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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000293/LER-1999-010-02, :on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With1999-10-18018 October 1999
- on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With
05000293/LER-1999-009-02, :on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With1999-10-13013 October 1999
- on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With
05000293/LER-1999-008-02, :on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With1999-09-0707 September 1999
- on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With
05000293/LER-1999-007-02, :on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With1999-08-13013 August 1999
- on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With
05000293/LER-1999-006-02, :on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With1999-08-0404 August 1999
- on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With
05000293/LER-1999-005, :on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With1999-07-0808 July 1999
- on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With
05000293/LER-1999-004, :on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With1999-06-28028 June 1999
- on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With
05000293/LER-1999-003, :on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With1999-06-15015 June 1999
- on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With
05000293/LER-1999-002, :on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With1999-06-0303 June 1999
- on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With
05000293/LER-1999-001, :on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With1999-05-0606 May 1999
- on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With
05000293/LER-1998-029, :on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With1999-02-0101 February 1999
- on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With
05000293/LER-1998-028, :on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With1999-01-28028 January 1999
- on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With
05000293/LER-1998-026, :on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with1998-12-23023 December 1998
- on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with
05000293/LER-1998-007, :on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With1998-12-22022 December 1998
- on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With
05000293/LER-1998-025, :on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With1998-12-18018 December 1998
- on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With
05000293/LER-1998-018, :on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With1998-12-18018 December 1998
- on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With
05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation1998-12-18018 December 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation
05000293/LER-1997-017, :on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With1998-12-18018 December 1998
- on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With
05000293/LER-1998-024, :on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans1998-11-13013 November 1998
- on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans
05000293/LER-1998-023, :on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With1998-11-0404 November 1998
- on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With
05000293/LER-1998-022, :on 981002,unplanned Actuation of a EDG Occurred During Surveillance Test of Related Logic Sys Testing.Caused by Util non-licensed I&C Technician Error. Will Review Surveillance Procedures.With1998-10-30030 October 1998
- on 981002,unplanned Actuation of a EDG Occurred During Surveillance Test of Related Logic Sys Testing.Caused by Util non-licensed I&C Technician Error. Will Review Surveillance Procedures.With
05000293/LER-1998-013, :on 980606,inconclusive Fire Barrier Test Data Was Noted.Caused by Concerns About Adequacy of Original Basis for Three Hour Rating.Declared Enclosures Inoperable & Posted Fire Watch within One Hour.With1998-09-30030 September 1998
- on 980606,inconclusive Fire Barrier Test Data Was Noted.Caused by Concerns About Adequacy of Original Basis for Three Hour Rating.Declared Enclosures Inoperable & Posted Fire Watch within One Hour.With
05000293/LER-1998-020, :on 980730,operating W/Less than Min Operating Shift Crew Composition Was Noted.Caused by off-going SCRE Not Ensuring Proper Relief of SCRE Function.Individual Was Appropriately Counseled1998-08-28028 August 1998
- on 980730,operating W/Less than Min Operating Shift Crew Composition Was Noted.Caused by off-going SCRE Not Ensuring Proper Relief of SCRE Function.Individual Was Appropriately Counseled
05000293/LER-1998-019, :on 980727,declared Standby Liquid Control Subsystem B Inoperable.Caused by Leakage Through Pipe Fitting on Pressure Gauge PI-1160B.Removed Subject Gauge, Cleaned Pipe Threads & Reinstalled Gauge1998-08-26026 August 1998
- on 980727,declared Standby Liquid Control Subsystem B Inoperable.Caused by Leakage Through Pipe Fitting on Pressure Gauge PI-1160B.Removed Subject Gauge, Cleaned Pipe Threads & Reinstalled Gauge
05000293/LER-1998-013, :on 980606,inconclusive Fire Barrier Test Data Occurred.Caused by Concerns About Adequacy of Original Basis for 3 H Rating.Encls Declared Inoperable & Fire Watch Posted1998-07-0303 July 1998
- on 980606,inconclusive Fire Barrier Test Data Occurred.Caused by Concerns About Adequacy of Original Basis for 3 H Rating.Encls Declared Inoperable & Fire Watch Posted
05000293/LER-1998-011, :on 961126,operator Discovered Two Shield Plugs Removed from Floor Directly Over Torus Compartment.Caused by Lack of Formal Program to Control sub-compartment Barriers. Developed Formal Program to Control Compartment Barriers1998-06-26026 June 1998
