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 Start dateReport dateSiteReporting criterionSystemEvent description
ENS 5668520 August 2023 20:00:00Fermi10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Reactor Coolant SystemThe following information was provided by the licensee via email: On 8/20/2023 at 1600 EDT, during plant walkdowns in the drywell while in mode 3 to identify a cause of increasing unidentified leakage rate, reactor coolant system pressure boundary leakage (approximately 2 gpm) was identified on the reactor recirculation sample line between the reactor recirculation sample line inboard isolation valve (B3100F019) and where the sample line taps off the B reactor recirculation jet pump riser. This requires entry into technical specification 3.4.4 condition C, identification of pressure boundary leakage with a required action to be in mode 3 in 12 hours and mode 4 in 36 hours. At 1630 EDT, a technical specification required shutdown to mode 4, cold shutdown, was initiated. A press release by DTE is anticipated. This event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i), a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(xi), and an eight-hour, non-emergency notification 10 CFR 50.72(b)(3)(ii)(A) for the degraded condition of the pressure boundary. Investigation into the cause of the reactor coolant system pressure boundary leakage is still ongoing. There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified.
ENS 565098 May 2023 07:07:00Cooper10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Core Spray

The following information was provided by the licensee via fax: At time 0207 CDT, Cooper Nuclear Station (CNS) entered Technical Specification (Limiting Condition for Operation) LCO 3.0.3 due to declaring core spray subsystems A and B inoperable. This declaration was based on an issue with relays installed from the same manufacturing batch. The ability of the relays to function correctly to annunciate loss of logic power was called into question and they were declared inoperable. The plant has initiated actions to repair/replace affected relays. This event is reportable under 10 CFR 50.72(b)(2)(i) as an initiation of any nuclear plant shutdown required by Technical Specifications. In addition, this event Is reportable under 10 CFR 50.72(b)(3)(v) as a condition that could have prevented the fulfillment of a safety function for the core spray systems. NRC Resident Inspector was notified.

  • * * UPDATE ON 5/8/2023 AT 1335 EDT FROM ANDREW ASKINS TO BRIAN LIN * * *

The following information was provided by the licensee via email: Technical Specification LCO 3.0.3 was exited at 0805 CDT on May 8, 2023. A reasonable expectation of operability was developed for the core spray subsystems A and B. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Shutdown was initiated and power was reduced approximately 45 percent. Reactor power is currently at 55 percent at the time of notification. Notified R4DO (Werner) via email.

  • * * UPDATE ON 5/9/2023 AT 1441 EDT FROM ANDREW ASKINS TO DONALD NORWOOD * * *

The following information was provided by the licensee via email: CNS is retracting the 8-hour 10 CFR 50.72(b)(3)(v) non-emergency notification, for a condition that could have prevented the fulfillment of a safety function, made on May 8, 2023, at 0207 CDT (EN# 56509). Subsequent evaluation concluded that the core spray subsystems remained operable in accordance with the Technical Specifications Requirements 3.5.1, ECCS - Operating. As a result of the core spray system remaining operable, no loss of safety function occurred. The NRC Senior Resident Inspector has been notified. Notified R4DO (Werner).

ENS 5649530 April 2023 06:00:00Hope Creek10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownPrimary containmentThe following information was provided by the licensee via email: At 0200 EDT on 04/30/23, a Technical Specification required shutdown was initiated at Hope Creek Unit 1. Technical Specification Action 3.6.1.1 Primary Containment Integrity was entered on 04/30/23 at 0100 with a required action to restore primary containment integrity within 1 hour. This required action was not completed within the allowed outage time; therefore, a Technical Specification required shutdown was initiated, and this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5640310 March 2023 08:37:00Waterford10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownReactor Coolant SystemThe following information was provided by the licensee via email: On 03/09/2023 at 2200 CST, Waterford (Unit) 3 entered OP-901-111, Reactor Coolant System Leakage, and OP-901-403, High Activity In Containment, due to elevated reactor coolant system (RCS) leakage in containment. On 03/10/2023, at 0030 Operations entered Technical Specification 3.4.5.2 action (c) due to unidentified leakage exceeding 1 gallon per minute (gpm). Technical Specification 3.4.5.2 action (c) requires reducing the leakage rate to within limits within 4 hours or be in at least hot standby within the next 6 hours and in cold shutdown within the following 30 hours. On 03/10/2023 at 0237 the plant discovered an unisolable RCS leak in the reactor coolant pump 1B cubicle and initiated action to complete a plant shutdown required by Technical Specifications. This event is being reported as a 4-hour report in accordance with 10 CFR 50.72(b)(2)(i) as the initiation of plant shutdown required by technical specifications. Reactor was tripped at 0521 CST on 3/10/2023.
ENS 5628423 December 2022 20:13:00Davis Besse10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownThe following information was provided by the licensee via email: At 1513 EST on 12/23/22, a Technical Specification required shutdown was initiated at the Davis-Besse Nuclear Power Station Unit 1. Technical Specification (TS) Action Limiting Condition of Operation (LCO) 3.7.9 for Ultimate Heat Sink water level minimum requirements was not met and condition 'A' was entered on 12/23/22 at 1412 EST with a required action to `Be in Mode 3' with a completion time of 6 hours and `Be Mode 5' with a completion time of 36 hours. This event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. At 1640 on 12/23/22, the NRC granted enforcement discretion for the shutdown requirements of TS LCO 3.7.9 and the shutdown was terminated with the unit remaining in Mode 1.
ENS 5605920 August 2022 04:42:00Grand Gulf10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownAutomatic Depressurization System

The following information was provided by the licensee via fax or email: At 2342 CDT on August 19, 2022, with Grand Gulf Nuclear Station in Mode 1 and at 40 percent power, the station initiated a normal shutdown to comply with its Technical Specifications (TS). The station entered Mode 3 at 0000 CDT August 20, 2022 to comply with (LCO) 3.5.1 Condition G Action G.1 due to the condition reported to NRC previously (EN 56058). This event is being reported under 10 CFR 50.72(b)(2)(i) as a shutdown required by the plant's technical specifications. The NRC Senior Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The plant is now in a 36-hour LCO to be in Mode 4 due to Low Low Set Valves inoperability per TS 3.6.1.6.

  • * * RETRACTION ON 10/14/2022 AT 1311 FROM JEFF HARDY TO LAUREN BRYSON * * *

Grand Gulf Nuclear Station (GGNS) is performing this notification to retract event EN 56059 that was reported on August 20, 2022. Previously, GGNS notified the NRC that it had initiated a shutdown required by Technical Specifications to comply with Limiting Condition of Operation (LCO) 3.5.1 Condition G.1 due to the inoperability of four Automatic Depressurization System (ADS) valves. Following the shutdown, GGNS completed walkdowns and determined that the condition affected only one ADS valve. As a result, the shutdown to satisfy the required actions of TS LCO 3.5.1 Condition G.1 was not required. The NRC Resident Inspector has been notified of the retraction. R4DO (Kellar) was notified.

ENS 557345 February 2022 20:14:00Davis Besse10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownReactor Coolant SystemThe following information was provided by the licensee via email: At approximately 1402 EST on 2/5/2022, with the Unit in Mode 1 at approximately 98 percent power, Operations was performing a valve lineup and inadvertently isolated a portion of the Reactor Coolant System (RCS) Letdown System, resulting in the system relief valve lifting and entry into the Makeup and Purification System Malfunction Abnormal Procedure due to loss of letdown. Pressurizer level increased and Technical Specification (TS) Limiting Condition for Operation (LCO) 3.4.9 CONDITION A was entered at 1414 EST due to Pressurizer level not below the limit of 228 inches, which has a REQUIRED ACTION to restore Pressurizer level within one hour. A rapid plant down power was initiated at approximately 1430 EST to reduce Pressurizer level. At 1514 EST on 2/5/2022, TS LCO 3.4.9 CONDITION B was entered, which has a REQUIRED ACTION to place the Unit in MODE 3 in 6 hours and in MODE 4 in 12 hours. As the Unit was continuing to down power, this represents initiation of a Technical Specification required shutdown, and this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). At approximately 1542 EST the down power was stopped at 15 percent power. Pressurizer level was restored to less than 228 inches at approximately 1603 EST, and TS LCO 3.4.9 was exited. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 556937 January 2022 00:37:00Saint Lucie10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownOn January 6, 2022 at 1937 (EST), St Lucie Unit 2 commenced a reactor shutdown as required by Technical Specification 3.1.3.1 Action 'e', due to Control Element Assembly number 27 slipping from 133 inches to 120 inches withdrawn and unable to be recovered within the prescribed time limits. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 2 entered 6 hour LCO to shutdown to mode 3 at 1539 EST as required by Technical Specification 3.1.3.1 Action 'e'. There was no impact on Unit 1.
ENS 5530311 June 2021 21:10:00Hatch10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown

At 1710 EDT on June 11, 2021, a Technical Specification required shutdown was initiated at Plant Hatch Unit 1. Technical Specification Condition 3.4.4.B unidentified LEAKAGE increase not within limits, was entered due to a greater than 2 gpm increase in unidentified LEAKAGE within the previous 24 hour period in MODE 1. This specification was entered on June 11, 2021, at 1615 EDT with a REQUIRED ACTION to restore leakage increase within limits within 4 hours. This REQUIRED ACTION could not be completed within the COMPLETION TIME; therefore, a Technical Specification required shutdown was initiated, and this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 6/17/2021 AT 1309 FROM JASON BUTLER TO JEFFREY WHITED * * *

Upon further review of the leakage rates, it was determined that at 1900 EDT on 6/11/2021 the drywell floor drain unidentified leakage increased greater than 2 gpm within the previous 24 hours while in MODE 1. Technical Specification (TS) 3.4.4.B was entered to reduce leakage increase to within limits within 4 hours. At 2000 EDT on 6/11/2021 unidentified leakage was reduced below the 2 gpm increase within the previous 24 hours due to actions taken to lower reactor power and pressure. Therefore, the TS required shutdown per TS 3.4.4.C was not applicable. Thus Event Report 55303 is being retracted. The NRC resident has been notified of the retraction. Notified R2DO (Miller).

