10-29-2004 | On May 5, 2004, at 1327 hours0.0154 days <br />0.369 hours <br />0.00219 weeks <br />5.049235e-4 months <br /> ( CDT), with Unit 3 at 100 percent power in Mode 1, an automatic scram occurred due to a Main Generator Load Reject when a loss of offsite power occurred. The Emergency Diesel Generators automatically started and powered their respective electrical busses. All control rods fully inserted and Group I, II and III isolations occurred as expected. Operations personnel manually initiated the Isolation Condenser System for reactor pressure control, the High Pressure Coolant Injection System for reactor water level control, and the Low Pressure Coolant Injection System for Torus cooling. All systems initially responded to the scram as expected except the Standby Gas Treatment System was unable to maintain the Secondary Containment at the Technical Specification Surveillance Requirement limit of greater than or equal to 0.25 inches of vacuum water gauge. An Unusual Event for the loss of offsite power was declared at 1342 hours0.0155 days <br />0.373 hours <br />0.00222 weeks <br />5.10631e-4 months <br /> ( CDT) and terminated at 1601 hours0.0185 days <br />0.445 hours <br />0.00265 weeks <br />6.091805e-4 months <br /> ( CDT) on May 5, 2004. Additionally, during restoration of offsite electrical power to Bus 33, the Emergency Diesel Generator 2/3 output electrical breaker tripped.
The root causes associated with the load reject and loss of offsite power and the low Secondary Containment vacuum were respectively, equipment failure in the "C" phase of the 345 kilovolt circuit breaker 8-15 and a degraded Secondary Containment boundary not detected due to an inadequate leak rate test procedure. The investigation into the apparent cause of the Emergency Diesel Generator output breaker trip was indeterminate.
NRC FORM 366A� U.S. NUCLEAR REGULATORY COMMISSION (7-2001) Dresden Nuclear Power Station Unit 3 05000249 NUMBER NUMBER |
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Dresden Nuclear Power Station (DNPS) Units 2 and 3 are a General Electric Company Boiling Water Reactor with a licensed maximum power level of 2957 megawatts thermal. The Energy Industry Identification System codes used in the text are identified as [XX].
A. Plant Conditions Prior to Event:
� Unit: 03� Event Date: 5-5-2004 Event Time: 1327 CDT � Reactor Mode: 1� Mode Name: Power Operation Power Level: 100 percent Reactor Coolant System Pressure: 1000 psig
B. Description of Event:
On May 5, 2004, electrical breaker switching was being performed in the DNPS switchyard to support the testing of a 345 kilovolt (kv) offsite electrical line. A loss of offsite power (LOOP) occurred to Unit 3 when 345 kv breaker 8 15 [BKR] located in the switchyard [FK] was opened.
On May 5, 2004, at 1327 hours0.0154 days <br />0.369 hours <br />0.00219 weeks <br />5.049235e-4 months <br /> (CDT), with Unit 3 at 100 percent power in Mode 1, an automatic scram occurred due a Main Generator Load Reject when the LOOP occurred. The Emergency Diesel Generators (EDGs) [DG] automatically started and powered their respective electrical busses. All control rods fully inserted and Group I, II and III isolations occurred as expected. Operations personnel manually initiated the Isolation Condenser System [BL] for reactor pressure control, High Pressure Coolant Injection System [BJ] for reactor water level control, and Low Pressure Coolant Injection System [BO] for Torus cooling. All systems initially responded as expected to the scram except for the Standby Gas Treatment System (SGT) [BH] that was unable to maintain the Secondary Containment at the Technical Specification Surveillance Requirement limit of greater than or equal to 0.25 inches of vacuum water gauge. Secondary containment was declared inoperable for Units 2 and 3.
An Unusual Event for the LOOP was declared at 1342 hours0.0155 days <br />0.373 hours <br />0.00222 weeks <br />5.10631e-4 months <br /> (CDT). An ENS call was made at 1429 hours0.0165 days <br />0.397 hours <br />0.00236 weeks <br />5.437345e-4 months <br /> (CDT) for the above-described event. The assigned ENS event number was 40727.
