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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000271/LER-1993-0121993-10-0707 October 1993 LER 93-012-00:on 930908,noted That Containment Air Valve & TIP Found to Have Seat Leakage Above That Permitted by Ts. Caused by Leakage Through Check Valve.C/As Will Be Reported in Suppl to LER.W/931007 Ltr 05000271/LER-1993-0101993-08-31031 August 1993 LER 93-010-00:on 930803,fire Protection Valve V76-420 Has Not Been Cycled Through Complete Cycle of Full Travel,Per TS 4.13.B.d.Caused by Human Error.Applicable Surveillance Procedure Revised to Include V76-420.W/930831 Ltr 05000271/LER-1993-0041993-08-19019 August 1993 LER 93-004-01:on 930225,discovered That Surveillance for Jet Pumps Not Performed During Single Loop Operations Due to Inadequate Plant Procedures.Procedures OP-4110 & OP-2428 revised.W/930819 Ltr 05000271/LER-1993-0051993-08-13013 August 1993 LER 93-005-01:on 930406,concluded Control Rod Scram Times Not in Compliance W/Ts Section 3.3.C.Caused by Faulty Scram Solenoid Pilot Valves.Solenoid Valves rebuilt.W/930813 Ltr 05000271/LER-1993-0091993-08-13013 August 1993 LER 93-009-00:on 930716,B Train of RHR Sys Declared Inoperable.Caused by Personnel Error Re Failure to Initiate Rev to Calibration Procedure OP 4347.Instrument re-calibrated & OP 4347 revised.W/930813 Ltr 05000271/LER-1990-0081990-06-29029 June 1990 LER 90-008-00:on 900529,identified That Cables Providing Power to post-accident Monitoring Instrument Loops Not Routed,Per Required Separation Criteria.Caused by Combination of Factors.Design Change prepared.W/900629 Ltr 05000271/LER-1987-003, :on 880412,personnel Found Functional Testing Not Been Tested in Accordance W/Tech Spec Requirements. Caused by Programmatic Tracking Program.Programmatic Tracking Sys Revised as Described in LER 87-031988-05-10010 May 1988
- on 880412,personnel Found Functional Testing Not Been Tested in Accordance W/Tech Spec Requirements. Caused by Programmatic Tracking Program.Programmatic Tracking Sys Revised as Described in LER 87-03
05000271/LER-1983-009, Followup LER 83-009/01T-0:on 830321,primary Containment Isolation Sys Isolation of Containment Ventilation Sys Occurred.Caused by Mods to Reactor Protection Sys Motor Generator.Fuel Handling Activities Suspended1983-04-0101 April 1983 Followup LER 83-009/01T-0:on 830321,primary Containment Isolation Sys Isolation of Containment Ventilation Sys Occurred.Caused by Mods to Reactor Protection Sys Motor Generator.Fuel Handling Activities Suspended 05000271/LER-1981-030, Updated LER 81-030/03L-1:cracks Found on Internal Surface of Valve Bodies & Seating Surfaces of Reactor Water Cleanup Valves Attributed to Surface Shrinking of Casting & Intergranular Stress Corrosion Cracking,Respectively1982-07-0101 July 1982 Updated LER 81-030/03L-1:cracks Found on Internal Surface of Valve Bodies & Seating Surfaces of Reactor Water Cleanup Valves Attributed to Surface Shrinking of Casting & Intergranular Stress Corrosion Cracking,Respectively 05000271/LER-1981-0261981-11-0303 November 1981 LER 81-026/03L-0:on 811005,during Weekly Review of Surveillance Test Data,Discovered That Max Monthly Interval for Functional Test of Atws/Rpt Sys Exceeded by 4 Days. Caused by Oversight in Scheduling ML20064H2211978-12-13013 December 1978 /03L-0 on 781113:during Weekly Surveillance Re Radiological Environ Prog,Air Pump Motor Was Found Inoper. Time Meter Indicated Pump Had Operated Only 0.4 Hours.Air Pump Replaced & New Weekly Air