ENS 5479621 July 2020 12:51:00Robinson10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownControl RodAt 0851 EDT on July 21, 2020, a Technical Specification required shutdown was initiated at Robinson Unit 2. Technical Specification LCO 3.0.3 was entered due to LCO 3.1.7 not being met as a result of indication loss on Control Rod positions with more than one position indication inoperable for a group. LCO 3.0.3 was entered at 0752 EDT to initiate action within 1 hour to place the unit in MODE 3 within 7 hours. Since a Technical Specification required shutdown was initiated, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). Technical Specification LCO 3.0.3 was exited at 1003 EDT on July 21, 2020. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Shutdown was initiated and power was reduced approximately 3 percent. Reactor power was back to 98.5 percent at the time of notification.
ENS 546871 May 2020 07:54:00Cook10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownReactor Coolant System

At 1000 EDT on May 1 2020, Operations commenced a shutdown of DC Cook Unit 2 to comply with LCO 3.4.13, Condition B Reactor Coolant System (RCS) pressure boundary leakage. At 0354 EDT on May 1, 2020, Operations detected an estimated 8 gpm Reactor Coolant System leak. The source of the leak could not be identified and Tech Spec 3.4.13, Condition A was entered for unidentified RCS leakage in excess of the 0.8 gpm limit. At 0745 EDT on May 1, 2020, Unit 2 entered LCO 3.4.13, Condition B when the 4-hour limit to complete the required actions of Condition A could not be met. At 0945 EDT on May 1, 2020, Unit 2 entered LCO 3.4.13, Condition B when the 4-hour limit to complete the required actions of Condition A could not be met. At 0945 EDT on May 1, 2020, inspections inside containment identified the leak as pressure boundary leakage from a pressurizer spray line which also requires entry into LCO 3.4.13, Condition B. At 1059 EDT on May 1, Unit 2 was tripped from 15 percent power. All systems functioned normally. This event is reportable under 10 CFR 50.72(b)(2)(i), the initiation of any nuclear plant shutdown required by the plant's Technical Specifications as a 4-hour report and under 10 CFR 50.72 (b)(3)(ii)(A), degraded condition, as an 8-hour report. The NRC Resident Inspector has been notified.

  • * * PARTIAL RETRACTION ON 5/15/2020 AT 1442 EDT FROM BUD HINCKLEY TO THOMAS HERRITY * * *

The condition identified in EN #54687, pursuant to 10 CFR 50.72 (b)(3)(ii)(a) has been evaluated, and has been determined not to be RCS pressure boundary leakage. As such, the 8-hour report is being retracted, as it is not an event or condition that results in, 'the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.' The leakage was subsequently determined to be from the tell-tale nipple of a pressurizer spray valve, not from the pressurizer spray line piping as previously reported. The Reactor Coolant Pressure Boundary (RCPB) is formed by the valve body, plug, seat, body to bonnet extension, and bonnet of the pressurizer spray valve. Therefore, the leakage is not RCPB leakage. There is no change to the 4-hour report made under 10 CFR 50.72(b)(2)(i), the initiation of any nuclear plant shutdown required by the plant's Technical Specifications. The NRC Resident Inspector was notified of this retraction. Notified R3DO (Stone).

ENS 546529 April 2020 05:00:00North Anna10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownReactor Coolant SystemOn April 9, 2020 at 0100 EDT, while performing a containment walkdown due to a small increased Reactor Coolant System (RCS) unidentified leakage, a leak was identified on the 'A' Reactor Coolant Pump (RCP) seal injection piping. The source of the leakage cannot be isolated and is considered RCS pressure boundary leakage. At that time, Condition B of Technical Specification (TS) LCO 3.4.13, 'RCS Operational Leakage' was entered due to pressure boundary leakage. TS 3.4.4 'RCS Loops - Mode 1 and 2' and Technical Requirement (TR) 3.4.6 'ASME Code Class 1, 2, and 3 Components' are also applicable. Unit 2 is projected to be taken to Mode 5 for repairs. This event is reportable in accordance with 10 CFR 50.72(b)(2) for 'Initiation of plant shutdown required by Technical Specifications' and 10 CFR 50.72(b)(3)(ii)(A) for 'Any event or condition that results in the condition of the nuclear power plant, including its principle safety barriers, being seriously degraded.' The licensee notified the NRC Resident Inspector. There is no effect on Unit 1
ENS 5460324 March 2020 16:05:00Brunswick10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownReactor Coolant System
Primary Containment Isolation System
Shutdown Cooling
At 1205 Eastern Daylight Time (EDT) on March 24, 2020, a Technical Specification-required shutdown was initiated on Unit 1 due to indication of a leak in the drywell. Technical Specification Action 3.4.4.A, Unidentified Reactor Coolant System (RCS) leakage increase not within limit, requires RCS leakage to be reduced to within limits within 8 hours. It was expected that the leakage would not have been reduced to within limits within the required Technical Specification completion time; therefore, this event is being reported in accordance with 10 CFR 50.72(b)(2)(i). Reactor water level reached low level 1 (LL1) following the reactor shutdown. The LL1 signal causes Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves), and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Due to the valid Primary Containment Isolation System (PCIS) actuation, this event is also being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). Unit 2 is not affected by this event. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5452413 February 2020 18:25:00Diablo Canyon10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownControl RodOn February 13, 2020, at 1025 hours (PST), during the performance of the quarterly control rod exercise surveillance test, Shutdown Bank 'B' Group 1 became misaligned greater than 12 steps from its group demand position. In accordance with Technical Specification 3.1.4, 'Rod Group Alignment Limits,' Action D, a Unit 2 shutdown to Mode 3 was commenced at 1233 hours. Investigation into the cause of the rod bank misalignment is in progress. There is no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 545082 February 2020 00:45:00Wolf Creek10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownAt 1845 CST on 2/1/2020, during surveillance testing (STS PE-015, Containment Purge Valve Leakage Test) containment leakage in excess of Technical Specification requirements was observed. A Technical Specification required shutdown was initiated at 2030 CST and Mode 3 was achieved at 2154 CST. All systems functioned as required during and following shutdown. The unit is proceeding to Mode 5. The licensee notified the NRC Resident Inspector.
ENS 5444918 December 2019 00:29:00Millstone10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownEmergency Diesel Generator
Residual Heat Removal
Decay Heat Removal
At 1929 EST, on 12/17/19, Millstone Unit 3 began preparations for shutting down the reactor as the 'A' Emergency Diesel Generator (EDG) could not be restored to operable status within the 14-day outage time, requiring a Technical Specification (Tech Spec) shutdown. Per Tech Spec 3.8.1.1., the reactor must be in Hot Standby in six (6) hours, and Cold Shutdown within the following 30 hours. Hot Standby is estimated by midnight, and Cold Shutdown by 1800 EST on 12/18/19. All other safety and shutdown systems are operable. Decay heat removal will be through the Shut Down Cooling and Residual Heat Removal systems. There was no impact to Unit 2. There was no impact to the health and safety of the public or plant personnel. The licensee notified the state of Connecticut, Waterford County, and the NRC Resident Inspector.
ENS 5432511 October 2019 17:00:00Calvert Cliffs10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownAt 1300 EDT, a Technical Specification required shutdown was initiated at Calvert Cliffs Unit 1. Technical Specification Action 3.1.4.C (Restore Control Element Assembly (CEA) alignment) was entered on 10/11/2019 at 1100 EDT, with a Required Action to reduce thermal power to less than 70 percent Rated Thermal Power and restore CEA alignment within 2 hours. This Required Action was not completed within the Completion Time; therefore, a Technical Specification required shutdown was initiated, and this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). At 1345 EDT, CEA alignment was restored and Technical Specification 3.1.4 (Control Element Assembly Alignment) was met. Reactor Power is being stabilized. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5419131 July 2019 17:06:00Waterford10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Reactor Coolant SystemOn July 31, 2019, at 1206 CDT, Waterford 3 commenced initiation of a plant shutdown as required by Technical Specification (TS) Limiting Condition for Operation (LCO) 3.0.3. Prior to this, on July 31, 2019, at 1108 CDT, the boron injection flow paths were declared inoperable in accordance with LCO 3.1.2.2, 'Flow Paths - Operating,' and the charging pumps were declared inoperable in accordance with LCO 3.1.2.4, 'Charging Pumps-Operating.' This was due to visual examination identifying that propagation had progressed on a previously identified flaw on piping upstream of the header supplying the charging pumps. TS LCO 3.0.3 was entered due to the action statements of LCOs 3.1.2.2 and 3.1.2.4 not being met. LCO 3.0.3 requires that action shall be initiated within one hour to place the unit in a mode in which the specification does not apply by placing it in hot standby within the next 6 hours and cold shutdown within the next 30 hours. At 1206 CDT, Waterford 3 commenced direct boration to the reactor coolant system. This condition meets the reporting criteria of 10 CFR 50.72(b)(2)(i) due to the initiation of plant shutdown required by Technical Specifications and 10 CFR 50.72(b)(3)(v)(A) and (D) due to an event or condition that could have prevented fulfillment of a safety function of structures or systems that are needed to (A) shutdown the reactor and maintain it in a safe shutdown condition and (D) mitigate the consequences of an accident.
ENS 5407822 May 2019 06:56:00Susquehanna10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
HVAC

