ML20202E709

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Insp Rept 50-271/97-08 on 970907-1031.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20202E709
Person / Time
Site: Vermont Yankee Entergy icon.png
Issue date: 11/28/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20202E698 List:
References
50-271-97-08, 50-271-97-8, NUDOCS 9712080126
Download: ML20202E709 (38)


See also: IR 05000271/1997008

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- U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No. 50 271

Licensee No. - DPR 28

Report No. 97 08

Licensee: Vermont Yankee Nuclear Power Corporation

Facility: Vermont Yankee Nuclear Power Station.

Location: Vernon, Vermont

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Dates: September 7 October 31,1997 .

Inspectors: William A. Cook, Senior Resident inspector -

Edward C. Knutson, Resident inspector

Jason C. Jang, Engineer, Division of Reactor Safety (DRS)

Robert J. Summers, Division of Reactor Projects

William A. Maler, Engineer, DRS .

Kenneth S. Kolaczyk, Engineer, DRS

Timothy L. Hoeg, Engineer, DRS

Mark Holbrook, Contractor, INEL

Approved by: Curtis J. Cowgill, Ill, Chief, Projects Branch 5

Division of Reactor Projects

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9712080126 971128

PDR ADOCK 05000271

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EXECUTIVE SUMMARY

Vermont Yankee Nuclear Power Station

NRC Inspection Report 50-271/97-08

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a seven week period of resident

inspection and includes results of announced inspections by regional specialist inspectors.

Operations

The inspector catermined that the VY staff had responded appropriately to the September

27 seismic monitor alarm and that the declaration of an Unusual Event had been in

accordance with their emergency procedurx. However, the inspector considered that the

timeliness of licensee action to address this previously observed overly conservative

Emergency Plan entry condition, (single, unconfirmed seismic monitor alarm), to have been

slow,

inspector review of the October 10 ENS call, involving the Alternate Cooling System (ACS)

cable separation issue, identified an appropriate immediate response to the ACS operability

concern and appropriate follow-up corrective actions.

Maintenance

Based upon observation of a variety of maintenance and surveillance testing items,

appropriate control and execution of these activities was noted,

The licensee identified and corrected reactor building ventilation radiation monitor testing

discrepancy (LER 96-23) was not cited. The procedural non-compliance which contributed

to the fuel oil sampling and analysis events discussed in LER 96-29 was not cited. The

low pressure coolant injection surveillance testing discrepancy discussed in LER 96-27 was

not cited.

Enaineerina

At the end of the inspection period, the VY staff had completed formal emergency diesel

generator (EDG) support piping stress analyses and had completed a metallurgical analysis

which VY believes supports their initial EDG operability determination. These items were

under review by the NRC staff. Pending the results of further NRC staff review, the EDG

support piping welds issue is being tracked as an inspector follow-up item (IFI 97-08-01).

The licensee's response to this issue, to date, has been consistent with the guidance of

Generic Letter 91-18.

VY established a program that met their commitments to GL 89-10, " Safety-Related Motor-

Operated Valve Testing and Surveillance." Final val;dation of switch settings is currently

scheduled to be completed by January 30,1998. Use of the Electric Power Research

Institute (EPRI) motor operated valve performance prediction program to validate switch

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-. settings for essentially all MOV's was exceptional and considered to be a program

strength.

. The failure to have included and tested a number of keep fill system check valves in the

VY Inservice Testing Program (reference LER 9611)was not cited.

Plant Supoort

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The radioractive liquid and gaseous effluent control programs were wellimplemented.

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  • The licensee implemented good management control and oversight of the quhlity of

4 .the radioactive liquid and gaseous effluent control programs,

* The effluent radiation monitoring s/ stem calibration program, including trending

analysis, was well-implemented.

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s The ventilation system surveillance program was well implemented. However, the

l plant air balance measured in 1971 might be invalid, as described in Section R.2.3

of this inspection report. (IFl 97-08-02)

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o Very good quality control for the chemistry laboratory and quality assurance audit -

programs were established.

The failure to have appropriately controlled the movement of reactor vessel shield blocks

preceding the 1990 and 1992 refueling outages (reference LER 96-03 and URI 96-03-05)

. was not cited. ,

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TABLE OF CONTENTS -

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- EXEC UTIVE S U M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . il

TA B LE O F C O NT ENT S 1. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . - iv

Summary of Plant Status ...........,................................1 -

1. Operations ....................................................1

01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.1 Unusual Event Declared Due to indication of Possible Seismic Event

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01.2 10 CFR 50.72 Notification involving inadequate Cable Separation of

the Alternate Cooling System . . . . . , . . . . . . . . . . . . . . . . . . . . 9

08 Miscellaneous Operations issues ...... ..................... 3 -!

08.1 (Closed) LER 9 7 1 1 . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

. 08.2 (Closed) LER 9 7-14 . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

08.3 (Closed) LER 97-17 . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

08.4 (Closed) LER 9 7 12 . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

ll . M aint e n a nc e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

M1 Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

M1.1 Maintenance Observations . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

M1.2 Surveillance Observations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

M8 Miscellaneous Maintenance issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

M8.1 (Closed) LER 96 23 and NCV 9 7-0 8-0 3 . . . . . . . . . ,. . . . . . . . . . 5

M8.2 (Closed) LER 96 29 and NCV 97-08-04 . . . . . . . . . . . . . . . . . . . . 6

- M8.3 (Closed) LER 96 24 and IFl 9 6-0 9 -01 . . . . . . . . . . . . . . . . . . . . . 7

M8.4 (Closed) LER 96-27 and NCV 97 08-05 . . . . . . . . . . . . . . . . . . . . 8

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Ill . Engine e rin g . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

E1 Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 9

E1,1 Safety Grade Qualification of Welds in Emergency Diesel Generator

S up p ort Syste m s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

E2 Motor-Operated Valve Program Review . . . . . . . . . . . . . . . . . . . . . . . 11

E2.1 I ntrodu ctio n . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 1

E2.2 Evaluation of High Risk MOV Dynamic Test Results . . . . . . . . . . 12

E2.3 Use of the Electric Power Research Institute Thrust Calculation

Pr og r a m . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 4

E2.4 Valve G rouping . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

E8 Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

E8.1 (Open) IFl 96-11-01: Emergency Diesel Generator (EDG) Tornado

Pro t e c t i o n . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

E8.2 (Closed) LER 96-11 and NCV 9 7-0 8-0 6 . . . . . . . . . . . . . . . . . . 17

E8.3 (Closed) LER 96-14, Supplement 1. . . , . . . . . . . . . . . . . . . . . . 17

E8.4 (Closed) LER 96 21 ................................18

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E8.5 (Open) URl 9 7 -0 3 -0 2 . . . . . . . . . . . . . . . . . . . . . . . . -. . . . . . . . 1 8 .