Sample Initiated ML20064E3281978-11-13013 November 1978 /03L-0 on 781014:during Surveillance Test of Main Steam Isolution Valves,V2-86C Closed in 2.6 Seconds Rather than 3-5 Seconds Req in Tech Spec 4.7.D.1.a.1.Caused by Closing Speed Control Valve Coming Loose from Actuator ML20064E3101978-11-13013 November 1978 /03L-0 on 781016:weekly Review of Completed Surveillance Test Following Plant Startup Noted That Monthly Hydrogen Detector Functional Test Was Not Performed Due to Personnel Error ML20064H2291978-08-10010 August 1978 /03L-1 on 780626:during Increase of Reactor Pwr, Noted That Critical Pwr Ratio in 4 Symmetrically Located Fuel Bundles Was Below Tech Spec Values.Caused by Pwr Increasing Xenon Transient ML20064H1681978-07-25025 July 1978 /03L-0 on 780629:during Steady State Oper Motor Control Ctr 893 Lost Voltage Because B Uninterruptible Pwr Supply (UP5) Tripped Due to Blown Inverter Leg Fuse.Failed Components Replaced & Operability Test Performed ML20064H2051978-07-24024 July 1978 /03L-0 on 780625:during Steady State Oper,Noted That Drywell Atmospheric Temp Recorder TR-1-149 Was Inoperable.Caused by Recorder Failure Due to Broken Cord on Chart Drive Mechanism ML20064H1741978-07-24024 July 1978 /03L-0 on 780626:during Reactor Pwr Increase Noted That Local Critical Pwr Ratio in 4 Symmetrically Located Fuel Bundles Was Lower than Tech Spec Levels.Caused by Pwr Increasing Xenon Transient ML20064H1321978-07-24024 July 1978 /03L-0 on 780612:during Steady State Oper,Noted That Drywell Atmospheric Temp Recorder TR-1-149 Was Inoperable.Recorder Failed Due to Failed Idler Assembly 05000271/LER-1976-005, Telecopy LER 76-005:on 760217,portion of Procedure Associated W/Securing Plant from Shutdown Cooling Mode Not Performed.Caused by Failure of Plant Personnel to Follow Appropriate Plant Procedure1976-02-18018 February 1976 Telecopy LER 76-005:on 760217,portion of Procedure Associated W/Securing Plant from Shutdown Cooling Mode Not Performed.Caused by Failure of Plant Personnel to Follow Appropriate Plant Procedure 05000271/LER-1975-003, Corrected LER 75-003:on 750204,core Spray Sys Pump Discharge Pressure Sensor PS-14-44A Actuated at 82 Psig.Caused by Setpoint Drift.Sensor replaced.W/750218 Ltr1975-02-14014 February 1975 Corrected LER 75-003:on 750204,core Spray Sys Pump Discharge Pressure Sensor PS-14-44A Actuated at 82 Psig.Caused by Setpoint Drift.Sensor replaced.W/750218 Ltr 1993-08-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8831999-10-21021 October 1999 Safety Evaluation Supporting Proposed Alternatives to Code Requirements Described in RR-V17 & RR-V18 ML20217G2041999-10-13013 October 1999 Safety Evaluation Supporting Amend 179 to License DPR-28 BVY-99-127, Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Vermont Yankee Nuclear Power Station.With ML20212C2551999-09-17017 September 1999 Safety Evaluation Supporting Amend 175 to License DPR-28 BVY-99-112, Monthly Operating Rept for Aug 1999 for Vermont Yankee.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Vermont Yankee.With BVY-99-109, Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 9908311999-08-19019 August 1999 Ro:On 990812,stack Ng Effluent Instrumentation for PAM Was Declared Oos.Caused by Instrument Drift Due to Electronic Components Based on Insps by Instrumentation & Controls Dept.Detector & Preamplifier Will Be Replaced on 990831 BVY-99-102, Monthly Operating Rept for July 1999 for Vermont Yankee. with1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Vermont