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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000293/LER-1999-010-02, :on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With1999-10-18018 October 1999
- on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With
05000293/LER-1999-009-02, :on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With1999-10-13013 October 1999
- on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With
05000293/LER-1999-008-02, :on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With1999-09-0707 September 1999
- on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With
05000293/LER-1999-007-02, :on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With1999-08-13013 August 1999
- on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With
05000293/LER-1999-006-02, :on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With1999-08-0404 August 1999
- on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With
05000293/LER-1999-005, :on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With1999-07-0808 July 1999
- on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With
05000293/LER-1999-004, :on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With1999-06-28028 June 1999
- on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With
05000293/LER-1999-003, :on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With1999-06-15015 June 1999
- on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With
05000293/LER-1999-002, :on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With1999-06-0303 June 1999
- on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With
05000293/LER-1999-001, :on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With1999-05-0606 May 1999
- on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With
05000293/LER-1998-029, :on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With1999-02-0101 February 1999
- on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With
05000293/LER-1998-028, :on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With1999-01-28028 January 1999
- on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With
05000293/LER-1998-026, :on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with1998-12-23023 December 1998
- on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with
05000293/LER-1998-007, :on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With1998-12-22022 December 1998
- on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With
05000293/LER-1998-025, :on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With1998-12-18018 December 1998
- on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With
05000293/LER-1998-018, :on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With1998-12-18018 December 1998
- on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With
05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation1998-12-18018 December 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation
05000293/LER-1997-017, :on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With1998-12-18018 December 1998
- on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With
05000293/LER-1998-024, :on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans1998-11-13013 November 1998
- on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans
05000293/LER-1998-023, :on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With1998-11-0404 November 1998
- on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With
05000293/LER-1998-022, :on 981002,unplanned Actuation of a EDG Occurred During Surveillance Test of Related Logic Sys Testing.Caused by Util non-licensed I&C Technician Error. Will Review Surveillance Procedures.With1998-10-30030 October 1998
- on 981002,unplanned Actuation of a EDG Occurred During Surveillance Test of Related Logic Sys Testing.Caused by Util non-licensed I&C Technician Error. Will Review Surveillance Procedures.With
05000293/LER-1998-013, :on 980606,inconclusive Fire Barrier Test Data Was Noted.Caused by Concerns About Adequacy of Original Basis for Three Hour Rating.Declared Enclosures Inoperable & Posted Fire Watch within One Hour.With1998-09-30030 September 1998
- on 980606,inconclusive Fire Barrier Test Data Was Noted.Caused by Concerns About Adequacy of Original Basis for Three Hour Rating.Declared Enclosures Inoperable & Posted Fire Watch within One Hour.With
05000293/LER-1998-020, :on 980730,operating W/Less than Min Operating Shift Crew Composition Was Noted.Caused by off-going SCRE Not Ensuring Proper Relief of SCRE Function.Individual Was Appropriately Counseled1998-08-28028 August 1998
- on 980730,operating W/Less than Min Operating Shift Crew Composition Was Noted.Caused by off-going SCRE Not Ensuring Proper Relief of SCRE Function.Individual Was Appropriately Counseled
05000293/LER-1998-019, :on 980727,declared Standby Liquid Control Subsystem B Inoperable.Caused by Leakage Through Pipe Fitting on Pressure Gauge PI-1160B.Removed Subject Gauge, Cleaned Pipe Threads & Reinstalled Gauge1998-08-26026 August 1998
- on 980727,declared Standby Liquid Control Subsystem B Inoperable.Caused by Leakage Through Pipe Fitting on Pressure Gauge PI-1160B.Removed Subject Gauge, Cleaned Pipe Threads & Reinstalled Gauge
05000293/LER-1998-013, :on 980606,inconclusive Fire Barrier Test Data Occurred.Caused by Concerns About Adequacy of Original Basis for 3 H Rating.Encls Declared Inoperable & Fire Watch Posted1998-07-0303 July 1998
- on 980606,inconclusive Fire Barrier Test Data Occurred.Caused by Concerns About Adequacy of Original Basis for 3 H Rating.Encls Declared Inoperable & Fire Watch Posted
05000293/LER-1998-011, :on 961126,operator Discovered Two Shield Plugs Removed from Floor Directly Over Torus Compartment.Caused by Lack of Formal Program to Control sub-compartment Barriers. Developed Formal Program to Control Compartment Barriers1998-06-26026 June 1998
- on 961126,operator Discovered Two Shield Plugs Removed from Floor Directly Over Torus Compartment.Caused by Lack of Formal Program to Control sub-compartment Barriers. Developed Formal Program to Control Compartment Barriers
05000293/LER-1998-007, :on 980330,discovered Single Failure Vulnerability of RHR Sys When in SPC Mode.Caused by Inadequate Original Design.Standing Order Issued to Declare LPCI Sys Inoperable When RHR Sys Is in SPC Mode1998-04-29029 April 1998
- on 980330,discovered Single Failure Vulnerability of RHR Sys When in SPC Mode.Caused by Inadequate Original Design.Standing Order Issued to Declare LPCI Sys Inoperable When RHR Sys Is in SPC Mode
05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Cause Is Attributed to Significant Effect Meteorlogical Conditions Have on EDG Room Temp.Completed Engineering Evaluation1998-04-17017 April 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Cause Is Attributed to Significant Effect Meteorlogical Conditions Have on EDG Room Temp.Completed Engineering Evaluation
05000293/LER-1997-004, :on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept1998-04-14014 April 1998
- on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept
