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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000293/LER-1999-010-02, :on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With1999-10-18018 October 1999
- on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With
05000293/LER-1999-009-02, :on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With1999-10-13013 October 1999
- on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With
05000293/LER-1999-008-02, :on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With1999-09-0707 September 1999
- on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With
05000293/LER-1999-007-02, :on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With1999-08-13013 August 1999
- on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With
05000293/LER-1999-006-02, :on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With1999-08-0404 August 1999
- on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With
05000293/LER-1999-005, :on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With1999-07-0808 July 1999
- on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With
05000293/LER-1999-004, :on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With1999-06-28028 June 1999
- on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With
05000293/LER-1999-003, :on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With1999-06-15015 June 1999
- on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With
05000293/LER-1999-002, :on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With1999-06-0303 June 1999
- on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With
05000293/LER-1999-001, :on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With1999-05-0606 May 1999
- on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With
05000293/LER-1998-029, :on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With1999-02-0101 February 1999
- on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With
05000293/LER-1998-028, :on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With1999-01-28028 January 1999
- on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With
05000293/LER-1998-026, :on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with1998-12-23023 December 1998
- on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with
05000293/LER-1998-007, :on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With1998-12-22022 December 1998
- on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With
05000293/LER-1998-025, :on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With1998-12-18018 December 1998
- on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With
05000293/LER-1998-018, :on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With1998-12-18018 December 1998
- on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With
05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation1998-12-18018 December 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation
05000293/LER-1997-017, :on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With1998-12-18018 December 1998
- on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With
05000293/LER-1998-024, :on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans1998-11-13013 November 1998
- on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans
05000293/LER-1998-023, :on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With1998-11-0404 November 1998
- on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With
05000293/LER-1998-022, :on 981002,unplanned Actuation of a EDG Occurred During Surveillance Test of Related Logic Sys Testing.Caused by Util non-licensed I&C Technician Error. Will Review Surveillance Procedures.With1998-10-30030 October 1998
- on 981002,unplanned Actuation of a EDG Occurred During Surveillance Test of Related Logic Sys Testing.Caused by Util non-licensed I&C Technician Error. Will Review Surveillance Procedures.With
05000293/LER-1998-013, :on 980606,inconclusive Fire Barrier Test Data Was Noted.Caused by Concerns About Adequacy of Original Basis for Three Hour Rating.Declared Enclosures Inoperable & Posted Fire Watch within One Hour.With1998-09-30030 September 1998
- on 980606,inconclusive Fire Barrier Test Data Was Noted.Caused by Concerns About Adequacy of Original Basis for Three Hour Rating.Declared Enclosures Inoperable & Posted Fire Watch within One Hour.With
05000293/LER-1998-020, :on 980730,operating W/Less than Min Operating Shift Crew Composition Was Noted.Caused by off-going SCRE Not Ensuring Proper Relief of SCRE Function.Individual Was Appropriately Counseled1998-08-28028 August 1998
- on 980730,operating W/Less than Min Operating Shift Crew Composition Was Noted.Caused by off-going SCRE Not Ensuring Proper Relief of SCRE Function.Individual Was Appropriately Counseled
05000293/LER-1998-019, :on 980727,declared Standby Liquid Control Subsystem B Inoperable.Caused by Leakage Through Pipe Fitting on Pressure Gauge PI-1160B.Removed Subject Gauge, Cleaned Pipe Threads & Reinstalled Gauge1998-08-26026 August 1998
- on 980727,declared Standby Liquid Control Subsystem B Inoperable.Caused by Leakage Through Pipe Fitting on Pressure Gauge PI-1160B.Removed Subject Gauge, Cleaned Pipe Threads & Reinstalled Gauge
05000293/LER-1998-013, :on 980606,inconclusive Fire Barrier Test Data Occurred.Caused by Concerns About Adequacy of Original Basis for 3 H Rating.Encls Declared Inoperable & Fire Watch Posted1998-07-0303 July 1998
- on 980606,inconclusive Fire Barrier Test Data Occurred.Caused by Concerns About Adequacy of Original Basis for 3 H Rating.Encls Declared Inoperable & Fire Watch Posted
05000293/LER-1998-011, :on 961126,operator Discovered Two Shield Plugs Removed from Floor Directly Over Torus Compartment.Caused by Lack of Formal Program to Control sub-compartment Barriers. Developed Formal Program to Control Compartment Barriers1998-06-26026 June 1998
- on 961126,operator Discovered Two Shield Plugs Removed from Floor Directly Over Torus Compartment.Caused by Lack of Formal Program to Control sub-compartment Barriers. Developed Formal Program to Control Compartment Barriers
