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U.S. NUCLEA2 REGULATORY -
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APPsIOVE3 OMS No. 3190-T104
- 'REs; st3ms LICENSEE EVENT REPORT (LER)
PACILITV esaasE (1)
OOCKET NUAsBER (3)
PAGE W Pilgrim Nuclear Power Station - Unit No. 1 o is I o t o I o 1219 I 3 1 loFl 012 TITLE E4 Standby Liquid Control System Inoperable
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NAME TELEPHONE NUMSER
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Paul J. Hamilton - Senior Plant Engineer 6:1 7 74,6 i 7,90,0 i
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I On 1/1/85, a reactor shutdown was completed due to an inoperable Standby Liquid Control System (SLCS).
Cause of the inoperable system was debris in the SLCS storage tank and test tank. Corrective action was to clean and/or flush the SLCS components and systems.
In addition, the cover for the test tank was reinstalled with locking mechanisms and the cover for the main tank bolted in place.
This event did not impact the health and safety of the public.
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Amovso ove No. 2 so_oio4 exeiRes. enims FAC8LITV NAME li)
DOCKET NUMSER (21 LER NUMSER IS)
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.m a nco m ew nn On 1/1/85, during post-refuel startup testing, the Standby Liquid Control System (SLCS) was declared inoperable. The reactor, which was at approximately 22% power, was brought to the cold shutdown condition in accordance with the requirements of Technical Specificatien (T.S.) Section 3.4.0.
The problem was discovered when the "A" SLCS relief valve lifted low (approximately 600 psi vs. a 1425 psi setpoint) during normal surveillance testing of the SLCS. The redundant "B" SLCS was then tested and, although the "B" train met T.S. flow requirements, it was declared inoperable when debris was observed to be floating in both the main and test SLCS tanks.
Corrective action was to drain, clean, and inspect both tanks. The "A" relief valve which had lifted low during the surveillance was bench tested several times and lifted at the required setpoint.
Cause of "A" relief valve lifting low is unknown.
The "B" relief valve which had lifted within specification but lower than its setpoint was found with pieces of rubber glove between the blowdown adjusting orifice and plunger. The pieces of glove were removed and the valve reassembled. Various check valves were inspected for blockage and none was found.
In addition to these visual inspections of some components' internals, the SLCS was air-blown and/or flushed in sub-sections in order to verify that the debris had been cleared from the process system. The SLCS surveillance was successfully completed on 1/5/85.
An investigation was initiated to determine why the debris, which included rubber gloves and masking tape, was in the tanks.
T' investigation found that both the test tank cover and the main tark manwt were open at certain times during the recently completed recirculation pipe replacement and refuel outage.
It is postulated that some time during the outage, the debris either fell or was thrown into the tanks.
Long-term corrective action was to reinstall the test tank cover with locking mechanisms and bolt the manway cover to the top of the main tank.
This event did not impact the health and safety of the public. A search of records indicates that this was an isolated event.
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EOSTON EOisON COMPANY 800 SOYLETON STREET BDaTON. MAmeAcHUSETTa 02199 WILLIAM D. HARRINGTON
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January 3Q 1985 BECo Ltr. #85- 021 Document Control Desk U.S. Nuclear Regulatory Commission-Washington, D.C. 20555 Docket Number 50-293 License DPR-35
Dear Sir:
The attached Licensee Event Report 85-001-00, " Standby Liquid Control System Inoperable," is hereby submitted in accordance with the requirements of 10CFR50.73.
If there are any questions on this subject, please do not hesitate to contact me.