Yankee. with ML20209J0081999-07-14014 July 1999 Special Rept:On 990615,diesel Driven Fire Pump Failed to Achieve Rated Flow of 2500 Gallons Per Minute.Pump Was Inoperable for Greater than 7 Days.Corrective Maint Was Performed to Reset Pump Lift Setting BVY-99-090, Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Vermont Yankee Nuclear Power Station.With ML20196G5071999-06-23023 June 1999 Vynp Assessment of On-Site Disposal of Contaminated Soil by Land Spreading BVY-99-077, Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Vermont Yankee Nuclear Power Station.With BVY-99-068, Monthly Operating Rept for Apr 1999 for Vynp.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Vynp.With ML20206E8741999-04-29029 April 1999 SER Determined That Flaw Evaluation Meets Rules of ASME Code & Assumed Crack Growth Rate Adequate for Application ML20206D9301999-04-27027 April 1999 1999 Emergency Preparedness Exercise 990427 Exercise Manual (Plume Portion) ML20205S4211999-04-16016 April 1999 Non-proprietary Version of Revised Page 4-3 of HI-981932 Technical Rept for Vermont Yankee Spent Fuel Pool Storage Expansion ML20205K7581999-04-0707 April 1999 Safety Evaluation Supporting Alternative Proposal for Reexamination of Circumferential Welds with Detected Flaw Indications in Plant RPV BVY-99-046, Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Vermont Yankee Nuclear Power Station.With ML20205F6631999-03-0404 March 1999 Jet Pump Riser Weld Leakage Evaluation BVY-99-035, Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Vermont Yankee Nuclear Station.With ML20205P8241999-02-28028 February 1999 Rev 2 to Vermont Yankee Cycle 20 Colr ML20203H9881999-02-18018 February 1999 SER Accepting Alternative to 10CFR50.55a(g)(6)(ii)(A) Augmented Reactor Vessel Exam at Vermont Yankee Nuclear Power Station.Technical Ltr Rept Encl ML20203A6951999-02-0404 February 1999 Revised Rev 2,App B to Vermont Yankee Operational QA Manual (Voqam) ML20199K7151999-01-21021 January 1999 Corrected Safety Evaluation Supporting Amend 163 Issued to FOL DPR-28.Pages 2 & 3 Required Correction & Clarification ML20199K6991999-01-20020 January 1999 Safety Evaluation Concluding That Request to Use YAEC-1339, Yankee Atomic Electric Co Application of FIBWR2 Core Hydraulics Code to BWR Reload Analysis, at Vermont Yankee Acceptable ML20199L5951999-01-14014 January 1999 Safety Evaluation Accepting Licensee Proposed Alternative to Code Requirement,Described in Rev 2 to Pump Relief Request RR-P10 Pursuant to 10CFR50.55a(a)(3)(i) BVY-99-071, Corp 1998 Annual Rept. with1998-12-31031 December 1998 Corp 1998 Annual Rept. with BVY-99-001, Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Vermont Yankee Nuclear Power Station ML20198H5481998-12-23023 December 1998 Rev 2 to Vermont Operational QA Manual,Voqam ML20196H8641998-12-0101 December 1998 Cycle 19 Operating Rept BVY-98-163, Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Vermont Yankee Nuclear Power Station.With ML20195C4161998-11-0909 November 1998 SER Accepting Request That NRC Approve ASME Code Case N-560, Alternative Exam Requirement for Class 1,Category B-J Piping Welds BVY-98-154, Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Vermont Yankee Nuclear Power Station.With ML20155B6471998-10-26026 October 1998 Safety Evaluation Accepting Jet Pump Riser Insp Results & Flaw Evaluation,Conducted During 1998 Refueling Outage ML20154N0891998-10-16016 October 1998 Rev 1 to Vermont Operational QA Program Manual (Voqam) ML20154B6951998-10-0101 October 