05000293/LER-1998-003, :on 980220,discovered That RBCCW & Tbccw Heat Exchanger Supports Outside Design Basis Seismic Requirements.Caused by Calculation Error.Reviewed Similar Calculations & Counseled Individuals Associated W/Errors1998-03-23023 March 1998
- on 980220,discovered That RBCCW & Tbccw Heat Exchanger Supports Outside Design Basis Seismic Requirements.Caused by Calculation Error.Reviewed Similar Calculations & Counseled Individuals Associated W/Errors
05000293/LER-1998-002, :on 980205,EDG Room Air Temperature Went Below Design Basis.Caused by Unawareness of Significant Effect Wind Direction Has on EDG Room Temp.Engineering Evaluation (Ee 97-066 R-1) Was Completed & Approved1998-03-0909 March 1998
- on 980205,EDG Room Air Temperature Went Below Design Basis.Caused by Unawareness of Significant Effect Wind Direction Has on EDG Room Temp.Engineering Evaluation (Ee 97-066 R-1) Was Completed & Approved
05000293/LER-1997-026, :on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly1998-01-0505 January 1998
- on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly
05000293/LER-1997-025, :on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B1997-12-23023 December 1997
- on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B
05000293/LER-1997-021, :on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F1997-12-0404 December 1997
- on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F
05000293/LER-1997-020, :on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.51997-12-0404 December 1997
- on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.5
05000293/LER-1997-019, :on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures1997-12-0404 December 1997
- on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures
05000293/LER-1997-015, :on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc1997-12-0303 December 1997
- on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc
05000293/LER-1997-023, :on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door1997-12-0101 December 1997
- on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door
05000293/LER-1997-014, :on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period)1997-09-24024 September 1997
- on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period)
05000293/LER-1997-012, :on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated1997-08-29029 August 1997
- on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated
05000293/LER-1997-003, :on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested1997-07-18018 July 1997
- on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested
05000293/LER-1997-010, :on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door1997-05-20020 May 1997
- on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door
05000293/LER-1997-005, :on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error1997-05-15015 May 1997
- on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error
05000293/LER-1997-007, :on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers1997-05-0101 May 1997
- on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers
05000293/LER-1997-008, :on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel1997-04-24024 April 1997
- on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel
05000293/LER-1997-006, :on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified1997-04-22022 April 1997
- on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified
05000293/LER-1997-004, :on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately1997-04-0707 April 1997
- on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately
05000293/LER-1997-002, :on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete1997-03-10010 March 1997
- on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete
05000293/LER-1997-001, :on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised1997-02-14014 February 1997
- on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised
ML20138Q5491997-02-0707 February 1997 LER 97-S02-00:on 970110,security Svcs Supervisor Received Improperly Mailed Safeguards Info.Caused by Personnel Error. Security Force Put on Heightened Awareness & Protected Area Patrol Frequency Increased 1999-09-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000293/LER-1999-010-02, :on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With1999-10-18018 October 1999
- on 990918,reactor Startup Was in Progress. Caused by Communications Breakdown That Resulted in Operations Personnel Failing to Complete Actions in IAW Procedures.Power Ascension Was Secured.With
05000293/LER-1999-009-02, :on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With1999-10-13013 October 1999
- on 990913,manual Scram at 27 Percent Power, Occurred.Caused by Degrading Main Condenser Vacuum. Inspection of Instrument Sensing Lines to E-306B Level Transmitters Was Performed.With
ML20217E3021999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pilgrim Nuclear Station.With ML20216G5991999-09-24024 September 1999 Corrected Safety Evaluation Supporting Amend 182 to License DPR-35,consisting of Corrected Page 1 ML20212C2921999-09-16016 September 1999 SER Accepting Licensee Request for Relief from ASME Code Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Pilgrim Nuclear Power Station ML20216F3511999-09-0808 September 1999 ISI Summary Rept for Refuel Outage 12 at Pnps 05000293/LER-1999-008-02, :on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With1999-09-0707 September 1999
- on 990805,automatic Scram Occurred While at 100% Power Due to Automatic Turbine Trip.Caused by Malfunction of Moisture Separator Drain Tank a Drain Valve Controller.Level Controllers Replaced.With
ML20216E6881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pilgrim Nuclear Power Station.With 05000293/LER-1999-007-02, :on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With1999-08-13013 August 1999
- on 990716,discovered That Bus B6 Voltage Restoration Was Not Consistent with Safety Analysis Assumptions.Caused by Personnel Error During Development of Design Change.Will Evaluate Need for Mod.With
05000293/LER-1999-006-02, :on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With1999-08-0404 August 1999
- on 990705,both EDGs Were Inoperable.Caused by Ambient Air Temp Exceeding 88 Degrees Fahrenheit.Temporary Mods Tm 99-41 & Tm 99-42,implemented for EDG a Were Completed on 990706.With
ML20210R3401999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Pilgrim Nuclear Power Station.With ML20209G3851999-07-15015 July 1999 Safety Evaluation Supporting Amend 182 to License DPR-35 05000293/LER-1999-005, :on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With1999-07-0808 July 1999
- on 990608,partial Actuation of Rhr/Lpci Circuitry During Surveillance Test Was Noted.Caused by Personnel Error.Revised Procedure.With