E8.6 '(Closed) URI 9316-01: Pressure Locking / Thermal Binding (PLTB) of l

Gate Valves .....................................18

E8.7 - (Closed) VIO 96-05-03: Update and Control of MOV Program Manual

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E8.8 - (Closed) EA 95-070,VIO 01013: Fa" * e to Correct a Condition '

Adverse to Quality . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

IV. Plant Support ................................................20

P3 EP Procedures and Documentation . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

R1 Radiological Protection and Chemistry (RP&C) Controls ... . . . . . . . . . . 20

R1.1 (Closed) URI 97 06-02: Implementation of the Radioactive Liquid and

Gaseous Ef fluent Control Programs . . . . . . . . . . . . . . . . . . . . . 20 -

R2 Status of RP&C Facilities and Equipment ..............,.......21

H2.1 Calibration of Effluent / Process / Area /Acciocet Radiation Monitoring

Systems (RMS) ...................................21 +

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' R2.2 Air Jiean!ng Systems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

R2.3 Plant Air Bala nce . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 3

R3 RP&C Procedures and Docuinentation' . . . . . . . . . . . . . . . . . . . . . . . . 24

R6 RP&C Organization and Administration . . . . . . . . . . . . . . . . . . . . . . . . 25

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R7 Quality Assurance (OA) in RP&C Activities . . . . . . . . . . . . . . . . . . . . . 26

R8 Miscellaneous issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 6

R8.1 Training ........................................26

R8.2 (Closed) URI 96-03-05, LER 96-03 Sup 1, and NCV 97-08-07 .. 27

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V. M a nagem e nt Mee ting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 8

X1 Exit Meeting Summary . . . . . . . . . .......................,..28  ;

X2 Review of Updated Final Safety Analysis Report (UFSAR) . . . . . . . . . . . 28 ,

INSPECTION PROCEDURES USED . . . . . . . . . . . . . . . . . . . . . . . , , . . . . . . . . . . . . 29

ITEMS OPENED, CLOSED, AND DISCUSSEO . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30 i

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PARTIAL LIST OF PERSONS CONTACTED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

LIST OF ACRONYMS USED . . ..................................... . 32 ,

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ATT A C H M E NT A . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3 3

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Report Details

Summerv of Plant Status

During this inspection period, Vermont Yankee (VY) operated at full power with the

exception of power reductions to conduct planned surveillance testing.

A region based specialist inspector was on site the week of September 22 to examine VY's

radioactive liquid and gaseous effluent control programs. The results of that inspection

have been integrated into this report.

A region based specialist inspector was on site the week of September 29 to conduct a

follow-up inspection of the Architect / Engineering Design Inspection (report No. 50-

271/97-201) findings. The results of that follow-up inspection will be documented in

inspection report No. 50-271/97 10.

During the week of October 13, region based specialist inspectors conducted a follow-up

inspection of the motor operated valve program developed in accordance with Generic

Letter 8910.

On October 6, the inspectors were provided an overview of the licensee's Human

Performance improvement Program which has the goals of: achieving excellence in human

performance; achieve a reduction in error rate; and achieve an improved rating in human

error probability index. This program was initiated, in part, in response to recent Notices of

Violation (refer to inspection reports 97-04 and 97-05) citing poor human performance and,

in part, to a licensee recognized adverse trend in this area. Training sessions 'with small

groups of the plant staff were scheduled to commence later in the month,

l. Operations

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01 Conduct of Operations' (93702)

01.1 Unusual Event Declared Due to Indication of Possible Seismic Event

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a. Insoection Scone (71707)

The inspector examined the licensee's response to a seismic monitor alarm and the

basis of their decision to declare an Unusual Event.

b. Observations and Findinas

At 9:08 pm on September 27, the plant seismic monitor alarmed. Control room

operators were alerted to the event via the seismic monitor main control board

annunciator. There were no other indications that a seismic event (earthquake) had

occurred. The licensee declared an Unusual Event (UE) based on emergency

procedure AP-3125, " Emergency Plan Classification and Action Level Scheme,"

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' Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized

reactor inspection report outline. Individual reports are not expected to address all outline topics.

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entry criteria U 5-c, "Any earthquake sensed on-site as recognized by observation or

detection." The states of Vermont and New Hampshire and the Commonwealth of

Massachusetts were notified and a one-hour emergency notification system (ENS 33001) call was made to the NRC, as required by 10 CFR 50.72.

The inspector observed that the VY staff properly responded in accordance with

operating procedure OP-3127, " Natural Phenomena." This included visual

inspection of selected plant structures for possible damage and the completion of a

seismic damage indicator walkdown. No evidence of earthquake damage was

observed. Civen that no other monitoring stations had detected an earthquake and

that a preliminary investigation of the seismic monitor ideatified an internal failure,

the licer.see declared the seismic monitor inoperable and terminated the UE at 11:10

p.m. bubsequent troubleshooting of the seismic monitor identified that the monitor

battery had f ailed, which caused the electrical transient that resulted in the monitor

alarm.

On May 31,1997, a malfunction of the seismic monitor had also resulted in the

declaration of an UE. As discussed in inspection report 50 271/97-04,the

inspector observed that the procedural requirement to declare an UE based upon a

single indicator was overly conservative. Accordingly, allowance to verify that a

seismic event has actually occurred, prior to making an Emergency Plan event

declaration, would potentially avoid the unnecessary mobilization of state and NRC

emergency response organizations, in light of ths September 27 occurrence, ute

inspector considered that the licensee has been slow to address this procedural

requirement. The inspector determined that procedure revisions were being

processed at the time of the Nptember 27 event, which were designed to provide

for a seismic event verification,if appropriate, prior to Emergency Plan entry,

c. Conclusions

The inspector determ;ned that the VY staff had responded appropriately to the

September 27 seismic monitor alarm and that the declaration of an Unusual Event

had been in accordance with their emergency procedures. However, tile inspector

considered that the timeliness of licensee action to address the previously identified

Emergency Plan entry condition problem, (single, unconfirmed seismic monitor

alarrn), to have been slow.

01.2 10 CFR 50.72 Notification involvina inadeauate Cable Separation of the Alternate

Coolina System

At 7:57 pm on October 10, the control room operators notified the Headquarters

Duty Officer (Event No. 33070)in accordance with 10 CFR 50.72, that a condition

outside the plant's Updated Final Safety Analysis Report (UFSAR) had been

. identified involving power cable separation of Alternate Cooling Systum (ACS)

cooling tower fan No. 21. Spechically, the two emergency power feeds, one from

motcr control center (MCC) 8C (safety related Division 1) and one from MC' 7C

(Division 11), were not properly separated per the UFSAR and Vermont how

Specification VYS-027 electrical separation criteria. The No. 2-1 fan is normally

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powered via a non safety related MCC (MCC-582A).- To address the immediate-

operability concern, the licensee tagged open both safety related power supply

breakers (MCC 8C, breaker 2C is normally closed) and the seven-day limiting j

condition for operation (LCO) was entered, in accordance with ACS Technical  !

Specification (TS) 3.5.D.3, pending further review,

inspector follow-up determined that the licensee revised the ACS operating

p. ocedure to maintain both of the cooling tower fan No. 2-1 safety related breakers

normally open and provided amplifying instructions for operators to closed the

breakers in the event that the alternate cooling tower fan was needed. The

inspector reviewed the safety evaluat;on (Safety Evaluation No. 97 28) supporting

the procedure changes to OP 2181, OP-2143, and OT 3122, and found the

licensee's assessment of the changes consistent with 10 CFR 50.59 requirements.