05000293/LER-1998-007, :on 980330,discovered Single Failure Vulnerability of RHR Sys When in SPC Mode.Caused by Inadequate Original Design.Standing Order Issued to Declare LPCI Sys Inoperable When RHR Sys Is in SPC Mode1998-04-29029 April 1998
- on 980330,discovered Single Failure Vulnerability of RHR Sys When in SPC Mode.Caused by Inadequate Original Design.Standing Order Issued to Declare LPCI Sys Inoperable When RHR Sys Is in SPC Mode
05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Cause Is Attributed to Significant Effect Meteorlogical Conditions Have on EDG Room Temp.Completed Engineering Evaluation1998-04-17017 April 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Cause Is Attributed to Significant Effect Meteorlogical Conditions Have on EDG Room Temp.Completed Engineering Evaluation
05000293/LER-1997-004, :on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept1998-04-14014 April 1998
- on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept
05000293/LER-1998-003, :on 980220,discovered That RBCCW & Tbccw Heat Exchanger Supports Outside Design Basis Seismic Requirements.Caused by Calculation Error.Reviewed Similar Calculations & Counseled Individuals Associated W/Errors1998-03-23023 March 1998
- on 980220,discovered That RBCCW & Tbccw Heat Exchanger Supports Outside Design Basis Seismic Requirements.Caused by Calculation Error.Reviewed Similar Calculations & Counseled Individuals Associated W/Errors
05000293/LER-1998-002, :on 980205,EDG Room Air Temperature Went Below Design Basis.Caused by Unawareness of Significant Effect Wind Direction Has on EDG Room Temp.Engineering Evaluation (Ee 97-066 R-1) Was Completed & Approved1998-03-0909 March 1998
- on 980205,EDG Room Air Temperature Went Below Design Basis.Caused by Unawareness of Significant Effect Wind Direction Has on EDG Room Temp.Engineering Evaluation (Ee 97-066 R-1) Was Completed & Approved
05000293/LER-1997-026, :on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly1998-01-0505 January 1998
- on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly
05000293/LER-1997-025, :on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B1997-12-23023 December 1997
- on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B
05000293/LER-1997-021, :on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F1997-12-0404 December 1997
- on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F
05000293/LER-1997-020, :on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.51997-12-0404 December 1997
- on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.5
05000293/LER-1997-019, :on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures1997-12-0404 December 1997
- on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures
05000293/LER-1997-015, :on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc1997-12-0303 December 1997
- on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc
05000293/LER-1997-023, :on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door1997-12-0101 December 1997
- on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door
05000293/LER-1997-014, :on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period)1997-09-24024 September 1997
- on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period)
05000293/LER-1997-012, :on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated1997-08-29029 August 1997
- on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated
05000293/LER-1997-003, :on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested1997-07-18018 July 1997
- on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested
05000293/LER-1997-010, :on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door1997-05-20020 May 1997
- on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door
05000293/LER-1997-005, :on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error1997-05-15015 May 1997
- on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error
05000293/LER-1997-007, :on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers1997-05-0101 May 1997
- on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers
05000293/LER-1997-008, :on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel1997-04-24024 April 1997
- on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel
05000293/LER-1997-006, :on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified1997-04-22022 April 1997
- on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified
05000293/LER-1997-004, :on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately1997-04-0707 April 1997
- on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately
05000293/LER-1997-002, :on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete1997-03-10010 March 1997
- on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete
05000293/LER-1997-001, :on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised1997-02-14014 February 1997
- on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised
ML20138Q5491997-02-0707 February 1997 LER 97-S02-00:on 970110,security Svcs Supervisor Received Improperly Mailed Safeguards Info.Caused by Personnel Error. Security Force Put on Heightened Awareness & Protected Area Patrol Frequency Increased 1999-09-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000293/LER-1999-010-02, :on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With1999-10-18018 October 1999
- on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With
05000293/LER-1999-009-02, :on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With1999-10-13013 October 1999
- on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With
ML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20216G5991999-09-24024 September 1999 Corrected Safety Evaluation Supporting Amend 182 to License DPR-35,consisting of Corrected Page 1 ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps 05000293/LER-1999-008-02, :on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With1999-09-0707 September 1999
- on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With
ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With 05000293/LER-1999-007-02, :on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With1999-08-13013 August 1999
- on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With
05000293/LER-1999-006-02, :on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With1999-08-0404 August 1999
- on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With
ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209G3851999-07-15015 July 1999 Safety Evaluation Supporting Amend 182 to License DPR-35 05000293/LER-1999-005, :on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With1999-07-0808 July 1999
- on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With
ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) 05000293/LER-1999-004, :on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With1999-06-28028 June 1999
- on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With
ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 05000293/LER-1999-003, :on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With1999-06-15015 June 1999
- on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With
ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant 05000293/LER-1999-002, :on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With1999-06-0303 June 1999
- on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With
ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant 05000293/LER-1999-001, :on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With1999-05-0606 May 1999
- on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With
ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With 05000293/LER-1998-029, :on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With1999-02-0101 February 1999
- on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With
05000293/LER-1998-028, :on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With1999-01-28028 January 1999
- on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With
ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With 05000293/LER-1998-026, :on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with1998-12-23023 December 1998
- on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with
05000293/LER-1998-007, :on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With1998-12-22022 December 1998
- on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With
ML20198H5671998-12-21021 December 1998 Safety Evaluation Supporting Amend 180 to License DPR-35 05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation1998-12-18018 December 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation
05000293/LER-1998-025, :on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With1998-12-18018 December 1998
- on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With
05000293/LER-1997-017, :on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With1998-12-18018 December 1998
- on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With
05000293/LER-1998-018, :on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With1998-12-18018 December 1998
- on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With
ML20198A2391998-12-11011 December 1998 Safety Evaluation Supporting Amend 179 to License DPR-35 ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With 05000293/LER-1998-024, :on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans1998-11-13013 November 1998
- on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans
ML20195B9161998-11-10010 November 1998 Safety Evaluation Supporting Amend 178 to License DPR-35 05000293/LER-1998-023, :on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With1998-11-0404 November 1998
- on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With
ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With 1999-09-08
[Table view] |
text
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10 CFR 50.73
[
MM i
Ngrim Nuclear Power station i
Rocky Hill Road Plymouth, Massachusetts 02360 Ralph G. Bird i
senior %ce President - Nuclear
[
March 12,1990 BECo Ltr. 90- 035 U.S. Nuclear Regulatory Commission Attn:
Document Control Desk Hashington, D.C.
20555 Docket No. 50-293 License No. DPR-35
Dear Sir:
The enclosed Licensee Event Report (LER) 90-001-00, "Two Reactor Coolatt System Instrumentation Excess Flow Check Valves Inappropriately Verifiei Operable During Testing", is submitted in accordance with 10 CFR Part 50.73.
Please do not hesitate to contact me if there are any questions regardirg this report.
r DHE/bal Enclosure: LER 90-001-00 cc:
Mr. Hilliam T. Russell Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Rd.
King of Prussia, PA 19406 f
Sr. NRC Resident Inspector - Pilgrim Station Standard BECo LER Distribution pennmae FDC
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,,9.,I.- % an,.,3m. r--~r-a o no990 at 130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br />, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Limiting Condition for Operation (LCO) im.
y was entered because the operability of two (one-inch) reactor coolant system (RCS) instrument line excess flow check valves had been inappropriately verified during a Technical Specification required functional test on November 3,1989.
The other 80 RCS instrument line excess flow check valves were satisfactorily tested.
The LCO was terminated at 21d hours following NRC relief from Technical Specification 4.7 A.2.b.1.d for the two check valves.
The cause for this problem had not been determined when this report was prepared.
A supplemental report will be submitted after the ongoing investigation for cause has been completed.
Corrective actions planned include the replacement of the two excess flow check valves during the mid-cycle outage that is scheduled to begin March 9, 1990.
Interim compensatory measures being taken include increased controls for access and work in the vicinity of the instrument lines, routine visual operator inspections of the instrumentation lines, and issuing a radiation work permit to promptly allow the closing of the related manual isolation valves upstream of the check valves if necessary.