- on 961126,operator Discovered Two Shield Plugs Removed from Floor Directly Over Torus Compartment.Caused by Lack of Formal Program to Control sub-compartment Barriers. Developed Formal Program to Control Compartment Barriers
05000293/LER-1998-007, :on 980330,discovered Single Failure Vulnerability of RHR Sys When in SPC Mode.Caused by Inadequate Original Design.Standing Order Issued to Declare LPCI Sys Inoperable When RHR Sys Is in SPC Mode1998-04-29029 April 1998
- on 980330,discovered Single Failure Vulnerability of RHR Sys When in SPC Mode.Caused by Inadequate Original Design.Standing Order Issued to Declare LPCI Sys Inoperable When RHR Sys Is in SPC Mode
05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Cause Is Attributed to Significant Effect Meteorlogical Conditions Have on EDG Room Temp.Completed Engineering Evaluation1998-04-17017 April 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Cause Is Attributed to Significant Effect Meteorlogical Conditions Have on EDG Room Temp.Completed Engineering Evaluation
05000293/LER-1997-004, :on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept1998-04-14014 April 1998
- on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept
05000293/LER-1998-003, :on 980220,discovered That RBCCW & Tbccw Heat Exchanger Supports Outside Design Basis Seismic Requirements.Caused by Calculation Error.Reviewed Similar Calculations & Counseled Individuals Associated W/Errors1998-03-23023 March 1998
- on 980220,discovered That RBCCW & Tbccw Heat Exchanger Supports Outside Design Basis Seismic Requirements.Caused by Calculation Error.Reviewed Similar Calculations & Counseled Individuals Associated W/Errors
05000293/LER-1998-002, :on 980205,EDG Room Air Temperature Went Below Design Basis.Caused by Unawareness of Significant Effect Wind Direction Has on EDG Room Temp.Engineering Evaluation (Ee 97-066 R-1) Was Completed & Approved1998-03-0909 March 1998
- on 980205,EDG Room Air Temperature Went Below Design Basis.Caused by Unawareness of Significant Effect Wind Direction Has on EDG Room Temp.Engineering Evaluation (Ee 97-066 R-1) Was Completed & Approved
05000293/LER-1997-026, :on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly1998-01-0505 January 1998
- on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly
05000293/LER-1997-025, :on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B1997-12-23023 December 1997
- on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B
05000293/LER-1997-021, :on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F1997-12-0404 December 1997
- on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F
05000293/LER-1997-020, :on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.51997-12-0404 December 1997
- on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.5
05000293/LER-1997-019, :on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures1997-12-0404 December 1997
- on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures
05000293/LER-1997-015, :on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc1997-12-0303 December 1997
- on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc
05000293/LER-1997-023, :on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door1997-12-0101 December 1997
- on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door
05000293/LER-1997-014, :on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period)1997-09-24024 September 1997
- on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period)
05000293/LER-1997-012, :on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated1997-08-29029 August 1997
- on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated
05000293/LER-1997-003, :on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested1997-07-18018 July 1997
- on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested
05000293/LER-1997-010, :on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door1997-05-20020 May 1997
- on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door
05000293/LER-1997-005, :on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error1997-05-15015 May 1997
- on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error
05000293/LER-1997-007, :on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers1997-05-0101 May 1997
- on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers
05000293/LER-1997-008, :on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel1997-04-24024 April 1997
- on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel
05000293/LER-1997-006, :on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified1997-04-22022 April 1997
- on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified
05000293/LER-1997-004, :on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately1997-04-0707 April 1997
- on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately
05000293/LER-1997-002, :on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete1997-03-10010 March 1997
- on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete
05000293/LER-1997-001, :on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised1997-02-14014 February 1997
- on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised
ML20138Q5491997-02-0707 February 1997 LER 97-S02-00:on 970110,security Svcs Supervisor Received Improperly Mailed Safeguards Info.Caused by Personnel Error. Security Force Put on Heightened Awareness & Protected Area Patrol Frequency Increased 1999-09-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000293/LER-1999-010-02, :on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With1999-10-18018 October 1999
- on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With
05000293/LER-1999-009-02, :on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With1999-10-13013 October 1999
- on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With
ML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20216G5991999-09-24024 September 1999 Corrected Safety Evaluation Supporting Amend 182 to License DPR-35,consisting of Corrected Page 1 ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps 05000293/LER-1999-008-02, :on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With1999-09-0707 September 1999