At 1558 hours0.018 days <br />0.433 hours <br />0.00258 weeks <br />5.92819e-4 months <br /> (CDT), the EDG 2/3 output electrical breaker tripped on reverse power during restoration of offsite electrical power to Bus 33 that was being fed from EDG 2/3. Bus 33 remained powered from the offsite source.
The Unusual Event was terminated at 1601 hours0.0185 days <br />0.445 hours <br />0.00265 weeks <br />6.091805e-4 months <br /> (CDT) when offsite power was restored to Unit 3.
At 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br /> (CDT), SGT was declared operable when the Secondary Containment pressure was restored to greater than 0.25 inches of vacuum water gauge.
This event is being reported in accordance with:
- 10 CFR 50.73(a)(2)(iv)(A), "Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B) of this section," and
These events are addressed in the NRC Special Inspection Report Number 05000249/2004009 dated June 21, 2004.
NRC FORM 366A� U.S. NUCLEAR REGULATORY COMMISSION (7-2001) Dresden Nuclear Power Station Unit 3 05000249 NUMBER NUMBER
C. Cause of Event:
The root causes associated with the load reject and LOOP and the low Secondary Containment vacuum were respectively, equipment failure in the "C" phase of the 345 kv circuit breaker 8-15 and a degraded secondary containment boundary not detected due to an inadequate leak rate test procedure. The investigation into the apparent cause of the EDG 2/3 output breaker trip was indeterminate.
The equipment failure of the 345 kv circuit breaker 8-15 circuit breaker occurred due to age-related and application related degradation. The vendor, prior to the event, did not provide information to Exelon Corporation, a product advisory issued in July 2003, regarding the possibility of breaker slow operation or failure to operate. This is applicable to circuit breakers 8-15 and 6-7. The corrective action to prevent reoccurrence is to revise the preventative maintenance procedure governing both circuit breakers 8-15 and 6-7 to implement the product advisory recommendations.
The degraded secondary containment boundary resulted from air in-leakage into the Unit 2 Drywell and Torus Purge Exhaust (DTPE) filter housings. At the time of the event, Unit 2 was in a maintenance outage and the DTPE fans were in operation due to activities in the Unit 2 drywell. The DTPE fans are not normally in operation and the secondary containment leak rate test procedure does not test with the DTPE fans operating as a part of the secondary containment barrier. Two corrective actions to prevent reoccurrence are being taken:
The first is to modify the current design to trip the DTPE fans on both units following an automatic SGT system initiation from either unit, rather than operate the DTPE fans during the secondary containment leak rate test. The second action is to develop a source document that clearly identifies the secondary containment boundaries.
The investigation into the apparent cause of the EDG 2/3 output breaker trip was indeterminate. The investigation identified an electrical relay that should have prevented the trip from occurring and the relay was sent to an offsite lab for analysis. No faults could be found with the relay when it was operated electrically. The lab did identify that one of the relay contacts would hang up when it was actuated manually, however, this is not the method used to actuate the relay when it is installed in the plant. The investigation concluded that the most probable cause for the EDG 2/3 output breaker trip was due the effect of the electrical transient experienced during the LOOP on contact fingers within an electrical relay which resulted in an automatic out-of-phase paralleling of offsite power with the EDG. Dresden procedure DGA 12, "Partial/Complete Loss of AC Power," was revised to require that affected transformer feed breaker control switches be placed in the pull-to-lock position during the restoration of normal off site power sources, to preclude automatic operation of the breakers.
D. Safety Analysis:
The safety significance of the LOOP event was minimal. All systems initially responded as expected to the scram except for the SGT system that was unable to maintain the secondary containment at the Technical Specification Surveillance Requirement limit of greater than or equal to 0.25 inches of vacuum water gauge. However, secondary containment was maintained at a negative pressure at all times during the event. The EDGs were supplying power to their respective busses, as designed, and offsite power was availiable through Unit 2.
