ML17252A326

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LER 77-040/03L-0 for Dresden 3 Regarding the Circuit Breaker for Service Water Makeup Valve MO-3-4102 to the Isolation Condenser Found in Off Position
ML17252A326
Person / Time
Site: Dresden Constellation icon.png
Issue date: 10/21/2017
From: Stephenson B
Commonwealth Edison Co
To: James Keppler
NRC/RGN-III
References
BBS LTR #980-77 LER 77-040/03L-0
Download: ML17252A326 (3)


Text

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  • Dresden Nuclear Power Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 October 21, 1977 BBS LTR /1980- 77 James G. Keppler, Regional Director Directorate of Regulatory Operations - Region III 5()- ~'f'I U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 Reportable Occurrence Report /f77-040/03L-0 is hereby submitted to you:n office in accordance with Dresden Nuclear Power Plant Technical Speci-fication 6.6.B.2.b., conditions leading to operation in a degraded mode permitted by a limiting condition for operation.

Stephenson Station Superintendent Dresden Nuclear Power Station BBS:dlz Enclosure CC: Dir.ector of Inspection & Enforcement Director of Management Information & Program Control File/NRC

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CON'f'ROL BLOCK: .____.__~__. _

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LICEN.SEE EVENT REPORT If,\ . (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

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7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T ffiJJ  :~~~~~ ~©I oI s I o I o I o I 2 I 4 I 9 101 o I 9 12 I 4 I 1 11 I© I l I o I 2I 1 I 1 I 1 10 7 8 . 60 . 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@ * .

[§:IIl*-t-I>-u-r4ng *no"rrii.af operation circuit breaker for service water makeup valve (Mo-3-4102) to

[QTIJ the isolation condens~r was found in off position on two separate occasions. Event

[QEJ reportable under T, S. 6. 6. B: 2. b ~j~{'afety significance minimal since two additional

[Q:TI] sources of makeup water available if needed. Event is not a repetitive occurrence.

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11 12 13 18 19 20 SEQUENTIAL OCCUR A ENCE REPORT REVISION

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21 22 23 24 26 27 28 29 c 30 31 32 ACTION FUTURE EFFECT SHUTDOWN (.'.;':;\ ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TA~.E,N ACTION ON PLANT METHOD . HOURS ~ SUBMITTED FOR,M~:;UB. . SUPPLIER MANUFACTURER 1<x1l@W@ WC§) LI I 01 01 01 01 L!J@ ,,~JI@. L!J@ I c Io 1s 10 I@

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  • 42 I 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

lJITI I Cause of event due to personnel error. Breaker immediately reset. To preyent re-currence breaker has been latched in the on position. This will not preyent normal breaker operation. I ITEl 7 8 9 80 FACILITY STATUS  % POWER OTHER STATUS fJ'

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O\* . METHOD OF DISCOVERY DISCOVERY DESCRIPTION. ~

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7 8 9 10 12 13 44 . 45 . 46 80 ACTIVITY CONTENT ~

RELEASED OF RELEASE AMOUNT OF ACTIVITY '2.V LOCATION OF RELEASE@

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NUMBER A TYPE DESCRIPTION

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7 8 9 10 80 PUBLICITY ~ NRC USE ONL y ISSJ.!EDQ DESCRIPTION~ 0

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ATTACHMENi~TO LICENSEE EVENT REPORT 77-040/03L-0 COMMONWEALTH EDISON COMPANY (CWE) i DRESDEN UNIT 3 (ILDRS-3) .  !

DOCKET II 50-249 f

On September 24, l977~ at _1325 hours the control room operator noticed that neither position indication lig):it o_n *control panel 903-3. for valve M03-4102 was lit. This valve is the service water makeup valve for the isolation condenser. When it was determined that the light bulb was t

not burned out, an operator was. sent to the breaker *and discov.ered it .

. was.in the off position. I The breaker was immediately returned to the ori position. ,On.September 29, 1977, the control room operator :reported *to the ~hift *,gngineer that this same breaker.had tripped. The operator performed procedure Doi> 040-1 "S.tation Motor Operated Valves.,; Th'e breaker was reset and the valve was  !

cycled 3 times successfully. A work."request (WR #8634} was issued to ipvestigate the problem. J Upon investigation, it was discovered that the valve had not been operated,* I!

and probably had not "Tripped'.:' due to valve motor operator problems~. It '

was decided that .the.breaker was probably in the "OFF" position, rather th.an tripped as was originally reported to the Shift Engineer. I t was also l!

noted that the breaker required only_ a smail amount of force exerted upon it '

to make it go from "on" to*. "off". The breaker is *1ocated *about waist high

. in a narrow passageway. on Bus 39-1 in the reactor building, and may have been inadvertently bumped.to the off :position *. To prevent recurrence, the breaket was::Jlatthed in the "on'.' position by *cutting a notch in the brea}cer housing into which a sliding metal tab on.the breaker haridle fits. This iI will prevent the breaker from being inadvertently turned -off in the future.

The breaker will still trip as*required when latched in this manner in the event a legitimate. trip signal*is received.

This event-had minimal consequences because there are two additional sup-plies cif makeup water* to the. emergency condenser: Since the operators

.. normally scan the console each shift~ the breaker .in both instances was not off for more than one shift.

  • The corregponding breaker on '.';¥,nit (J.d ~ill a,l~o be latched in this manner.

The Unit ,\'JYW breaker is located* in a similar location.

These are the first occurrences of this event at Dresden, and it has not recurred sirice the breaker has been latched.