- on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With
ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With 05000293/LER-1999-007-02, :on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With1999-08-13013 August 1999
- on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With
05000293/LER-1999-006-02, :on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With1999-08-0404 August 1999
- on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With
ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209G3851999-07-15015 July 1999 Safety Evaluation Supporting Amend 182 to License DPR-35 05000293/LER-1999-005, :on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With1999-07-0808 July 1999
- on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With
ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) 05000293/LER-1999-004, :on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With1999-06-28028 June 1999
- on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With
ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 05000293/LER-1999-003, :on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With1999-06-15015 June 1999
- on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With
ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant 05000293/LER-1999-002, :on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With1999-06-0303 June 1999
- on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With
ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant 05000293/LER-1999-001, :on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With1999-05-0606 May 1999
- on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With
ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With 05000293/LER-1998-029, :on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With1999-02-0101 February 1999
- on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With
05000293/LER-1998-028, :on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With1999-01-28028 January 1999
- on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With
ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With 05000293/LER-1998-026, :on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with1998-12-23023 December 1998
- on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with
05000293/LER-1998-007, :on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With1998-12-22022 December 1998
- on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With
ML20198H5671998-12-21021 December 1998 Safety Evaluation Supporting Amend 180 to License DPR-35 05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation1998-12-18018 December 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation
05000293/LER-1998-025, :on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With1998-12-18018 December 1998
- on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With
05000293/LER-1997-017, :on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With1998-12-18018 December 1998
- on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With
05000293/LER-1998-018, :on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With1998-12-18018 December 1998
- on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With
ML20198A2391998-12-11011 December 1998 Safety Evaluation Supporting Amend 179 to License DPR-35 ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With 05000293/LER-1998-024, :on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans1998-11-13013 November 1998
- on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans
ML20195B9161998-11-10010 November 1998 Safety Evaluation Supporting Amend 178 to License DPR-35 05000293/LER-1998-023, :on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With1998-11-0404 November 1998
- on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With
ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With 1999-09-08
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On January 6,1988 at 1450 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.51725e-4 months <br />, automatic actuations of portions of the Primary Containment Isolation Control System (PCIS) and Reactor Building Isolation Control System (RBIS) occurred.
The actuations resulted in the following automatic responses.
The Train "B" Primary Containment System (PCS) Group 2 isolation valves received an isolation signal.
The outboard (Train "B") ventilation system dampers of the Secondary Containment System (SCS) closed.
The "B" Train of the SCS/ Standby Gas Treatment System (SGTS) started.
Following immediate investigation the SGTS was secured, the ventilation dampers were opened, and the isolation reset on January 7, 1988 at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />.
The cause for the actuations was the failure of the coil in a logic relay that is part of the outboard PCIS/RBIS logic circuitry. The relay coil was replaced.
Based on analysis, additional relays (or relay coils) have been selected for replacement prior to startup.
The actuations occurred during an extended outage while in the cold shutdown condition with negligible core decay heat and with the mode switch in the SHUTDOWN position. No control rods were in the withdrawn position at the time of the actuations. The actuations posed no threat to the public health and safety.
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EVENT DESCRIPTION
On January 6, 1988 at 1450 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.51725e-4 months <br />, automatic actuations of portions of the Primary Containment Isolation Control System (PCIS) and Reactor Building Isolation Control System (RBIS) occurred.
The actuations resulted in the following automatic responses.
The Train "B" Primary Containment System (PCS) Group 2 isolation valves received an isolation signal.
The outboard (Train "B") ventilation system dampers of the Secondary Containment System (SCS) closed.
The "B" train of the SCS/ Standby Gas Treatment System (SGTS) started.