On 5/22/2019, the 'A' Control Structure Chiller (Div I) tripped due to a loss of (motor control center) MCC 0B136. The 'B' Control Structure Chiller was already inoperable due to Div II (Emergency Service Water) ESW being out of service for planned maintenance. With the loss of Control Structure HVAC System the ability to maintain temperatures in various spaces including relay rooms, Control Room Floor Cooling and Emergency Switchgear rooms was lost. The 'B' Control Structure Chiller was restarted at 0251 EDT and cooling was reestablished to the required areas, however the 'B' chiller is not considered operable at this time. Units 1 and 2 entered (Technical Specification) TS 3.0.3 at 0256 EDT and a controlled shutdown of both units commenced, Unit 2 at 0340 EDT and Unit 1 0350 EDT. This constitutes a TS required shutdown and requires a 4 hour (Emergency Notification System) ENS notification in accordance with 10 CFR 50.72(b)(2)(i). The failure also requires an 8 hour ENS notification in accordance with 10 CFR 50.72(b)(3)(v) due to the loss of a safety function. The licensee needs to restore the 'B' loop of ESW to exit the Limiting Condition of Operation (LCO). The licensee is currently performing a flow surveillance, once complete and assuming the data is acceptable, the licensee will be able to exit the LCO. The units are in a normal electrical lineup. The licensee will be notifying the state of Pennsylvania FEMA Operations Center. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE ON 05/22/2019 AT 1302 FROM SCOTT MYRTHEL TO THOMAS KENDZIA * * *

On 5/22/2019 at 0601 EDT Susquehanna Steam Electric Station reported a shutdown had been commenced at 0340 EDT for Unit 2 and 0350 EDT for Unit 1 due to inoperability of both control structure chillers. Power has been restored to MCC 0B136, and at 0901 EDT the 'A' control structure chiller was declared operable and LCO 3.0.3 was exited. Power reduction for both units was halted at 0901 EDT and preparations for power restoration initiated. As of 1255 EDT on 5/22/2019, Unit 1 power is 94% and Unit 2 power is 92%. Notified the R1DO (Arner).

ENS 5396128 March 2019 18:50:00Brunswick10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Reactor Coolant System

At 1450 EDT on March 28, 2019, the licensee observed that the Unit 1 unidentified Reactor Coolant System (RCS) leakage was greater than 10 gallons per minute (gpm) for greater than or equal to 15 minutes. The licensee declared an Unusual Event in accordance with their EAL SU 5.1. The licensee initiated a unit shutdown in accordance with their procedures and the unit was approximately 58 percent reactor power at 1507 EDT, with unit shutdown in progress. The licensee also received an alarm due to increasing Drywell Pressure at 1.7 pounds drywell pressure. At 1600 EDT the licensee called with an update. Unit 1 was still in an Unusual Event with the unit at 37 percent power with the shutdown continuing. Drywell Pressure had decreased to 0.8 pounds. At 1603 the licensee scrammed Unit 1. Notified DHS SWO, FEMA Operations Center, DHS NICC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE ON 3/28/2019 AT 1808 EDT FROM MARK TURKAL TO THOMAS KENDZIA * * *

At 1437 EDT on March 28, 2019, with Unit 1 in Mode 1 at approximately 100 percent power, a Technical Specification-required shutdown was initiated due to indication of a leak in the drywell. Technical Specification Action 3.4.4.A, Unidentified Reactor Coolant System (RCS) leakage increase not within limit, requires RCS leakage to be reduced to within limits within 8 hours. It is expected that the leakage would not have been reduced to within limits within the required Technical Specification completion time; therefore, this event is being reported in accordance with 10 CFR 50.72(b)(2)(i). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 03/29/19 AT 0302 EDT FROM TOM FIENO TO BETHANY CECERE * * *

At 0259 EDT on March 29, 2019, the Unusual Event was terminated because RCS leakage was reduced to less than 10 gallons per minute. The most recent leakage rate measured at 0225 EDT was 3.9 gpm. The source of the leak will be identified when plant conditions allow containment entry. No elevated radiation levels were observed during this event. Drywell pressure is currently 0.0 psig. Unit 1 is in Mode 4. The licensee notified the NRC Resident Inspector. Notified R2DO (Bonser), NRR EO (Miller), IRD MOC (Grant), DHS SWO, FEMA Operations Center, DHS NICC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

ENS 5367821 October 2018 05:00:00Browns Ferry10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown

At 0200 Central Daylight Time on 10/21/2018, Browns Ferry Nuclear Plant Unit 3 commenced a reactor shutdown as required by the Technical Requirements Manual Limiting Condition for Operation 3.4.1 Coolant Chemistry Condition D due to conductivity greater than 10 micro mho/cm at 25 degrees Celsius. The required action for this condition is to immediately initiate an orderly shutdown and be in Mode 4 as rapidly as cooldown rate permits. This event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). There was no impact on the health and safety of the public or plant personnel. The NRC Senior Resident Inspector has been notified.

  • * * RETRACTION AT 1719 EST ON 12/13/2018 FROM NEEL SHUKLA TO MARK ABRAMOVITZ * * *

ENS Event Number 53678, made on 10/21/18, is being retracted. NRC notification 53678 was made to ensure that the four-hour non-emergency reporting requirements of 10 CFR 50.72 were met when the licensee discovered a condition requiring shut down of a reactor. 10 CFR 50.72 requires a report in accordance with 50.72(b)(2)(i) for any Technical Specifications (TS) required reactor shutdown. NUREG-1022 only specifies TS applicability and makes no mention of a Technical Requirements Manual (TRM) required shutdown. Because the shutdown comes from the TRM and not the TS as discussed in 10 CFR 50.72 and NUREG-1022, an EN was not required. TVA's evaluation of this event notification is documented in the corrective action program. The licensee notified the NRC Resident Inspector. Notified the R2DO (Ehrhardt).

ENS 5361721 September 2018 04:00:00Peach Bottom10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
High Pressure Coolant Injection
Reactor Core Isolation Cooling
Emergency Core Cooling System

On 9/21/18, at 1755 EDT, Peach Bottom Atomic Power Station Unit 3 declared the High Pressure Coolant Injection system (HPCI) inoperable due to an inoperable differential pressure indicating switch (DPIS). The DPIS is used to isolate the HPCI system when there is a high steam line flow condition. Operations declared the HPCI system inoperable and entered Technical Specification 3.5.1 Condition C for HPCI being inoperable. Technical Specification 3.3.6.1 was also entered for HPCI instrumentation being inoperable. Other standby systems (Reactor Core Isolation Cooling and Low Pressure Emergency Core Cooling Systems) are OPERABLE. HPCI is a single train system. Therefore, per NUREG-1022, this condition is being reported pursuant to 10CFR 50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of the safety function of a system required to mitigate the consequences of a design event. This condition has been entered into the corrective action program (IR 4175355). Investigation of the exact cause of the indication issue is in progress. The NRC Resident has been informed of this notification.

  • * * UPDATE AT 1317 EDT ON 09/22/2018 FROM CRAIG TAULMAN TO JEFF HERRERA * * *

On 09/22/18 at 0955 EDT, RCS (Reactor Coolant System) pressure boundary leakage was identified as the cause of the HPCI high steam flow indication issue. Technical Specification 3.4.4 was entered which will require the initiation of a nuclear plant shutdown. This indicates a degradation of a principal safety barrier. Current Unit 3 reactor power is 35%. This condition is being reported pursuant to 10 CFR 50.72(b)(2)(i) and 50.72(b)(3)(ii). This condition is being tracked in the corrective action program (IR 4175355). The NRC Resident has been informed". Peach Bottom will be notifying State and local agencies regarding the event. Notified the R1DO (Greives).

