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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000271/LER-1993-0121993-10-0707 October 1993 LER 93-012-00:on 930908,noted That Containment Air Valve & TIP Found to Have Seat Leakage Above That Permitted by Ts. Caused by Leakage Through Check Valve.C/As Will Be Reported in Suppl to LER.W/931007 Ltr 05000271/LER-1993-0101993-08-31031 August 1993 LER 93-010-00:on 930803,fire Protection Valve V76-420 Has Not Been Cycled Through Complete Cycle of Full Travel,Per TS 4.13.B.d.Caused by Human Error.Applicable Surveillance Procedure Revised to Include V76-420.W/930831 Ltr 05000271/LER-1993-0041993-08-19019 August 1993 LER 93-004-01:on 930225,discovered That Surveillance for Jet Pumps Not Performed During Single Loop Operations Due to Inadequate Plant Procedures.Procedures OP-4110 & OP-2428 revised.W/930819 Ltr 05000271/LER-1993-0051993-08-13013 August 1993 LER 93-005-01:on 930406,concluded Control Rod Scram Times Not in Compliance W/Ts Section 3.3.C.Caused by Faulty Scram Solenoid Pilot Valves.Solenoid Valves rebuilt.W/930813 Ltr 05000271/LER-1993-0091993-08-13013 August 1993 LER 93-009-00:on 930716,B Train of RHR Sys Declared Inoperable.Caused by Personnel Error Re Failure to Initiate Rev to Calibration Procedure OP 4347.Instrument re-calibrated & OP 4347 revised.W/930813 Ltr 05000271/LER-1990-0081990-06-29029 June 1990 LER 90-008-00:on 900529,identified That Cables Providing Power to post-accident Monitoring Instrument Loops Not Routed,Per Required Separation Criteria.Caused by Combination of Factors.Design Change prepared.W/900629 Ltr 05000271/LER-1987-003, :on 880412,personnel Found Functional Testing Not Been Tested in Accordance W/Tech Spec Requirements. Caused by Programmatic Tracking Program.Programmatic Tracking Sys Revised as Described in LER 87-031988-05-10010 May 1988
- on 880412,personnel Found Functional Testing Not Been Tested in Accordance W/Tech Spec Requirements. Caused by Programmatic Tracking Program.Programmatic Tracking Sys Revised as Described in LER 87-03
05000271/LER-1983-009, Followup LER 83-009/01T-0:on 830321,primary Containment Isolation Sys Isolation of Containment Ventilation Sys Occurred.Caused by Mods to Reactor Protection Sys Motor Generator.Fuel Handling Activities Suspended1983-04-0101 April 1983 Followup LER 83-009/01T-0:on 830321,primary Containment Isolation Sys Isolation of Containment Ventilation Sys Occurred.Caused by Mods to Reactor Protection Sys Motor Generator.Fuel Handling Activities Suspended 05000271/LER-1981-030, Updated LER 81-030/03L-1:cracks Found on Internal Surface of Valve Bodies & Seating Surfaces of Reactor Water Cleanup Valves Attributed to Surface Shrinking of Casting & Intergranular Stress Corrosion Cracking,Respectively1982-07-0101 July 1982 Updated LER 81-030/03L-1:cracks Found on Internal Surface of Valve Bodies & Seating Surfaces of Reactor Water Cleanup Valves Attributed to Surface Shrinking of Casting & Intergranular Stress Corrosion Cracking,Respectively 05000271/LER-1981-0261981-11-0303 November 1981 LER 81-026/03L-0:on 811005,during Weekly Review of Surveillance Test Data,Discovered That Max Monthly Interval for Functional Test of Atws/Rpt Sys Exceeded by 4 Days. Caused by Oversight in Scheduling ML20064H2211978-12-13013 December 1978 /03L-0 on 781113:during Weekly Surveillance Re Radiological Environ Prog,Air Pump Motor Was Found Inoper. Time Meter Indicated Pump Had Operated Only 0.4 Hours.Air Pump Replaced & New Weekly Air Sample Initiated ML20064E3281978-11-13013 November 1978 /03L-0 on 781014:during Surveillance Test of Main Steam Isolution Valves,V2-86C Closed in 2.6 Seconds Rather than 3-5 Seconds Req in Tech Spec 4.7.D.1.a.1.Caused by Closing Speed Control Valve Coming Loose from Actuator ML20064E3101978-11-13013 November 1978 /03L-0 on 781016:weekly Review of Completed Surveillance Test Following Plant Startup Noted That Monthly Hydrogen Detector Functional Test Was Not Performed Due to Personnel Error ML20064H2291978-08-10010 August 1978 /03L-1 on 780626:during Increase of Reactor Pwr, Noted That Critical Pwr Ratio in 4 Symmetrically Located Fuel Bundles Was Below Tech Spec Values.Caused by Pwr Increasing Xenon Transient ML20064H1681978-07-25025 July 1978 /03L-0 on 780629:during Steady State Oper Motor Control