ML20209C4731999-07-0707 July 1999 Addendum to SE on Proposed Transfer of Operating License & Matls License from Boston Edison Co to Entergy Nuclear Generation Co ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209E6191999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Pilgrim Nuclear Power Station.With ML20196H2451999-06-29029 June 1999 SER Denying Licensee Proposed Alternative in Relief Request PRR-13,rev 2.Staff Determined That Proposed Alternative Provides Insufficient Info to Determine Adequacy of Scope of Implementation ML20209A8901999-06-28028 June 1999 SER Accepting Licensee Proposed Alternative to Use Code Case N-573 for Remainder of 10-year Interval Pursuant to 10CFR50.55a(a)(3)(i) 05000293/LER-1999-004, :on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With1999-06-28028 June 1999
- on 990529,setpoint of Target Rock Relief Valves Were Found Out of Tolerance During Testing.Caused by Setpoint Drift.Replaced Pilot Assemblies with Certified Spare Pilot Assemblies.With
ML20209B9861999-06-23023 June 1999 Rev 13A to Pilgrim Nuclear Power Station COLR for Cycle 13 ML20217N9061999-06-21021 June 1999 Rept of Changes,Tests & Experiments for Period of 970422-990621 05000293/LER-1999-003, :on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With1999-06-15015 June 1999
- on 990516,discovered That LLRT Results Exceeded Allowable TS Leakage Rates.Cause Indeterminate. Affected Valves Were Disassembled & Inspected & Damaged or Worn Parts Were Reworked or Replaced.With
ML20195K3431999-06-15015 June 1999 Safety Evaluation Granting Licensee Request to Use Guidance of GL 90-05 to Repair Flaws in ASME Class 3 Salt Svc Water System Piping for Plant 05000293/LER-1999-002, :on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With1999-06-0303 June 1999
- on 990504,HPCI & RCIC Sys Surveillance Testing Outside Design Bases,Was Identified.Caused by Incorrect Ts. Proposed License Amend to Change TS Surveillance Testing Requirements,Submitted on 990511.With
ML20195G8231999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Pnps.With ML20207E7471999-05-27027 May 1999 Safety Evaluation Granting Request Re Reduction of IGSCC Insp of Category D Welds Due to Implementation of HWC to License DPR-35 ML20206M1971999-05-11011 May 1999 SER Accepting Request for Approval to Repair Flaws in ASME Code Class 3 Salt Svc Water Piping at Plant 05000293/LER-1999-001, :on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With1999-05-0606 May 1999
- on 990412,environ Enclosures of MCCs Outside Design Basis,Were Found.Caused by Failure to Translate Design Function of Pressure Relieving Devices.Removed Obstructions of Pressure Relieving Devices.With
ML20206J6611999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Pilgrim Nuclear Power Station.With ML20205L0221999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Pilgrim Nuclear Power Station.With ML20207J5471999-03-0909 March 1999 Training Simulator,1999 4-Yr Certification Rept ML20207F9401999-03-0101 March 1999 Long Term Program Semi-Annual Rept for Pilgrim Nuclear Power Station ML20207H5451999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Pilgrim Nuclear Power Station.With 05000293/LER-1998-029, :on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With1999-02-0101 February 1999
- on 981231,discovered That Intake Structure Indoor Air Temp Was Less than Winter Design Temp,Per Ufsar. Caused by Lack of Info & Administrative Controls.Will Repair Ventilation Sys & Will Revise Procedures.With
05000293/LER-1998-028, :on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With1999-01-28028 January 1999
- on 981230,CR High Efficiency Air Filtration Sys Relative Humidity Switches Were Inoperable.Caused by Gradual Degradation of Nylon Filaments.Modified Sys Control Circuitry.With
ML20206Q2741998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Pilgrim Nuclear Power Station.With ML20196E2151998-12-31031 December 1998 1998 Annual Rept for Boston Edison & Securities & Exchange Commission Form 10-K Rept.With 05000293/LER-1998-026, :on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with1998-12-23023 December 1998
- on 981202,HPCI Sys Declared Inoperable.Caused by Failed Power Inverter.Failed Inverter Replaced. with
05000293/LER-1998-007, :on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With1998-12-22022 December 1998
- on 980330,single Failure Vulnerability of RHR Sys When in Suppression Pool Cooling Mode Was Noted.Caused by Inadequate Original Design.Problem Rept Pr 98.9159 Was Written to Document Concern.With
ML20198H5671998-12-21021 December 1998 Safety Evaluation Supporting Amend 180 to License DPR-35 05000293/LER-1998-004, :on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation1998-12-18018 December 1998
- on 980321,EDG Room Air Temp Was Below Design Basis.Caused by Significant Effect of Meteorogical Conditions.Completed Engineering Evaluation
05000293/LER-1998-025, :on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With1998-12-18018 December 1998
- on 981118,setpoint of Target Rock Relief Valve Was Found out-of-tolerance During Testing.Caused by Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel.With
05000293/LER-1997-017, :on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With1998-12-18018 December 1998
- on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With
05000293/LER-1998-018, :on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With1998-12-18018 December 1998
- on 980722,EDGs Were Declared Inoperable When Ambient Air Temp Exceeded 88 F.Caused by Inadequate EDG Cooling & Bldg Ventilation Design.Will Develop EDG Cooling & EDG Bldg Ventilation Modifications.With
ML20198A2391998-12-11011 December 1998 Safety Evaluation Supporting Amend 179 to License DPR-35 ML20197J3591998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Pilgrim Nuclear Power Station.With 05000293/LER-1998-024, :on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans1998-11-13013 November 1998
- on 981015,determined That CR High Efficiency Aire Filtration Sys (Crheafs) Found Outside Design Basis Due to Installation of Duct Tape on Trains a & B Crheafs Supply Fans.Installed Mechanical Seals on Crheafs Supply Fans
ML20195B9161998-11-10010 November 1998 Safety Evaluation Supporting Amend 178 to License DPR-35 05000293/LER-1998-023, :on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With1998-11-0404 November 1998
- on 981005,incorrect Wiring Mods Affected RBCCW Train B Alternate Shutdown Panel.Caused by Error Made During Preparation of Electrical Connection Drawing to Implement Plant Design.Blown Fuse Replaced.With
ML20195C9951998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Pilgrim Nuclear Power Station.With 1999-09-08
[Table view] |
text
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i 10 CFR 20.2201 4
- ,e so.um an.an Pilgrim Nuclear Power Staten Rocky Hill Rosd Plymouth, Massachusetts 02360 February 14, 1997 BECo Ltr. #2.97,018 j
E. T. Boulette, PhD Senior Vice President - Nuclear l
U.S. Nuclear Regulatory Commission Attn: Document Control Desk i
i Washington, D.C. 20555 1
).
Docket No. 50-293 License No. DPR-35 The enclosed Licensee Event Report (LER) 97-001-00, "Very Small Quantity of Unaccountable j
Special Nuclear Material,"is submitted in accordance with 10 CFR Part 20.2201.
This report contains no commitments.
Please do not hesitate to contact me if there are any questions regarding this report.
1 i
T, j
. T. Boulette, PhD.