The inspector also observed the Plant Operations Review Committee's deliberation 1

and approval of SE No. 97-28 and concluded their safety review was appropriate. I

The licensee satisfactorily implemented the procedure changes and exited the 1S

LCO on October 16.

08 Miscellaneous Operations issues (92700) j

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i 08.1 (Closed) LER 97-11: The crimary containment torus was not Lnert_ed to Technical  !

Soecifications reauirements due to an inadeauate orocedure who resulted in an  !

Lqntfficient nitroaen inertino ourae flowrate.

LER 97-11, dated June 1 i,1997, was previously reviewed by the inspectors, as

docurnented in inspectica report 97-C5, section 01.2. As a result of this event, a

- Notice of Violation (VIO 97-05-01) was issued citing the non-compliaace with

Tect:nical Specification 3.7.A.7.b. Inspector review of the licensee's response,

dated September 18,1997, and any additional corrective action verification will be

tracked via VIO 97 05 01. LER 97-11 is closed.

08.2 (Closed) LER 97-14: Lack of understandina of clant licensina and desian bases

results in an inadeauste resoonse to industry operatina exoerience which allowed

resumotion of olant operations inconsistent with its desian basis.

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LER 97-14, dated September 5,1997, was previously reviewed by the inspectors,

as documented in inspection report 97 06, section E.8.2. As a result of this event,

a Notice of Violation (VIO 97 06-03)was issued citing ineffective corrective action,

inspector review of licensee's response, dated October 1,1997, and any additional

corrective actions verifications will be tracked via VIO 97-06 03. LER 97-14 is

closed.

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08.3 (Closed) LER 07:,1,7: An eauioment malfunction remainina undetected by thq

poeratina crew renults in olant operation in excess of rated thermal power.

LER 9717, dated October 2,1997, documented the licensee's assessment and

corrective acti.ans for the violation of the reactor thermal power limit which occurred

on Septemb'.,r 2,1997, due to a plant process computer data acquisition system

componen*. f ailure. This event was previously reviewed by the inspectors and

documented in inspection ieport 97-06, section 01.2. As stated in report 97-06,

this non-compliance with the VY thermal power limit was non-cited, consistent with  !

section Vll.B.1 of the NRC Enforcement Poliev. The inspector determined that LER

9717 clearly and concisely deceribed the circumstances involving this event and ,

that the action taken by the VY staff to correct the problem and preclude a

recurrence were appropriate and well documented. LER 9717 is closed.

08.4 (Closed) LER 97-12: Residual heat removal service water fk,w could be potentially

less than the desian. basis flow due to instrument inaccuracies.

This event was previously discussed in Inspection report 97-04, section E.7.1 and

assigned an inspection follow item (IFl 97-04-04). The root cause for this event

remains under investigation. However, a Basis for Maintaining Operation (BMO) No.

97-27, dated June 13,1997, was initiated to summarize the residual heat removal

(RHR) service water system operability assessment and document the correctM

action plan. The inspector reviewed the licensee's interim corrective actiont I!nd

found them to be appropriate. Adequate RHR service water system cooling

capacity wcs demonstrated, via analysis, provided river water temperature remained

equal to or less than 80 degrees F (revised from the May 2,1997 limit of 70

degrees F). As of the conclusion of this inspection period, BMO No. 97 27 was

still in of fect.

LER No. 97-12 is c;osed. However, the licensee's actions to resolve this issue will

continue to be tracked via IFl 97 04-04. The inspector notes that the broader issue

of instrumentriion accuracy was identified as a concern in inspectioni report 97-201

(reference sectioli E.2,2.2.f, URI 97 201-16)and will be tracked separately,

ll Maintenance

M1 Conduct of Maintenanc.e

M 1.1 Maintenance Observations

a. Insoection Scope (62707)

The inspectors ob.,erved portions of plant maintenance activities to verify that the

, correct parts and tools were utilized, the applicable industry code and Technical

Specification requirements were satisfied, adeauate measures were in place to

ensure personnel safety and prevent damat. o plant structures, cystems, and

components, and to ensure that equipmer gerability was verified upon completion

of post-maintenance testing,

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b.- Qbservations. Findinas, and Conclusions

The inspector observed all or portions of the following maintenance activities:

  • Preventive maintenance to MCC 10C, on September 30.
  • Scram solenoid pilot valve replacements (18 31,22-43, and 38 27), on

September 12.

Octob6.' 23.

  • Scram solenoid pilot valve replacement and single rod scram time testing

on October 20 and 21.

The inspectors observed proper adherence to procedure and appropriate control and

execution of the above activities.

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M1.2 Surveillance Observations

a. Inspection Scope (61726)

The inspectors observed portions of surveillance tests to verify proper calibration of

test instrumentation, use of approved procedures, performance of work by qualified

personnel, conformance to limiting condition for operations (LCOs), and correct

post test system restoration.

b. Observations Findinas, and Conclusions

The inspector observed all or portions of the following surveillance tests:

  • Core spray system quarterly surveillance test, observed October 7.

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The inspectors observed proper adherence to procedure and appropriate control and

execution of the above activities.

M8 Miscellaneous Maintenance issues (92700,92903)

M8.1 ' (Closed) LER 96-23 and NCV 97-08-03: Inadeouate surveillance orocedure results

in failure to meet Technical Soecification reauirements for radiation monitor

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functional testino.

LER 96-23, dated October 15,1996, documented a licensee identi9sd logic system

functional testing deficiency discovered during the biennial review of procedure OP-

4326. " Reactor building ventilation and refueling floor radiation monitors

functienrWealibration." After identification of the testing oversight and revision of

the surveillance procedure, the radiation monitors' high alarm output contacts,

previously not verified to actuate, were tested satisf actorily. Consequently,

although OP-4326 did not satisfy the Technical Specification functional testing

- requirements (per TS Table 4.2.3), the radiation monitors were demonstrated to

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function, as designed. This non-repetitive, licensee identified and corrected

violation was treated as a non-cited violation (NCV 97 08 03), consistent with

Section Vll.B.1 of the NRC Enforcement Poliev.

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The inspector noted that concurrent with this event, the VY staff was conducting a

< re evaluation of their logic system functional test (LSFT) procedures in accordance

with their April 18,1996 response to Generic Letter (GL) 96-01. By letter dated

September 20,1997, VY revised their August 31,1997 commitment to complete

GL 96-01 actions by February 20,1998. Inspector review of the licensee's

completed LSFT actions is being tracked by IFl 97 06-01 (reference inspection

report 97-06, section M1.5). LER 96-23 is closed.

M8.2 (Closed) LER 96-29 and NCV 97-M-04: Process and communication inadeoue::les

result in the failure to analyze em. roency diesel oenerator fuel oil within time

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allotted by Technical Soecification surveillance reouirements. .