ENS 535897 September 2018 04:00:00Indian Point10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
(Indian Point Unit 3) entered Technical Specification 3.0.3 for Safety Injection Boron Injection Tank Header Inoperable due to a thru weld leak at the thermal well rendering two Safety Injection Pumps Inoperable. Plant shutdown was started 1803 hours EDT. The licensee plans to be in Mode 4 at 0600 EDT on 9/8/2018. There is no impact to Unit 2. The licensee notified the NRC Resident Inspector and the State of New York.
ENS 5354812 August 2018 04:00:00Beaver Valley10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Emergency Diesel Generator

EN Revision Text: TECHNICAL SPECIFICATION REQUIRED SHUTDOWN - LOSS OF 480 VOLTAGE EMERGENCY BUS On 8-12-18 at 0158 EDT, Beaver Valley Unit 2 experienced a loss of 480 Volt 2P Emergency Bus. This resulted in a Loss of Safety Function due to the 2-2 Emergency Diesel Generator (EDG) being Inoperable coincident with the Residual Heat Release Valve (2SVS-HCV104). A Technical Specification shutdown is required per LCO 3.0.3. The Licensee also stated they were in an unanalyzed condition due to the EDG and Residual Heat Release Valve being inoperable at the same time. The Licensee is shutting down to Mode 5 (Cold Shutdown). The Licensee is notifying the Resident Inspector. The Licensee will be making a Press Release about the unplanned shutdown.

  • * * UPDATE ON 08/16/2018 AT 1424 EDT FROM BLASE BARTKO TO KEN MOTT * * *

On 8-12-18 at 0158 (EDT) Beaver Valley Unit 2 experienced a loss of 480 Volt 2P Emergency Bus. Per operational guidance, this was determined to be a Loss of Safety Function due to the Unit 2 Emergency Diesel Generator (EDG) being INOPERABLE coincident with the Residual Heat Release Valve (2SVS-HCV104) 10 CFR 50.72(b)(3)(v)(B) and (D). This was also reported as an Unanalyzed Condition 10 CFR 50.72(b)(3)(ii)(b). No Press Release was performed for this event. The NRC Resident Inspector was notified. At 0410 (EDT) a Technical Specification Shutdown was commenced 10 CFR 50.72(b)(2)(i). At 2011 (EDT) the 480 Volt 2P Emergency Bus was restored and energized. Further evaluation of the event has determined that this event was not an Unanalyzed Condition and did not result in a Loss of Safety Function. The classifications of Unanalyzed Condition and Loss of Safety Function are being retracted. The accuracy of the existing guidance relative to Safety Function has been entered in the Corrective Action Program and interim actions have been taken to provide accurate guidance. Notified R1DO (Young) via email.

ENS 5341922 May 2018 04:00:00Beaver Valley10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown

EN Revision Text: GAS VOIDS DISCOVERED IN BOTH TRAINS OF LOW HEAD SAFETY INJECTION On 5/22/2018, while operating at approximately 100 percent power, Ultrasonic Testing of the Beaver Valley Power Station (BVPS) Unit 1 Low Head Safety Injection (LHSI) pump suction piping identified gas voids in excess of the acceptable limit for void volume. Both trains of LHSI were declared inoperable. Technical Specification (TS) 3.5.2 for both trains of the LHSI system was entered along with TS 3.0.3 which requires the initiation of a plant shutdown. Time of TS entry was 12:56 (EDT). Plant shutdown was commenced at 15:56 (EDT) in accordance with plant procedures. At 15:59 (EDT) Train 'A' LHSI was restored to operable status, TS 3.0.3 Action was exited and the power reduction was stopped at approximately 99 percent. At 17:43 (EDT) Train 'B' LHSI was restored to operable status, TS 3.5.2 Actions were exited. This is reportable per 10 CFR 50.72(b)(3)(ii) Unanalyzed Condition, 10 CFR 50.72(b)(3)(v) Event or Condition that Could Have Prevented the Fulfillment of a Safety Function and 10 CFR 50. 72(b )(2)(i) TS Required Shutdown. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 6/21/18 AT 1535 EDT FROM SHAWN KEENER TO RICHARD SMITH * * *

Further engineering evaluation has determined that the gas voids that existed at the time of discovery would not have rendered the LHSI (Low Head Safety Injection) system inoperable if it were required to actuate. The engineering evaluation concluded that filling of the containment sump during a Design Basis Accident would result in a void volume reduction such that the void in the LHSI suction piping would not be large enough to significantly impact the operability of the system. Therefore, the system remained operable but degraded. No TSs (Technical Specifications) were required to be entered and no shutdown was required. As such, all three reporting criteria do not apply and are being retracted. The NRC Resident Inspector has been notified. Notified R1DO (Burritt).

ENS 5327622 March 2018 08:00:00LaSalle10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Reactor Coolant System
Reactor Recirculation Pump
This notification is being provided in accordance with 10CFR50.72(b)(2)(i), Plant Shutdown required by Technical Specifications, and 10 CFR 50.72(b)(3)(ii)A, Degraded or Unanalyzed Condition. At 0300 CDT on 3/22/18, on LaSalle Unit 1, a through-wall (welded joint) leak was identified on a 3/4 inch vent line off of the bonnet of the 1B33-F067B, 1B Reactor Recirculation Pump Discharge Valve. This condition qualifies as pressure boundary leakage, which requires entry into Technical Specification 3.4.5, Reactor Coolant System Operational Leakage, Required Action C, to be in Mode 3, Hot Shutdown, by 1500 on 3/22/18 and Mode 4, Cold Shutdown, by 1500 on 3/23/18. This leakage is significantly less than 10 gallons per minute and therefore, does not meet the threshold for entry into the Emergency Action Plan. At the time of discovery, Unit 1 was in Mode 1 - Run. Shutdown began at 0500 CDT and the estimated completion to cold shutdown is 2000 CDT. All necessary shutdown equipment is available. There is no impact to Unit 2. NRC Resident Inspector was notified.
ENS 530004 October 2017 06:50:00Perry10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
HVAC
High Pressure Core Spray

On October 4, 2017, at 0250 hours (EDT), the Perry Nuclear Power Plant commenced a Technical Specification (TS) shutdown by lowering reactor power from 100 percent rated thermal power to 98 percent to comply with TS LCO 3.0.3. Reactor power was further reduced to 82 percent rated thermal power at 0430 hours (EDT). The plant had entered TS 3.0.3 at 0155 hours (EDT) upon loss of MCC (Motor Control Center), Switchgear, and Miscellaneous Electrical Equipment Areas HVAC System train A while train B was removed from service for maintenance. MCC switchgear ventilation train A was declared inoperable based on excessive belt noise and a dropped belt on MCC switchgear supply fan A. This also constitutes a loss of safety function. This event is being reported in accordance with 10 CFR 50.72(b)(2)(i) and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector was notified.

  • * * UPDATE ON 10/04/17 AT 0926 EDT FROM DAN HARTIGAN TO STEVEN VITTO * * *

Due to the loss of both trains of MCC, Switchgear, and Miscellaneous Electrical Equipment Areas HVAC, actions were taken in LCO 3.8.7 for AC and DC Distribution Systems, LCO 3.8.4 for DC Sources, LCO 3.8.1 for AC Sources, and the associated support systems, the High Pressure Core Spray system was also declared inoperable, which is a single train safety system and therefore, an additional loss of safety function. This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(B), 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72 (b)(3)(v)(D). At 0620 hours (EDT) the A train of MCC, Switchgear, and Miscellaneous Electrical Equipment Areas HVAC and High Pressure Core Spray was declared operable and LCO 3.0.3 was exited. The plant was restored to 100% (percent) power at 0804 (EDT). The NRC Resident Inspector was notified. Notified R3DO(Hills).

ENS 5293629 August 2017 17:00:00Grand Gulf10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownResidual Heat Removal
Containment Spray

On August 22, 2017 at 2321 hours, Grand Gulf Nuclear Station entered Technical Specification conditions for three Limiting Condition for Operations (LCOs) not met due to Residual Heat Removal 'A' (RHR 'A') being declared inoperable. LCOs not met:

  1) 3.5.1 for one low pressure ECCS (Emergency Core Cooling System) injection/spray subsystem.
  2) 3.6.1.7 for one RHR containment spray subsystem, and
  3) 3.6.2.3 for one RHR suppression pool cooling subsystem.

The station has made the decision to shutdown the plant based on the results of troubleshooting performed on the RHR 'A' pump. The restoration of RHR 'A' pump will not be completed prior to the end of the 7 day LCO completion time. Grand Gulf Nuclear Station initiated plant shutdown required by Technical Specifications 3.5.1, 3.6.1.7, and 3.6.2.3 at 1200 hours CDT on 08/29/2017 due to expected restoration of RHR 'A' exceeding the completion time of 7 days prior to restoring operability. The licensee notified the NRC Resident Inspector.