DWE/dmc/9700100 cc:
Mr. Hubert J. Miller Regional Administrator, Region I i
. U.S. Nuclear Regulatory Commission i
475 Allendale Road l
King of Prussia, PA 19406 I
Sr. NRC Resident inspector - Pilgrim Station i
Standard BECo LER Distribution l
a I
9702260176 970214 n
C PDR ADOCK 05000293 S
4 PDR i
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NRC Form 386 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB No. 31A194
[
4 (4-e5)-
EXPIRES waties t
[
i
- - LICENSEE EVENT REPORT (LER)
ES M ATE SURDEN PER RESPONSE TO COMPLY WITH THIS i
INFORMATION COLLECTION REQUEST: 50.0 HRS. REPORTED
'3 j
s LESSONS LEARNED ARE INCORPORATED INTO THE i
(See reverse for number of UCENSING PROCESS AND FED BACK TO INDUSTRY.
digits / characters for each block)
FORWARD COhadENTS REGARDING BURDEN ESTIMATE TO j
THE INFORMATION AND RECORDS MANAGEENT BRANCH (T-6 F33),
U.S.
NUCLEAR REGULATORY COhASSSION, f
i WASHINGTON, DC 20565-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150 0104) OFFICE OF MANAGEMNT l
AND SUDGET, WASHINGTON, DC 20503.
FACSJTY NAME (1)
DOCKET NUMBER (2)
PAGE(3).
f PILGRIM NUCLEAR POWER STATION
' 05000-293 Tm.E is)
Vzry Small Quantity of Unaccountable Special Nuclear Material l
[
EVENT DATE (5)
LER NUMSER (S)
REPORT DATE m oTHER FACIUTIES INVOLVED (B)
MONTH DAY
' YEAR
~ YEAR' R
MONTH DAY YEAR N/A 1^
FACluTV NAME DOCKET NUMBER j
01 20 97 97 001 00 02 14 97.
N/A OMM i
OPERATING TIGS REPORT IS SUBMITTED PURSUANT TO TDE REQUWtEMENTS OF 1S CFR: (Check one or more) (11) j MODE 19)
N x
20.2201 (b) 20.2203(sM2)(v) 50.73(a)(2MI) 50.73(aM2)(vHi)
{
POWER 22.2203(aM1) 20.2203(a)(3MI) 50.73(a)(2Mii) 50.73(aM2Mx) f.'
LEVEL (10) 97 20.2203(aM2MI) 20.m M3Mii) 50.73(aM2)(Ni) 73.71 l
e 20.2203 tam 2MN) 20.2203(aM4) 50.73(aM2Miv) oTHER l
l 20.2205aM2 MIN) 50.36(c)(1) 50.73(aM2)(v)
Specify in Abelrect below i
20.2203(sM2Xiv) 50.36(cM2) 50.73(a)(2Mvti) or in NRC Form 3sSA LICENSEE CONTACT FOR THIS LER (12)
.[
NAME TELEPHONE NUMBER (include Area Code)
I (508) 830-8160 l
Douglas W. Ellis - Regulatory Affairs Principal Engineer COMPLETE ODE LINE FOR EACH COMPOfENT FAILURE DESCRSED pl THIS REPORT (13)
REPORTA8LE TO REPO9 TABLE TO I
CAUSE
SYSTEM COhPONENT MANUFACTURER NPRDS
CAUSE
SYSTEM COhPONENT MANUFACTURER N8RDS l
l i
SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH lDW YEAR
{
YES X
NO SUBMISSION l
(if yes, compiste EXPECTED SUBh4SSION DATE)
DATE(15) l' ABSTRACT (umn to 1400 spaces Le., appr_
- 15 n.-_
.- _ typewenienlines)(16)
On JInuary 20,1997, the NRC Operations Center was notified that a very small quantity of special nuclear
+
mitIrlal (SNM) contained in sealed devices could not be accounted for. The discovery was the result of l,
reconciling a 1996 baseline inventory of portable devices containing SNM.
i L
Tha most probable cause was less than effective methods for control and accounting of devices containing less i
thin one gram of SNM in the 1975 - 1987 time frame. The previous (1987) baseline inventory of portable d: vices containing SNM relied on a review of documentation for items located in the spent fuel pool or installed '
L in tha reactor, and piece counts of portable devices located in other plant areas. The method used for the 1996 bis line inventory was a piece part count of portable devices containing SNM including the devices in the spent t
full pool.
i Corrective actions taken in 1987 included revision of the procedure goveming the control and accounting of SNM to include devices containing less than one gram of SNM. Corrective actions taken in 1996 included rsvision of the procedure govemirig the control and accounting of SNM including the transfer of SNM, revision of j
mIintenance procedures that involve SNM, training on SNM, and the establishment of a new baseline inventory i-of portable devices containing SNM.
I Tha devices containing the SNM that could not be accounted for were most probably shipped to a licensed disposal facility and pose or posed no threat to national defense or public health and safety.
. NRC FORM 308 (45) m.,
m
_, ~
NRC Form.3(4A.
U.S. NUCLEAR REOULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
SEoUENTIAL REVISloN YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000-293 2 of 7 97 001 00 TEXT (if more space is required, use additional copies of NRC Form 366A) (17)
BACKGROUND Special nuclear material (SNM) is defined in 10 CFR 70.4 as, "(1) plutonium, uranium 233, uranium enriched in th2 isotope 233 or in the isotope 235, and any other material which the Commission, pursuant to the provisions of section 51 of the act, determines to be special nuclear material, but does not include source material; or (2) cny material artificially enriched by any of the foregoing but does not include source material..."
At Pilgrim Station, the isotope uranium 235 (U-235) is contained in reactor fuel (fuel pins) and in sealed devices utiliz:d for the detection of neutrons. The neutron monitoring system source range monitors (SRMs),
int:rmediate range monitors (IRMs), and local power range monitors (LPRMs) utilize sealed detectors containing U-235. The circuitry associated with the SRMs, IRMs, and LPRMs provide trip functions to the reactor manual control system and reactor protection system during reactor startup, reactor power operation, reactor shut down, cnd refueling operations. Fuel loading chambers (FLCs) also contain sealed U-235 and function to detect n utrons during reactor fuelloading operations. The traversing incore probes (TIPS) also contain sealed U-235 and function to detect neutrons, and are used for calibration of the LPRMs. Installed or spent reactor fuel, instilled devices (SRMs, IRMs, LPRMs, and TIPS), and devices stored in the spent fuel pool are considered iniccessible.