This LER was previously discussed in Section R8.2 of NRC Inspection Report 50-

271/96 11. The NRC concluded in that inspection report that the licensee's

description of the reported violation of plant Technical Specification (TS)

surveillance requirements was incorrect, in that the licensee erroneously assumed

that the diesel generator fuel oil sampling and quality verificatica surveillance

requirement (TS 4.10.C.2) had two separate surve!!!ance intervals, one for the act

of sampling the fuel oil and another for the ana!ysis of the sample (quality

verification).

I in this inspection period, further NRC follow up of this LER and the associated

requirerrents identified additional findings and a necessary clarification to the prior

inspection report discussion. The prior inspection findings included a statement that

"this TS requires the fuel oil to be sampled every 30 days and implies that the

sample sheuld be analyzed prior to the next 30-day sample being taken." Upon

further review, the NRC recognized that the actual requirement of the VY TS was

based on a "once a month" requirement and not "30 days" as stated in inspection

, report 50 271/96 11. While this difference does not change :he overall NRC

conclusion that no violation of the TS occurred, the interpretation of the

requirement in the previous inspection report was not completely accurate. To

clarify, the NRC determined that-TS 4.10.C.2 requires the diesel generator fuel oil to

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be sampled once a month. Implied with this requirement is that the sample analysis

be completed prior to the next monthly sampling activity. While noting that there

are various interpretations of "once a month," the NRC concludes this could be as

long as 31 days or as short as 28 days. For exampie, if the surveillance is

conducted on the 15th of the month, the next ',urveillance would be due on the

15th of the next month. In addition, the NRC noted that the surveillance interval

could be extended by a plus 25 percent, in accordance with the licensee's TS

definition for surveillance frequency.

_

The inspector reviewed the licenseo's internal event report documentation for this

issue and determined that once identified, the concern was appropriately handled by

p station personnel. Based on the fact that the analyses results were already known

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to be acceptable, alt'eit late, and since the fuel oil quality integrity had been

maintained appropriately throughout, the licensee concluded that the emergency

diesel generators were unaffected by this event. Based on the review of the

licensee's analysis at the time of the event, the inspector agreed that the '

emergency diesel generators remained operable.

.

As outlined in the discussion above, the NRC concluded that no technical

specification violation occurred as stated in the LER. Upon review of the timing of

the sampling and analysis of the diesel fuel oil contained in the LER, the inspector

determined that the surve:llance requirements were met. However, the NRC

concluded that the licensee failed to implement station procedures used to schedule

and track the timely completion of important-to-safety activities, like TS required

surveillance tests. The f ailure to properly implement the associated station

procedures was a violation. The licensee's corrective actions described in the LER

were determined appropriate to correct this procedure violation. This non-repetitive,  !

licensee identified and corrected violation was treated as a non-cited violation (NCV

97-08-04), consistent with Section Vll.B.1 of the NRC Enforcement Poliev.

M8.3 (Closed) LER 96-24 and IFl 96-09-01: Incomplete desian bases documentation

results in a f ailure to clearly describe Anoendix J methodoloav in the oroaram

descriotion delivered to the NRC for evaluation.

On October 2,1996, the VY staff notified the NRC staff that an engineering

evaluation had concluded that the lack of closure capability of the motor operated

core spray minimum flow valves (CS-5A and SB) was a condition outsde the plant

design basis. The ikensee had determined that the valve wiring and logic prohibited

minimum flow valve closure unless the core spray pump was running with injection

flow. This valve logic and wiring condition resulted in the inability to close the

minimum flow valves for containment isolation purposes. At that time, the licensee

modified the core spray minimum flow valve logic to permit valve closure from the

'

control room.

The inspector reviewed the licensee's evaluation of this event and corrective

actions. The licensee's evaluation considered various aspects of the plant's design

i and licensing bases and resulted in clearly determir.ing that the original design basis

i for this system did not require the minimum flow valves to be containment isolation

,

valves. That portion of the system was required to open for accident purposes and

was considered an extension of the containment boundary. This position was also

clearly reflected in the licensee's response to the TMl Action Plan for containment

'

isolation dependability, as stated in a licensee letter to the NRC on January 8,

1980. At that time, the core spray system was identified as one of a number of

systems that communicated directly with the containment space without an

automatic isolation valve. The licensee implemented routine inspections of the

associated piping as a means for ensuring the integrity of the containment

boundary. The licensee's evaluation noted that the conflicting information between

the design and licensing bases rogarding containment isolation capability .or the CS

mini-flow valves resulted from an incomplete review of the FSAR requirements for

i these particular valves. That resulted in an error translation into the Appendix J

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mini-flow valves resulted from an incomplete review of the FSAR requirements for

these particular valves. That resulted in an error translation into the Appendix J

program. The licensee's corrective actions appropriately addressed the causes of

the design bases documentation error. Further, as a result of the licensee's review,

they modified the controls design for these valves in order to enhance the

operator's capability to erisure containment isolation by installing a remote manual

isolation function.

The inspector concluded that the licensee's evaluation, root cause determination

and corrective actions were acceptable, in that the design bases of the plant was

accurate, and that the as-built configuration met the design basis, this condition

was not a violation of NRC requirements. The licensee's action to modify the plant

configuration to provide an enhanced operator control for containment isolation

function was viewed as a positive measure. LER 96-024is closed.

M8.4 (Closed) LER 96 27 and NCV 97-08-05: Lack of reouired yerificadons results in

inconsistency between technical specification instrument settino description and the

as-built confiouration of the low oressure coolant iniection (LPCI) oumo control

lonic.

This LER describes the licensee's discovery of use of a time de;ay relay with a

setpoint inconsistent with the TSs while testing the LPCI system actuation log c

during the refueling outage in October 1996.

The time delay relay minimum time delay cetting was 0.55 seconds for LPCI pump

start and the plant TS recuired no time delay for two affected LPCI pumps. The

licensne determined that the installed time delay relays were consistent with the

materials used since initial plant startup and that the plant TS requirements (TS

7,4.3.5.2) have also not changed since initial plant startup. Therefore, this

inconsistency between the as-built design and the TSs always been present. Due

to the age of the issue, the licensee was not able to determine an actual root cause.

However, the apparent cause was an inadequato verification of the license

requirements versus the system design specifications during the development of the

TSs. The licensee replaced the time delay relays with a modified design to permit

instantaneous starts of the affected LPCI pumps. This corrected the inconsistency.

Further, the licensee was already implementing a major Technical Specification

improvement project that would result in verifying that the TSs and as-built design '

criteria were consistent.

The inspector concluded that the licensee's assessment, root cause determint.aon,

and corrective actions for this event were appropriate. However, failing to ensure

that tha LPCI surveillance tests met the acceptance criteria stated ir. the TSs was a

violation of the TS. This non-repetitive, licensee identified and corrected violation

was treated as a non-cited violation (NCV 97-08-05), consistent with Section

Vll.B.1 of the NRC Enforcement Poliev.

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lil. Engineering

E1 Engineering Support of Facilities and Equipment

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E1.1 Safety Grade Qualification of Welds in Emeroency Diesel Generator Suocort  !

