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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000293/LER-1999-010-02, :on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With1999-10-18018 October 1999
- on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With
05000293/LER-1999-009-02, :on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With1999-10-13013 October 1999
- on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With
05000293/LER-1999-008-02, :on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With1999-09-0707 September 1999
- on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With
05000293/LER-1999-007-02, :on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With1999-08-13013 August 1999
- on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With
05000293/LER-1999-006-02, :on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With1999-08-0404 August 1999
- on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With
05000293/LER-1999-005, :on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With1999-07-0808 July 1999
- on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With
05000293/LER-1999-004, :on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With1999-06-28028 June 1999
- on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With
05000293/LER-1999-003, :on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With1999-06-15015 June 1999
- on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With
05000293/LER-1999-002, :on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With1999-06-0303 June 1999
- on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With
05000293/LER-1999-001, :on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With1999-05-0606 May 1999
- on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With
05000293/LER-1998-029, :on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With1999-02-0101 February 1999
- on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With
05000293/LER-1998-028, :on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With1999-01-28028 January 1999
- on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With
05000293/LER-1998-026, :on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with1998-12-23023 December 1998
- on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with
05000293/LER-1998-007, :on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With1998-12-22022 December 1998
- on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With
05000293/LER-1998-025, :on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With1998-12-18018 December 1998
- on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With
05000293/LER-1998-018, :on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With1998-12-18018 December 1998
- on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With
05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation1998-12-18018 December 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation
05000293/LER-1997-017, :on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With1998-12-18018 December 1998
- on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With
05000293/LER-1998-024, :on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans1998-11-13013 November 1998
- on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans
05000293/LER-1998-023, :on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With1998-11-0404 November 1998
- on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With
05000293/LER-1998-022, :on 981002,unplanned Actuation of a EDG Occurred During Surveillance Test of Related Logic Sys Testing.Caused by Util non-licensed I&C Technician Error. Will Review Surveillance Procedures.With1998-10-30030 October 1998
- on 981002,unplanned Actuation of a EDG Occurred During Surveillance Test of Related Logic Sys Testing.Caused by Util non-licensed I&C Technician Error. Will Review Surveillance Procedures.With
05000293/LER-1998-013, :on 980606,inconclusive Fire Barrier Test Data Was Noted.Caused by Concerns About Adequacy of Original Basis for Three Hour Rating.Declared Enclosures Inoperable & Posted Fire Watch within One Hour.With1998-09-30030 September 1998
- on 980606,inconclusive Fire Barrier Test Data Was Noted.Caused by Concerns About Adequacy of Original Basis for Three Hour Rating.Declared Enclosures Inoperable & Posted Fire Watch within One Hour.With
05000293/LER-1998-020, :on 980730,operating W/Less than Min Operating Shift Crew Composition Was Noted.Caused by off-going SCRE Not Ensuring Proper Relief of SCRE Function.Individual Was Appropriately Counseled1998-08-28028 August 1998
- on 980730,operating W/Less than Min Operating Shift Crew Composition Was Noted.Caused by off-going SCRE Not Ensuring Proper Relief of SCRE Function.Individual Was Appropriately Counseled
05000293/LER-1998-019, :on 980727,declared Standby Liquid Control Subsystem B Inoperable.Caused by Leakage Through Pipe Fitting on Pressure Gauge PI-1160B.Removed Subject Gauge, Cleaned Pipe Threads & Reinstalled Gauge1998-08-26026 August 1998
- on 980727,declared Standby Liquid Control Subsystem B Inoperable.Caused by Leakage Through Pipe Fitting on Pressure Gauge PI-1160B.Removed Subject Gauge, Cleaned Pipe Threads & Reinstalled Gauge
05000293/LER-1998-013, :on 980606,inconclusive Fire Barrier Test Data Occurred.Caused by Concerns About Adequacy of Original Basis for 3 H Rating.Encls Declared Inoperable & Fire Watch Posted1998-07-0303 July 1998
- on 980606,inconclusive Fire Barrier Test Data Occurred.Caused by Concerns About Adequacy of Original Basis for 3 H Rating.Encls Declared Inoperable & Fire Watch Posted