In e I:tter submitted to the NRC on July 21,1995, Boston Edison Company replied to a notice of violation (VIO 95-09-03) pertaining to portable devices containing SNM. In summary, six IRMs, one SRM, and one FLC were discovered misplaced in the March - April 1995 time frame, coinciding with the beginning of the 1995 refueling outage (RFO-10). The misplaced SRM, IRMs, and FLC were subsequently located in the controlled, contzminated material stream. The letter contair.ed several corrective actions including a commitment to conduct a physical inventory of portable devices containing SNM located in the spent fuel pool in order to est:blish a new SNM inventory baseline. The nevi baseline would supersede the previous baseline of SNM cst blished in 1987.
Tha definition of physical inventory is provided in 10 CFR 70.51 subpart (a)(8): "Physicalinventory means d:t:rmination on a measured basis of the quantity of special nuclear material on hand at any given time. The m ;thods of physical inventory and associated measurements will vary depending on the material to be inv:ntoried and the process involved."
Th2 definition of material balance is provided in 10 CFR 70.51 subpart (a)(6): " Material balance means a ditirmination of material unaccounted for (MUF) by subtracting ending inventory (EI) plus removals (R) from beginning inventory (BI) plus additions to inventory (A). Mathematically, MUF = BI + A - El-R."
NRC Form.386A U.S. NUCLEAR RE2ULATORY COMMISSION W85)
I i
LICENSEE EVENT REPORT (LER)
}
TEXT CONTINUATION FACRJTY NAME (1) oOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
SEQUENTIAL REVISloN j
YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05030-293 3 of 7 l
97
@1 TEXT (if more space is required, use addetsonal copies of NRc Form 386A)(17) b Th3 physical inventory of portable devices containing SNM in the spent fuel pool was completed on Junn 30,1996. The method used for the inventory was visual verification (piece count) and segregation from l
i othsr materials into one of four discrete storage locations. Once identified as an item or device containing SNM, l
th3 item was added to inventory and moved under the controls of procedure 4.0, "SNM Inventory and Transfer i
Control," and material balance transfer forms. The completed material balance transfer forms provided the formil documentation for each item included in the inventory. After the inventory, a reconciliation was made of tha portable devices containing SNM inventoried in 1996 to the SNM inventory baseline established in 1987 and subsequent movements of devices containing SNM prior to the 1996 physicalinventory. The 1987 baseline invIntory was reconfirmed as part of the reconciliation. The results of the physicalinventory of SNM and reconciliation were documented in a memorandum dated December 30,1996. The memorandum (OSD 96-135) concluded that the inventory could not account for 18 devices (14 SRMs/lRMs and 4 TIPS). SRMs and IRMs are
]
id:ntical in appearance and, therefore, no distinction between an SRM and an IRM was made for purposes of J
j tha 1996 inventory.
Th3 chemical and physical forms of SRMs and IRMs are as follows. SRMs and IRMs are similar. Each contains U-235 enriched to greater than 90 percent, sealed in a circular fission chamber having a lustrous sheen, dark j
brown to black in color, approximately two inches in length and approximately three-eighths inch in diameter.
Tha sealed fission chamber is integral to a metallic, sheathed cable having a woven appearance and gray in color. Each sealed SRM fission chamber typically contains approximately 0.003 grams of U-235. Each sealed i
IRM fission chambar typically contains approximately 0.001 grams of U-235. The actuallength of the l
SRMs/lRMs that could not be accounted for would vary, depending upon the location of severance from the cabis. - Typically, the cable is severed approximately three to five inches from the end containing the fission chimber.
j Th3 chemical and physical forms of a TIP are as follows: each typically contains approximately 0.001 grams of U-235 enriched to greater than 90 percent, sealed in a circular fission chamber having a dull gray to dark app:arance, approximately two and one-half inches in length anci approximately three-eighths inch in diameter.
Ths sealed fission chamber is integral to an unsheathed, metallic cable. The actual length of the TIPS that could not be accounted for would a'so vary,' depending upon the location of severance from the cable. Typically, the cabin is severed approximatcly <.hree to five inches from the end containing the fission chamber, Problem Report 97.0027 documented the devices containing the SNM that could not be accounted for collnctively contained 0.056 grams U-235, and identified that an evaluation was necessary for applicability of rcporting. This total quantity was conservatively determined assuming each of the SRMs/lRMs and TIPS contlined an amount of U-235 equal to that contained in one SRM detector. The problem report was written on J:nuary 8,1997, and subsequently assigned for reportabnity evaluation.
EVENT DESCRIPTION
On January 17,1997, it was determined that the total activity contained in the devices containing the SNM that could not be accounted for was approximately 0.1211 microcuries. This total activity exceeded 10 times the activity specified by 10 CFR 20.2201(a)(1)(ii) and identified in 10 CFR 20 Appendix C as 0.001 microcuries (for U-235). Problem Report 97.9047 was written on January 17,1997, to document the determination.
~
NRc Forrr>366A.
U.S. NUCLEAR REZUt ATORY COMMISSION i
(4-95)
LICENSEE EVENT REPORT (LER) i TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
SEQUENTIAL REVISloN YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000-293 4 of 7 97 001 00 TEXT (if more space is required. use addmonal copies of NRC Form 366A)(17) l A m:eting was held on January 20,1997, to assess the notification requirements for the loss, theft, or misplacement of the SNM that could not be accounted for. The meeting was attended by applicable personnel including personnel from the operations, radiation protection, and regulatory affairs departments. At cpproximately 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br />, the assessment concluded that notifications were applicable in accordance with 10 CFR parts 20.2201(a)(1)(ii) and 70.52(a). Consequently, the on-shift NWE was contacted and, in turn, the NRC Operations Center was notified in accordance with the one hour notification requiremen*. of 10 CFR 70.52(a) at 1817 hours0.021 days <br />0.505 hours <br />0.003 weeks <br />6.913685e-4 months <br /> on January 20,1997; the notification included the 30 day notificatirm requirement of 10 CFR 20.2201(a)(1)(ii).
