter Number Cross-References: N/A Verify and Distribute Letter to the organization as needed: MJG LE / Initials Update Lop as needed: MJG LE / Initials Commitment Review per EN-LI-110 completed: MJG LE / Initials Results: No new commitments were identified.
Posting Required? (10 CFR 19.11(a)(4):
Y / If Yes, Posting completed by on LE / Initials Date Action Required?: Y / Action Items:
_Tracking Number Action Licensing Correspondence Control Sheet 2/6/07
|
---|
|
|
| | Reporting criterion |
---|
05000498/LER-2007-001 | Turbine-Driven Auxiliary Feedwater Pump Failed to Start During Surveillance Testing (Supplement 1) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2007-001 | -f Unit 1 Automatic Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000263/LER-2007-001 | | | 05000266/LER-2007-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000269/LER-2007-001 | Dual Unit Trip from Jocassee Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000272/LER-2007-001 | ESF Actuation of Auxiliary Feedwater Pumps in Mode 3. | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000265/LER-2007-001 | Manual Reactor Scram on Increasing Condenser Backpressure Due to a Decrease in 2A Offgas Train Efficiency | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000278/LER-2007-001 | Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000249/LER-2007-001 | Unit 3 High Pressure Coolant Injection System Declared Inoperable | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000282/LER-2007-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President Administration February 28, 2007 Indian Point Unit No. 2 Docket No. 50-247 NL-07-013 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2007-001-00, "Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure" Dear Sir: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The enclosed LER identifies an event where the plant was operated in a condition prohibited by Technical Specifications, which is reportable under 10 CFR 50.73(a)(2)(i)(B). This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP2-2007-00013. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, -Thr red R. Dacimo ite Vice President Indian Point Energy Center E Docket No. 50-247 NL-07-013 Page 2 of 2 Attachment: LER-2007-001-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 2 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104DEXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours.DReported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 2. DOCKET NUMBER 1 3. PAGE1. FACILITY NAME: INDIAN POINT 2 05000-247 1 OF 4 4. TITLE: Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix) | 05000483/LER-2007-001 | . Single Train Inoperability in the Essential Service Water System due to Inadequate Valve Closure Setup | | 05000286/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President June 4, 2007 Indian Point 3 Docket No. 50-286 N L-07-052 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop O-P1-17 Washington, D.C. 20555-0001 Subject:LLicensee Event Report # 2007-001-00, "Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply" Dear Sir or Madam: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The attached LER identifies an event where the reactor was manually tripped while critical, which is reportable under 10 CFR 50.73(a)(2)(iv)(A) . This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP3-2007-01775. There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. T. R. Jones, Manager, Licensing at (914) 734-6670. Sincerely, Fred R. Dacimo Site Vice President Indian Point Energy Center cc:LMr. Samuel J Collins, Regional Administrator, NRC Region I NRC Resident Inspector's Office, Indian Point 3 Mr. Paul Eddy, New York State Public Service Commission INPO Record Center pP,c.1)-1
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 6/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request:D50 hours.DReportedDlessons learned areDincorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME INDIAN POINT 3 2. DOCKET NUMBER 13. PAGE 05000-286 1 OFTD5 4. TITLE Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000309/LER-2007-001 | Uncompensated Degradation in a Security System | | 05000414/LER-2007-001 | Failure to Comply with Action Statement in Technical Specification (TS) 3.3.1 for Loss of a Channel of the Solid State Protection System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000311/LER-2007-001 | Inoperability of the Chilled Water System - (21 and 22 Chillers Inoperable) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000331/LER-2007-011 | . Undervoltage ConditiOn Resulted in the Actuation of the Emergency Diesel Generators | | 05000346/LER-2007-001 | Station Vent Radiation Monitor in Bypass due to Faulty Optical Isolation Board | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2007-001 | Vire President - Farley Operating Company, Inc. Po51 Office Drawer 470 Ashford, Alabarid 36312-0470 Tel 334 814 4511 Fax 334 814 4728 SOUTHERN June 22, 2007 COMPANY Energy to Serve Your World Docket Nos.: 50-348 NL-07-1231 50-364 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555-0001 Joseph M. Farley Nuclear Plant — Units 1 and 2