Failure and Halfunction Report 88-6 was written to document the actuations, Notification was made to the NRC Operations Center on January 6, 1988 at 1712 hours0.0198 days <br />0.476 hours <br />0.00283 weeks <br />6.51416e-4 months <br />. Following immediate investigation, the SGTS was secured and the ventilation dampers were reopened, and the isolation reset on January 7, 1988 at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />. A priority Maintenance Request (MR 88-9) was also issued to investigate.
The actuations occurred during an extended outage while in the cold shutdown condition with negligible core decay heat and with the mode selector switch in the SHUTDOHN position. The reactor vessel head was installed and no control rods were in the withdrawn position at the time of the actuations.
CAUSI The cause for the actuations was the failure of the coil in logic relay 16A-K57.
The failure of the coil resulted in excessive current and caused the 120VAC circuit's fuse (16A-F22) to blow thereby de-energizing the circuit.
The probable cause for this and other failed (burned) coils in CR120A relays has been attributed to the end of useful life; reference Memorandum TCH87-464, "CR120A Relay Evaluation". The failure mode appears to be mechanical stressing of the coil terminal connection resulting in physical separation, overheating and burning of the connection internal to the coil encapsulation.
1 Relay 16A-K57 is located in logic Panel C-942.
The relay (type CR120A) is manufactured by General Electric.
Inboard and outboard logic relays (of the PCIS and RBIS) are located in PCIS/RBIS logic panels C-941 and C-942, respectively.
The CR120A logic relays located in these panels are mounted in a closely packed array and are continuously energized.
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CORRECTIVE ACTION
A new coil was installed in relay 16A-K57 via MR 88-9 (MSC 88-9-1).
Post work testing was performed using procedure number 8.H.2-1.5.2, "Hain Steam Line Isolation Valve Logic-Test B-Outboard".
A discrepancy unrelated to the cause for the actuations was identified at Step 31 of the procedure.
The step is performed to verify that the "Outboard Main Steam Isolation Valve Logic Test" light is 0FF; the light was ON.
Investigation revealed that contacts M1 and Tl of relay 16A-K16X were not separated as expected for this part of the test.
Examination of the relay revealed that the pivot points of the contacts (M1 and il) were bound.
The binding appeared to be caused by a misalignment of the plastic parts that house the relay reeds.
Relay 16A-K16X is an Agastat Model GPIC 750 relay. A review of database (SEEK) records and interviews with Instrumentation and Control Supervisors revealed no known previous failures for this type of relay at Pilgrim Station.
Relay 16A-K16X was replaced via MSC 88-9-2.
F.ollowing the replacement, post work testing was completed satisfactorily.
Previous failures of CR120A relays led to the evaluation documented in Memorandum TCH 87-464.
The evaluation resulted in the issuance of an Engineering Service Request (ESR 87-643).
The E$R requested Nuclear Engineering Department evaluation for reporting CR120A relay failures pursuant to 10CFR Part 21. The evaluation performed concluded that reporting (10CFR Part 21) was not applicable because the relays were installed in accordance with the technical requirements included in the procurement design documents and because the relays operated properly for approximately 10 years prior to the first failure.
The ESR also requested implementation of recommendations (TCH 87-464) to improve the reliability of CR120A relays.
The technical evaluation documented in TCH 87-464 reviewed CR120A relays installed at Pilgrim Station. The review included the specific application of each individual relay, the overall operating history of these relays as compared to industry information and a failure effects analysis of the safety related relays.
Based on this technical evaluation, specific relays (or relay coils) have been selected for replacement prior to startup.
The recommendations regarding the remaining items are being evaluated for incorpcration into the long term maintenance program.
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..e Pilgrim Nuclear Power Station 0l0 0l4 oF o l4 0lOl1 0 1510lol012 19l 3 818 f tKT is snog apese a seuru was eseessw bec ppe assa s>lih SAFETY CONSE0'JENCES Based on the redundancy of systems and procedures available, the actuations posed no threat to the health and safety of the public. Control Room operator corrective actions for response to alarms or malfunctions are addressed in written procedures that include the following: ARP-C7L, "Alarm Response Procedure"; and 2.4.147, "Reset of Secondary Containment Isolation on Panel C7".
This event was determined to be reportable pursuant to 10CFR50.73(a)(2)(iv) because (false) PCIS/RBIS signals actuated accident mitigating systems (SCS,5GTS and PCS).