1998 SER Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Vermont Yankee Nuclear Power Station BVY-98-149, Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Vermont Yankee Nuclear Power Station.With ML20239A1361998-09-0202 September 1998 SER Re License Request for NRC Review & Concurrence W/Changes to NRC-approved Fire Protection Program BVY-98-135, Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Vermont Yankee Nuclear Power Station.With ML20151U0361998-08-28028 August 1998 Non-proprietary Rev 1 to Holtec Rept HI-981932, Vermont Yankee Nuclear Power Station Spent Storage Expansion Project ML20237E9221998-08-20020 August 1998 Vynp 1998 Form NIS-1 Owners Summary Rept for ISI, 961103-980603 BVY-98-122, Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Vermont Yankee Nuclear Power Station ML20205F6491998-07-31031 July 1998 Rev 1 to GE-NE-B13-01935-02, Jet Pump Assembly Welds Flaw Evaluation Handbook for Vermont Yankee ML20236G0011998-06-30030 June 1998 Individual Plant Exam External Events BVY-98-098, Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station1998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Vermont Yankee Nuclear Power Station ML20248C5081998-05-31031 May 1998 Rev 2 to 24A5416, Supplemental Reload Licensing Rept for Vermont Yankee Nuclear Power Station Reload 19 Cycle 20 ML20248C4951998-05-31031 May 1998 Rev 1 to Vermont Yankee Nuclear Power Station Cycle 20 Colr BVY-98-081, Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station1998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Vermont Yankee Nuclear Power Station ML20247J8341998-05-31031 May 1998 Peak Suppression Pool Temp Analyses for Large Break LOCA Scenarios, for May 1998 ML20247G4001998-05-12012 May 1998 Interview Rept of Ej Massey ML20247E6351998-04-30030 April 1998 Rev 1 to GE-NE-B13-01935-LTR, Jet Pump Riser Welds Allowable Flaw Sizes Ltr Rept for Vermont Yankee 1999-09-30
[Table view] |
LER-2083-009, Followup LER 83-009/01T-0:on 830321,primary Containment Isolation Sys Isolation of Containment Ventilation Sys Occurred.Caused by Mods to Reactor Protection Sys Motor Generator.Fuel Handling Activities Suspended |
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RM3 U.S. NUCLEAR REGDLAToRY COMMISSION (7-77 )
Follow Up Report - Pr gRegr ag / /83 LER 83-09/1T CONTROL BLOCK: l l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION!
1 6 10111 I vlLICENSEE Tl vlCODE Yi Sl il@l010 l- 10101010 14 l 01 - [ 0 i 025 l@l LICENSE NUMBER 26 4 lLICENSE 1l 11 TYPE l
Il JOll@l57 L AT 56 lg 7 8 9 15 CON'T IOI1i SbRCE lL l@l0 l 5 DOCKET l0l0 l 0 l 2 l 768l 1 69@l 0EVENT l 3 lDATE 2 l ll 8 l743 l@l0 75 14 l0 l1 l8 l380l@
REPORT DATE 7 8 60 61 NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lol2l l During the refueling outage, planned modifications of the RPS MG Set resulted in a l lol3l l PCIS isolation of the Containment Ventilation System. Slide links TAC-3 and TP-1 l l o 141 l were opened on Control Room panel 9-26 to restore ventilation while allowing work onl loIsl I the MG sets to continue. This action resulted in the loss of SBGT auto-start capa- I lo16II bility from 0817-1023. Contra ry to T.S. 3.7.C.1. irradiated fuel was moved during i IoI7ll that time neriod in the Rx. blda. with SBGT (and therefore. secondary containment) l I
IoIri l inonerable. 80 7 8 9 DE CCDE SUBC E COM*0NENT CODE SUBC DE S E ITTT1 IS lC I@ g@ lC l@ l zl zi zl zl zl zl@ l z l@ LZ_J @ IB 19 29
!< SEQUENTI AL O CC'. RPENCE REFORT REVISION EVENT YE AR REPORT NO. COOE TYPE NO.