Ctr 893 Lost Voltage Because B Uninterruptible Pwr Supply (UP5) Tripped Due to Blown Inverter Leg Fuse.Failed Components Replaced & Operability Test Performed ML20064H2051978-07-24024 July 1978 /03L-0 on 780625:during Steady State Oper,Noted That Drywell Atmospheric Temp Recorder TR-1-149 Was Inoperable.Caused by Recorder Failure Due to Broken Cord on Chart Drive Mechanism ML20064H1741978-07-24024 July 1978 /03L-0 on 780626:during Reactor Pwr Increase Noted That Local Critical Pwr Ratio in 4 Symmetrically Located Fuel Bundles Was Lower than Tech Spec Levels.Caused by Pwr Increasing Xenon Transient ML20064H1321978-07-24024 July 1978 /03L-0 on 780612:during Steady State Oper,Noted That Drywell Atmospheric Temp Recorder TR-1-149 Was Inoperable.Recorder Failed Due to Failed Idler Assembly 05000271/LER-1976-005, Telecopy LER 76-005:on 760217,portion of Procedure Associated W/Securing Plant from Shutdown Cooling Mode Not Performed.Caused by Failure of Plant Personnel to Follow Appropriate Plant Procedure1976-02-18018 February 1976 Telecopy LER 76-005:on 760217,portion of Procedure Associated W/Securing Plant from Shutdown Cooling Mode Not Performed.Caused by Failure of Plant Personnel to Follow Appropriate Plant Procedure 05000271/LER-1975-003, Corrected LER 75-003:on 750204,core Spray Sys Pump Discharge Pressure Sensor PS-14-44A Actuated at 82 Psig.Caused by Setpoint Drift.Sensor replaced.W/750218 Ltr1975-02-14014 February 1975 Corrected LER 75-003:on 750204,core Spray Sys Pump Discharge Pressure Sensor PS-14-44A Actuated at 82 Psig.Caused by Setpoint Drift.Sensor replaced.W/750218 Ltr 1993-08-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8831999-10-21021 October 1999 Safety Evaluation Supporting Proposed Alternatives to Code Requirements Described in RR-V17 & RR-V18 ML20217G2041999-10-13013 October 1999 Safety Evaluation Supporting Amend 179 to License DPR-28 BVY-99-127, Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With ML20212C2551999-09-17017 September 1999 Safety Evaluation Supporting Amend 175 to License DPR-28 BVY-99-112, Monthly Operating Rept for Aug 1999 for Vermont Yankee.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Vermont Yankee.With BVY-99-109, Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 9908311999-08-19019 August 1999 Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 990831 BVY-99-102, Monthly Operating Rept for July 1999 for Vermont Yankee. with1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Vermont Yankee. with ML20209J0081999-07-14014 July 1999 Special Rept:On 990615,diesel Driven Fire Pump Failed to Achieve Rated Flow of 2500 Gallons Per Minute.Pump Was Inoperable for Greater than 7 Days.Corrective Maint Was Performed to Reset Pump Lift Setting BVY-99-090, Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With ML20196G5071999-06-23023 June 1999 Vynp Assessment of On-Site Disposal of Contaminated Soil by Land Spreading BVY-99-077, Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With BVY-99-068, Monthly Operating Rept for Apr 1999 for Vynp.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Vynp.With ML20206E8741999-04-29029 April 1999 SER Determined That Flaw Evaluation Meets Rules of ASME Code & Assumed Crack Growth Rate Adequate for Application ML20206D9301999-04-27027 April 1999 1999 Emergency Preparedness Exercise 990427 Exercise Manual (Plume Portion) ML20205S4211999-04-16016 April 1999 Non-proprietary Version of Revised Page 4-3 of HI-981932 Technical Rept for Vermont Yankee Spent Fuel Pool Storage Expansion ML20205K7581999-04-0707 April 1999 Safety Evaluation Supporting Alternative Proposal for Reexamination of Circumferential Welds with Detected Flaw Indications in Plant RPV BVY-99-046, Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With ML20205F6631999-03-0404 March 1999 Jet Pump Riser Weld Leakage Evaluation BVY-99-035, Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With ML20205P8241999-02-28028 February 1999 Rev 2 to Vermont Yankee Cycle 20 Colr ML20203H9881999-02-18018 February 1999 SER Accepting Alternative to 10CFR50.55a(g)(6)(ii)(A) Augmented Reactor Vessel Exam at Vermont Yankee Nuclear Power Station.Technical Ltr Rept Encl ML20203A6951999-02-0404 February 1999 Revised Rev 2,App B to Vermont Yankee Operational QA Manual (Voqam) ML20199K7151999-01-21021 