ENS 528949 August 2017 20:06:00Surry10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Reactor Coolant SystemOn 8/9/17, a Unit 1 containment entry was made in order to investigate increased Reactor Coolant System (RCS) unidentified leakage. The team noted a through-wall leak from the tubing/socket weld area of 'C' Hot Leg Sample Valve. The sample valve and RCS pressure boundary were declared inoperable, and a 6-hour action statement to place Unit 1 in Hot Shutdown was entered at 1338 (EDT) hours as required by Technical Specification 3.1.C.3. At 1606 (EDT) hours on 8/9/17, Unit 1 shutdown was commenced, and at 1637 (EDT), Unit 1 was at Hot Shutdown. This report is being submitted pursuant to 10CFR50.72(b)(2)(i) as a result of power reduction required by Technical Specifications. Further, this report is being submitted pursuant to 10CFR50.72(b)(3)(ii)(A) for any event or condition that results in the condition of the nuclear power plant, including its principle safety barriers, being seriously degraded. The NRC Resident (Inspector) has been notified of this event and is on site. There was no radiation release associated with this event, nor were there any personnel injuries or contamination events.
ENS 5262318 March 2017 15:07:00Turkey Point10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Emergency Diesel Generator
Auxiliary Feedwater

On 3/18/17 at 1107 (EDT), the Unit 3 reactor tripped as a result of the loss of the 3A 4kV bus. All three reactor coolant pumps (RCP) tripped and the 3B RCP was restarted for forced recirculation. The reactor is stable in Mode 3. The 3A 4kV bus remains deenergized until troubleshooting and repairs are complete. In addition, Technical Specification 3.8.1.1, Action C requires a four hour report for the concurrent inoperability of the Unit 4 startup transformer to Unit 3 via the 3A 4kV bus and the Unit 3 3A diesel generator. The NRC Senior Resident Inspector will be notified.

  • * * UPDATE ON 3/18/2017 AT 1854 EDT FROM JAMES SPICHER TO BETHANY CECERE * * *

Update to previous report (EN 52623) to include additional reporting criteria. On 3/18/17 at 1107 (EDT) the Unit 3 reactor tripped as a result of the loss of the 3A 4kV bus. The 3A Emergency Diesel Generator (EDG) started on the loss of power signal but did not load, as designed, due to the bus fault. The 3A EDG was manually stopped at 1332. The Auxiliary Feedwater (AFW) System also initiated as expected. AFW was stopped at 1135. The actuations of the 3A EDG and AFW are reportable in accordance with 10 CFR 50.72(b)(3)(iv)(A). A loss of safety function affecting Units 3 and 4 occurred due to the loss of the 3A high head safety injection (HHSI) pump because it could not be powered from the faulted 3A 4kV bus with both Unit 4 HHSI pumps earlier (0624) removed from service due to planned maintenance. This caused three of the four HHSI pumps to be inoperable. The four HHSI pumps are shared by both Units 3 and 4. The safety function is achieved by two of the four HHSI pumps. Both Unit 4 HHSI pumps were restored to operable status at 1336. The loss of safety function is reportable in accordance with 10 CFR 50.72(b)(3)(v)(D). The Unit 3 reactor is stable in Mode 3. The 3A 4kV bus remains deenergized until troubleshooting and repairs are complete. Unit 4 remains operating at 100% power. The licensee will notify the NRC Resident Inspector. Notified R2DO (Ehrhardt) and NRR EO (Miller).

ENS 5258128 February 2017 15:00:00Salem10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Reactor Coolant System

On February 28, 2017 at 0930 (EST), a containment visual inspection was performed to identify the source of elevated RCS (Reactor Coolant System) leakage. A leak was identified between 13RC6 and 13SS661, 13 RCS hot leg sample isolation valves at 1000 (EST). These valves are manual isolation valves in the reactor coolant hot leg sample line. Leak isolation could not be initially verified and is considered RCS pressure boundary leakage. Salem Unit 1 entered Technical Specification 3.4.6.2a, RCS operational leakage, for the existence of pressure boundary leakage. This event is being reported under the requirements of 10 CFR 50.72(b)(2)(i) for 'The initiation of a plant shutdown required by Technical Specifications' and 10 CFR 50.72(b)(3)(ii)(A) or 'Any event of condition that results in the condition of the nuclear power plant, including its principal safety barriers being seriously degraded.' The unit was placed in mode 3 at 1554 (EST) on 02/28/2017. This condition has no impact on public health and safety. Per Technical Specifications, the unit is proceeding to mode 5. The leak rate at the time of shutdown was 0.33 gpm. This event has no effect on Unit 2. The licensee has notified the NRC Resident Inspector. The licensee will be notifying the Lower Alloways Creek Township, the State of New Jersey and the State of Delaware.

  • * * RETRACTION FROM MATT MOG TO HOWIE CROUCH AT 1144 EDT ON 4/14/17 * * *

The purpose of this notification is to retract event report number 52581 made on 2/28/2017 at 1624 (EST). Previously, PSEG notified the NRC that Salem Unit 1 initiated a shutdown required by Technical Specifications (TS) for Reactor Coolant System (RCS) Pressure Boundary Leakage. Subsequent to the initial report, PSEG has determined that the leak occurred in tubing downstream of the design specification break between Safety Related, Nuclear Class 1, Seismic Class1 and Non-Safety-Related, Nuclear Class 2, Seismic Class 2. Therefore, the observed leakage is not RCS pressure boundary leakage as defined in the Salem Unit 1 Technical Specifications and in the tubing design classification specification. At the time of the event, during initial entry into the containment, the volume of steam present and the height of the break above the floor made it difficult to ascertain the location of the steam source with certainty. The initial judgment of RCS Pressure Boundary Leakage was conservative under these circumstances. The plant was taken offline to minimize radiation exposure when personnel operated the isolation valves. Following the shutdown, the leak was isolated. Based on an observed reduction in RCS leak rate and visual verification of leakage isolation, the TS Limiting Condition for Operation (LCO) was exited and the unit remained in Mode 3, Hot Standby, to affect repairs. The condition did not meet the Technical Specification Pressure Boundary Leakage definition of leakage through a non-isolable fault in a RCS component body, pipe wall or vessel wall. The leakage did not impact the ability to shut down the unit and no TS limits were exceeded during this event. Therefore, the plant shutdown to investigate and correct leakage from flawed sample system tubing does not meet the reporting requirements of 10 CFR 50.72 and PSEG is retracting the notifications made under 10 CFR 50.72(b)(2)(i) and 10 CFR 50.72(b)(3)(ii)(A). The NRC Resident Inspector was notified of this retraction by the licensee. Notified R1DO (Jackson).

ENS 5257324 February 2017 00:22:00McGuire10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
On February 23, 2017, a containment visual inspection was performed to identify the source of elevated RCS (Reactor Coolant System) leakage. A leak was identified at the nozzle connection of the boron injection line to 2D RCS cold leg at 1922 (EST). It was determined that the leak cannot be isolated and is considered RCS pressure boundary leakage. Unit 2 entered TS LCO 3.4.13, RCS Operational Leakage, Condition B, for the existence of pressure boundary leakage. This event is reportable in accordance with 10CFR50.72(b)(2)(i) (4 hours) for 'initiation of plant shutdown required by Technical Specifications' and 10CFR50.72(b)(3)(ii)(A) (8 hours) for 'any event or condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.' The unit will shutdown and repairs will be performed in Mode 5. This condition has no impact on public health and safety. The licensee has informed the NRC Resident Inspector. At the time of the event notification, Unit 2 was at 33 percent power. Unidentified RCS leakage is estimated at 0.28 gpm. Unit 2 is expected to be in Mode 3 by 0122 EST on 02/24/2017. Unit 1 is not affected by this event.
ENS 5242310 December 2016 01:42:00Vogtle10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownOn December 09, 2016 at 1734 EST, U2 Train-A NSCW (Nuclear Service Cooling Water) Transfer Pump #8 tripped during Return To Service Surveillance testing for Train-B NSCW Transfer pump #7. Technical Spec 3.7.9 Condition E entered at 1734 with Required Actions to be in M3 (mode 3, Hot Standby) in 6 hours AND M4 (mode 4, Hot Shutdown) in 12 hours. A unit shutdown was commenced at 2042 EST (as a conservative measure) to comply with TS 3.7.9 Condition E. At 1937, U2 B-train NSCW Transfer Pump #7 was declared operable and TS 3.7.9 Condition E was exited. The plant is currently raising power to 100%. The licensee notified the NRC Resident Inspector.
ENS 5237418 November 2016 00:59:00Farley10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownAt 1859 CST on November 17, 2016, Farley Nuclear Plant Unit 1 initiated a shutdown from approximately 99 percent reactor power. The shutdown was initiated per Technical Specification LCO 3.0.3. This LCO entry was based on having no operable steam flow channels on the C loop for Farley Nuclear Plant Unit 1. Unit 2 as not affected. The NRC Resident Inspector has been notified.
ENS 5226728 September 2016 12:45:00Arkansas Nuclear10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownEmergency Diesel GeneratorOn September 16, 2016, at 0036 (CDT), during a 24-hour Technical Specification (TS) endurance run, the Arkansas Nuclear One, Unit 2 (ANO-2) red train Emergency Diesel Generator (EDG) became inoperable when its inboard generator bearing failed. ANO-2 TS 3.8.1.1, 'AC Sources', requires an inoperable EDG to be restored to service within 14 days or actions to place the unit in a shutdown condition initiated. It has been determined that repair options cannot be completed within the Allowed Outage Time (AOT) due to unforeseen circumstances which evolved during recovery efforts. At 0745 (CDT), ANO-2 initiated plant shutdown due to the inability to restore the red train EDG. ANO-2 will be shutdown and cooled down to Mode 5. The licensee informed the NRC Resident Inspectors.
ENS 522258 September 2016 08:00:00Grand Gulf10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownResidual Heat Removal
Containment Spray
On September 4, 2016 at 0258 (CDT), Grand Gulf Nuclear Station entered three (Technical Specification) Limiting Conditions for Operations (LCOs) due to residual heat removal pump 'A' (RHR 'A') being declared inoperable. LCOs entered: 1) 3.5.1 for one low pressure ECCS injection/spray subsystem, 2) 3.6.1.7 for one RHR containment spray subsystem, and 3) 3.6.2.3 for one RHR suppression pool cooling subsystem. Station management has made the decision to shutdown the plant to repair the RHR 'A' pump prior to the end of the 7 day LCO completion time based on troubleshooting and testing performed on the RHR 'A' pump. Grand Gulf Nuclear Station initiated plant shutdown required by Tech Spec Actions 3.5.1, 3.6.1.7, and 3.6.2.3, at 0300 CDT on 09/08/2016 due to expected inability to restore RHR 'A' to operable status prior to exceeding the LCO time of 7 days. The unit is currently at 82 percent power. There are no other systems out of service that would complicate the orderly shutdown to Mode 4. The licensee will notify the NRC Resident Inspector.
ENS 522182 September 2016 13:08:00Wolf Creek10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownReactor Coolant System