Therefore, the consequences of this event had minimal impact on the health and safety of the public and reactor safety.
NRC FORM 366A� U.S. NUCLEAR REGULATORY COMMISSION (7-2001) Dresden Nuclear Power Station Unit 3 05000249 NUMBER NUMBER
E. Corrective Actions:
345 kv circuit breaker 8-15 was repaired and a vendor upgrade kit was installed. The circuit breaker upgrade kit will be installed on circuit breaker 6-7 at the next availiable opportunity.
The preventive maintenance procedure for circuit breakers 8-15 and 6-7 will be revised to incorporate appropriate vendor advisory recommendations.
DNPS procedures were revised to require the securing of the DTPE Fans upon initiation of SGT.
The DTPE filter housing in-leakage has been repaired to correct air in leakage.
The SGT initiation logic will be changed to include the tripping of the DTPE Fans for both units.
The final corrective actions to prevent reoccurrence for the Emergency Diesel Generator output breaker will be described in a supplemental report scheduled to be submitted no later than October 30, 2004.
Dresden procedure DGA 12 was revised to require that affected transformer feed breaker control switches be placed in the pull-to-lock position during the restoration of normal off-site power sources, to preclude automatic operation of the breakers.
F. Previous Occurrences:
A review of Dresden Nuclear Power Station Licensee Event Reports (LERs) and operating experience identified the following LER.
Unit 3 LER 89-001-01 described a March 25, 1989, event in which an electrical fault in the 345 kilovolt circuit breaker 8-15 phase A internal ground capacitor and slow transfer of the 4 kv Bus 32 from transformer 32 to 31 caused a LOOP for Unit 3. The corrective actions included the removal of the internal ground capacitors from 345 kilovolt circuit breaker 8-15.
G. Component Failure Data:
I.T.E. Power Circuit Breaker, Model C Type GA
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05000348/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2004-001 | Inadvertent Actuation of ECCS and EDGs While in Refueling Mode | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2004-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2004-001 | Failure To Comply With Technical Specification 3 .7 .5 .1, Control Room Emergency Ventilation System | | 05000301/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000313/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000285/LER-2004-001 | Failure To Perform A Leakage Test Due To Lack Of Understanding of Penetration Design | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000271/LER-2004-001 | Main Steam Isolation Valve Leakage Exceeds a Technical Specification Leakage Rate Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2004-001 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000318/LER-2004-001 | . Reactor Trip Due to Low Steam Generator Water Level After Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000289/LER-2004-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-001 | | | 05000247/LER-2004-001 | Manual Reactor Trip Due to Oscillating Feedwater Flow and Steam Generator Level with Flow Perturbations Caused by a Degraded Feed Water Regulating Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000244/LER-2004-001 | Gaps in the Control Room Emergency Zone Boundary | | 05000255/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000461/LER-2004-001 | Clinton Power Station 05000461 1 OF 4 | | 05000414/LER-2004-001 | relPowere Vice President A Duke Energy Company Duke Power Catawba Nuclear Station 4800 Concord Rd. / CNO1VP York, SC 29745-9635 803 831 4251 803 831 3221 fax November 9, 2004
U. S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, DC 20555-0001
SUBJECT: Duke Energy Corporation
Catawba Nuclear Station Unit 2
Docket No. 50-414
Licensee Event Report 414/04-001 Revision 0
Reactor Coolant System Pressure Boundary Leakage
Due to Small Cracks Found in Steam Generator
Channel Head Bowl Drain Line on 2C & 2D Steam
Generators
Attached please find Licensee Event Report 414/04-001
Revision 0, entitled "Reactor Coolant System Pressure
Boundary Leakage Due to Small Cracks Found in.Steam
Generator Channel Head Bowl Drain Line on 2C & 2D Steam
Generators."
This Licensee Event Report does not contain any regulatory
commitments. Questions regarding this Licensee Event Report
should be directed to R. D. Hart at (803) 831-3622.