January 1999 Corrected Safety Evaluation Supporting Amend 163 Issued to FOL DPR-28.Pages 2 & 3 Required Correction & Clarification ML20199K6991999-01-20020 January 1999 Safety Evaluation Concluding That Request to Use YAEC-1339, Yankee Atomic Electric Co Application of FIBWR2 Core Hydraulics Code to BWR Reload Analysis, at Vermont Yankee Acceptable ML20199L5951999-01-14014 January 1999 Safety Evaluation Accepting Licensee Proposed Alternative to Code Requirement,Described in Rev 2 to Pump Relief Request RR-P10 Pursuant to 10CFR50.55a(a)(3)(i) BVY-99-071, Corp 1998 Annual Rept. with1998-12-31031 December 1998 Corp 1998 Annual Rept. with BVY-99-001, Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station ML20198H5481998-12-23023 December 1998 Rev 2 to Vermont Operational QA Manual,Voqam ML20196H8641998-12-0101 December 1998 Cycle 19 Operating Rept BVY-98-163, Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With ML20195C4161998-11-0909 November 1998 SER Accepting Request That NRC Approve ASME Code Case N-560, Alternative Exam Requirement for Class 1,Category B-J Piping Welds BVY-98-154, Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With ML20155B6471998-10-26026 October 1998 Safety Evaluation Accepting Jet Pump Riser Insp Results & Flaw Evaluation,Conducted During 1998 Refueling Outage ML20154N0891998-10-16016 October 1998 Rev 1 to Vermont Operational QA Program Manual (Voqam) ML20154B6951998-10-0101 October 1998 SER Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Vermont Yankee Nuclear Power Station BVY-98-149, Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With ML20239A1361998-09-0202 September 1998 SER Re License Request for NRC Review & Concurrence W/Changes to NRC-approved Fire Protection Program BVY-98-135, Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With ML20151U0361998-08-28028 August 1998 Non-proprietary Rev 1 to Holtec Rept HI-981932, Vermont Yankee Nuclear Power Station Spent Storage Expansion Project ML20237E9221998-08-20020 August 1998 Vynp 1998 Form NIS-1 Owners Summary Rept for ISI, 961103-980603 BVY-98-122, Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station ML20205F6491998-07-31031 July 1998 Rev 1 to GE-NE-B13-01935-02, Jet Pump Assembly Welds Flaw Evaluation Handbook for Vermont Yankee ML20236G0011998-06-30030 June 1998 Individual Plant Exam External Events BVY-98-098, Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station ML20248C5081998-05-31031 May 1998 Rev 2 to 24A5416, Supplemental Reload Licensing Rept for Vermont Yankee Nuclear Power Station Reload 19 Cycle 20 ML20248C4951998-05-31031 May 1998 Rev 1 to Vermont Yankee Nuclear Power Station Cycle 20 Colr BVY-98-081, Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station1998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station ML20247J8341998-05-31031 May 1998 Peak Suppression Pool Temp Analyses for Large Break LOCA Scenarios, for May 1998 ML20247G4001998-05-12012 May 1998 Interview Rept of Ej Massey ML20247E6351998-04-30030 April 1998 Rev 1 to GE-NE-B13-01935-LTR, Jet Pump Riser Welds Allowable Flaw Sizes Ltr Rept for Vermont Yankee 1999-09-30
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text
s VERMONT YANKEE ,
NUCLEAR POWER CORPORATION ,
e
'~T ;- - P.O. Box 157, Governor Hunt Road
'g y T Vemon, Vermont 05354-015'7 x V (A02) 257-7711 h9 (L.'k:'~'l,'V \
,]
v August 13, 1993 i
U.S. Nuclear Regulatory Commission '
Document Control Desk washington, D.C. 20555
REFERENCE:
Operating License DPR-28 Docket No. 50-271 Reportable Occurrence No. LER 93-09
Dear Sirs:
As defined by 10 CFR 50.73, we are reporting the attached Reportable Occurrence as LER 93-09. t Very truly yours, VERMONT YANKEE NUCLEAR POWER CORPORATION Robert J. Wa czyk Plant Manager cc: Regional Administrator USNRC Region I ;
475 Allendale Road '
King of Prussia, PA 19406 ,
170005
[SE**%88!A!!88537, m
F y
fM8I i
b WltC Form 366 U.S. NUCLEAR REcVLATORY C0m!SSIDW APPROVED OMS NO. 3150-0104
, (6-E9) EXPIRES 4/30/92
, ESTIMATED BURDEN PER CIESPONEE TO COMPLY WITH THIS
' INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD
. COMMENTS RECARDING BURDEN ESTIMATE TO THE RECORDS AND l
! REPORTS MANAGEMENT BRANCH (P-350), U.S. NUCLEAR REGULATORY l COMMISSION, WASHlWGTON DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMENT AND ,
BUDGET, WASH!NGTON, DC 20603.