05000293/LER-1998-011, :on 961126,operator Discovered Two Shield Plugs Removed from Floor Directly Over Torus Compartment.Caused by Lack of Formal Program to Control sub-compartment Barriers. Developed Formal Program to Control Compartment Barriers1998-06-26026 June 1998
- on 961126,operator Discovered Two Shield Plugs Removed from Floor Directly Over Torus Compartment.Caused by Lack of Formal Program to Control sub-compartment Barriers. Developed Formal Program to Control Compartment Barriers
05000293/LER-1998-007, :on 980330,discovered Single Failure Vulnerability of RHR Sys When in SPC Mode.Caused by Inadequate Original Design.Standing Order Issued to Declare LPCI Sys Inoperable When RHR Sys Is in SPC Mode1998-04-29029 April 1998
- on 980330,discovered Single Failure Vulnerability of RHR Sys When in SPC Mode.Caused by Inadequate Original Design.Standing Order Issued to Declare LPCI Sys Inoperable When RHR Sys Is in SPC Mode
05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Cause Is Attributed to Significant Effect Meteorlogical Conditions Have on EDG Room Temp.Completed Engineering Evaluation1998-04-17017 April 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Cause Is Attributed to Significant Effect Meteorlogical Conditions Have on EDG Room Temp.Completed Engineering Evaluation
05000293/LER-1997-004, :on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept1998-04-14014 April 1998
- on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept
05000293/LER-1998-003, :on 980220,discovered That RBCCW & Tbccw Heat Exchanger Supports Outside Design Basis Seismic Requirements.Caused by Calculation Error.Reviewed Similar Calculations & Counseled Individuals Associated W/Errors1998-03-23023 March 1998
- on 980220,discovered That RBCCW & Tbccw Heat Exchanger Supports Outside Design Basis Seismic Requirements.Caused by Calculation Error.Reviewed Similar Calculations & Counseled Individuals Associated W/Errors
05000293/LER-1998-002, :on 980205,EDG Room Air Temperature Went Below Design Basis.Caused by Unawareness of Significant Effect Wind Direction Has on EDG Room Temp.Engineering Evaluation (Ee 97-066 R-1) Was Completed & Approved1998-03-0909 March 1998
- on 980205,EDG Room Air Temperature Went Below Design Basis.Caused by Unawareness of Significant Effect Wind Direction Has on EDG Room Temp.Engineering Evaluation (Ee 97-066 R-1) Was Completed & Approved
05000293/LER-1997-026, :on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly1998-01-0505 January 1998
- on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly
05000293/LER-1997-025, :on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B1997-12-23023 December 1997
- on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B
05000293/LER-1997-021, :on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F1997-12-0404 December 1997
- on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F
05000293/LER-1997-020, :on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.51997-12-0404 December 1997
- on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.5
05000293/LER-1997-019, :on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures1997-12-0404 December 1997
- on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures
05000293/LER-1997-015, :on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc1997-12-0303 December 1997
- on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc
05000293/LER-1997-023, :on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door1997-12-0101 December 1997
- on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door
05000293/LER-1997-014, :on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period)1997-09-24024 September 1997
- on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period)
05000293/LER-1997-012, :on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated1997-08-29029 August 1997
- on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated
05000293/LER-1997-003, :on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested1997-07-18018 July 1997
- on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested
05000293/LER-1997-010, :on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door1997-05-20020 May 1997
- on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door
05000293/LER-1997-005, :on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error1997-05-15015 May 1997
- on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error
05000293/LER-1997-007, :on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers1997-05-0101 May 1997
- on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers
05000293/LER-1997-008, :on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel1997-04-24024 April 1997
- on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel
05000293/LER-1997-006, :on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified1997-04-22022 April 1997
- on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified
05000293/LER-1997-004, :on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately1997-04-0707 April 1997
- on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately
05000293/LER-1997-002, :on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete1997-03-10010 March 1997
- on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete
05000293/LER-1997-001, :on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised1997-02-14014 February 1997
- on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised
ML20138Q5491997-02-0707 February 1997 LER 97-S02-00:on 970110,security Svcs Supervisor Received Improperly Mailed Safeguards Info.Caused by Personnel Error. Security Force Put on Heightened Awareness & Protected Area Patrol Frequency Increased 1999-09-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000293/LER-1999-010-02, :on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With1999-10-18018 October 1999