The January 20,1997, conclusion that NRC notification was required occurred while at approximately 97 percent reactor power with the reactor mode selector switch in the RUN position. The reactor vessel pressure wrs approximately 1031 psig with the reactor vessel water at saturation temperature.
CAUSE
l Th3 most probable cause was less than effective methods used for control and accounting of devices containing 1:ss than one gram of SNM in the 1975 - 1987 time frame. The cause(s) appears to be similar to those d: scribed in NRC Information Notice 88-34, " Nuclear Material Control and Accountability of Non-Fuel Special Nuclear Material at Power Reactors."
In October 1974, an NRC inspection of the program for control of special nuclear material was conducted. The insp:ction report (74-16) for the inspection documented findings pertaining to procedure 4.0, "SNM Inventory tnd Transfer Control." As a result of the findings, procedure 4.0 was revised (to rev. 2) in January 1975. The control and accounting of portable devices containing less than one gram of SNM - SRMs, IRMs, LPPMs, and TIPS -- was discontinued (that is, deleted) as part of the revision. Fuelloading chambers contain more than one gram of SNM and were not affected by the procedure revision. The cause or reason for the deletion of the SRMs, IRMs, LPRMs, and TIPS from the controls of procedure 4.0 could not be determined with certainty. The procedure change form accompanying the procedure revision (from rev.1 to rev. 2) did not indicate a reason for d:liting devices containing less than one gram of SNM from the controls of the procedure. Apparently, the r:Ison(s) is similar to the reasons or causes described in Information Notice 88-34 in that devices containing 1:ss than one gram of SNM were not tracked or accounted for.
As e consequence of the revision of procedure 4.0 in 1975, devices containing less than one gram of SNM were n:ither controlled as SNM nor included in physical inventories of SNM in the 1975 to 1987 time frame.
M:reover, in the 1975 - 1985 time frame, general cleanups of the spent fuel pool were conducted. The purpose of the cleanups was to remove and ship radioactive waste materials that had acer 1 the spent fuel pool.
Tha spent fuel pool contained numerous irradiated or contaminated SRMs, IRMs, and TIPS. None of tha SRMs, IRMs, LPRMs, and TIPS were tracked or identified as SNM because thw.: emces contained less th2n one gram of special nuclear material (U-235). Radioactive materials were packaged, shipped, and dilivered for disposal at the licensed Bamwell, South Carolina, facility in the 1975 - 1985 time frame. The portable devices containing less than one gram of SNM that could not be accounted for were most likely included in the shipments identified as miscellaneous shipments, not shipments containing SNM.
'i M85)
U.S. NUCLEAR RECULATORY COMMISSION LICENSEE EVENT REPORT (LER)
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TEXT CONTINUATION 5
FACIUTY NAME (4 DOCKET NUMaER (2)
LER NUMBER (S)
PAGE (3)
SEQUENTIAL REVIStoN p
YEAR NUMBER NUMBER
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PILGRIM NUCLEAR POWER STATION 05000-293 5 of 7 97 001 00 TEXT (if more space is required. use additional copies of NRc Form 306A)(17) l An NRC inspection of SNM controls and accounting was conducted in early February 1987 (inspection 87-06).
l Tha inspection resulted in a finding that procedure 4.0 (then rev. 9) did not provide for the effective control and accounting of items (devices) containing less than one gram of SNM. As a result of the finding, procedure 4.0 i
wIs revired (to rev.10) in March 1987 and a baseline inventory of portable devices containing SNM was ast"blished in 1987. The revision of procedure 4.0 included the addition of devices that contain less than one gram of SNM to the controls of procedure 4.0. In other words, devices containing less than one gram of SNM -
SRMs, IRMs, LPRMs, and TIPS - that had been deleted from the controls of procedure 4.0 when the procedure w:s revised in 1975, were re-added as items controlled by the procedure when the procedure was revised in
[
MIrch 1987.
t I'
Tha 1987 baseline inventory was based on review of SNM material balanc? transfer forms and SNM inventories, i
surches for and review of historical documentation that included receipt inspections of devices that contain j
SNM, radioactive shipments identified as containing SNM, and maintenance requests pertaining to devices contIining SNM. The method used for the 1987 baseline inventory was a piece count of portable devices -
containing SNM except for installed devices ~ or devices in the spent fuel pool. For the 1987 baseline inventory End subsequent semi-annual physical inventories of devices containing SNM, installed devices (SRMs, IRMs, LPRMs, and TIPS) or devices stored in the spent fuel pool were considered inaccessible. Subsequent semi-1 I
annual physical inventories of SNM, including portable devices containing SNM located in the spent fuel pool, l
conducted after the 1987 baseline inventory and prior to the 1996 baseline inventory were similar in that each j.
invsntory was based primarily on review of documentation that included material balance transfer forms and r: conciliation. The method used for the inventories of devices containing SNM prior to the 1996 baseline.
3 inventory, although including a reconciliation, did not include a visual verification (piece count) of installed j
dsvices (SRMs, IRMs, LPRMs, and TIPS) or devices in the spent fuel pool because the devices were considered t'
intecessible. Based on the results of the 1996 baseline inventory, the control and inventory practices for.
port:ble devices containing SNM are adequate for tracking and accounting the addition or deletion of materials from the spent fuel pool.
}
Thrrefore, the most probable cause for the devices containing the SNM that could not be accounted for was I:ss than effective methods used for control and accounting of portable devices containing less than one gram i
{
of SNM in the
l i
t
CORRECTIVE ACTION
i i'
Tha corrective actions taken and planned for the control of devices containing SNM was contained in the July 21,19E5, reply to the notice of violation. In summary, the corrective actions taken included the following:
I The baseline inventory of portable devices containing SNM located in the spent fuel pool was completed on Juna 30,1996. The inventory established a new baseline for portable devices containing SNM located in the spent fuel pool. After the 1996 baseline inventory, SRMs, IRMs, and TIPS in the spent fuel pool were included in a shipment made to the Bamwell, South Carolina, licensed disposal facility. The disposition of the devices j
j containing the SNM that could not be accounted for was that the devices were most probably included in one or j
mora shipments made to the licensed Bamwell, South Carolina, disposal facility in the 1975 - 1985 time frame, and most probably identified as miscellaneous waste.