SIMILARITY OF PREVIOUS EVENTS A review of Pilgrim Station Licensee Event Reports (LER's) written since January 1984 was conducted.
The review focused on LCR's submitted pursuant to 10CFR50.73 (a)(2)(iv) that were caused by a failed coil in CR120A relay.
The review revealed a previous failure reported in LER 50-293/87-018-00.
The failure of the coil in relay 16A-K55 resulted in the automatic closure of the outboard PCS/ Group 6 (Reactor Water Cleanup System) isolation valves.
ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for the actuations are as follows:
CO@0NENTS CODES Coil CL 04 Relay, tripping (16A-K57)
SYSTEMS Containment Isolation Control System (PCIS/RBIS)
JH Engineered Safety Features Actuation System (PCIS/RBIS) JE Primary Containment System (PCS)
JH Reactor Building (SCS)
NG Standby Gas Treatment System (SGTS)
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10CFR50.73 Pilgrim Nuclear Ptmer Station Rocky HalRoad Plymouth, Massachusetts o236o February 5, 1988 -
Ralph G. Sini 8ECo Ltr. #88-19 Serwor Vice President - Nuclear U.S. Nuclear Regulatory Commission Attn: Document Control Desk Hashington, D.C. 20555 Docket No. 50-293 License No. DPR-35
Dear Sir:
The attached Licensee Event Report (LER) 88-001-00 "Automatic Actuations of Portions of Primary containment, Secondary Containment and Standby Gas Treatment Systems" is submitted in accordance with 10CFR Part 50.73.
Please do not hesitate to contact me if you have any questions.regarding this subject.
A.G.(Bird DHE/b1
Enclosure:
LER 88-001-00 cc: Mr. Hilliam Russell Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Rd.
King of Prussia, PA 19406 Sr. Resident Inspector - Pilgrim Station Standard BECo LER Distribution
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05000293/LER-1988-001, :on 880106,automatic Isolations of Portions of Primary Containment & Reactor Bldg Isolation Control Sys Occurred.Caused by Failure in Logic Relay 16A-K57.Coil in Relay Replaced & Other Relay Coils Analyzed |
- on 880106,automatic Isolations of Portions of Primary Containment & Reactor Bldg Isolation Control Sys Occurred.Caused by Failure in Logic Relay 16A-K57.Coil in Relay Replaced & Other Relay Coils Analyzed
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-002, :on 880117,full Scram Trip Signal Followed by Incomplete Automatic Actuations Occurred.Caused by Inadequate Procedure & High Resistance of Contacts in Logic Relay.Procedure Revised & Logic Relay Replaced |
- on 880117,full Scram Trip Signal Followed by Incomplete Automatic Actuations Occurred.Caused by Inadequate Procedure & High Resistance of Contacts in Logic Relay.Procedure Revised & Logic Relay Replaced
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-003, :on 880130,setpoints of Degraded Grid Voltage Relays Identified as Too Low.Caused by Incorrect Assumption Made in Model Used for Voltage Analysis Originally Performed in 1976.Addl Analysis & Review Being Performed |
- on 880130,setpoints of Degraded Grid Voltage Relays Identified as Too Low.Caused by Incorrect Assumption Made in Model Used for Voltage Analysis Originally Performed in 1976.Addl Analysis & Review Being Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-1988-004, :on 880202,unplanned Automatic Actuations of Portions of Primary Containment & Reactor Bldg Isolation Control Sys Occurred.Caused by Inadequate Instructions. Sys Restored to Svc.Instructions Revised |
- on 880202,unplanned Automatic Actuations of Portions of Primary Containment & Reactor Bldg Isolation Control Sys Occurred.Caused by Inadequate Instructions. Sys Restored to Svc.Instructions Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-005, :on 880202,automatic Actuation of Portions of Primary Containment & Reactor Bldg Isolation Control Sys (Pcis/Rbis) Occurred.Caused by Pcis/Rbis Logic Relay Coil Failure.Logic Relay Coil Replaced |
- on 880202,automatic Actuation of Portions of Primary Containment & Reactor Bldg Isolation Control Sys (Pcis/Rbis) Occurred.Caused by Pcis/Rbis Logic Relay Coil Failure.Logic Relay Coil Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-006, :on 880203,ATWS Div 2 Trip Signal & Subsequent Scram Signal Generated.Cause of ATWS Trip Signal Not Yet Identified But Being Investigated.Stop Work Order Issued, Halting Further Implementation of Mods |