- on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With
05000293/LER-1999-009-02, :on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With1999-10-13013 October 1999
- on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With
ML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20216G5991999-09-24024 September 1999 Corrected Safety Evaluation Supporting Amend 182 to License DPR-35,consisting of Corrected Page 1 ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps 05000293/LER-1999-008-02, :on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With1999-09-0707 September 1999
- on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With
ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With 05000293/LER-1999-007-02, :on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With1999-08-13013 August 1999
- on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With
05000293/LER-1999-006-02, :on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With1999-08-0404 August 1999
- on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With
ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209G3851999-07-15015 July 1999 Safety Evaluation Supporting Amend 182 to License DPR-35 05000293/LER-1999-005, :on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With1999-07-0808 July 1999
- on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With
ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) 05000293/LER-1999-004, :on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With1999-06-28028 June 1999
- on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With
ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 05000293/LER-1999-003, :on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With1999-06-15015 June 1999
- on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With
ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant 05000293/LER-1999-002, :on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With1999-06-0303 June 1999
- on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With
ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant 05000293/LER-1999-001, :on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With1999-05-0606 May 1999
- on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With
ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With 05000293/LER-1998-029, :on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With1999-02-0101 February 1999
- on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With
05000293/LER-1998-028, :on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With1999-01-28028 January 1999
- on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With
ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With 05000293/LER-1998-026, :on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with1998-12-23023 December 1998
- on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with
05000293/LER-1998-007, :on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With1998-12-22022 December 1998
- on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With
ML20198H5671998-12-21021 December 1998 Safety Evaluation Supporting Amend 180 to License DPR-35 05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation1998-12-18018 December 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation
05000293/LER-1998-025, :on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With1998-12-18018 December 1998
- on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With
05000293/LER-1997-017, :on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With1998-12-18018 December 1998
- on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With
05000293/LER-1998-018, :on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With1998-12-18018 December 1998
- on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With
ML20198A2391998-12-11011 December 1998 Safety Evaluation Supporting Amend 179 to License DPR-35 ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With 05000293/LER-1998-024, :on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans1998-11-13013 November 1998
- on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans
ML20195B9161998-11-10010 November 1998 Safety Evaluation Supporting Amend 178 to License DPR-35 05000293/LER-1998-023, :on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With1998-11-0404 November 1998
- on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With
ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With 1999-09-08
[Table view] |
text
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JJ BOSTON EDISON Pilgum Nuclear Power Station Rocky Hill hoad Plymouth, Massachusetts 02360 George W. Davis sener Vice President - Nuclear February 25, 1991 BECo Ltr 91-019 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Hashington, D.C. 20555 Docket No. 50-293 License No. DPR-35
Dear Sir:
The enclosed Licensee Event Report (LER) 91-001-00, " Automatic Closing of the Primary Containment System Group 5 Isclation Valves During Surveillance Testing", is submitted in accordance with 10 CFR Part 50.73.
Please do not hesitate to contact me if there are any questions regarding this report.
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LER 91-001-00 cc:
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On January 25, 1991 at 0956 hours0.0111 days <br />0.266 hours <br />0.00158 weeks <br />3.63758e-4 months <br /> and at 1407 hours0.0163 days <br />0.391 hours <br />0.00233 weeks <br />5.353635e-4 months <br />, an automatic Primary Containment Isolation Control System (PCIS) Group 5 actuation occurred during-surveillance testing.