Licensee Event Report 2007-001-00
Technical Specification 3.8.1 Violation Due to
Failure of Breaker / Mechanism-Operated Cell Switch
Ladies and Gentlemen: Joseph M. Farley Nuclear Plant - Licensee Event Report (LER) No. 2007-001-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(v)(B). This letter contains no NRC commitments. If you have any questions, please advise. Sincerely, 7e. R. Johnson Vice President — Farley Joseph M. Farley Nuclear Plant 7388 North State Highway 95 Columbia AL 36319 JRJ/CHM Enclosure: Licensee Event Report 2007-001-00 - Unit 1 U. S. Nuclear regulatory Commission NL-07-1231 Page 2 cc:� Southern Nuclear Operating Company Mr. J. T. Gasser, Executive Vice President Mr. J. R. Johnson, Vice President — Farley Mr. D. H. Jones, Vice President — Engineering RTYPE: CFA04.054; LC # 14596 U. S. Nuclear Regulatory Commission Dr. W. D. Travers, Regional Administrator Ms. K. R. Cotton, NRR Project Manager — Farley Mr. E. L. Crowe, Senior Resident Inspector— Farley NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nudear Regulatory Commission, Washington, DC 2055570001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to infocolledsanrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information(See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Joseph M. Farley Nuclear Plant - Unit 1 05000 348 1 OF 4 4. TITLE Technical Specification 3.8.1 Violation Due to Failure of Breaker / Mechanism-Operated Cell (MOC) Switch | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2007-001 | As-Found Local Leak Rate Tests Not Performed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000456/LER-2007-001 | Unit 1 Reactor Trip Following a 345 Kv Transmission Line Lightning Strike | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2007-001 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000389/LER-2007-001 | S, Reactor Shutdown Due to Unidentified RCS Leakage | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2007-001 | 369 5McGuire Nuclear Station Unit 1 05000 1 OF5 | | 05000335/LER-2007-001 | Mispositioned Service Air Containment Isolation Valves | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000362/LER-2007-001 | Failure to declare Emergency Diesel Generator Inoperable and enter TS Action | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000353/LER-2007-001 | Scram Discharge Volume Vent and Drain Valves Opened Due To Fuse Removal | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000400/LER-2007-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2007-001 | Reactor Trip Due to a Loose Wire in the Main Transformer Monitoring Circuitry | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000389/LER-2007-002 | 2B2 Reactor Coolant Pump (RCP) Seal Housing Leakage | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000395/LER-2007-002 | Failure to Follow Administrative Controls Results in LCO 3.6.4 Violation | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2007-002 | Shutdown Cooling Pump Trip Results in Operation Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000414/LER-2007-002 | Technical Specification Violation Associated with Containment Valve Injection Water System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000416/LER-2007-002 | Reactor SCRAM due to Turbine Trip caused by Loss of Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000423/LER-2007-002 | Loss of Offsite Power Caused by Transmission System Operator While Defueled | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000311/LER-2007-002 | RReactor Trip Due to a Breach in the Condensate System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2007-002 | | | 05000454/LER-2007-002 | Technical Specification Required Shutdown of Unit 1 and Unit 2 Due to an Ultimate Heat Sink Pipe Leak Common to Both Units | | 05000282/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000315/LER-2007-002 | Failure to Declare Essential Service Water Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-002 | Technical Specification Prohibited Condition Due to Exceeding Containment Air Temperature Limit Allowed Outage Time as a Result of Changes in Instrument Uncertainty | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2007-002 | Completion of Shutdown Required by Technical Specifications due to Inoperable Rod Position Indication for Two Control Rods in the Same Control Bank | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000353/LER-2007-002 | Automatic Actuation of Main Condenser Low Vacuum Isolation Logic During Refueling Outage | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000272/LER-2007-002 | MManual Reactor Trips Due to Degraded Condenser Heat Removal | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
|