While operating in MODE 1 at 100 percent rated thermal power and placing Excess Letdown in service for Reactor Coolant System (RCS) leak detection, RCS operational leakage exceeded 1 gpm (gallon per minute) unidentified leakage as identified by performing RCS Water Inventory Balance using the Nuclear Plant Information System Computer. This required the entry into Technical Specification (TS) Limiting Condition of Operation (LCO) 3.4.13 Condition B at 0808 (CDT) on 9/2/16. The associated action is to place the unit into Mode 3 in 6 hours. Trending of containment sump level indicates the leakage is inside containment with the exact location within containment unknown. Containment inspection is being performed to try and identify the source of Reactor Coolant System leakage. NRC Resident Inspector has been notified. Re-alignment of the Letdown System back to its normal arrangement has subsequently reduced RCS leak rate to 0.521 gpm at 0652 CDT on 9/2/16. Unusual or Not Understood - Leak Location is not known at this time. Maximum leak rate recorded was 1.358 gpm. The leak was first discovered at 08/31/16 at 1519 CDT. Safety Related Equipment not operational - Reactor Vessel Level Indicating System (TS 3.3.3).

  • * * RETRACTION AT 1101 EDT ON 10/21/2016 FROM LARRY HAUTH TO JEFF HERRERA * * *

Wolf Creek Nuclear Operating Corporation is retracting the 10 CFR 50.72(b)(2)(i) notification based on subsequent review of the event. The calculation of unidentified leak rate which triggered entry into the Mode 3 Required Action Statement was performed immediately after placing RCS Excess Letdown in service. An evaluation of the leak rate calculation determined that the leak rate was invalid due to performance of the RCS water inventory balance during non-steady state operating conditions. This was contrary to the requirements of TS Surveillance Requirement 3.4.13.1, as this test was performed while charging and letdown flows were being stabilized following the alignment of excess letdown. A walk down of the Excess Letdown system while in-service determined no leakage. Subsequent RCS water inventory balances performed with Excess Letdown in service under steady state operating conditions while in Mode 3 at normal operating pressure and temperature determined the maximum calculated unidentified leak rate was 0.675 gpm. After the plant entered Mode 3 a non-RCS pressure boundary leak was identified during equipment walk downs on a seal weld from the reactor vessel head core exit thermocouple nozzle assembly 77. The leakage did not impact the ability to shut down the unit. No TS limits were exceeded during this event. Therefore, the plant shutdown to investigate and correct leakage past the seal weld of a threaded connection does not meet the reporting requirements of 10 CFR 50.72. The NRC Resident Inspector has been notified. Notified the R4DO (Kramer).

ENS 521381 August 2016 07:42:00Saint Lucie10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownReactor Coolant System
Emergency Core Cooling System

On August 1, 2016 at 0342 EDT St. Lucie Unit 1 commenced a unit shutdown required by Technical Specifications due to Reactor Coolant System Pressure Boundary Leakage in excess of the allowable limit of zero leakage. The leak was initially identified on July 31, 2016 at 2115 EDT as not Pressure Boundary leakage. After further analysis, the leak was determined to be Reactor Coolant System Pressure Boundary leakage at 0123 on August 1, 2016. The leakage is estimated as less than one tenth of a gallon per minute and is not impacting the ability to shut down the unit. Additional impact of the leak is under evaluation. This report is submitted in accordance with 10CFR50.72(b)(2)(i) as 'The initiation of any nuclear plant shutdown required by the plant's Technical Specifications.' The location of the leak is on the Instrumentation piping welded connection at Flow Element FE-3311 attached to (the) Emergency Core Cooling System Injection header to Reactor Coolant System Loop 1A2. The leak activity is 0.167 microCuries per ml. The NRC Resident Inspector has been notified.

  • * * RETRACTION AT 1335 EDT ON 09/23/16 FROM RICHARD SCISCENTE TO JEFF HERRERA * * *

The purpose of this notification is to retract a previous report made on EN 52138. NRC notification was initially made as a result of a plant shutdown required by technical specifications (TS) for Reactor Coolant System (RCS) pressure boundary leakage. Subsequent to the initial report, St. Lucie has determined that the RCS leakage was from a seal weld on a threaded connection that was not pressure boundary leakage. However, the leak was non-isolable and required RCS depressurization to allow immediate investigation to ensure there were no faults in a RCS component body or pipe wall. The leakage was estimated to be less than one tenth of a gallon per minute and did not impact the ability to shut down the unit. No TS limits were exceeded during this event. Therefore, the plant shutdown to investigate and correct leakage past the seal weld of a threaded connection does not meet the reporting requirements of 10 CFR 50.72 or 10 CFR 50.73. The NRC Resident Inspector has been notified. Notified the R2DO (Blamey).

ENS 5213730 July 2016 15:52:00North Anna10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Reactor Coolant SystemOn July 30, 2016 at 1152 hours (EDT) following a containment walkdown to investigate an increase in RCS unidentified leakage to 0.15 gpm, a leak was identified on the seal return line from 2-RC-P-1C, 'C' Reactor Coolant Pump. The source of the leakage cannot be isolated and is considered RCS pressure boundary leakage. (Technical Specification) LCO 3.4.13, RCS Operational Leakage, Condition B for the existence of pressure boundary leakage was entered. Technical Requirement TR 3.4.6, ASME Code Class 1, 2, and 3 Components is also applicable. Unit 2 is projected to be taken to Mode 5 for repair. This event is reportable in accordance with 10 CFR 50.72(b)(2) for 'the initiation of any nuclear plant shutdown required by the plant's Technical Specifications' and 10 CFR 50.72(b)(3)(ii)(A) for 'any event or condition that results in the condition of the nuclear plant including its principal safety barriers, being seriously degraded.' The licensee will be notifying the Louisa County Administrator and has notified the NRC Resident Inspector.
ENS 5212928 July 2016 09:41:00Salem10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Reactor Coolant System
Auxiliary Feedwater
Decay Heat Removal
Control Rod
Main Steam

This four and eight hour notification is being made to report that at 0541 (EDT) on 7/28/16, Salem Unit 1 initiated a shutdown to comply with Technical Specifications due to the inoperability of both source range nuclear instruments. During a reactor startup, with Unit 1 in Mode 2, both source range instruments were reading approximately one decade lower than expected compared to intermediate range and Gamma-Metric instruments and due to the proximity to the estimated critical condition. The condition could also have prevented the fulfilment of the source range instruments safety function to trip the reactor when required. Salem Unit 1 is currently stable in Mode 3. Reactor Coolant system pressure is 2235 psig and reactor coolant system temperature is 547 F with decay heat removal via the main steam dump and auxiliary feedwater systems. Unit 1 has one active shutdown tech spec action statement in effect due to the inoperability of the containment radiation monitor 1R11A. The inoperability of this radiation monitor had no effect on the event. All control rods were manually inserted to place Unit 1 in Hot Standby (Mode 3). No ECCS (emergency core cooling system) or ESF (emergency safety features) systems were required to function during this event. No major secondary equipment was tagged for maintenance prior to this event. No personnel were injured during this event. The reactor was manually shut down and a shutdown margin calculation verified sufficient margin. The licensee notified the NRC Resident Inspector and the local township.