The actuations resulted in the automatic closing of the Reactor Core Isolation Cooling Systam (RCICS) turbine steam supply isolation valves. - The RCICS was declared inoperable and a 7 day Technical Specification
- - Limiting Condition for Operation (LCO) began.
The actuations were caused by a RCICS turbine steam supply line high flow condition.
The high steam flow condition occurred due to a failed transistor
=in the system's turbine speed control electric governor (EG-M) which was manufactured by the Woodward Governor Company (part number 8720-849).
An exact cause of the transistor failure could not be_ identified.. However, the signal cable-connecting the EG-M to the turbine control-valve hydraulic actuator (EG-R) was found to be degraded.
This degradation could hav_e-led _to the transistor failure.
The cable was supplied by the-Hoodward Governor Company (part number 232007).- The transistor and the cable were-replaced.
The RCICS turbine speed control system was subsequently calibrated.
The RCICS was satisfactorily tested and the 7 day LC0 was terminated on January 29, 1991
.at 2139 hours0.0248 days <br />0.594 hours <br />0.00354 weeks <br />8.138895e-4 months <br />.
- - This event-occurred during power operation while at 100 percent reactor power.
The reactor mode selector switch was in the RUN position.
This report is submitted in accordance with 10 CFR 50.73 subparts (a)(2)(iv) and (a)(2)(v)(D), and this event posed no threat to the public health and safety.
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3 *,72 Pilgrim Nuclear Power Station o p lo j o j o l2 l 9[3 31 0l0l1 40 q2 oF 0 l4 TEXT (# awe pose e reewed ces edersorw Nec Ann msCsJ (171 BACKGROUND The Reactor Core Isolation Cooling System (RCICS) turbine steam supply line flow is sensed by differentia'l pressure transmitters (DPIS 1360-1A and -18) that provide a steam line break detection function. A high steam flow-signal in one or both logic channels will actuate the Group 5 portion of the Primary Containment Isolation Control System (PCIS)- to limit the release of steam if a break in the RCICS turbine steam supply line occurs.
The Group 5 portion of the PCIS controls the RCIC turbine steam supply valves (H0-1301-16 and -17) which close on the isolat'.on signal.
EVENT DESCRIPTION
On January 25, 1991 at 0956 hours0.0111 days <br />0.266 hours <br />0.00158 weeks <br />3.63758e-4 months <br />, an unplanned automatic actuation of the RCICS portion of the PCIS occurred during a monthly surveillance test.
The RCICS was being tested in accordance with procedure number 8.5.5.1 (Rev. 31),
"RCIC Pump Operability Flow Rate and Valve Test at Approximately 1000 PSIG".
When the operator opened the RCICS turbine steam inlet valve (H0-1301-61), the turbine tripped with a RCICS high steam flow alarm indication in the control Toom.
Inspections of the accessible RCICS steam piping outside Primary Containment did not identify any leakage from the RCICS steam supply piping.
The RCICS was declared inoperable on January 25, 1991 at 1053 hours0.0122 days <br />0.293 hours <br />0.00174 weeks <br />4.006665e-4 months <br /> and a seven (7) day Technical Specification (3.5.0) Limiting Condition for Operation (LCO) was entered.
Operability testing of_ the High Pressure Coolant Injection System (HPCIS) began in accordance with Technical Specification 3.5.0.2 on January 25, 1991 at 1215 hours0.0141 days <br />0.338 hours <br />0.00201 weeks <br />4.623075e-4 months <br /> and was completed satisfactorily at 1338 hours0.0155 days <br />0.372 hours <br />0.00221 weeks <br />5.09109e-4 months <br />.
- - The RCICS steam line flow instrumentation (DPIS 1360-1 A and -18) was then functionally tested and calibrated in accordance with Procedure 8.H.2-2.6.1 (Rev. 19), "PCIC Steam Line High flow", with satisfactory as-found results.
The operators attempted to re-test RCICS in accordance with Procedure 8.5.5.1 as part of the initial troubleshooting and investigation.