Systems

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a. Backoround and insoection Scope (93702,92903,37551) 1

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1

The inspector observed and assessed the licensee's response to an industry event

at Millstone, involving safety class support systems (such as the Jacket water

cooling and lubricating oil systems) that had been fabricated and installed as part of

the EDG unit by Fairbanks Morse which were apparently not welded to ANSI B31.1 ,

standards or an equivalent, i

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b. Observations and Findinos

On September 4, the inspector discussed the EDG subsystems weld issue with VY

< systems engineering staff. The inspector was informed that VY had received

information about the problem and would be investigating. The inspector visually

examined piping welds in the EDG lubricating oil and jacket water cooling systems.

- The inspector observed that there was a strong possibility that the VY EDG

subsystem piping had likewise not been welded to ANSI B31.1. The inspector

.

observed that the welds had not been ground smooth to support any form of non-

destructive testing, and areas of concavity existed in some welds Due to the

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potential operability impact on both EDGs, the inspector p:omptly discussed this

issue and his preliminary observations with the plant manager. .

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On September 10, Event Report (ER) No. 97-1224 was generated which addressed )

the potential weld problem with the EDGs. The immediate operability determination

was that the EDGs were operable, bamd on the vendor's conclusion that the

Millstone EDGs' piping welds had been found to satisfy Northeast Utilities' Millstone

'

Unit 2 seismic analysis, and based on a walkdown by engineering personnel who

judged the welds to be satisfactory by visual examination. ER 97-1224 was

reviewed by plant management during the September 11 ER screening meeting.

Initially, VY did not consider the Millstone problem to be an immediate concern

because their procurement specifications had been different than Millstone.

Specifically, Millstone had purchased the EDGs and dona their own seismic analysis,

, whereas VY had specified in the procurement specifications that the EDGs were to

be fabricated and delivered seismically qualified. The inspector expressed concern

regarding discovery of the partial penetration welds and the implications uf this

discovery on the seismic qualification of the VY EDG welds. He discussed this

concern with both NRC regional management and VY station management.

Subsequently, VY initiated development of a Basis for Maintaining Operation (BMO)

for the EDG weld issue, to be completed by September 17.

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- BMO 97 39,"Possible Less than Full Penetreion Welds on Vendor Supplied Skid

Mounted Piping for the Emergency Diesel Generators," was reviewed by the plant

operations review committee (PORC) on September 17. The licensee determined

the EDGs were operable based on:

1. Visualinspection of the welds ' hat showed no obvious external defects.

.

2. The vendor's position that the w? ids were deemed acceptable based on many

'

years of successfulin-service operation of their equipment.

3. Succusful operation of Fairbanks Morse diesels in harsh environments, including

temperature, vibration, and shock.

4. Analyses that had been performed by ancther licensee, which indicated that less e

than full penetration welds (in the;r case,66 porcent) were acceptable.  ;

5. VY EDGs had been evaluated as part of the seismic qualification upgrade

(SOUG); the SQUG data base included diesels of similar vintage that had gone

through seismic events of magnitudes in excess of VY's design basis and did not

fall.

6. Preliminary calculations indicated that the EDG piping of concern had significant

margin to ASME Code B31.1 limits, for both normalloading and seismic loading.

'

On September 22, VY started an LCO maintenance outage on the 'B' EDG. As a

result of the weld issue, a section of lube oil system piping was removed for

destructive examination. The piping is approximately 4-inch diameter and contains

6 welds. There are two material thicknesses,0.250 and 0.120-inch, and three

weld combinations,0.250 to 0.250,0.250 to 0.120, and 0.120 to 0.120. Weld

penetration was determined by an off-site lab (Massachusetts Materials Research)

to be 50% for the 0.250-to-0.250 weld, and 22% for the 0.120-to-0.12Oweld.

During the inspection, a crack was found in the 0.250-to-0.250 weld, through wall,

starting from the root. The crack was about 0.5-inch in length, or 4% of the

circumference. The crack was on the same weld (first weld downstream of the LO

pump discharge) and in tt.e same location on the weld as had developeo a leak at

Millstone Unit 2. The VY engineering staff concluded that the crack would self-

arrest at about 120* circumferential due to reaching the compressive side of the

weld, and would result in a leak rather than a catastrophic failure. During this

inspection period, VY had also conducted structural testing by applying tensile

- stress equivalent to the operating stress, and then applying a bending moment of 6

times the combined operating and seismic stress to the weld. The weld did not fail

this structural test,

c. Conclusions

At the end of the inspection period, the licensee had completed formal EDG support

piping stress analyses and had completed a metallurgical analysis which the licensee

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has concluded supports their initial operability determination. These items were

under review by the NRC staff. Pending the results of further NRC staff review, the

EDG support piping welds issue is being tracked as an inspector follow-up item (IFl

97-08-01). The licensee's response to this issue, to date, has been consistent with

the guidance of Generic Letter 91 18 for identification and resoluiion of a degraded

or non conforming condition.

E2 Motor Operated Valve Program Review (Tl 2515/109)

E 2.1 Introduction

On Jun9 28,1989, the NRC issued Generic Letter (GL) 8910, " Safety-

Related Motor-Operated Valve Testing and Sur" ': lance," wWeh requested

licensees to establish a program to ensure that switch settings for safety-

related motor operated valves (MOV)s were selected, set, and maintained

properly. Seven supplements to the GL have been issued to provide

additionalinivrmation and guidance on development of programs,. NRC

inspections at Vermont Yankee (VY) were conducted based on guidance

contained in NRC Temporary Instruction (TI) 2515/109," Inspection

Requirements for Generic Letter 8910."

On December 29,1995, VY notified the NRC that the GL 89-10 program was

corr.plete. The NRC had previously conducted an initial programmatic (Part 1)

inspection at VY in May 1991, cs documented in Inspection Report (IR) 91-80.

During October 1993, the NRC performed an implementation (Part 2) inspection, as

documented in IR 9316. A closure (Part 3) inspection for the purpose of verifying

that VY completed its commitments to develop and implement a safety-related MOV

program as described in GL 89-10 and its supplements was performed in May

1996,(IR 96-05). During that inspection, the NRC determined although the VY

staff had generally implemented an acceptable GL 8910 program, the following

items were noted:

  • Design basis evaluations of non-dynamically tested MOV's in accordance

with Attachment 6 of " Engineering Guideline for Evaluation of Motor-

Operated Valve Design Basis Capability" were nct completed.

  • The assumptions applied to grouped MOVs were not adequately cupported

by test data.

To address the above items, in letters dated April 18, and May 9,1996,

respectfully, VY agreed to use the Electric Power Research lnstituto (EPRI) thrust

performance preo.ction program on six MOVs identified in GL 8910 supplement 3

and two valves classified as "high risk" in the Individual Plant Examination (IPE)

report. Additionally, the design basis evaluations of non-dynamically tested MOV's

described in the MOV program manual would be completed by July 1,1996.

Finally, fifteen additional "high risk" valves would receive dynamic tests during the

1996 refuel outage.

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The purpose of this fourth inspection was to examine the actions implemented at

VY to address the closure i, sues identified during the Part 3 inspection and

determine if those actions were sufficient to warrant " closure" of the NRC staff

review of the GL 89-10 MOV program.