  • * * RETRACTION FROM MATT MOG TO VINCE KLCO ON 9/26/16 AT 1519 EDT * * *

The purpose of this notification is to retract event report number 52129 made on 7/28/2016 at 0925 (EDT). Previously PSEG reported that Salem Unit 1 initiated a shutdown to comply with Technical Specifications (TS) due to the inoperability of both source range nuclear instruments. Additionally PSEG reported that the condition could have prevented the fulfillment of the safety function needed to, 'Shut down the reactor and maintain it in a safe shutdown condition.' Subsequent review identified that the condition did not meet either reporting criteria. Maintenance and Engineering evaluation of the source range nuclear instruments determined that the instruments were fully operable at the time of the event. TS 3.3.1.1, Reactor Trip Instrumentation remained met, no TS shutdown was required and the instruments were capable of performing their required function. Therefore PSEG is retracting the notifications made under 10 CFR 50.72(b)(2)(i) and 10 CFR 50.72(b)(3)(v)(A). The NRC Resident Inspector was notified of this retraction by the licensee. Notified the R1DO (Cook).

ENS 520791 July 2016 09:42:00Davis Besse10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown

At 2342 (EDT), June 30, 2016, the Control Room received panel alarms associated with Safety Features Actuation System (SFAS) Channel 2. Subsequent investigation revealed the alarms were due to a loss of supplied power caused, in part, by a level permissive in the Borated Water Storage Tank (BWST) to be inoperable. With SFAS Channel 1 BWST level transmitter previously declared inoperable for maintenance, the on-shift operating crew did not correctly identify that technical specification (TS) 3.3.5, Condition B applied which is a 6-hour shutdown required action. At 0245, following a duty team call when the condition was re-assessed, the crew entered the proper additional Condition B and correctly identified they were approximately 3 hours into a 6-hour shutdown specification. At 0330 the condition was inappropriately exited on the premise that an operable but degraded situation could be justified. The plant did not initiate a shutdown required by technical specification but, in retrospect, should have initiated and completed a shutdown within 6 hours of 2342.

On July 1 at 1351, the BWST level transmitter for SFAS Channel 1 was repaired and declared operable (and exited TS 3.3.5 Condition B), however, the total time exceeded the 6-hour shutdown action. The plant remained stable throughout this event.  On July 9, 2016, while internally discussing the event among FENOC senior leadership, it was determined that a 4-hour report would have been made if the shutdown was initiated. Hence, this report is retrospective in that a 10 CFR 50.72(h)(2)(i) required report should have been made upon the initiation of any nuclear plant shutdown required by plant's technical specification.

A Licensee Event Report will be provided pursuant to 10 CFR 50.73(a)(2)(i)(B) as a condition that was prohibited by the plant's technical specification. The NRC Resident Inspector has been notified. (At 1325 EDT on July 1, it was determined that the justification for SFAS channel 2 BWST level permissive to be operable but degraded could not be supported and reentered TS 3.3.5 Condition B.)

ENS 5203924 June 2016 08:00:00Indian Point10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownService waterAt 0400 (EDT) on June 24, 2016, Indian Point Unit 2 initiated actions to commence reactor shutdown to comply with Technical Specification (TS) LCO 3.7.7, Condition B. TS LCO 3.7.7, Condition A had been entered at 0230 on June 21, 2016 in order to repair a leaking weld on the 20 inch service water pipe to nozzle weld on the 21 Component Cooling Water Heat Exchanger (CCW HX). Condition A allows 72 hours to restore the inoperable CCW train to service or Condition B is entered which requires the plant to be in Mode 3 in 6 hours and Mode 4 in 12 hours. The initiation of a nuclear plant shutdown required by TS requires a 4-hour report in accordance with 50.72(b)(2)(i) which is being made by this notification. The licensee notified the New York Independent System Operator and the New York Public Service Commission. The licensee notified the NRC Resident Inspector.
ENS 519836 June 2016 09:56:00Susquehanna10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Main Turbine
Reactor Recirculation Pump
Control Rod
Susquehanna Unit 1 commenced a manual shutdown on 06/05/2016 for a maintenance outage. At 2202 hours (EDT) on 06/05/2016, operators began reducing power in accordance with plant procedures. At 0352 hours on 06/06/2016, the Main Turbine was tripped with reactor power at approximately 15%. The Mode switch was taken to 'STARTUP/HOT STANDBY' (Mode 2) at 0515 hours on 06/06/2016. Manual insertion of control rods was paused as scheduled for entry into the drywell for inspections. There were no ESF actuations. At 0556, the licensee identified leakage from a weld on seal water line piping connected to the 1B reactor recirculation pump seal area. The location is within the reactor recirculation loop isolation valves, therefore is isolable from the reactor vessel. The piping is ASME Class 2 and is reactor coolant pressure boundary. The reactor was in Mode 2 at the time of discovery. This event is being reported as a plant shutdown required by technical specifications pursuant to 10CFR50.72(b)(2)(i) and degraded condition pursuant to 10CFR50.72(b)(3)(ii)(A). Activities are continuing to achieve cold shutdown. The licensee informed the Commonwealth of Pennsylvania and the NRC Resident Inspector.
ENS 5180921 March 2016 01:54:00Limerick10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Reactor Coolant SystemDuring a planned Unit 1 shutdown for a refueling outage, a 0.5 gpm 'pressure boundary leak' was identified on a 1 inch pipe connected to the '1A' RHR-Shutdown Cooling return line by the drywell leak inspection team during a drywell inspection at approximately 15% power. The leak exceeded the TS 3.4.3.2 'Operational Leakage' LCO of no pressure boundary leakage. TS action 'a' was entered which requires to be in at least Hot Shutdown within 12 hours and Cold Shutdown within the next 24 hours. Therefore, the event is reportable within 4 hours per 10CFR50.72(b)(2)(i) due to the initiation of a plant shutdown required by the plant's TS. The event is also reportable within 8 hours per 10CFR50.72(b)(3)(ii) due to an event that resulted in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. TS 1.28 defines Pressure Boundary Leakage as leakage through a nonisolable fault in a reactor coolant system component body, pipe wall or vessel wall; therefore, the leak is a 'pressure boundary leak' as defined in TS. The licensee notified the NRC resident Inspector.
ENS 5167924 January 2016 02:22:00Perry10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Reactor Coolant System
Feedwater
Reactor Protection System
Main Condenser

At 2100 hours (EST), on January 23, 2016, the Perry Nuclear Power Plant commenced a reactor shutdown due to unidentified leakage in the drywell. At 2122 hours, drywell unidentified leakage exceeded the Technical Specification 3.4.5.d limit of 'less than or equal to 2 gpm increase in unidentified LEAKAGE within the previous 24 hour period in Mode 1.' The unidentified leakage increased to approximately 3.8 gpm at 2122 hours. Current unidentified leakage is 3.02 gpm. Technical Specification 3.4.5 actions allow 4 hours to reduce the leakage within limits or be in Mode 3 within 12 hours and Mode 4 within 36 hours. The plant is required to be in Mode 3 by 1322 hours on January 24, 2016 and Mode 4 by 1322 hours on January 25, 2016. A drywell entry will be made in Mode 3 to identify the leak source.

This notification is being made due to an expected inability to restore the leakage within limits prior to exceeding the LCO action time. Follow up question from NRC: Event times do not match (2100 versus 2122) - explained downpower was commenced at 2100 with leakage less than TS limit. When Reactor Core flow was reduced, un-identified leakage increased above the TS limit. The Licensee has notified the NRC Resident Inspector.

  • * * UPDATE FROM MIKE DOTY TO DANIEL MILLS AT 1123 EST ON 1/24/16 * * *

At 1007 hours, on January 24, 2016 with the plant at 8% power during a feedwater shift to place the motor feed pump in service, reactor level rose to the level 8 scram set point and the Reactor Protection System (RPS) initiated, scramming the reactor. During the scram, all rods fully inserted into the core. Decay heat is being removed via turbine bypass valves to the main condenser. Reactor level control is currently being maintained via feedwater. The plant is stable with cool down and depressurization to Mode 4 to follow. The cause of the rise in feedwater level is under investigation. This notification is being made under 50.72(b)(2)(iv)(B) for a RPS initiation while critical. All safety shutdown systems are available. The electric plant is in its normal shutdown alignment being supplied by offsite power. The licensee has notified the NRC Resident Inspector. Notified R3DO (Cameron). NRR (Morris) and IRD (Gott) were notified via email.