'l n
a e--
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m-,%-,
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-+-= -
m --U.S. NUCLEAR RE1ULATORY COMMISSION (t95)
LICENSEE EVENT REPORT (LER) l TEXT CONTINUATION FACILITY NAME (1) l DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
SEQUENTIAL REVIStoN YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000-293 6 of 7 I
97 001 00 l
TEXT (if more space is required, use additional copies of NRC Form 366A)(17)
Procedure 4.0, "SNM Inventory and Transfer Control," was revised (to rev.18). The focus of the revision was to strengthen the procedural controls goveming the control and accounting of SNM.
M intenance procedures were similarly revised to strengthen the controls goveming the use or transfer of d; vices containing SNM. The procedures included:
Procedure 3.M.2-5.1.2, "lRM/SRM Drive Assemblies Removal and Reinstallation for Dry Tube Replacement." The procedure was revised (to rev. 7)in August 1995.
Procedure 3.M.2-5.6.12, "TIP Detector Removal and Replacement." The procedure was revised (to rev. 6) in August 1995.
Procedure 3.M.2-5.7, " Installation and Checkout of the Fuel Loading Chambers." The procedure was revised (to rev. 6) in August 1995.
Procedure 3.M.2-5.13, "lRM and SRM Detector Changeout." The procedure was revised (to rev.10) in August 1995.
Procedure 3.M.2-5.14, "SRM/lRM and TIP Detector Testing." The procedure was revised (to rev. 7) in August 1995.
Tr-ining on SNM and devices containing SNM was conducted. The training was included as part of general cmployee training. Training of greater focus was also conducted for personnel who may work with devices containing SNM.
SAFETY CONSEQUENCES
The devices containing the SNM that could not be accounted for pose or posed no threat to national defense or public health and safety.
Th:) devices containing the SNM that could not be accounted for contained a total of 0.056 grams U-235. The qu:ntity is less than the quantity defined in the 10 CFR 70.4 definition of special nuclear material of low strategic significance.I
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!U.S. NUCLEAR RECULATORY COMMISSION
(&es)",,.
LICENSEE EVENT REPORT (LER)
}_
TEXT CONTINUATION 1
FACKJTY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (4)
PAGE (3)
SEQUENTIAL REVISION 1-YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATloN 05000-293 I
7 of 7 97 001 00
" TEXT (if more space is requred. use adetonal copes of NRc Form 366A) (17)
Th3 total activity in the devices containing the SNM that could not be accounted for is approximately 0.1211 microcuries. This activity, although greater than 10 times the activity specified in 10 CFR 20(a)(1)(ii) and id::ntified in Appendix C for U-235 (0.001 microcuries), is less than 1000 times the activity for U-235 specified by 10 CFR 20.2201(a)(1)(i). The SNM that could not be accounted for was contained in sealed devices (SRMs, IRMs, TIPS). These sealed devices were most probably irradiated and/or contaminated. Contaminated or not, thtse devices were and are handled as devices that contain radioactive material. Radiation detection and monitoring is regulated and controlled and is accomplished through several means including radiation surveys s
and survey instrumentation, radiation work permits, postings and/or barriers, personnel dosimetry, friskers, area
[
r dirtion monitors, and portal monitors. It is reasonable to conclude the devices containing the SNM that could not be accounted for were maintained in the controlled waste process stream. Therefore, it is reasonable to conclude that no unregulated exposures occurred to persons in restricted areas as a result of exposure to the
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devices containing the SNM that could not be accounted for. The device's containing the SNM that could not be accounted for were most probably included in radioactive materials shipments made to the licensed Bamwell, South Carolina, disposal facility. The packaging, transport, and disposal of radioactive materials is regulated and controlled. Therefore, it is reasonable to conclude that no unregulated exposures occurred to persons in unrzstricted areas as a result of the devices containing the SNM that could not be accounted for. Based on the smtll amount of SNM contained in the devices that could not be accounted for, and that the devices were most likIly included in shipments to a licensed disposal facility in the 1975 - 1985 time frame, there are no actions 3
planned to recover the devices that could not be accounted for.
This report is submitted in accordance with 10 CFR 20.2201(b) becausa the activity of the devices containing ths SNM that could not be accounted for was greater than 10 times the activity identified by 10 CFR 20 j
Appendix C (0.001 microcuries for U-235).
j SIMILARITY TO PREVIOUS EVENTS A rsview of Pilgrim Station LERs submitted since January 1984 was conducted. The review focused on reports involving special nuclear material (SNM). The review identified no LERs involving the loss, theft, or misplacement of SNM. A similar review of LERs submitted since 1972 was conducted and the review identified no LERs involving the loss, theft, or misplacement of SNM.