The LCO was entered during power operation with the reactor mode selector switch in the RUN position.
The reactor power level was 100 percent.
The Reactor Vessel (RV) pressure was 1035 psig with the RV water temperature at 549 degrees Fahrenheit.
This report is submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) and the problem posed no threat to the public health and safety.
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- a Pilgrim Nuclear Power Station itxw g g m p.m.ml On February 9,1990 at 1830 hours0.0212 days <br />0.508 hours <br />0.00303 weeks <br />6.96315e-4 months <br />, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Limiting Condition for Operation (LCO) was entered because the operability of two (one-inch) reactor coolant system (RCS) instrument line excess flow check valves had been inappropriately verified during a functional test on November 3, 1989.
Technical Specification 4.7.A.2.b.l.d specifies that the operability of RCS instrument line (excess) flow check valves shall be verified at least once per operating cycle.
The (82) RCS excess flow check valves are functionally tested via procedure 8.M.3-2, " Instrument Line Flow Check Valve Test".
The excess flow check valves, CK-125A and CK-1258, were installed new in September 1987.
The test procedure was inappropriately signed as completed on November 4,1989 based on a previously written memorandum that indicated the two check valves were not required to be functionally tested until the next refueling outage.
The memorandum was written because sufficient flow (i.e., greater than two GPM), needed to actuate the check valves (CK-125A/B), could not be achieved during post installation testing due to instrument line configuration.
Failure and Halfbnction Report 90-32 was written to document the problem. The NRC Operations Center was notified in accordance with 10 CFR 50.72 on February 9, 1990 at 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br />.
The LCO was entered during power operation with the reactor mode selector switch in the RUN position.
The reactor power level was approximately 100 percent.
The l
Reactor Vessel (RV) pressure was 1035 psig with the RV water temperature at 549 l
degrees Fahrenheit.
The LC0 was terminated as a result of a formal relief request made by Boston Edison Company from Technical Specification 4.7.A.2.b.1.d for the excess flow check valves (CK-125A/B).
The request was subsequently discussed with the NRC (offices of Region I and NRR) via a teleconference call that began on February 9, 1990 at approximately 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br />.
The request was granted by the NRC at approximately 2115 l
hours.
The 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO was terminated on FeLruary 9, 1990 at 2119 hours0.0245 days <br />0.589 hours <br />0.0035 weeks <br />8.062795e-4 months <br />.
The relief extends to the mid-cycle outage that is scheduled to begin on March 9, 1990.
BACKGROUND The two (one-inch) excess flow check valves, CK-125A and CK-125B, are installed in reactor coolant system instrument (high side) lines that extend from primary containment penetrations X-82A and X-828, respectively.
Upstream of these penetrations, and within primary containment, each instrument line includes a restricting orifice. Downstream of these penetrations, and outside primary containment, each line includes a manual isolation valve, H0-126A or H0-126B, and in-series excess flow check valve, CK-125A or CK-125B.
From the flow check valve, the one-half inch instrument line extends to racks that house sensors (transmitters) and local indicators that function to monitor Reactor Vessel pressure and water level.
The sensors provide signals to the circuitry of systems that include the following:
Reactor Protection High Pressure Coolant Injection, Reactor Core Isolation Cooling, Automatic Depressurization, Core Spray, Residual Heat Removal, Primary Containment Isolation Control, and Reactor Building Isolation Control.
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If the isolation valves upstream of the excess flow check valves (CK-125A/B) were to be closed, the number of operable instrument channels and trip systems would be less than the minimum specified by the Technical Specification (s) for the related systems.
CMSI A Human Performance Evaluation System (HPES) investigation is being conducted to determine the cause(s) for the problem and is expected to be completed during the week of March 12, 1990.
A supplemental report will be submitted after the investigation is completed and is expected to be submitted by June 1, 1990.
CORRECTIVE ACTION
A modification (PDC 90-13) has been prepared for the replacement of the excess flow check valves (CK-125A/B).
The replacement (one-inch) excess flow check valves have a (flow) actuation (i.e., two GPM or less) that is lower than the currently installed check valves that actuate at a flow of greater than two GPM.