Respectfully submitted, W. D. riarrington PH: caw Enclosure: LER 85-001-00 cc: Dr. Thomas-E. Murley Regional Administrator, Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406 Standard BECo LER Distribution f
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| 05000293/LER-1985-001, :on 850101,reactor Shut Down Due to Inoperable Standby Liquid Control Sys (Slcs).Caused by Debris in SLCS Storage Tank & Test Tank.Slcs Components & Sys Cleaned.W/ |
- on 850101,reactor Shut Down Due to Inoperable Standby Liquid Control Sys (Slcs).Caused by Debris in SLCS Storage Tank & Test Tank.Slcs Components & Sys Cleaned.W/
| | | 05000293/LER-1985-002, :on 850128,Tech Spec Implementing Procedures for Surveillance Tests Inadequate.Caused by Mgt Deficiency. Procedures Revised to Include Provisions for Functional Testing of Valve Closure Alarms |
- on 850128,Tech Spec Implementing Procedures for Surveillance Tests Inadequate.Caused by Mgt Deficiency. Procedures Revised to Include Provisions for Functional Testing of Valve Closure Alarms
| | | 05000293/LER-1985-003, :on 850210,reactor Shut Down.Caused by Oil Leak in Recirculation Pump Which Resulted in Bearing Damage.Oil Leak Repaired & Damaged Components Replaced |
- on 850210,reactor Shut Down.Caused by Oil Leak in Recirculation Pump Which Resulted in Bearing Damage.Oil Leak Repaired & Damaged Components Replaced
| | | 05000293/LER-1985-004, :on 850215,reactor Shut Down Due to Small Leak in Socket Weld.Spool Piece & Weld Replaced |
- on 850215,reactor Shut Down Due to Small Leak in Socket Weld.Spool Piece & Weld Replaced
| | | 05000293/LER-1985-005, :on 850221,rod Block Monitor Functional & Calibr Surveillance Tests Identified as Having Exceeded Required Test Interval.Caused by Personnel Error.Tests Performed & Personnel Counseled |
- on 850221,rod Block Monitor Functional & Calibr Surveillance Tests Identified as Having Exceeded Required Test Interval.Caused by Personnel Error.Tests Performed & Personnel Counseled
| | | 05000293/LER-1985-006, :on 850315,reactor Scram from 100% Power Occurred.Caused by False High Reactor Pressure Signal When Valve Momentarily Stuck,Then Released.Valve & Manifold Replaced |
- on 850315,reactor Scram from 100% Power Occurred.Caused by False High Reactor Pressure Signal When Valve Momentarily Stuck,Then Released.Valve & Manifold Replaced
| | | 05000293/LER-1985-007, :on 850316,two in-series Secondary Containment Isolation Dampers Found Inoperable.Caused by Broken Damper Control Drive Gears.Broken Gears Replaced & Insp Frequency Increased |
- on 850316,two in-series Secondary Containment Isolation Dampers Found Inoperable.Caused by Broken Damper Control Drive Gears.Broken Gears Replaced & Insp Frequency Increased
| | | 05000293/LER-1985-008, :on 850331,while Performing Routine HPCI Operability Flow Test,Hpci Turbine Tripped on Overspeed. Caused by Faulty Connector in Turbine Control Sys.Connector & Rupture Disc Replaced |
- on 850331,while Performing Routine HPCI Operability Flow Test,Hpci Turbine Tripped on Overspeed. Caused by Faulty Connector in Turbine Control Sys.Connector & Rupture Disc Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000293/LER-1985-009, :on 850404,reactor Scrammed from 85% Power as Result of Turbine Trip on High Vibration Signal.Caused by Inadequate Lubrication of Turbine Vibration Detector.Lube Oil Orifice Cleaned & Detector Replaced |
- on 850404,reactor Scrammed from 85% Power as Result of Turbine Trip on High Vibration Signal.Caused by Inadequate Lubrication of Turbine Vibration Detector.Lube Oil Orifice Cleaned & Detector Replaced
| | | 05000293/LER-1985-010, :on 850412,two in-series Secondary Containment Isolation Dampers Would Not Fully Close.Caused by Slippage in Drive Gears & Cracking Due to Aging & Fatigue.Gears Replaced |
- on 850412,two in-series Secondary Containment Isolation Dampers Would Not Fully Close.Caused by Slippage in Drive Gears & Cracking Due to Aging & Fatigue.Gears Replaced
| | | 05000293/LER-1985-011, :on 850424,two Absolute Pressure Transmitters Discovered Installed Instead of Required Gauge Pressure Transmitters.Caused by Engineering Oversight.Transmitters Recalibr Per Temporary Mod-85-27 |
- on 850424,two Absolute Pressure Transmitters Discovered Installed Instead of Required Gauge Pressure Transmitters.Caused by Engineering Oversight.Transmitters Recalibr Per Temporary Mod-85-27