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@ ,a'E P RO ua'y l-l 10 l0 l 9 ! l/l 1011 j lT l l-l Dl
_ l21813l 22 23 24 26 27 2Y 29 30 31 32 TA Er ') ON PLA T T D HOURS ! E IT FO P B CUPPLIE MN AC LAER i33H l@l34 z l@ [_zj@ lz l@ l 0l0 l010 l W@ lNl@ lzl@ lz l9 l9 l9 l@ 47 35 36 3/ 40 41 42 4? 44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l,lOglThe slide links were removed before completing the full revice and approval of the l lil ) i lifted lead and jumper requesL. When it was discovered that this action resulted ini i,,7i l the loss of SBGT all fuel handling activities were suspended until the auto-start l
[il3l l capability of the SBUr System was returned to service. l I
11 14 1 I 80 7 8 9 STA S *.POWE R OTHER STATUS SCO RY DISCOVERY DESCRIPTION l1 15 l lH l@ l 0 l 0 l 0l@l NA l l A l@l Review of lif ted lead request l ACTIVITY CO TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOC ATION OF RELEASE l1 lc* *l d @ bj@l NA l l NA l PERSONNEL E XPOS ES NUVBER TYPE DESCRIPTION NA l l1 l 71 l 01 0l Ol@l z l@l PERSONNE L INJURIES NUMBER DESCRIPTION lilallolol0l@l 7 8 9 11 12 NA 80 l
LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION I'I gRADOCKO4180256 830404 8 PunoCiTY gv g 05000271 NRC USE ONLY 7 P 9 issuEn ly_Loj IN lhl oEseRiPriON to NA PDR l
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NAYE OF PREPARER vs Wr-
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. . j 05000271 .
LER 83-09/lT DESCRIPTION OF THE OCCURRENCE:
Reactor shutdown for refueling with all fuel removed from the reactor vessel. "A" SBGT System considered inoperable due to P/M work in progress on "A" Diesel Generator. "B" SBGT System operable. Reactor Protection System Bus "A" removed from service for preventative maintenance and planned modifications. With RPS Bus "A" out of service, SBGT Systems A and B auto started and Reactor Building HVAC auto isolated due to power loss and subsequent downscale indication on refuel floor radiation monitor. ,
With the loss of normal RB ventilation (1 volume change per day versus 75 volume changes per day) and the extensive work being performed in the Reactor Building, it was expected that ambient temperature would increase
. thereby deterioratin,g working environmenta.
At approximately 0715 the oncoming Shif t Supervisor (SS), upon noting the isolation of normal R/B ventilation, requested a senior 1 & C technician to see what could be done to restore normal R/B ventilation.
The SS then left the Control Room to attend the' morning outage status meeting, leaving the SCR0 in command. At approximately 0817 following applicable circuit diagram review and discussion with the SCRO, the senior I&C technician opened slide links TAC-3 and TP-1 in CRP 9-28 while being observed by the SCRO. No approved Lifted Lead / Jumper Request per AP 0020 was issued at this time. After verifying a successful restart of the RB HVAC, the I&C technician then returned to the shop to process the Lifted Lead / Jumper Request. When the SS returned to the Control Room at approximately 0830, he was made aware of the change in status in the RB ventilation but not of the slide link repositioning without a Lifted Lead / Jumper Request. A second SCR0 was already in route to the refuel floor.to support speat fuel pool fuel moves. At approximately 0915 when the Lifted Leed/ Jumper Request was approved by the 16C Supervisor and forwarded to the Operaticas Supervisor in the Control Room, the Shif t Supervisor first became aware that the change in R/B ventilation status was due to earlier slide link repositioning. Discussion of the proposed Lifted Lead / Jumper Request between the Operations Superintendent, Tech-nical Services Superintendent, Engineering Support Supervisor, and Oper-ations Supervisor raised the concern that if implemented, this would defeat the SBGT auto-start features. At approximately 1020, plant management was made aware.that the RB ventilation system had previously been altered. ' Fuel movement operations in the spent fuel pool were halted once a stable fuel condition was achieved, and no further moves were made until after the SBGT auto-start had been restored. NRC notification required by 10 CFR 50.72 was not performed.
PROBABLE CONSEQUENCES OF THE EVENT:
, With the slide links TAC-3 and TP-1 open, the automatic initiation function for the Standby Gas Treatment and Rx Bldg. auto isolation were removed rendering the systems inoperable. During the time the systems were disabled, fuel was being moved in the spent fuel pool.
Had a high airborn radiation condition occurred which would have required the Reactor Building Ventilation System to isolate and Standby Gas Treatment to start, this would not have functioned automatically. These systems would have had to be aligned manually, e .