However, the RCICS-turbine steam supply valves automatically closed after the turbine steam inlet valve was opened at 1407 hours0.0163 days <br />0.391 hours <br />0.00233 weeks <br />5.353635e-4 months <br />.
Failure and Halfunction Report (F&MR) 91-33 was written to document the first event and F&HR 91-34 was written to document the second event.
The NRC Operations Center was notified of the first and second events on January 25, 1991 at-1059 hours and 1426 hours0.0165 days <br />0.396 hours <br />0.00236 weeks <br />5.42593e-4 months <br />, respectively.
This event occurred during power operation with the reactor mode selector l
switch in the RUN position.
The Reactor Vessel (RV) pressure was 1035 psig l
with the RV temperature at 530 degrees Fahrenheit.
The reactor-power level was 100 percent.
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4 regwest, ese emanas/ AMC #srm JUL4 W im The direct cause of the PCIS actuations was RCICS turbine steam supply line high flow.
The high flow setpoint was satisfactorily checked af ter the first event in accordance with Procedure 8.M,2-2.6.1 (Rev. 19) Attachment 2, "RCIC Steam Line High Flow Instrument functional and Calibration Test".
Further troubleshooting identified the cause of the high steam flow condition to be the failure of a transistor (Q10) in the turbine speed control system electric governor.(EG-M).
The EG-H provides a signal to the turbine speed control system hydraulic-actuator (EG-R) which positions the turbine governor valve to achieve the desired speed control.
Transistor Q10 functions to transmit the close signal to close the governor valve, thus reducing speed.
Due to the transistor = failure, no close signal was transmitted to the EG-R; therefore.
- - the governor valve remained in the full open position throughout the RCICS start sequence.
The exact cause of the transistor failure was not identified.
However, the cable connecting the EG-M to the EG-R was found to be embrittled inside the EG-H control box.
The cable embrittlement may have led to the transistor failure. An investigation is ong ig to the cause of the cable embrittlement.
Initial results i, the cable embrittlement resulted from thermal ~ aging due to past exposure
. eat _and humidity.
Recent testing found that the RCICS quadrant temperatures were below the cable temperature rating.
Handling of the cable during maintenance and surveillance activities may have contributed _to_the cable failure.
The EG-M and cable were manufactured by the Hoodward Governor Company (part numbers 8720-849 and 232007, respectively).
CORRECTIVE ACTIONS
The transistor was replaced.
Field Revision Notice 91-02-02 was implemented that replaced the EG-M to EG-R cable with a spare cable. Other cables in the RCICS quadrant were inspected and were found to be satisfactory.
This LER will be updated if any significant corrective actions are taken as a result of the ongoing investigation.
Following the replacement of the transistor and cable the system was successfully calibrated in accordance with Procedure 8.E.13.1 (Rev. 1), "RCIC
- - Turbine Speed Control System Calibration", with satisfactory results.
The RCICS operability test was completed satisfactorily in accordance with Procedure 8,5.5.1.
The RCICS was declared operable and the-seven day LC0_was terminated on lanuary 29. 1991-at 2139 hours0.0248 days <br />0.594 hours <br />0.00354 weeks <br />8.138895e-4 months <br />.
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"*a Pilgrim Nuclear Power Station o l6 l0 l0 l0 l2 l 9l 3 9l1 0l0(l g0 0 l4 0l 4 or AYE N 6N YO YU N YS This event posed no threat to the public health and safety.
The RCICS high steam flow isolation is designed to mitigate the consequences l
of a break in the RCICS turbine steam supply line.
The automatic closing of the RCIC turbine steam supply isolation valves prevents excessive loss of
]
reactor coolant and the release of significant amounts of radioactive materials from the nuclear-system process barrier if a break occurs.
For this event i no break in the RCICS turbine steam line occurred.
The high steam flow i
trip setpoint is set conservatively low at Pilgrim StLtion to provide timely i
l detection of a RCICS turbine steam line break.
The HPCIS was operable during the period the RCICS was inoperable.