- on 880203,ATWS Div 2 Trip Signal & Subsequent Scram Signal Generated.Cause of ATWS Trip Signal Not Yet Identified But Being Investigated.Stop Work Order Issued, Halting Further Implementation of Mods
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-007, :on 880223,unexpected Automatic Actuation of Primary Containment Isolation Control Sys & Reactor Bldg Isolation Control Sys Occurred.Caused by Removal of Fuse from Power Supply of Circuit.Fuse Replaced |
- on 880223,unexpected Automatic Actuation of Primary Containment Isolation Control Sys & Reactor Bldg Isolation Control Sys Occurred.Caused by Removal of Fuse from Power Supply of Circuit.Fuse Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-008, :on 880226,automatic Closing of Primary Containment Sys Group 6 Isolation Valve Occurred.Caused by Momentary Flow Fluctuation in RWCU Sys.Util Evaluating Components Installed in Flow Sensing Lines |
- on 880226,automatic Closing of Primary Containment Sys Group 6 Isolation Valve Occurred.Caused by Momentary Flow Fluctuation in RWCU Sys.Util Evaluating Components Installed in Flow Sensing Lines
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-009, :on 880304,documentation for Completion of Surveillance Procedure 8.9.13 Not Located for Diesel Generator B.Cause Undetermined.Operating Supervisor Required to Log Initiation & Completion of Tests |
- on 880304,documentation for Completion of Surveillance Procedure 8.9.13 Not Located for Diesel Generator B.Cause Undetermined.Operating Supervisor Required to Log Initiation & Completion of Tests
| 10 CFR 50.73(a)(2)(1) | 05000293/LER-1988-010, :on 880311,automatic Actuation of Portion of Primary Containment Isolation Control Sys Occurred.Caused by Blown Fuse in Inboard Containment Logic Circuitry During Removal of Temp Switch.Fuse Replaced |
- on 880311,automatic Actuation of Portion of Primary Containment Isolation Control Sys Occurred.Caused by Blown Fuse in Inboard Containment Logic Circuitry During Removal of Temp Switch.Fuse Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-011, :on 880331,reactor Bldg Isolation Control Sys Inadvertently Actuated,Resulting in Automatic Closing of Secondary Containment Sys Ventilation Dampers.Caused by Personnel Error.Procedure Improvement Started |
- on 880331,reactor Bldg Isolation Control Sys Inadvertently Actuated,Resulting in Automatic Closing of Secondary Containment Sys Ventilation Dampers.Caused by Personnel Error.Procedure Improvement Started
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-012, :on 880425,automatic Start of Loop a Reactor Bldg Closed Cooling Water Sys Pump a Occurred.Caused by Accelerated Wear Induced Failure of Coupling in Pump B. Failed Coupling Replaced & Addl Measures Taken |
- on 880425,automatic Start of Loop a Reactor Bldg Closed Cooling Water Sys Pump a Occurred.Caused by Accelerated Wear Induced Failure of Coupling in Pump B. Failed Coupling Replaced & Addl Measures Taken
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-013, :on 880425,inadvertent Manual Start of Emergency Diesel Generator (EDG) B Occurred.Caused by Personnel Error.Improvements to Local Control Panel to EDG Identified & Tracked |
- on 880425,inadvertent Manual Start of Emergency Diesel Generator (EDG) B Occurred.Caused by Personnel Error.Improvements to Local Control Panel to EDG Identified & Tracked
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-014, :on 880426,automatic Closing of Outboard Primary Containment Sys Group 6 Isolation Valves Occurred. Caused by Failure of Coil of Outboard Primary Containment Isolation Control Sys.Coil & Fuse Replaced |
- on 880426,automatic Closing of Outboard Primary Containment Sys Group 6 Isolation Valves Occurred. Caused by Failure of Coil of Outboard Primary Containment Isolation Control Sys.Coil & Fuse Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-015, :on 880504,inadvertent Actuation of Portions of Primary Containment Isolation Control Sys & Reactor Bldg Isolation Control Sys Occurred.Caused by Technician Removing Wrong Fuse from Logic Panel.Fuse Reinstalled |