The modification will be implemented during the mid-cycle outage that is scheduled to begin on March 9, 1990.
The currently installed check valves (CK-125A/B) were manufactured by Dragon Valve Incorporated, part number 15960N-1; the replacement check valves are similar, but are pp.rt number 15960N-2.
Other co rective actions are indeterminate at this time in that the investigation for caus) has not been completed.
INTERIM COMPENSATORY MEASURES l
The following compensatory measures were initiated on February 9, 1990 at approximately 2057 hours0.0238 days <br />0.571 hours <br />0.0034 weeks <br />7.826885e-4 months <br /> and are being taken during continued operation:
Access controls were increased for areas in the vicinity of the instrument lines from the penetrations (X-82A/B) upstream of the check valves (CK-125A/B) to the related downstream instrumentation racks.
The increased controls include roping and the posting of appropriate notices in the areas.
Controls were increased for work or maintenance in the vicinity of the instrument lines from the penetrations (X-82A/B) upstream of the check valves (CK-125A/B) to the related downstream instrumentation racks.
The increased controls include authorization by the shift Hatch Engineer for work or maintenance in the vicinity of the instrument lines.
A Radiation Work Permit (RHP 90-161) was issued to promptly allow Operations personnel to close the related upstream isolation valve (s),
H0-126A/B, if an instrumentation line break were to occur downstream of a flow check valve (s),
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- =,- monni The areas in the vicinity of the instrumentation lines from the penetrations (X-82A/B) upstream of the flow check valves to the related downstream instrumentation racks are being visually inspected for leakage at least once-per-shift.
SAFETY CONSEOUENCES This condition posed no threat to the public health and safety.
The RCS instrument line excess flow check valves, including excess flow check valves CK-125A/B, provide two functions:
The active function is part of Technical Specifications 3/4.7.A.2 because the check valves function to reduce an RCS leak into the Reactor Building (secondary containment) if an instrument line break were to occur downstream of a check valve (e.g., CK-125A).
The safety analysis for a potential instrument line break is provided in the Pilgrim Station Updated Final Safety Analysis Report (FSAR) section 5.2.3.5.3.
This section describes the instrument line containment boundary as an upstream orifice located inside primary containment and a downstream instrument line flow check valve (e.g., CK-125A) located outside primary containment, The passive function is not specifically a part of the Pilgrim Station e
Technical Specifications because the instrument lines, including flow check valves CK-125A/B, function to provide a passive pressure boundary as part of the pathway for sensing Reactor Vessel pressure and water level.
The active function of primary containment instrument line excess flow check valves is tested in accordance with procedure 8.M.3-2, " Instrument Line Flow Check Valve Test".
The other 80 instrument line flow check valves were functionally tested with satisfactory results during the October-November 1989 outage.
Routine and periodic assurance of the excess flow check valves' (CK-125A/B) passive function is demonstrated as follows:
Routine once-per-shift operator tours within the Reactor Building are performed in accordance with procedure 2.1.16. " Nuclear Power Plant l
Operator Tour", Attachment 2 (OPER-8).
These tours include various checks in the vicinity of the instrument lines from the penetrations (X-82A/B) upstream of the check valves (CK-125A/B) to the related downstream instrumentation racks. These tours also include a check for Reactor Vessel pressure and water level indications at the applicable instrument.
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indications in the Control Room are performed in accordance with procedure 2.1.15. " Daily Surveillance Log", Attachment 1.
The indications in the Control Room are derived from instrumentation including transmitters downstream of flow check valves CK-125A/B.
Routine trending of Reactor Vessel pressure and water level transmitters, by the Systems Engineering Division, includes monitoring the performance and response of transmitters downstream of the flow check valves (CK-125A/B).
Periodic surveillance testing of instrumentation downstream of the flow check valves (CK-125A/B) is performed in accordance with procedures. The procedures include:
8.M.1-32.1 (typical), " Analog Trip System - Trip Unit Calibration Cabinet C2228-Al", 8.M.1-32.5 (typical), " Analog Trip System -
Trip Unit Calibration - Cabinet C2233A, Section A", 8.M.2-6.1, " Reactor Pressure Readout", 8.M.2-6.3, " Reactor Level Readout", 8.M.2-8.1 (typical), " Calibration of ATS Transmitters Rack C2205", and 8.M.2-8.6,
" Calibration of ATS Transmitters Rack C2251 and C2252".