| | | 05000293/LER-1985-013, :on 850529,HPCI Sys Isolated During Steady Operation Due to False Steam Line High Flow Signal from Differential Pressure Indicating Switch.Caused by Setpoint Shift.Internal Switch Components Replaced |
- on 850529,HPCI Sys Isolated During Steady Operation Due to False Steam Line High Flow Signal from Differential Pressure Indicating Switch.Caused by Setpoint Shift.Internal Switch Components Replaced
| | | 05000293/LER-1985-014, :on 850615,unplanned Reactor Scram Occurred Due to MSIV Isolation of High Water Level.Caused by Personnel Error.Personnel Counseled |
- on 850615,unplanned Reactor Scram Occurred Due to MSIV Isolation of High Water Level.Caused by Personnel Error.Personnel Counseled
| | | 05000293/LER-1985-015, :on 850624,both Trains of Standby Gas Treatment Sys Started After Secondary Containment Isolation Received. Caused by Operator Error.Operations Personnel Instructed in Handling of Radiation Monitors |
- on 850624,both Trains of Standby Gas Treatment Sys Started After Secondary Containment Isolation Received. Caused by Operator Error.Operations Personnel Instructed in Handling of Radiation Monitors
| | | 05000293/LER-1985-016, :on 850704,weekly Analysis for Gross Radioactivity of Reactor Bldg Vent Particulate Filter Not Performed Per Tech Specs.Caused by Nonlicensed Util Personnel Error.Personnel Counseled |
- on 850704,weekly Analysis for Gross Radioactivity of Reactor Bldg Vent Particulate Filter Not Performed Per Tech Specs.Caused by Nonlicensed Util Personnel Error.Personnel Counseled
| | | 05000293/LER-1985-017, On 850712,secondary Containment Isolation Received During Routine High Drywell Pressure,Low Water Level & High Radiation Sys Functional Test.Caused by Personnel Error.Personnel Counseled | On 850712,secondary Containment Isolation Received During Routine High Drywell Pressure,Low Water Level & High Radiation Sys Functional Test.Caused by Personnel Error.Personnel Counseled | | | 05000293/LER-1985-018, :on 850715,secondary Containment Damper Would Not Fully Close.Tech Spec Compensatory Action Not Taken for 19 H.Caused by Maint Personnel Error.Drive Gears on Damper Aligned & Personnel Counseled |
- on 850715,secondary Containment Damper Would Not Fully Close.Tech Spec Compensatory Action Not Taken for 19 H.Caused by Maint Personnel Error.Drive Gears on Damper Aligned & Personnel Counseled
| | | 05000293/LER-1985-019, :on 850716,two in-series Secondary Containment Dampers Would Not Fully Close During post-secondary Containment Isolation Insp.Caused by Slippage in Drive Gears.Dampers Will Be Replaced |
- on 850716,two in-series Secondary Containment Dampers Would Not Fully Close During post-secondary Containment Isolation Insp.Caused by Slippage in Drive Gears.Dampers Will Be Replaced
| | | 05000293/LER-1985-020, :on 850726,operations Personnel Notified by Chemistry Group That Emergency Diesel Fuel Oil Storage Tank a Test Results Did Not Meet Tech Spec Criteria.Caused by Personnel Error & Procedural Inadequacy |
- on 850726,operations Personnel Notified by Chemistry Group That Emergency Diesel Fuel Oil Storage Tank a Test Results Did Not Meet Tech Spec Criteria.Caused by Personnel Error & Procedural Inadequacy
| | | 05000293/LER-1985-021, :on 850814,two Main Steam Line Radiation Monitors Had Trip Setpoints Greater than Tech Spec Requirements.Caused by Nonlicensed Util Personnel Error. Setpoints Adjusted within Tech Spec Limits |
- on 850814,two Main Steam Line Radiation Monitors Had Trip Setpoints Greater than Tech Spec Requirements.Caused by Nonlicensed Util Personnel Error. Setpoints Adjusted within Tech Spec Limits
| | | 05000293/LER-1985-022, :on 850812,part of Maint Hot Shop Ventilation Contaminated & Provided Unmonitored Release Path to Environ. Caused by Design Inadequacy.Associated Fan & Breaker Tagged & Ductwork Inlet Sealed |
- on 850812,part of Maint Hot Shop Ventilation Contaminated & Provided Unmonitored Release Path to Environ. Caused by Design Inadequacy.Associated Fan & Breaker Tagged & Ductwork Inlet Sealed
| | | 05000293/LER-1985-023, :on 850827,HPCI Turbine Control Valve Failed to Operate Properly.Caused by Leaking Nipple Due to Personnel Inadvertently Stepping on Oil Supply Line to HPCI Hydraulic Control Valve.Nipple Repaired |
- on 850827,HPCI Turbine Control Valve Failed to Operate Properly.Caused by Leaking Nipple Due to Personnel Inadvertently Stepping on Oil Supply Line to HPCI Hydraulic Control Valve.Nipple Repaired