FACILITY NAME (1) DOCKET No. (2) PACE (3)
VERMONT YANKEE NUCLEAR POWER STATION Ol5l0l0l0l2l7l1 0 1 0F 0 3 TITLE (4) "B" CORE SPRAY SYSTEM DECLARED INOPERABLE DUE TO INSTRUMENT DUT OF TOLERANCE AS A RESULT OF PERSONNEL ERROR l
l 1
i EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR SEQ # REV # MONTH DAY YEAR FACILITY WAMES DOCKET NO. (S) 0 5 0 0 0 i
0 7 1 6 9 3 9 3 -
0 0 9 -
0 0 0 8 1 3 9 3 0 5 0 0 0 l
OPERATING THis REPORT IS SUBMITTED PURSUANT TO REQ'MTS OF 10 CFR i: CHECK ONE OR MORE (11)
MODE (9)
N 20.402(b) ?0.405(c) 50.73(a)(2)(iv) 73.71(b) -
POWER 20.405(a)(1)(1) 50.36(c)(1) x 50.73(a)(2)(v)+(vi) 73.71(c)
LEVEL (10) 1l0l0 20.405(a)(1)(li) 50.36(c)(2) 50.73(a)(2)(vii) OTHER:
.................. 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) !
.......... ... ... 20.405(a)(1)(iv) 50.73(a)(2)(li) 50.73(a)(2)(viii)(B)
.................. 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
EAME TELEPHONE NO.
J AREA CabE ROBERT J. WANCZYK, PLANT MANAGER 8l0l2 2l5l7l-l7l7l1l1 ,
COMPLETE ONE LINE FOR EACH COMPONENT FA!LUPE DESCRIBED IN THIS REPORT (13)
CAUSE SYST COMPONENT MFR REPORTABLE CAUSE SYST COMPONENT MTR REPORTABLE TO WPRDs .... TO NPRDS ....
A BlG P DlI l5 Bl0l8l0' Y .... kA l l l l l l l l 1 SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MO DAY YR SUBMISSION DATE (15)
YES (If yes, cocplete EXPECTED SUBMISSION E. ATE) X WO l l l ABSTRACT (Limit to 1400 spaces, i.e., approx. fif teen single space typewritten lines) (16)
On 7/16/93 at 0840, with the plant operating at 100% power and the *B* Train of the Residual Heat Removal System (RHR) removed from service, the *B* Train of the Core Spray System (CS) was declared inoperable. In accordance with l Technical Specifications, with one RHR System and one Core Spray System inoperable, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> shutdown LCO was entered. l The basis for declaring the *B* Train of the CS System inoperable was the identification that the respective Sparger Break i Detection System differential pressure indicating switch (DPIS) setpoint was out of specification. DPIS-14-43B was cahbrated to within the required limits and at 0930 on 7/16/93 the *B" Core Spray System was returned to service.
As discussed in LER 93-006, an interim administrative setpoint for the Sparger Break Detection Sensors was imposed by Plant fAanagement on 5/27/93 due to questions relative to the appropriateness of the TS setpoint. On 7/12/93, DPIS 43B was cal:brated and left outside the administrative limit due to the f act that the calabration procedure had not been revised to the new interim setpoint values. The root cause of this event is personnel error irs that timely revision to the instrument calibration procedure was not performed by the responsible manager. The instrument was immediately re calibrated to within the interim administrative setpoint, the calibration procedure was revised to reflect the new setpoint, and a corrective action report is being prepared.