These routine and periodic activities provide assurance that the passive function of the check valves (CK-125A/B) is functional.
The failure of an excess flow check valve body, or the instrument line upstream of the check valve, could result in a maximum leakage of 20 GPM into the Reactor Building. The leakage, limited by the upstream orifice, is within the makeup capacity of the Control Rod Drive or feedwater Systems.
The amount of steam resulting from a 20 GPM leak into the Reactor Building does not endanger the integrity of the Reactor Building.
If a leak were to occur and the Reactor Building is not isolated, a l
significant pressure increase would not occur because of the relatively high Reactor Building ventilation exhaust rate.
If a leak were to occur and the Reactor Building is isolated, the operation of either one of the two Standby Gas Treatment System trains would prevent the Reactor Building from exceeding its design value for internal (positive) pressure.
The total radiological dose at the site boundary resulting from a 20 GPM leak with either of these two Reactor Building configurations would be substantially below the guidelines of 10 CFR Part 100.
Excess flow check valves CK-125A/B and the related upstream flow restricting orifices were installed new in 1987.
Except for periodic surveillance testing, the flow restricting orifices and check valves are not subjected to a fluid flow environment.
Therefore, it is reasonable to assume that these flow restricting i
orifices have not degraded in any way which could result in an increase in the l
limiting flow of 20 GPH.
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~ ~av au w m, This report is submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) because the operability of excess flow check valves CK-125A/B was not verified as specified by Technical Specification 4.7.A.2.b.l.d.
This report is also submitted in accordance with 10 CFR 50.73(a)(2)(1)(B) because the related manual isolation valves HO-126A/B, located upstream of excess flow check valves CK-125A/B, were not secured in the isolated position as specified by Technical Specification 3.7.A.2.a.(5).
This action was not taken because of the relief granted from Technical Specification 4.7.A.2.b.l.d for excess flow check valves CK-125A/B.
SIMILARITY TO PREVIO'JS EVENTS Similarity to previous events is indeterminate at this time in that the investigation for cause has not been completed.
ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for this report are as follows:
COMPONENTS CODES Valve (CK-125A/B)
V Valve, Control. Flow (CK-125A/B)
FCV SYSTEMS Containment Leakage Control System BD Incore Monitoring System IC g,o..
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| | Reporting criterion |
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05000293/LER-1990-001, :on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves Replaced |
- on 900209,24 H Limiting Condition for Operation Entered When Two RCS Instrumentation Excess Flow Check Valves Inappropriately Verified Operable During Testing.Cause Undetermined.Two Valves Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | 05000293/LER-1990-002, :on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs Changed |
- on 900228,determined That Max Fraction of Limiting Power Density Not Checked Daily During Reactor Power Operation,Per Tech Spec 4.1.B.On 900323,addl Tech Spec Issue Discovered.Tech Specs Changed
| 10 CFR 50.73(a)(2)(1) | 05000293/LER-1990-003, :on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re Backfill |
- on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re Backfill
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1990-004, :on 900316,leakage for Feedwater Check Valves Found to Be in Excess of Limits.Caused by Damaged Soft Seat & Inconsistencies in Valves.Soft Seat Matl & Bushings in Valves Replaced & Hinge Pins Reinstalled |
- on 900316,leakage for Feedwater Check Valves Found to Be in Excess of Limits.Caused by Damaged Soft Seat & Inconsistencies in Valves.Soft Seat Matl & Bushings in Valves Replaced & Hinge Pins Reinstalled
| 10 CFR 50.73(a)(2)(1) | 05000293/LER-1990-005, :on 900320,GE Type AK-2A-50 480-volt Circuit Breaker Did Not Trip Automatically During Planned Bus Transfer.Caused by Latch Prop Misalignment Due to Missing Retaining Ring.Offsite Insp Performed |
- on 900320,GE Type AK-2A-50 480-volt Circuit Breaker Did Not Trip Automatically During Planned Bus Transfer.Caused by Latch Prop Misalignment Due to Missing Retaining Ring.Offsite Insp Performed
| | 05000293/LER-1990-006, :on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review Performed |