E2.2 Evaluation of Hiah Risk MOV Dynamic Test Results

a. Insnection Scoce

Fifteen valves received dynamic tests durir g the previous refuel outage. Of those

va;ves, the inspectors selected the test results for the following MOVs for review:

V10-16A/B Residual Heat Removal (RHR) Pump Discharge Mini Flow

Returns to the Suppression Pool

V10-25 A/B RHR to Recirculation Loop Isolation Valves

V10-39 A/G RHR Containment Spray / Suppression Pool Cooling Supply

Valves

V14-5 A Core Spray Pump Minimum Flow Valve

V70-19B Service Water Supply Header Cross Connect Valve

The review consisted of examining data associated with: (1) valve factor, which

correlates differential pressure to the stem-thrust requirement; (2) stem friction

coefficient, which affects the conversion of actuator output torque to valve-stem

thrust; and (3) rate of loading or load sensitive behavior, which reflects the change

(usually a loss) in deliverable stem thrust under dynamic conditions as compared -

with the available thrust measured under static conditions. The inspectors also

reviewed, " Vermont Yankee Engineering Guideline for Evaluation of MOV Design

Basis Capability," Rev.1, dated March 12,1996, and calcu:ctions which evaluated

difierential pressure tests performed on the Residual Heat Removal (RHR) Service

Water (SW) and Core Spray (CS) systems.

b. Observations and Findinas

General

The " Vermont Yankee Engineering Guideline for Evaluation of MOV Design Basis

Capability," outlined the process used to establish MOV switch settings, evaluate

data and monitor valve performance. The document also contained the

assumptions used to determine valve factor, load sensitive behavior, stem friction

coefficient, and various capability margins. The engineering guideline also specified

the statistical methods used to ovaluate multiple test results.

When performing MOV testing (under static or dynamic conditions), valves were

stroked three times in each direction. This allowed personnel to assess the valve's

ability to perform in a consistent manner. Each performance parameter was

determined or evaluated using a " student's t~ statistical evaluation of the three test

results using a 95% confidence level. The inspectors noten VY completed the

- evaluations required in Attachment 6 of the MOV program manual. Therefore, tnis

closure item identified in NRC inspection report 50-271/96-05,was resolved.

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Test Results

VY used the standard industry equations and a statistical evaluation of three

dynamic tests (for each valve), to determine actuator capability margins, structural

margins, valve f actors, load sensitive behavior, and stem friction coefficients. MOV

. performance parameters (i.e. , valve f actor, load sensitive behavior, and stem

friction coefficient) were compared with previous dynamic test results to verify

program ascumptions we's valid.

Apparent valve factors and loari sensitive behavior values measured during dynamic

testing of the selected MOVs were bounded by the current program assumptions

(i.e.,0.60 for gate valve f actors,1.10 for globe valve f actors, and 10% margin for

load sensitive behavior). However, the test results for globe valveh V10 34B and

V13 27 had measured load sensitive behavior values of 17.9% and 13.8%,

respectfully. Further, the test results were not fed back into the individual valve's

component thrust calculation.

The inspectors noted this observation appeared to be restricted to a few valves. To

ensure future MOV thrust calculations ref.'ected the results of test data, VY

comm;tted to rev!so the existing calculations to reflect the results of test data for

each dynamically tested valve. Program documents would also be revised as

appropriat- +L 'eflect this expectation. The inspectors determined the corrective

action was :%,ropriate to resolve this obsvvation,

based on the load sensitive behavior performance noted for valves V10 34B and

V13 27, the inspectors reviewed the dynamic test data for the remaining population

of globe valves. Tnis review included performing a " student's t" statistical analysis

of all available in plant globe valve load sensitive behavior data. Based on this

review, the irspectors determinod an 18% margin for load sensitive behav;or should

be applied to notedynamically tested globe valves. The inspectors also performed a

similar review of globe valve dynamic stem friction coefficient performance and

determined that the assumeo value of 0.15 was non conservative as compared to a

0.16 value that resulted from analysis of the wailable in plant globe valve test data.

Although the VY staff's assumptions for load sensitive behavior and stem friction

coefficient did not bound the majority of the globo valve test data, the inspectors

noted this finding did not effect valve operability since the non-dynamically tested

globe valves had adequate design margin. At the conclusion of this inspection, VY

committed to perform a review of the globe valve dynamic test data and provide an

additional allowance to account for the offects of Icad sensibve behavior for non-

tested globe valves.

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c. Conclusions l

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Overall, the dynamic test results reaffirmed the design assumptions used to

establist h0V switch settings. The exception was the load sensitive behavior l

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assumpthn (c.' globe valves, which did not appear to bound the majority of the test

data, in some instances, component calculations were not updated to reflect the

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latest test data. Neither of these observations was significant, since the examined -

MOVs had adequate capability and the thrus( calculations were generally up to-

date. VY committed to resolve these items by January 30,1998, which was

acceptable for program closure.

E2.3 Use of the Electric Power Research Institute Thrust Calculation Procram

a. insoection Scope

The inspectors reviewed calculations performed on valves in the Reactor Water

Cleanup (RWCU), High Pressure Coolant injection (HPCl), and the Reactor Core

isolation Cooling (RCIC) systems to assess how VY used the Electric Power

Research Institute (EPRI) performance prediction methodology MOV thrust

calculation program. Additionally, the inspector reviewed a summary analysis,

which compared the thrust calculated by the EPRI program to the thrust produced >

by valves with their current switch settings.

'

b. Observations and Findinas

The VY staff had properly used the EPRI calculational program. Specifically, def ault ,

friction coefficients were used when necessary, the appropriate valve disc and

guide material comt,inations were specified, and the system model used blowdown

flow parameters to establish the design basis requirements. However, one

exception was noted, V( did not perform the calculations needed to estimate the

unwedging loads for valves V13 21 and V2319, which had open safety functions.

VY indicated these calculations would be completed by December 1997.

The six Supplement 3 MOVs were evaluatect for the closing safety function under

blowdown flow. The initial EPRI calculation for these valves indicated that the

thrust requirements were unpredictable. This result was caused by the software

inputs that specified sharp guide edges for the valve disc. VY revised the input

values to reflect a 0.04" chamfer for the guide edges, which resolved the

sof tware's unpredictable results. This change was based on valve internals

inspections performed on all of the affected valves.

The results of the EPRI program were reconciled in an analysis, dated March 10,

1997, which compared the EPRI predicted thrust requirements to the current thrust

requirements contained in the component calculations. The existing in-plar.t valve

switch settings exceeded the EPRI predicted thrust requirements for ull six

Supplement 3 MOVs. However, the in-plant open thrust requirements were non-

conservative for two non Supplement 3 valves, which had open safety functions.

The VY staff indicated both valves had adequate thrust capability to ensure proper

operation considering the higher EPRI values. Therefore, the EPRI results did not

affect valve operability.

VY is corrntly using the EPRI program to validate the current switch setting on all

applicable valves. The inspector considered this initiative to be a program strength.

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c. Conclusions

VY properly used the EPRI program to develop predicted thrust values. The

exception was the failure to complete and apply the unwedging hand calculations

for two valves. This omission will be corrected by December 1997, which would

be acceptable for program closure.

