ENS 56509
ENS Event | |
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07:07 May 8, 2023 | |
Title | Shutdown Required by Technical Specifications Due to Inoperable Core Spray |
Event Description | The following information was provided by the licensee via fax:
At time 0207 CDT, Cooper Nuclear Station (CNS) entered Technical Specification [Limiting Condition for Operation] LCO 3.0.3 due to declaring core spray subsystems A and B inoperable. This declaration was based on an issue with relays installed from the same manufacturing batch. The ability of the relays to function correctly to annunciate loss of logic power was called into question and they were declared inoperable. The plant has initiated actions to repair/replace affected relays. This event is reportable under 10 CFR 50.72(b)(2)(i) as an initiation of any nuclear plant shutdown required by Technical Specifications. In addition, this event Is reportable under 10 CFR 50.72(b)(3)(v) as a condition that could have prevented the fulfillment of a safety function for the core spray systems. NRC Resident Inspector was notified.
The following information was provided by the licensee via email: Technical Specification LCO 3.0.3 was exited at 0805 CDT on May 8, 2023. A reasonable expectation of operability was developed for the core spray subsystems A and B. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Shutdown was initiated and power was reduced approximately 45 percent. Reactor power is currently at 55 percent at the time of notification. Notified R4DO (Werner) via email.
The following information was provided by the licensee via email: CNS is retracting the 8-hour 10 CFR 50.72(b)(3)(v) non-emergency notification, for a condition that could have prevented the fulfillment of a safety function, made on May 8, 2023, at 0207 CDT (EN 56509). Subsequent evaluation concluded that the core spray subsystems remained operable in accordance with the Technical Specifications Requirements 3.5.1, ECCS - Operating. As a result of the core spray system remaining operable, no loss of safety function occurred. The NRC Senior Resident Inspector has been notified. Notified R4DO (Werner). |
Where | |
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Cooper Nebraska (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
Time - Person (Reporting Time:+-0.7 h-0.0292 days <br />-0.00417 weeks <br />-9.5886e-4 months <br />) | |
Opened: | Curtis Martin 06:25 May 8, 2023 |
NRC Officer: | Adam Koziol |
Last Updated: | May 9, 2023 |
56509 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (70 %) |