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t ENERGY INDUSTRY IDENTIFICATION SYSTEM (Ells) CODES e
l Tha Ells cooes for th;s report are as follows:
COMPONENTS CODES 4
Det:ctor (SRMs, IRMs, LPRMs, TIPS)
DET j
Monitor (SRMs, IRMs, LPRMs, TIPS)
MON SYSTEMS 3
Incore monitoring system IG
!i e
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._y_
r y
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05000293/LER-1997-001, :on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised |
- on 970120,very Small Quantity of Unaccountable Special Nuclear Material Was Identifed Due to Less than Effective Methods for Control & Accounting of Devices. Procedures Revised
| | 05000293/LER-1997-002, :on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete |
- on 970206,SJAE Sampling Was Not Performed in Accordance with Ts.Caused by Improper Conclusion Contained in Response to Request for Licensing Interpretation in 1990. Validation Project Is Now Complete
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | 05000293/LER-1997-003, :on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested |
- on 970215,manual Scram Occurred Due to Increasing Rwl During Power Reduction for Refueling Outage. FW Regulating Valves FV-642A & FV-642B & Startup FW Regulating Valve FV-643 Tested
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | 05000293/LER-1997-004, :on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept |
- on 970307,loss of Preferred off-site Power & Oil Spill Occurred.Caused by Degraded Winding Condition or Static Electrification of Main Transformer.Replaced Main Transformer & Updated Fire Hazards Analysis Rept
| | 05000293/LER-1997-004, :on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately |
- on 970307,automatic Start of B Train EDG & Actuation of Secondary Containment Isolation Control Sys Occurred.Caused by Electrical Fault in Main Transformer. Initial Efforts for Oil Containment Initiated Immediately
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000293/LER-1997-005, :on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error |
- on 970308,declared Turbine Bldg Effluent Monitoring Instrumentation Inoperable.Caused by Failed Power Supply to RT-1001-610.Will Perform Initial Rept Screening & Counseled Personnel on Human Error
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-1997-006, :on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified |
- on 970321,inadvertent Group Three Isolation Occurred While Troubleshooting 125 Volt Dc Ground on Battery a as Result of Relay Race When Circuit Breaker D4-8 Was Cycled.Electrical Print Reviewed & Verified
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) | 05000293/LER-1997-007, :on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers |
- on 970401,safeguard Buses Were de-energized Due to Severe Storm.Replacement of Microprocessor Control Units Installed in Voltage Regulating Transformers
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | 05000293/LER-1997-008, :on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel |
- on 970312,setpoint of Target Rock Relief Valve Pilot Assembly Was Out of Tolerance During Testing,Due to Setpoint Drift.Valve Was Disassembled,Inspected & Reworked by Target Rock Corp Personnel
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | 05000293/LER-1997-010, :on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door |
- on 970420,postulated Pipe Break Pressure Relieving Pathway Boundary Door Found Opened During Power Operation.Caused by Human Performance in That Door Was Not Closed After Maint Activity.Obtained Lock & Closed Door
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(iii) | 05000293/LER-1997-011-02, Forwards LER 97-011-02 Re SSW Sys Single Failure Vulnerability IAW 10CFR50.73.Commitments Made within Ltr, Submitted | Forwards LER 97-011-02 Re SSW Sys Single Failure Vulnerability IAW 10CFR50.73.Commitments Made within Ltr, Submitted | | 05000293/LER-1997-012, :on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated |
- on 970729,failure of Relay to Energize During Surveillance Test Occurred.Caused by Relay 10A-K10B Contacts 9-10 Not Closing.Relay Replaced & LCO Terminated
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-1997-012-01, Informs That New Date for Implementation of PNPS Procedure 3.M.3-30,contained in LER 97-012-01, Failure of Relay to Energize During Suveillance Test, Is 981101 | Informs That New Date for Implementation of PNPS Procedure 3.M.3-30,contained in LER 97-012-01, Failure of Relay to Energize During Suveillance Test, Is 981101 | | 05000293/LER-1997-013, Discusses Commitment Made in LER 97-013-00.Deferral of Target Completion Date to 980430 Made.Mod Will Not Be Completed Until Spring 1999 Refueling Outage 12 | Discusses Commitment Made in LER 97-013-00.Deferral of Target Completion Date to 980430 Made.Mod Will Not Be Completed Until Spring 1999 Refueling Outage 12 | | 05000293/LER-1997-014, :on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period) |
- on 970825,determined That Transmitters Had Not Been Calibr IAW Tss.Cause Indeterminate.Calibr Transmitters W/Satisfactory as-found Results Prior to Expiration of Suveillance Interval (24 Months Plus 25% Grace Period)
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000293/LER-1997-014-01, Forwards LER 97-014-01 Re Transmitters Not Calibr in Accordance W/Tech Specs,Per 10CFR50.73.Ltr Contains Listed Commitment | Forwards LER 97-014-01 Re Transmitters Not Calibr in Accordance W/Tech Specs,Per 10CFR50.73.Ltr Contains Listed Commitment | | 05000293/LER-1997-015, :on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc |
- on 971104,SSW Pumps Overload Settings Were Too Low for Single SSW Pump Operation W/Degraded Voltage.Cause Is Still Under Investigation.Entered 24 H Cold Shutdown LCO (A97-355) on 971104,to Remove SSW Pumps from Svc
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000293/LER-1997-017, :on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With |
- on 971104,past Operation with SW Temps Were Greater than Design.Caused by Licensing Basis Ambiguity. Issued SE & License Amend Request Was Submitted.With
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | 05000293/LER-1997-019, :on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures |
- on 971104,discovered That Closure of RBCCW Sys Valves Which Isolate non-essential Heat Loads Were Not Translated Into Procedure.Caused by Inadequate Design Control.Performed SE & Revised Procedures
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000293/LER-1997-020, :on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.5 |
- on 971104,RHR Operating Procedure Did Not Reflect Analysis.Caused by Inadequate Translation of Analysis Parameters to Operating Procedure Parameters. Revised Procedure 2.2.19.5
| | 05000293/LER-1997-021, :on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F |
- on 971104,EDG Ambient Air Temperature Was Noted.Caused by Ambiguity in Fsar.Conservative Operability Evaluation Has Been Completed to Show That Diesels Are Operable to 95 F
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000293/LER-1997-023, :on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door |
- on 971031,discovered That Both Radwaste Bldg Trucklock Doors Were Closed.Caused by Inadequate Control of Subcompartment Barriers.Opened & Tagged Rollup Steel Door
| | 05000293/LER-1997-025, :on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B |
- on 971123,required Shutdown Was Completed. Caused by Two Inoperable Msivs.Work Was Performed on All Eight MSIVs to Improve Design Margin Based on Degradation of Actuators in MSIVs AO-203-1C & -2B
| 10 CFR 50.73(a)(2)(1) | 05000293/LER-1997-026, :on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly |
- on 971206,automatic Scram Was Initiated.Caused by High Reactor Water Level During Power Ascension.Pilot Valve Clip Was Repositioned Inside Bailey Positioner & Valve Was Stroked Smoothly
| 10 CFR 50.73(a)(2)(iv), System Actuation |
|