  • * * UPDATE FROM DAVID O'DONNELL TO HOWIE CROUCH AT 1915 EST ON 1/24/16 * * *

Following a shutdown required by plant Technical Specifications a small leak was identified coming from the Reactor Recirculation Loop A Pump Discharge Valve vent line. The Recirculation Loop is part of the reactor coolant system making this reportable under 50.72(b)(3)(ii)(A) as a degraded condition. It was subsequently determined to require a plant cool down in accordance with Technical Specification 3.4.5, Action C which requires the plant to be in MODE 4 within 36 hours. Technical Specification 3.4.5 was previously entered for increased unidentified leakage in the drywell. The plant is required to be in Mode 4 by 1322 hours on January 25, 2016. The licensee has notified the NRC Resident Inspector. Notified R3DO (Cameron). NRR (Morris) and IRD (Gott) were notified via email.

ENS 5125323 July 2015 06:15:00Callaway10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Reactor Coolant System

On July 23, 2015 at 0115 (CDT), Callaway Plant initiated a shutdown required by Technical Specifications (TS). At 2139 (CDT) on July 22, 2015, TS 3.4.13 Condition A was entered due to unidentified RCS leakage being in excess of the 1 gpm TS limit. The leak was indicated by an increase in containment radiation readings, increasing sump levels, and decreasing levels in the Volume Control tank (VCT). A containment entry identified a steam plume; due to personnel safety the exact location of the leak inside the containment building could not be determined. At this time radiation levels inside (the) containment are stable and slightly above normal. There have been no releases from the plant above normal levels. The (NRC) Senior Resident Inspector was notified.

  • * * UPDATE PROVIDED BY ROB STOUGH TO JEFF ROTTON AT 1757 EDT ON 07/23/2015 * * *

Callaway entered TS 3.4.13 Condition B at 0053 (CDT on July 23, 2015) for the subject leakage since reactor coolant pressure boundary leakage could not be ruled out by visual inspection. The estimated leak rate when the decision was made to shut down the plant was approximately 1.8 gpm. The plant entered Mode 3 at 0600 CDT. Additionally, at approximately 1315, it was determined that the duration of the required outage would be greater than three days, thus requiring notification to the Missouri Public Service Commission. This offsite notification is reportable to the NRC (per 10CFR50.72(b)(2)(xi)), and the above table has been updated to reflect this reporting requirement. The licensee notified the NRC Resident Inspector. Notified R4DO (Gepford).

  • * * UPDATE FROM RICHARD HUGHEY TO VINCE KLCO AT 0728 EDT ON 7/26/2015 * * *

Clarification to the initial event notification: the term 'RCS' used above means 'Reactor Coolant System.' Therefore the second sentence from the initial notification is clarified to read, 'At 2139 (CDT) on July 22, 2015, TS 3.4.13 Condition A was entered due to unidentified Reactor Coolant System (RCS) leakage being in excess of the 1 gallon per minute (gpm) TS limit.' The licensee notified the NRC Resident Inspector. Notified the R4DO (Gepford).

ENS 5123114 July 2015 22:15:00Browns Ferry10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownAt 1810 (Central Daylight Time) on July 14, 2015, Browns Ferry Units 1, 2, and 3 initiated actions to commence a reactor shutdown to comply with TS (Technical Specifications) LCO 3.0.3. TS LCO 3.0.3 was entered at 1715 (Central Daylight Time) due to concurrent losses of the A and B Control Bay Chillers. This resulted in a loss of cooling to the U1 and U2 4kV Shutdown Board Rooms. Required actions for the loss of cooling to the U1 and U2 4kV Shutdown Board Rooms are to declare the electrical equipment in the 4kV Shutdown Board Rooms inoperable. The declaration of inoperability of the equipment supported by the U1 and U2 4kV Shutdown Boards resulted in TS LCO 3.0.3 for Units 1, 2, and 3. TS LCO 3.0.3 requires actions to be initiated within one hour to place the affected units in MODE 2 within 10 hours; MODE 3 within 13 hours; and MODE 4 within 37 hours. This event requires a 4-hour report in accordance with 50.72(b)(2)(i), 'The initiation of any nuclear plant shutdown required by the plant's Technical Specifications.' The NRC Resident Inspector has been notified. Condition Report #1056829 has been initiated in the Corrective Action Program. The 4kV shutdown electrical boards are required in all modes of operation.
ENS 5110631 May 2015 20:00:00Cook10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownEmergency Diesel Generator

At 1600 (EDT) on May 31, 2015, (DC Cook) operations commenced a shutdown of DC Cook Unit 1 to comply with LCO 3.8.1 Condition G, when the 14 day limit to complete Condition B Required Action could not be met. At 0010 (EDT) on May 18, 2015, Unit 1 AB Emergency Diesel Generator was removed from service for planned maintenance. LCO 3.8.1 Condition B was entered which allows 14 days to restore diesel to operable. At 1049 (EDT) on May 21, 2015, Unit 1 AB Emergency Diesel Generator tripped during post maintenance testing due to high bearing temperatures. Subsequent actions to repair and restore the diesel to operable status have been unsuccessful. This event is reportable under 10 CFR 50.72(b)(2)(i), the initiation of any nuclear plant shutdown required by the plant's Technical Specifications, as a four (4) hour report. The DC Cook Sr. Resident NRC Inspector has been notified. Unit 1 is expected to be in Mode 5 by 2030 EDT on June 1, 2015. There is no impact on Unit 2.

  • * * UPDATE FROM CHRIS PEAK TO JOHN SHOEMAKER ON 6/1/15 AT 1704 EDT * * *

This update is to correct the information contained in the block titled 'Power/Mode After'. The power and mode after the event requiring notification (TECHNICAL SPECIFICATION REQUIRED SHUTDOWN DUE TO INABILITY TO RESTORE UNIT 1 AB EDG WITHIN THE COMPLETION TIME PRESCRIBED IN LCO 3.8.1 CONDITION B) was 99% power and mode 1. The licensee has notified the NRC Resident Inspector. D.C. Cook Unit 1 is currently in Mode 3 and conducting a normal cooldown to Mode 4. Notified R3DO (Passehl).

  • * * UPDATE FROM CHRIS PEAK TO HOWIE CROUCH AT 0734 EDT ON 6/2/15 * * *

DC Cook Unit 1 reactor was shut down (Mode 3) at 0231 hours (EDT) June 01, 2015 and achieved Mode 5 at 0410 hours (EDT) June 02, 2015 to comply with LCO 3.8.1 Condition G with all systems operating normally. The licensee has notified the NRC Resident Inspector. Notified R3DO (Passehl).

ENS 5107416 May 2015 02:48:00Wolf Creek10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown

Class 1E A/C Unit SGK05A cools safety related electrical train 'A' and was found tripped at 2148 (CDT). As a result, the following supported safety related electrical equipment were declared inoperable: 4.16 KV Bus NB01, 480 Volt Buses NG01 and NG03, 120 volt Instrument AC Inverters and Buses NN11, NN13, NN01 and NN03, 125 VDC Chargers and Buses NK11, NK13, NK01 and NK03. T/S 3.0.3 was entered from T/S 3.8.7 due to two out of four 120 volt AC Inverters (NN11 and NN13) being inoperable. All electrical systems listed above remain available but are declared inoperable due to inadequate room cooling capability. Plant shutdown to mode 5 commenced at 2244 (CDT). No major equipment is out-of-service. All systems have functioned normally. Plant is currently at 99% with power ramping down. Plant must be in mode 3 by 0448 CDT. No compensatory measures have been established. The NRC Resident Inspector has been notified. See EN #51071 for an earlier T/S required shutdown required at 0436 CDT on 5/15/15, due to the same conditions.

  • * * UPDATE FROM BRET DAVIS TO VINCE KLCO ON 5/18/15 AT 1600 EDT * * *

For both EN 51071 and 51074, the low lube oil pressure switch tripped the SGK05A unit. Oil pressures were verified to be normal and the SGK05A unit was successfully started. The plant shutdown each time was terminated. A fault in the Electronic Oil Pressure control which monitors the low lube oil pressure switch was identified. A jumper has been installed that bypasses the oil switch while maintenance is being conducted. The unit was declared functional but degraded. Indication of low oil pressure is still provided. The licensee notified the NRC Resident Inspector. Notified the R4DO (Okeefe).

ENS 5107115 May 2015 09:36:00Wolf Creek10 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownClass 1E A/C Unit SGK05A cools safety related electrical train 'A' and was found tripped at 0436 (CDT). As a result, the following supported safety related electrical equipment were declared inoperable: 4.16 KV Bus NB01, 480 volt Buses NG01 and NG03, 120 volt Instrument AC Inverters and Buses NN11, NN13, NN01 and NN03, 125 VDC Chargers and Buses NK11, NK13, NK01 and NK03. T/S 3.0.3 was entered from T/S 3.8.7 due to two out of four 120 volt AC Inverters (NN11 and NN13) being inoperable. All electrical systems listed above remain available but are declared inoperable due to inadequate room cooling capability. Plant shutdown to mode 5 commenced at 0530 (CDT). No major equipment is out-of-service. All systems have functioned normally. Plant is currently at 95 % power ramping down. Plant must be in mode 3 by 1136 CDT. No compensatory measures have been established. The NRC Resident Inspector has been notified.