- on 880504,inadvertent Actuation of Portions of Primary Containment Isolation Control Sys & Reactor Bldg Isolation Control Sys Occurred.Caused by Technician Removing Wrong Fuse from Logic Panel.Fuse Reinstalled
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-016, :on 880517,unexpected Actuation of Inboard Portion of Reactor Bldg Isolation Control Sys Occurred, Resulting in Closure of Train a Isolation Dampers.Caused by Personnel Error.Work Process Revised |
- on 880517,unexpected Actuation of Inboard Portion of Reactor Bldg Isolation Control Sys Occurred, Resulting in Closure of Train a Isolation Dampers.Caused by Personnel Error.Work Process Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-017, :on 880608,crack Discovered in Yoke Portion of RHR Sys Loop B Valve.Cause Being Investigated by multi- Disciplinary Team.Valve Yoke Removed & Metallurgical Exam Performed |
- on 880608,crack Discovered in Yoke Portion of RHR Sys Loop B Valve.Cause Being Investigated by multi- Disciplinary Team.Valve Yoke Removed & Metallurgical Exam Performed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000293/LER-1988-018, :on 880705,full Scram Signal Occurred.Caused by Procedure Weakness & Previous Administrative Controls That Were Not Entirely Adequate for Previous Changes Made to Procedure.Procedure Revised |
- on 880705,full Scram Signal Occurred.Caused by Procedure Weakness & Previous Administrative Controls That Were Not Entirely Adequate for Previous Changes Made to Procedure.Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000293/LER-1988-020, :on 880711,automatic Start of Emergency Diesel Generator B Occurred When Emergency 4,160 Volt Ac Bus A-6 Intentionally Deenergized for Mod Work.Caused by Personnel Error.Emergency Switch Position Added to Sheet |
- on 880711,automatic Start of Emergency Diesel Generator B Occurred When Emergency 4,160 Volt Ac Bus A-6 Intentionally Deenergized for Mod Work.Caused by Personnel Error.Emergency Switch Position Added to Sheet
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-021, :on 880719,discovered Problem Involving Solenoid Valves Installed in safety-related Applications. Caused by Incorrect Assumption.Mod Prepared to Replace Four Valves & Form Specifying Design Data Revised |
- on 880719,discovered Problem Involving Solenoid Valves Installed in safety-related Applications. Caused by Incorrect Assumption.Mod Prepared to Replace Four Valves & Form Specifying Design Data Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) | 05000293/LER-1988-022, :on 881010,full Scram Signal Occurred.Caused by Cognitive Util Operator Error.Operator Reclosed Breaker & Energized Reactor Protection Sys Channel a Logic Circuitry |
- on 881010,full Scram Signal Occurred.Caused by Cognitive Util Operator Error.Operator Reclosed Breaker & Energized Reactor Protection Sys Channel a Logic Circuitry
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-023, :on 881012,automatic Actuation of Secondary Containment & Standby Gas Treatment Sys Occurred.Caused by Util Licensed Operator Error.Shift Licensed Operators Being Retrained Re Reactor Protection Sys |
- on 881012,automatic Actuation of Secondary Containment & Standby Gas Treatment Sys Occurred.Caused by Util Licensed Operator Error.Shift Licensed Operators Being Retrained Re Reactor Protection Sys
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000293/LER-1988-024, :on 871006,safety-related 4160 Vac Load Ctr Breaker 152-508 Tripped Causing Loss of Power to 480 Vac Emergency Bus B-1.Cause Undeterminded.Equipment Returned to Svc |
- on 871006,safety-related 4160 Vac Load Ctr Breaker 152-508 Tripped Causing Loss of Power to 480 Vac Emergency Bus B-1.Cause Undeterminded.Equipment Returned to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1988-024-01, :on 881017,Group 1 Isolation Signal Due to High Water Level in Reactor Vessel Occurred.Caused by Disassociation of Pin from Feedback Cam Linkage of Valve Positioner for Valve.Linkage Secured |
- on 881017,Group 1 Isolation Signal Due to High Water Level in Reactor Vessel Occurred.Caused by Disassociation of Pin from Feedback Cam Linkage of Valve Positioner for Valve.Linkage Secured
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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