E2.4 Valve Grouoina

a. Insocction Scan

The inspectors reviewed the grouping methodology used to analyze the performance

characteristics of non dynamically tested MOVs. The review consisted of an

examination of dynamic test data and grouping criteria outlined in the MOV program

manual.  !

b. Observations and Findinas

VY divided their MOVs into six valve groups based upon manuf acturer, type, and

stem orientation. However, the inspectors determined that the grouping criteria

were too broad to provide meaningful comparisons between valve types.

For example, one group contained Anchor Darling double disc gate valves which

ranged in size from four to 28 inches. VY was not able to dynamically test any of

the val /es, so a valve factor of 0.50 was assumed based on analysis of eleven

Anchor Darling valves tested at another nuclear station. However, the inspectors

noted that the largest valves tested at the other station were six inches in diameter.

It wac not evident that this data would be applicabl' to all valves in this group

population. The VY staff was also unsure if the data was obtained from valves

oriented in the " preferred" direction (i.e., with the lower wedge downstream).

Industry testing has shown that disc orientation in the "non-preferred" location can

increase the thrust requirements to close the valve.

Based upon this observation, the VY staff committed to improve upon the current

grouping methodology by anulyzing the performance of the non dynamically tested

valves using the EPRI PPM program, if the thrust predicted by the EPRI program !.,

greater than the current MOV setup, the licensee committed to revise the MOV

switch settings. The licensee agreed to complete the validation process by

January 30,1998,

c. Conclusions

Although the current MOV grouping criteria were questionable, VY intends to

address this observation by using the EPRI PPM program and adjusting MOV switch

settings as appropriate bs January 30,1998. The mspector concluded this

approach would be acceptable for program closure.

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E8 Miscellaneous Engineering issues (92700)

E8.1 IQuen) IFl 96-11 01: Ememency Diesel Generator (EDG) Tornado Protection

a. Backaround and Inspection Scone (92903)

Licensee staff follow up of an industry operating event report (NRC Information

Notice 96 06, involving plant structures' tornado pressure relief), identified that the

EDG enclosures did not contain the differential pressure relieving capability specified

by the construction drawings. EDG operability was promptly assessed by the VY

staff and the Basis for Maintaining Operation (BMO) process was initiated. As

documented in inspection report 9611, the inspector foand the compensatory

actions taken to have been appropriate, however, final resolution to this plant

design issue was pending. The inspector conducted a follow up inspection of this

issue to evaluate the licensee's corrective actions and their progress in resolving

this design concern.

b. Observations and Findinas

The inspector determined that the current revision to BMO No. 96-08,"Effect of

design basis tornado pressure load on the diesel / day tank room enclosure "

(revision 4, dated 9/11/97) maintains the compensatory measures to block open the

= EDG enclosurs access doors when tornado conditions are anticipated. These

manual actions have remained in effect, even though the EDG enclosures were

modified in April 1997 with automatic spring actuated differential pressure relieving

dampers. The inspector determined that the compensatory measures remain in

place to address a discrepancy found in the tornado loading accident analysis.

Specifically, the discovery by the VY staff that the turbine building does not have a

pressure relieving capability in the event of a high energy line break (HELB)

(reference inspection report 97-02, section 01.4), potentially invalidates the

analysis assumption that the turbine building pressure is essentially atmospheric at

time zero in the tornado loading ac-ident scenario response time line.

Consequently, the design basis tornedo load (300 mph winds whh an

accompanying 3 psig pressure change in 5 seconds) impacting on the current EDG

enclosure and turbine building would petontially result in the EDG to turbine building

concrete block wall being subjected to a differential pressure in excess of its

allowable design limit (1 psig).

The inspector determined that engineering design change request (EDCR) 97 419 is

under development to address the turbine building HELB pressure relieving concern

and is targeted for field installation by December 1997. Preliminary discussions

with the responsible design engineering staff and plant management identified that

EDCR 97-419 was not originally proposed as a vehicts to resolve the apparent

discrepancy with the tornado accident analysis time-line assumption. However, the

licensee acknowledged the inspector's observation that the two design issues were

connected and, at the conclusion of the inspection period, VY was examining

avenues to resolve this apparent design assumption conflict within the scope of

EDCR 97 419.

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c. Conclusions

The VY staff's pursuit of resolving the EDG enclosure tornado ioading differential

pressure vulnerability demonstrated a generally thorough examination of ro ited a

turbine building HELB structural design attributes. IFl 961101 remains open,

persding inspector review of the VY staff's final resolution of this EDG enclosure

differential pressure concern.

E8.2 (Closed) LER 9811 and NCV 97-08 06: Failure to perform Intervice Testina (IST)

on valves that should have been included in the IST Pronram.

These licensee identified IST Program deficiencies involved the f allure to include the

high pressure coolant injection (HPCll, reactor core isolation cooling (RCIC), and

core spray (CS) systems' alternate keep fill system (condensate transfer system)

check valves (V23 208, V13 20B,V14 22A/B, and V14 23A/B)in the IST Program ,

< for quarterly reverse flow cessation stroke testing. The identification of these

testing oversights was part of an ongoing comprehensive IST Program review

initiated in late 1995 (reference inspection reports 95 22 and 95 23 and associated

LERs 9517 and 96 01).

As stated in LER 9611, dated May 16,1996,the Aoril 25 radiography testing (and

subsequent testing) of the effected check valves identified proper valve seating to

prevent reverse flow. The VY staff revised the IST Program to include these valves

for future testing and continued their comprehensive IST program review with no

additional discrepancies noted. The inspector determined that VY appropriately ,

'

documented and reported this event. The inspector also verified that a dedicated

IST Prooram coordinator was assigned, as stated in LER 9611. The inspector -

assessed that corrective actions taken for prior violations in this area would not

have reasonably prevented this violation. This licensee identified and corrected

violation was treated as a non cited violation (NCV 97 08 06), consistent with

Section Vll.B.1 of the NRC Enforcement Policy. LER 9611 is closed.

E8.3 (Closed) LER 96-14 Sucolement 1: Tornado orotection not orovided for diesel

aenerator rooms as specified in the Final Safety Analysis Report due to f ailure to

implement olant construction /confiauration chanae documenth

Supplement 1, dated January 29,1997, documented the results of the licensee's

root cause evaluation for this event and the associated corrective actions. As

previously documented in inspection report 9611 and in Section E8.1 of this report,

this condition is being addressed via BMO No. 96 08, revision 4. As stated in

Section E8.1,IFl 961101 remains open to track licensee final resolution and

inspector review of this issue. LER 9614, Supplement 1 is closed.

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'i94 IClh ) LER

1 96 21: Inadgquate orocenural controls of MOV limit switch settinos

$1ML 3 ootential commen cause f ailu.e mode with the capacity to affect multinie

NM unnificant componente.

.

LER 96 21, dated October 7,1996, was reviewed in congnetion with inspection

follow up item IFl 96-09 03, which was closed in inspection report 97 05, section

,

E8.2. As previously documented, this licensee identified and corrected violation

was treated as a non cited violation consistent with Section Vll B.1 of the N_flQ

Enforcement Poliev. The inspector concluded that LER 96 21 appropriately satisfied

the NRC reporting requirements of 10 CFR 50.73. LER 96 21 is closed.