Sincerely,
Dhiaa Jamil
Attachment
www.dukepower.corn 00- U.S. Nuclear Reguldhory Commission
November 9, 2004
Page 2
XC: W.D. Travers
U.S. Nuclear Regulatory Commission
Regional Administrator, Region II
Atlanta Federal Center
61 Forsyth St., SW, Suite 23T85
Atlanta, GA 30303
E.F. Guthrie
Senior Resident Inspector (CNS)
U.S. Nuclear Regulatory Commission
Catawba Nuclear Station
S.E. Peters (addressee only)
NRC Project Manager (CNS)
U.S. Nuclear Regulatory Commission
One White Flint North, Mail Stop 10-B3
11555 Rockville Pike
Rockville, MD 20852-2738
NRC FORM 366� U.S. NUCLEAR REGULATORY APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004)� COMMISSION Estimated burden per response to comply with this mandatory collection request 50
hours. Reported lessons learned are Incorporated Into the licensing process and fed back
to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy
Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, WashinMon, DC 2055
LICENSEE EN/ENT REPORT (LER) 0001, or by Internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104). Office of Management(See reverse for required number of and Budget, Washington, DC 20503. If a means used to impose an Information col ectiond( inverse �for each block) does not display a currently valid OMB control number, the NRC may not conduct or sponsor. and a person Is not required to respond o. the Information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 050- 00414 1 OF�6 4. TITLE Reactor Coolant System Pressure Boundary Leakage Due to Small Cracks Found in
Steam Generator Channel Head Bowl Drain Line on 2C & 2D Steam Generators | | 05000368/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2004-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2004-001 | Gas Accumulation in Centrifugal Charging Pump Suction Piping | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000395/LER-2004-001 | Reactor Trip Due to Valve Failure During Forced Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000390/LER-2004-001 | Automatic Reactor Trip Due to a Invalid Turbine Trip Signal (P-4) | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2004-001 | Auxiliary Feedwater System in prohibited condition due to inadequate procedure. | | 05000454/LER-2004-001 | Exelent
Exelon Generation Company, LLCRwww.exeloncorp.com NuclearByron Station 4450 North German Church Road Byron, IL 61010-9794 October 17, 2004 LTR: BYRON 2004-0111 File: 2.01.0700 United States Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Subject:RLicensee Event Report (LER) 454-2004-001-00, "Reactor Containment Fan Coolers Flow Rates Below Technical Specification Requirements Due to Inaccurate Flow Indication" Byron Station, Unit 1
Facility Operating License No. NPF-37
NRC Docket No. STN 50-454
Enclosed is an LER involving the August 17, 2004, event involving low flow conditions discovered in Unit 1 Reactor Containment Fan Coolers for a time period longer than allowed by the Technical Specifications. This event is reportable to the NRC in accordance with 10CFR 50.73 (a)(2)(i)(B), as a condition prohibited by Technical Specifications. Should you have any questions concerning this matter, please contact Mr. William Grundmann, Regulatory Assurance. Manager, at (815) 234-5441, extension 2800. Respectfully, Stephen E. Kuczynski Site Vice President Byron Nuclear Generating Station Attachment LER 454-2004-001-00 cc:RRegional Administrator, Region III, NRC NRC Senior Resident Inspector— Byron Station NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7.2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T.6 E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail toLICENSEE EVENT REPORT (LER) *I@ nrc.gov, and to the Desk Officer, Office of Informabon and Regulatory Affairs, NEOB:10202 (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose information collection does not display a currently valid OMB control number, the NRC may not _ conduct or sponsor, and a person is not required to respond to, the information collection. 