| | | 05000293/LER-1985-024, :on 850602,surveillance Test of Station 250-volt Batteries Missed.Caused by Procedural Deficiency. Procedure Revised & Batteries Retested |
- on 850602,surveillance Test of Station 250-volt Batteries Missed.Caused by Procedural Deficiency. Procedure Revised & Batteries Retested
| | | 05000293/LER-1985-025, :on 850901,reactor Scram Occurred When Insulator in Switchyard Arced to Ground & Disintegrated. Caused by Salt Buildup Resulting from Storm.Insulator Replaced & Washdown Procedures Reviewed |
- on 850901,reactor Scram Occurred When Insulator in Switchyard Arced to Ground & Disintegrated. Caused by Salt Buildup Resulting from Storm.Insulator Replaced & Washdown Procedures Reviewed
| | | 05000293/LER-1985-026, :on 850830,during QA Audit of Operations, Failure to Perform Instrument Check of 28-volt Control Rod Position Indicating Lights Indicated.Caused by Inadequate Surveillance Procedure.Procedure Modified |
- on 850830,during QA Audit of Operations, Failure to Perform Instrument Check of 28-volt Control Rod Position Indicating Lights Indicated.Caused by Inadequate Surveillance Procedure.Procedure Modified
| | | 05000293/LER-1985-027, :on 850919,LPCI Injection Valve Would Not Open During Testing.Caused by Failed Motor in Valve Motor Operator.Motor Replaced |
- on 850919,LPCI Injection Valve Would Not Open During Testing.Caused by Failed Motor in Valve Motor Operator.Motor Replaced
| | | 05000293/LER-1985-028, :on 851010,discovered All Active Components of Standby Gas Treatment Sys Not Documented as Tested.Caused by Previous Mgt Deficiency.Tech Spec Implementing Procedure Revised |
- on 851010,discovered All Active Components of Standby Gas Treatment Sys Not Documented as Tested.Caused by Previous Mgt Deficiency.Tech Spec Implementing Procedure Revised
| | | 05000293/LER-1985-029, :on 851018,HPCI Inverter Circuit Failure Alarm & ATWS Trouble Alarm Received in Control Room Due to Breaker Trip.Caused by Fluctuation of Input Voltage.Hpci Inverter Previously Modified |
- on 851018,HPCI Inverter Circuit Failure Alarm & ATWS Trouble Alarm Received in Control Room Due to Breaker Trip.Caused by Fluctuation of Input Voltage.Hpci Inverter Previously Modified
| | | 05000293/LER-1985-030, :on 851030,during Review of NRC Insp 85-26, Discovered That,Control to Tech Spec 4.6.A.5,Procedure 2.1.9.A Did Not Require Logging of Dome & Bottom Head Drain Temps When Starting Recirculation Pump |
- on 851030,during Review of NRC Insp 85-26, Discovered That,Control to Tech Spec 4.6.A.5,Procedure 2.1.9.A Did Not Require Logging of Dome & Bottom Head Drain Temps When Starting Recirculation Pump
| | | 05000293/LER-1985-031, :on 851029,min Shift Crew Composition Not Met. Caused by Misinterpretation of Note B in Tech Spec Table 6.2-1 & Procedure 1.3.34.Shift Crew Composition Changed & Personnel Counseled on Tech Spec Requirements |
- on 851029,min Shift Crew Composition Not Met. Caused by Misinterpretation of Note B in Tech Spec Table 6.2-1 & Procedure 1.3.34.Shift Crew Composition Changed & Personnel Counseled on Tech Spec Requirements
| | | 05000293/LER-1985-032, :on 851125,5 of 16 Main Steam Line High Flow Switches Found Outside of Required Setpoint During Routine Primary Containment Isolation Sys Surveillance.Caused by Improper Alignment of Switch Linkage |
- on 851125,5 of 16 Main Steam Line High Flow Switches Found Outside of Required Setpoint During Routine Primary Containment Isolation Sys Surveillance.Caused by Improper Alignment of Switch Linkage
| | | 05000293/LER-1985-033, :on 851127,during Insp 85-32 Identified That Monthly Instrument Channel Checks of Main Stack & Reactor Bldg Vent Waste Gas Monitors Not Performed,Per Tech Spec Section 4.8.B.10.New Procedure Developed |
- on 851127,during Insp 85-32 Identified That Monthly Instrument Channel Checks of Main Stack & Reactor Bldg Vent Waste Gas Monitors Not Performed,Per Tech Spec Section 4.8.B.10.New Procedure Developed
| | | 05000293/LER-1985-034, :on 851231,discovered That 21 Fire Dampers Required by Tech Specs Found Degraded.Caused by Insufficient Installation Instructions & Improper Rev to Design Change During Mod Work in 1980-1984 |
- on 851231,discovered That 21 Fire Dampers Required by Tech Specs Found Degraded.Caused by Insufficient Installation Instructions & Improper Rev to Design Change During Mod Work in 1980-1984
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