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, , , 05000271 LER 83-09/lT CORRECTIVE ACTION
- 1. Immediate Actions Immediately following suspicion of compromised secondary containment all fuel moves were terminated (fuel pin move in progress was allowed to be completed) and the improperly positioned slide links were repositioned. Once secondary containment status was verified satisfactory, permission was granted to continue fuel moves. A properly initiated, reviewed, and approved Lifted Lead / Jumper Request (No. 83-0050) was issued to restore normal RB ventilation without defeating SBGT auto start or RB ventilation auto-isolation logic.
- 2. Subsequent Actions A) A critique was held with all parties involved with the situation and with plant management. The purpose of the critique was to determine the chronology of the events and to try and understand how these events occurred. The senior I&C technician and the I&C Supervisor were ques-tioned on their rolo's in the matter. The Plant Manager and Maintenance Superintendent gained assurance that they showed an understanding of the errors made, and their responsibilities to comply in the future to all administrative requirements and they were allowed to continue normal duties. The involved licensed personnel have been removed from license duties until management can be assured that they understand their duties and responsibilities and will implement them in the future.
B) Additional clarification was made to the two administrative procedures involved in the situation.
- 1) AP 0020, Lifted Lead / Jumper Request, was modified by Departmental Instruction to specifically address the fact that the originating depart-ment head review must constitute an independent detailed technical evaluation of the necessity for the lifted lead, the methodology for obtaining the desired end result, and the consequences of implementing the request as far as loss of function and impact to other plant opera-tions. Signature by the originating department now specifies that all the above reviews are complete and satisfactory.
- 2) AP 0010, Occurrence Reports, was clarified by note in the Operations Department night orders specifying that the Shift Supervisor is primar-ily responsible for making the one hour notification to the NRC for events identified in Appendix D of this procedure. A detailed review of these procedures is to be completed and available for PORC review by April 1,1983.
C) The Engineering Support Supervisor was directed to review an adequate and random sampling of previously issued Lifted Lead / Jumper Requests to ensure that adequate technical reviews were completed en each request.
Also to review the description of loss of function and consequences associ-ated with each request to ensure completeness and correctness. The results of this investigation is to be presented to the Plant Manager and PORC by April 9,1983.
VTVYS1
- 05000271 LER 83-09/lT D) A meeting of plant Department IIcads and Superintendents was held on 3/26/83 to thoroughly review the facts in the situation and to assess the problems identified. Each Department Head and Superintendent was tasked with relaying the below listed information to each and every member of their departments and to document such briefing / training sessions and present the results of this action to the Plant Manager by April 2,1983.
Key topics to be incorporated into the discussion are:
- 1) Factors which could influence personnel to bypass procedural require-ments.
( 2) Approach people take with the Operations Department. Differential between when you should be requesting permission vs. notifying.
Operators should be aware of this as well.
- 3) The necessity for thorough understanding prior to doing work even when the event seems insignificant.
- 4) The need to comply with procedures.
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05000271/LER-1983-001, Forwards LER 83-001/01T-0 | Forwards LER 83-001/01T-0 | | 05000271/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | 05000271/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | 05000271/LER-1983-005, Forwards LER 83-005/01P-0 | Forwards LER 83-005/01P-0 | | 05000271/LER-1983-006, Forwards Updated LER 83-006/01X-0 | Forwards Updated LER 83-006/01X-0 | | 05000271/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | 05000271/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | 05000271/LER-1983-009, Followup LER 83-009/01T-0:on 830321,primary Containment Isolation Sys Isolation of Containment Ventilation Sys Occurred.Caused by Mods to Reactor Protection Sys Motor Generator.Fuel Handling Activities Suspended | Followup LER 83-009/01T-0:on 830321,primary Containment Isolation Sys Isolation of Containment Ventilation Sys Occurred.Caused by Mods to Reactor Protection Sys Motor Generator.Fuel Handling Activities Suspended | | 05000271/LER-1983-010, Forwards LER 83-010/03L-0 | Forwards LER 83-010/03L-0 | | 05000271/LER-1983-012, Forwards LER 83-012/01P-0 | Forwards LER 83-012/01P-0 | |
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