1 rand ITV NAUP o natuerr An warn q par= . Byron Station, Unit 1 0500454 1 OF 5 4. Reactor Containment Fan Coolers Flow Rates Below Technical Specifications Requirements Due to Inaccurate Flow Indication | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2004-001 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000336/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2004-002 | Dresden Nuclear Power Station Unit 2 05000237 1 of 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000244/LER-2004-002 | Consolidated Rod Storage Canister Placed in Incorrect Storage Location | | 05000530/LER-2004-002 | Main Turbine Control System Malfunction Results in Automatic Reactor Trip on Low DNBR | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000305/LER-2004-002 | | | 05000247/LER-2004-002 | Manual Reactor Trip Due to Decreasing 23 Steam Generator Level Caused by Feedwater Regulating Valve Closure Due to a De-energized Solenoid Operated Valve from Wiring Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000414/LER-2004-002 | Manual Reactor Trip Initiated Due to Control Rods from Shutdown Bank D Dropping into the Core | | 05000251/LER-2004-002 | AAA | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv)(b) | 05000397/LER-2004-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000346/LER-2004-002 | Reactor Trip During Reactor Trip Breaker Testing Due To Fuse Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2004-002 | Emergency Diesel Generator Start and Load Due to Momentary Fault on Incoming Feed | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000269/LER-2004-002 | eif Powere RON A. JONES Vice President A Duke Energy Company Oconee Nuclear Site Duke Power ONO1VP / 7800 Rochester Highway Seneca, SC 29672 864 885 3158 864 885 3564 fax September 9, 2004
U.S. Nuclear Regulatory Commission
Document Control Desk
Washington, D.C. 20555
Subject: Oconee Nuclear Station
Docket Nos. 50-269,-270, -287
Licensee Event Report 269/2004-02, Revision 1
Problem Investigation Process No.: 0-04-2808
Gentlemen:
Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached
is Licensee Event Report 269/2004-02, Revision 1, regarding
a Main Steam Line Break mitigation design/analysis
deficiency which could result in the main and startup
feedwater control valves being technically inoperable for
mitigation of some steam line break scenarios.
This report is being submitted to supplement Revision 0
submitted July 6, 2004. At that time the root cause
investigation and an analysis of the consequences of
potentially exceeding the Environment Qualification (EQ)
envelope curve were still in progress.
This event is being reported in accordance with 10 CFR
50.73 (a)(2)(i)(B) as a condition prohibited by Technical
Specifications, 50.73(a)(2)(ii)(B) as an Unanalyzed
Condition, and 50.73(a)(2)(V)(D) as a potential loss of
safety function for Accident Mitigation. This event is
considered to be of no significance with respect to the
health and safety of the public.
www.dukepower.corn Document Control Desk
Date: September 9, 2004
Page 2
Attachment: Licensee Event Report 269/2004-02, Revision 1
cc: Mr. William D. Travers
Administrator, Region II
U.S. Nuclear Regulatory Commission
61 Forsyth Street, S. W., Suite 23T85
Atlanta, GA 30303
Mr. L. N. Olshan
Project Manager
U.S. Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Washington, D.C. 20555
Mr. M. C. Shannon
NRC Senior Resident Inspector
Oconee Nuclear Station
INPO (via E-mail)
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7-2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T-6 E6), U.S. Nuclear Regulatory Commission, Washington. DCLICENSEE EVENT REPORT (LER) 20555-0001, or by Internet e-mail to bpi @nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management and(See reverse for required number of Budget, Washington, DC 20503. If a means used to impose information collection doesdigits/characters for each block) not display a currently valid OMB control number, the NRC may not conduct or sponsor, and,1 nnmnn lc not rent Owl to tocnnni-I to the intnrmatinn rntlentinn 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Oconee Nuclear Station, Unit 1 050-81 OF 0269 11 4. TITLE Main Steam Line Break Mitigation Design/Analysis Deficiency | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000313/LER-2004-002 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000271/LER-2004-002 | Special Nuclear Material Inventory Location Discrepancy | | 05000285/LER-2004-002 | Inoperable Diesel Generator for 28 Days Due to Blown Fuse During Shutdown | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2004-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000311/LER-2004-002 | Failure To Comply With Technical Specifications During Reactor Protection Instrument Calibration . | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2004-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-002 | | | 05000302/LER-2004-002 | Emergency Diesel Generator Inoperable Due To Fuel Oil Header Outlet Check Valve Leaking Past Seat | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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