During the period the RCICS was inoperable, appropriate LCO testing was conducted in i
accordance with Procedure 8.5.4.1 Rev. 37, "High Pressure Coolant Injection System Pump and Valve Monthly / Quarterly Operability".
This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv) because the PCIS actuations were not a planned part of the surveillance test.
This report
- - is also submitted in accordance with 10 CFR 50.73(a)(2)(v)(0) because the RCICS was inoperable.
SIMILARITY TO PREVIOUS EVENTS A review was' conducted of Pilgrim Station Licensee Event Reports (LERs) submitted since January 1984.
The review was focused on LERs submitted in accordance with 10 CFR 50.73(a)(2)(iv) or (a)(2)(v) involving the RCICS and the HPCIS.- ihis-review did not identify any simliar events.
l ENERGY INDUSTRY IDENTIFICATION (EIIS) CODES The EIIS codes for this report are as follows:
COMPONENTS CODES Control, speed SC o
Governor-65 Cable CBL 1
SYSTEMS Engineered Safety Features Actuation System (PCIS)
JE Reactor Core Isolation Cooling System (RCICS)
BN High Pressure Coolant Injection System (HPCIS)
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05000293/LER-1991-001, :on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow Conditions |
- on 910125,automatic Primary Containment Isolation Control Sys Group 5 Actuation Occurred,Resulting in Closing of RCIC Turbine Steam Supply Isolation Valves. Caused by High Flow Conditions
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(v)(0) | 05000293/LER-1991-002, :on 910211,one Salt Svc Water Sys Pump Not Surveillance Tested Per Tech Spec.Caused by Procedural Error.Procedure Revised |
- on 910211,one Salt Svc Water Sys Pump Not Surveillance Tested Per Tech Spec.Caused by Procedural Error.Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) | 05000293/LER-1991-003, :on 910307,HPCI Sys Made Inoperable When Two HPCI Turbine Steam Exhaust Vacuum Breaker Containment Isolation Valves Discovered Closed.Caused by Loss of Fill Oil in Transmitter.Transmitter Replaced |
- on 910307,HPCI Sys Made Inoperable When Two HPCI Turbine Steam Exhaust Vacuum Breaker Containment Isolation Valves Discovered Closed.Caused by Loss of Fill Oil in Transmitter.Transmitter Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-1991-004, :on 910319,RCIC Sys Made Inoperable Due to Area Temp Switch Terminal Stripped During Quarterly Functional Test & Calibr.Caused by Repeating Torquing of Screws. Terminal Replaced W/Spare |
- on 910319,RCIC Sys Made Inoperable Due to Area Temp Switch Terminal Stripped During Quarterly Functional Test & Calibr.Caused by Repeating Torquing of Screws. Terminal Replaced W/Spare
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-1991-005, :on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator Failure |
- on 910325,diesel Generator Inoperable,Causing Loss of Ac Power to Train B Components of Safety Sys & Actuating Portions of Primary/Secondary Containment Sys. Caused by Voltage Regulator Failure
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1991-007, :on 910429,TS Required Shutdown Completed Due to Drywell Floor Sump Leakage Rate & Subsequent Scram Signal While Shutdown.Seal Cartridges Replaced & Responsible Operator Counseled |
- on 910429,TS Required Shutdown Completed Due to Drywell Floor Sump Leakage Rate & Subsequent Scram Signal While Shutdown.Seal Cartridges Replaced & Responsible Operator Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(1) | 05000293/LER-1991-008, :on 910430,three Automatic Group I Isolations Occurred Due to False High Reactor Water Level Signals During Shutdown.Cause Not Determined.Review of Plant Info Computer Traces |
- on 910430,three Automatic Group I Isolations Occurred Due to False High Reactor Water Level Signals During Shutdown.Cause Not Determined.Review of Plant Info Computer Traces
