The following information was provided by the licensee via fax or email:
At 2342 CDT on August 19, 2022, with Grand Gulf Nuclear Station in Mode 1 and at 40 percent power, the station initiated a normal shutdown to comply with its Technical Specifications (TS). The station entered Mode 3 at 0000 CDT August 20, 2022 to comply with (LCO) 3.5.1 Condition G Action G.1 due to the condition reported to NRC previously (EN 56058).
This event is being reported under 10 CFR 50.72(b)(2)(i) as a shutdown required by the plant's technical specifications.
The NRC Senior Resident Inspector was notified.
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The plant is now in a 36-hour LCO to be in Mode 4 due to Low Low Set Valves inoperability per TS 3.6.1.6.
- * * RETRACTION ON 10/14/2022 AT 1311 FROM JEFF HARDY TO LAUREN BRYSON * * *
Grand Gulf Nuclear Station (GGNS) is performing this notification to retract event EN 56059 that was reported on August 20, 2022. Previously, GGNS notified the NRC that it had initiated a shutdown required by Technical Specifications to comply with Limiting Condition of Operation (LCO) 3.5.1 Condition G.1 due to the inoperability of four Automatic Depressurization System (ADS) valves.
Following the shutdown, GGNS completed walkdowns and determined that the condition affected only one ADS valve. As a result, the shutdown to satisfy the required actions of TS LCO 3.5.1 Condition G.1 was not required.
The NRC Resident Inspector has been notified of the retraction.
R4DO (Kellar) was notified.