- on 900330,determined That Position of Primary Containment Sys Isolation Valve Not Recorded Daily,Per Tech Specs.Review Performed to Determine If Other Problems Existed.Plant Shut Down & Review Performed
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) | 05000293/LER-1990-007, :on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of Requirements |
- on 900507,discovered That Drywell to Suppression Chamber Vacuum Breaker Surveillance Not Performed Prior to Startup in 1988.Caused by Misunderstanding of Requirements
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) | 05000293/LER-1990-008, :on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay Replaced |
- on 900513,automatic Scram Resulting from Load Rejection Occurred While at Full Power,Resulting in Trip of Generator Field Breakers.Caused by Fault on Offsite 345 Kv Transmission sys.Loss-of-field Relay Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1990-010, :on 900703,shutdown Completed Due to Inoperable Recirculation Sys Loop.Caused by Combination of Factors Including Malfunction of Recirculation motor-generator. Oil Samples Obtained & Analyzed |
- on 900703,shutdown Completed Due to Inoperable Recirculation Sys Loop.Caused by Combination of Factors Including Malfunction of Recirculation motor-generator. Oil Samples Obtained & Analyzed
| 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000293/LER-1990-011, :on 900703,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred While Shut Down.Caused by Hydrodynamic Transient. Procedure Revised |
- on 900703,automatic Actuation of RHR Sys Portion of Primary Containment Isolation Control Sys Occurred While Shut Down.Caused by Hydrodynamic Transient. Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1990-012, :on 900712,discovered Two Radioactive Sources Not Leak Checked within Tech Spec Required Interval.Caused by Procedural Weakness.Sources Inventoried & Leak Checked & Procedure 6.6-010 Will Be Revised |
- on 900712,discovered Two Radioactive Sources Not Leak Checked within Tech Spec Required Interval.Caused by Procedural Weakness.Sources Inventoried & Leak Checked & Procedure 6.6-010 Will Be Revised
| 10 CFR 50.73(a)(2)(1) | 05000293/LER-1990-013, :on 900902,unplanned Manual Reactor Scram Initiated W/Reactor Power at 60%.Fuse Blew in Feedwater Control Circuit Power Supply Causing Feedwater Regulating Valves to Lockup.Trip Linkage Repaired |
- on 900902,unplanned Manual Reactor Scram Initiated W/Reactor Power at 60%.Fuse Blew in Feedwater Control Circuit Power Supply Causing Feedwater Regulating Valves to Lockup.Trip Linkage Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1990-014, :on 900903,automatic Closing of Primary Containment Sys Group 3 Isolation Valves Occurred While Shut Down.Caused by Transient That Actuated Stated Pressure Switches |
- on 900903,automatic Closing of Primary Containment Sys Group 3 Isolation Valves Occurred While Shut Down.Caused by Transient That Actuated Stated Pressure Switches
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1990-015, :on 900913,unplanned Partial Isolations of Hydrogen & Oxygen Analyzer Sys & Reactor Coolant Pressure Boundary Leak Detection Sys Occurred |
- on 900913,unplanned Partial Isolations of Hydrogen & Oxygen Analyzer Sys & Reactor Coolant Pressure Boundary Leak Detection Sys Occurred
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1990-016, :on 900917,automatic Actuation of Main Steam Sys/Group 1 Portion of PCIS Occurred |
- on 900917,automatic Actuation of Main Steam Sys/Group 1 Portion of PCIS Occurred
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1990-017, :on 901009,HPCI Sys Declared Inoperable Due to Turbine Trip on Overspeed During Scheduled Surveillance Test.Caused by Mechanical Overspeed trip.Electro-mechanical Hydraulic Actuator Replaced |
- on 901009,HPCI Sys Declared Inoperable Due to Turbine Trip on Overspeed During Scheduled Surveillance Test.Caused by Mechanical Overspeed trip.Electro-mechanical Hydraulic Actuator Replaced
| | 05000293/LER-1990-018, :on 901022,inadvertent Actuation of Portion of Secondary Containment Sys Occurred During Surveillance Testing |
- on 901022,inadvertent Actuation of Portion of Secondary Containment Sys Occurred During Surveillance Testing
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000293/LER-1990-019, :on 901109,fire Dampers & Penetration Found Degraded in Intake Structure |
- on 901109,fire Dampers & Penetration Found Degraded in Intake Structure
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) |
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