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000293/LER-1991-009, :on 910518,fire Barrier Discovered Breached in Intake Structure.Caused by Personnel Overlooking Tech Spec Barrier.Establishing Continuous Fire Watch in Pump Room & Eliminating Drain Check |
- on 910518,fire Barrier Discovered Breached in Intake Structure.Caused by Personnel Overlooking Tech Spec Barrier.Establishing Continuous Fire Watch in Pump Room & Eliminating Drain Check
| 10 CFR 50.73(a)(2)(1) | 05000293/LER-1991-010, :on 910527,secondary Containment Sy Isolation Occurred While Backing Out of Surveillance Testing.Caused by Personnel Error.Test Personnel Counseled & Procedure 8.9.8 Revised |
- on 910527,secondary Containment Sy Isolation Occurred While Backing Out of Surveillance Testing.Caused by Personnel Error.Test Personnel Counseled & Procedure 8.9.8 Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1991-011, :on 910604,inadvertent Primary Containment & Secondary Containment Isolation Signal Occurred Due to Util Licensed Operator Error.Responsible Engineer Counseled |
- on 910604,inadvertent Primary Containment & Secondary Containment Isolation Signal Occurred Due to Util Licensed Operator Error.Responsible Engineer Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1991-012, :on 910607,inadvertent Automatic Start of EDG a Occurred During Scheduled Surveillance Test While Shutdown for Refueling Outage.Caused by non-licensed Personnel Error |
- on 910607,inadvertent Automatic Start of EDG a Occurred During Scheduled Surveillance Test While Shutdown for Refueling Outage.Caused by non-licensed Personnel Error
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1991-013, :on 910613,as-found Leak Test Results for Four Feedwater Check Valves Discovered to Be in Excess of TS Limits.Caused by Disc Misalignment,Resulting in Improper Valve Seating.Valve Internals Rebuilt |
- on 910613,as-found Leak Test Results for Four Feedwater Check Valves Discovered to Be in Excess of TS Limits.Caused by Disc Misalignment,Resulting in Improper Valve Seating.Valve Internals Rebuilt
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-1991-014, :on 910627,determined That Setpoint of Dresser Safety Valve & Target Rock Relief Valves Out of Setpoint Tolerance.Caused by Incorrect Popping Pressures for Valves. Maint Procedures Reviewed |
- on 910627,determined That Setpoint of Dresser Safety Valve & Target Rock Relief Valves Out of Setpoint Tolerance.Caused by Incorrect Popping Pressures for Valves. Maint Procedures Reviewed
| 10 CFR 50.73(a)(2)(1) | 05000293/LER-1991-015, :on 910628,north Wall of a Train Salt Svc Water Pump Room in Intake Structure Discovered Breached. Caused by Broken Two Inch Conduit Fitting.Continuous Fire Watch Established |
- on 910628,north Wall of a Train Salt Svc Water Pump Room in Intake Structure Discovered Breached. Caused by Broken Two Inch Conduit Fitting.Continuous Fire Watch Established
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | 05000293/LER-1991-016, :on 910718,settings of Degraded Voltage Relays Found Out of Tolerance During Surveillance.Caused by Differences in Accuracy of Measuring & Test Equipment Used to Calibr Relays |
- on 910718,settings of Degraded Voltage Relays Found Out of Tolerance During Surveillance.Caused by Differences in Accuracy of Measuring & Test Equipment Used to Calibr Relays
| 10 CFR 50.73(a)(2)(1) | 05000293/LER-1991-017, :on 910720-21,three Automatic Actuations of Portions of Primary Containment Control Sys Occurred.Caused by Air in Sensing Lines.Procedures Revised & Training of Personnel Conducted |
- on 910720-21,three Automatic Actuations of Portions of Primary Containment Control Sys Occurred.Caused by Air in Sensing Lines.Procedures Revised & Training of Personnel Conducted
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1991-018, :on 910710,setpoints of Degraded Voltage Relays Discovered Too Low Probability Degraded Voltage Conditions. Cause Unknown.Mods Planned to Replace Applicable Control Power Transformers |