I NRC Foira 366 (6-29)
i
.NRC Form 366A U.S. NUCLEAR REGULATC3i coMMiss10N APP 30VED oms No. 3150-0104 l' (6-G9) EXPIRES 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY VITH THIS INFORMATION COLLECTION REoVEST: 50.0 hrs. FORWARD COMMENTS RECARDING BURDEN ESTIMATE TO THE RECORDS AND I
' LICENSEE EVENT REPORT (LER) !
TEXT CONTINUATION REPORTS MANAGEMENT BRANCH (P-350), U.S. NUCLEAR REGULATORT COMMISSION, WASHINGTON DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMENT AND BUDCET, WASHINGTON, DC 20603.
FACILITY NAME (t) DOCKET NO (2) LER NUMBER (6) PAGE (3) !
YEAR SEQ # REV # f VERMONT YANKEE NUCLEAR POWER CORPORATION 9 3 -
0 0 9 -
0 0 0 0F 0 0l5l0l0l0l2l7l1 l2 l3 TEXT (If more space is required, use additional NRC Form 366A) (17) !
DESCRIPTION OF EVRE On 7/16/93 " 0840, with the plant operating at 100% power and the *B* Train of the Residual Heat Removal System (RHR)(*BO) removed from service for Limiting Condition for Operation (LCO) Maintenance, the *B' Train of the Core Spray ,
System (CS)(*BG) was declared inoperable. In accordance with Technical Specifications (TS) section 3.5.A.6, with one train of the RHH System removed from service and one train of the Core Spray System declared inoperable, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> shutdown LCO was entered. The reason for declaring the *B' Train of the CS System inoperable was the identification that the respective '[
Sparger Break Detection System differential pressure indicating switch (DPIS) setpoint was out of specification. The condition L was identified during the review of the calibration procedure data sheet by the system engineer. DPIS-14-43B was calibrated ;
to within the required limits and at 0930 on 7/16/93 the "B" Core Spray System was retumed to service. l i
in LER 93-006 (event date 5/27/93) Vermont Yankee reported to the Commission that sufficient information existed to suspect that the Technical Specification Table 3.2.1 setpoint for CS Sparger Break Detection Sensors DPIS-14-43A/P d 5 5 psid was non-conservative based upon information contained in Generr' Electric (GE) Services information Letter (SIL, MO and ;
recent discussions with GE. Information in SIL 300 indicates that the A 5 psid TS setpoint for the sparger break detection sensors may be inappropriate and that a setpoint of i 4 psid would be consistent with the Sll data.
l On 5/27/93 Plant Management had determined that the setpoint of the CS Break Detection System would be n.aintained at S 4 psid until a more thorough review could be conducted of the data contained in the SIL 300, this review is currently ongoing and scheduled to be commted by 8/31/93. Since the previous setpoint for the DPISs was 4 psid + /-0.3 psid, the immediate response to the potentially inappropriate TS setpoint was to set both DPIS-14-43A and B to the low side of the existing setpoint tolerance band (eg: 3.7 psid). A ionnal change to the setpoint was to follow on the next day that would remove the upper tolerance band from the cabbratu procedure (eg: + 0.3). Contrary to the above, the setpoint change was not initiated on the following day and the calibration procedure was not revised. On 7/12/93, DPIS-14-43B was calibrated and the trip point was left at 4.2 psid, this is above the 14 psid setpoint determined necessary on 5/27/93. Although this is not technically a violation of a Technical Specification setpoint, based upon the information presented above and the intent to administratively maintain the setpoint of 14 psid until further review of the setpoint could be performed, this event is conservatively being reported to the Commission.
CAUSE OF EVENT The root cause of this event is personnel error. The ccgnizant manager was informod on 5/27/93 of the need to initiate a revision to the calibration procedure OP 4347
- to include the revised setpoint tolerance. It was identified on 7/16/93 that the procedure revision was not done and that the DPIS-14-43B was out of the administrative tolerance.
ANALYSIS OF EVENT ,
The purpose of the Core Spray Sparger Break Detection System is to alert Control Room Operators of a pipe break in !
the Core Spray Sparger piping within the reactor vessel. l There were negligible safety implications resulting from declaring the *B' Train of the Core Spray System inoperable.
The instrument was calibrated to within specification approximately 50 minutes after identification of the error. It is estimated that the DPIS setpoint was above the 4.0 psid setpoint since mid-June 1993. It should be noted that both Trains of the Core Spray System were intact during this avent and would have functioned if required. *
- Energy industry identification System (Ells) Identifier L
NRC form 366 l (6-89) ,
i
- NRC Forn 366A U.S. NUCLEAR REGULATORY COMMISS10N APPROVED OMS NO. 3150-0104 (6 09)
EXPleES 4/30/92
+
ESTIMATED BURDEN PER RESPONSE TO COMPLY LIITH THIS t
~
INFORMATION COLLECTION REQUEST: 50.0 HRS. FoRWARG LICENSEE EVENT REPORT (LER) COMMENTS RECARDING BURDEN ESTIMATE TO THE RECORDS AND i TEXT CONTINUATION REPORTS MANAGEMENT BRANCH (P-350), U.S. NUCLEAR REGULATORY I COMMISSION, WASHINGTON DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3160-0104), OFFICE OF MANAGEMEkT AND 1 BUDGET, WASHINGTON, DC 20603. ;
FACILITY NAME (1) DOCKET No (2) LER NUMBER (6) PAGE (3) i YEAR SEQ # REV #
VERMONT YANKEE NUCLEAR POWER CORPORATION 9 3 -
0 0 9 -
0 0 0 0 0l5l0l0l0l2l7l1 l3 DF l3 TEXT (if more space is required, use additional NRC Form 366A) (17) j l ?
ANALYSIS OF EVENT (continued)
The safety implication associated with the personnel error is that the potential existed for both Core Spray System Sparger Break Detection System DPISs to be set high. Therefore had a break in the Core Spray Sparger Piping occurred, the instruments would not have provided the alarm function. The safety significance of this is considered to be minor since the Core Spray Sparger Piping is inspected each outage to verify physical integrity and only one train of the Break Detection System I was found to be out-of specification. ;
CORRECTIVE ACTIONS [
Immediate:
- 1. Upon discovery of the personnel error, the instrument was immediately re-calibrated to the f. 4 psid setpoint.
i
- 2. OP 4347 was revised to reflect the removal of the upper tolerance band (eg: + 0.3 psid). The current setpoint in the procedure is 4 psid + 0, -0.3. i Long-Term:
i
- 1. Preparation of a corrective action report has been assigned to the instrument and Control Department to document the cause and recommend further corrective actions if required.
ADDITIONAL INFORM ATION As described previously in this report, a similar condition was reported to the Commission in LER 93-006 in that a concern with the Core Spray Break Detection System Setpoint resulted in the determination that a Core Spray System Train (s) l was inoperable.
l l
j l 4 ,
j
- Energy Industry identification System (Ells) Identifier i
I 1
4 J
NRC Form 366 (6-89) l
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05000271/LER-1993-004 | LER 93-004-01:on 930225,discovered That Surveillance for Jet Pumps Not Performed During Single Loop Operations Due to Inadequate Plant Procedures.Procedures OP-4110 & OP-2428 revised.W/930819 Ltr | | 05000271/LER-1993-005 | LER 93-005-01:on 930406,concluded Control Rod Scram Times Not in Compliance W/Ts Section 3.3.C.Caused by Faulty Scram Solenoid Pilot Valves.Solenoid Valves rebuilt.W/930813 Ltr | | 05000271/LER-1993-009 | LER 93-009-00:on 930716,B Train of RHR Sys Declared Inoperable.Caused by Personnel Error Re Failure to Initiate Rev to Calibration Procedure OP 4347.Instrument re-calibrated & OP 4347 revised.W/930813 Ltr | | 05000271/LER-1993-010 | LER 93-010-00:on 930803,fire Protection Valve V76-420 Has Not Been Cycled Through Complete Cycle of Full Travel,Per TS 4.13.B.d.Caused by Human Error.Applicable Surveillance Procedure Revised to Include V76-420.W/930831 Ltr | | 05000271/LER-1993-012 | LER 93-012-00:on 930908,noted That Containment Air Valve & TIP Found to Have Seat Leakage Above That Permitted by Ts. Caused by Leakage Through Check Valve.C/As Will Be Reported in Suppl to LER.W/931007 Ltr | |
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