- on 910710,setpoints of Degraded Voltage Relays Discovered Too Low Probability Degraded Voltage Conditions. Cause Unknown.Mods Planned to Replace Applicable Control Power Transformers
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000293/LER-1991-019, :on 910525,circuit Breaker of safety-related Bus Transfer Scheme Discovered Open.Caused by Interference Between Breakers Forged Type Trip Latch Roller.Circuit Breaker Repaired by GE Personnel |
- on 910525,circuit Breaker of safety-related Bus Transfer Scheme Discovered Open.Caused by Interference Between Breakers Forged Type Trip Latch Roller.Circuit Breaker Repaired by GE Personnel
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000293/LER-1991-020, :on 910815,RCIC Declared Inoperable & Seven Day Tech Spec LCO Entered.Caused by Turbine Speed Oscillations Occurring Minutes After Steady operation.EG-R Replaced & Turbine Speed Control Sys Adjusted |
- on 910815,RCIC Declared Inoperable & Seven Day Tech Spec LCO Entered.Caused by Turbine Speed Oscillations Occurring Minutes After Steady operation.EG-R Replaced & Turbine Speed Control Sys Adjusted
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-1991-021, :on 911009,RCIC Declared Inoperable Due to Lack of Sufficient Battery Charger Test Data.Caused by Unavailability of Backup Battery Charger.Alarm Response Procedure for Alarm Window I4 Changed |
- on 911009,RCIC Declared Inoperable Due to Lack of Sufficient Battery Charger Test Data.Caused by Unavailability of Backup Battery Charger.Alarm Response Procedure for Alarm Window I4 Changed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-1991-022, :on 911024,both RWCU Sys Sensors Found to Have Trip Setpoints Greater than TS Limits.Caused by Setpoint Drift Due to Misalignment of Internal Mechanical Linkages. Sensors Recalibr & Linkages Aligned |
- on 911024,both RWCU Sys Sensors Found to Have Trip Setpoints Greater than TS Limits.Caused by Setpoint Drift Due to Misalignment of Internal Mechanical Linkages. Sensors Recalibr & Linkages Aligned
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-1991-023, :on 910728,11 of 76 Drywell Head Bolts Discovered Loose During Integrated Leak Rate Test.Caused by Failure of spherical-type Washer Sets & Use of Wrong Matl. Washer Sets Replaced & Procedure Revised |
- on 910728,11 of 76 Drywell Head Bolts Discovered Loose During Integrated Leak Rate Test.Caused by Failure of spherical-type Washer Sets & Use of Wrong Matl. Washer Sets Replaced & Procedure Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-1991-024, :on 911030,loss of Preferred & Secondary Offsite Power Occurred Due to Severe Coastal Storm While Shut Down.Caused by Flashover Switchyard Insulator. Westinghouse Type Relay 62/5 Will Be Replaced |
- on 911030,loss of Preferred & Secondary Offsite Power Occurred Due to Severe Coastal Storm While Shut Down.Caused by Flashover Switchyard Insulator. Westinghouse Type Relay 62/5 Will Be Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(1) | 05000293/LER-1991-025, :on 911030,RCIC Sys Turbine Tripped as Operators Started Sys for Reactor Vessel Water Level Control.Caused by Mechanical Overspeed Trip & Inverter Trip.Operator Counseled & Trip Reset |
- on 911030,RCIC Sys Turbine Tripped as Operators Started Sys for Reactor Vessel Water Level Control.Caused by Mechanical Overspeed Trip & Inverter Trip.Operator Counseled & Trip Reset
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) | 05000293/LER-1991-026, :on 911030 & 31,automatic Actuations Occurred in RWCU Sys Portion of Primary Containment Isolation Control Sys.Possibly Caused by Momentary Fluctuations in RWCU Sys Flow.High Flow Sensor Settings Verified |
- on 911030 & 31,automatic Actuations Occurred in RWCU Sys Portion of Primary Containment Isolation Control Sys.Possibly Caused by Momentary Fluctuations in RWCU Sys Flow.High Flow Sensor Settings Verified
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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