E8.5 (Onen) URI 97-03-02: Cable separation does not satisfy UFSAR seoaration criteria.

This unresolved item portains to a number of licensee identified discrepancies

between the as built wiring at the plant and the cable separation criteria stated in

the UFSAR associated with safety related circuits. The following information

updates the unresolved item.

The licensee reported in LER 96-028, dated November 18,1996, another example

of inadequate cable separation for the LPCI outboard isolation valve actuating

circuits. This was identified and corrected during the October 1996 refueling

outage. The licensee determined that the root cause for this event was an

erroneous mis-labeling of the associated circuit i during a 1976 design change.

While the 1976 modification did not cause the circuits to violate the electrical

separation criteria in the FSAR at that time,it resulted in the engineers not

recognizing that the circuits were required to be separated since they were from

different electrical divisions. Subsequent modifications resulted in the circuts being

placed in a common, non nuclear safety panduct, in violation of the cable separation

criteria.

The inspector concluded that the licensee's immediate corrective actir<ns were

appropriate and brought the configuratior of the affected circuits bacx into

conformance with the FSAR criteria. Accordingly, LER 96 28 is closad, but the

overallissue regarding cable separation remains unresolved pending further review

of the licensee's evaluation and additional corrective actions, as necessary to

prevent recurrence. A determination of future enforcement action for this

unresolved item will include information from the licensee's efforta discussed in LER

96-28. URI 97 03-02 remains open.

E8.6 (Closed) URI 9316-01: Pressure Lockina/ Thermal Bindina (PLTB) of Gate Valves

This item was opened to track the status of VY's corrective actions for gate valves

determined to be susceptible to pressure locking, in a letter dated February 8,

1996, VY described the process used to evaluate valves for susceptibility to PLTB

and its program to modify valves that may be susceptible to these phenomena.

Currently only V13 20, the Reactor Core Isolation Cooling (RCIC) injection test

valve, is susceptible to pressure locking. To address the pressure locking concern

for this valve, a hole will be drilled in one side of the valve disc daring the 1998

refuel outage. The actions taken by the licensee to address PLTB are currently

_ _ _ - - - - - - -_- - - - _ _ - - - ..- - - -. - -.- . - .

.

. .

19

f

under the review of the Office of Nuclear Reactor Regulation (NRR) who will  !

evaluate the acceptability of the program in a safety evaluation report. Since NRR is '

t

now tracking the status of the PLTB program, maintaining a separate redundant

unresolved item for the same purpose is no longer necessary. This item is closed.  :

,

E8.7 (Closed) VIO 96-05 03: Uodate and Control of MOV Proaram Manual i

'

This violation was issued to document that the MOV program manual was not being ,

updated in accordance with VY station administrative guidelines. As a result, the

program manual contained outdated, conflicting, and contradictory information. To

address this violation, the VY staff revised the program manual so that it described

the current MOV practices. Further, the manual was placed under the document

i

control procedure AP 6805 to ensure future program changes are routed and

distributed in a timely manner. The inspector reviewed the program document and

verified it described the approach used to establish MOV switch settings. The i

inspector concluded the licensee's actions were appropriate and this item is closei

E8.8 (Closed) EA 95 070, VIO 01013: Failure to Correct a Condition Adverse to Quality ,

This violation documented weaknesses in the VY's corrective action processes

including a f ailure to correctly analyze the susceptibility of core spray injection

,

valves to pressure locking. As outlined in NRC inspection report 50 271/96-05,the

inspector concluded VY's corrective actions appeared to be acceptable. However,

1

two areas for improvement were noted and the violation was not closed.

Specifically, the Basis for Maintaining Operability (BMO) guideline did not limit the

time a degraded condition could remain in service before full equipment qualification

was restored. Further it was not evident, the Nuclear Safety Audit Review

Committee (NSARC) had performed a comprehensive assessment of the

eMectiveness of the corrective actions implemented in response to this violation.

>

Based upon a review of the N"; ARC charter, the inspector concluded such a review

was appropriate in exercising the full extent of the ommittee's responsibilities.  ;

The inspector reviewed the BMO process and concluded adequate controls were

established to limit the time a degraded or non conforming condition could exist.

The procedure now requires that a condition adverse to quality be dispositioned

within specified time periods as defined in Administrative Procedure (AP) 0009,

Event Reports. For example, category 1 event reports should be dispositioned

within 45 days, category 2 within 90 days, and category 3 within 120 days. In

addition, the BMO instruction states a periodic review (semi annual) of all open

items to verify that the conditions and assumptions remain valid shall be performed.

The results of this review are then presented to the plant operations review

committee (PORC).

The inspector noted there were 44 BMOs in place. VY intended to resolve each

BMO before startup from the winter 1998 refuel outage. The VY staff had also

performed an assessment to ensure the cumulative effect of outstanding BMOs

would not have a deleterious effect on the operator's response to a transient.

--

Based upon the corrective action, the inspectors concluded this issue was resolved.

.

- -. - .- .. _= -- .. - . . __

_ - _ . . . . - . _ _ --

.

4

20

To improve the oversight of plant operations, it appeared oversight groups increased

the number of self assessments and independent audits performed on individual

program areas. For example, a MOV program audit was completed in March 1997.

The inspector noted such periodic reviews could provide valuable insight into the

effectiveness of plant operations and should f acilitate the evaluation of the

licensee's corrective action process and resolve this weakness. This issue is

closed.

IV. Plant Support

P3 EP Procedures and Docurnentation

a. inspection Scoce (82701)

Regional inspectors reviewed several changes the licensee made to the emergency

plan and implementi!q) procedures. The inspectors reviewed these changes in the

NRC Region I office. They conducted this review to verify that the changes made

to the Emergency Plan and implementing procedures were made in accordance with

Part 50.54(q) of NRC regulations, (i.e., that they did not decrease the ef fectiveness

of the Emergency Plan). The list of Emergency Plan sections and implementing

procedures reviewed is contained in Attachment A of this report.

c. Conclusions

Based on the licensee's determinations that the changes did not decrease the

overall effectiveness of the Emergency Plan, and that the Plan, as changed,

continues to meet the standards of 10 CFR 50.47(b) and the requirements of

Appendix E to Part 50, NRC approval of these changes is not required. The in-

office review of these changes indicated them to have been made in accordance

with 10 CA 50.54(q).

R1 Radiological Protection and Chemistry (RP&C) Controls

t

R 1.1 (Closed) URI 97 06-02: Imolementation of the Radioactive Liould and Gasaput

Etfluer.t Control Proarams

a. insocction Scone (84750 01)

The inspection consisted of: (1) tour of the plant, including the control room; (2)

review of liquid and gaseous effluent release permits; and (3) review of unplanned

and unmonitored release pathways,

b. Observations and Findinas

The inspector toured the control room and selected radioactive liquid and gas

processing f acilities and equipment, including effluent / process radiation monitoring

systems (RMS) and air cleaning systems. All equipment was operable at the time M

the tour. The inspector also noted that the licensee maintained air balances for

--- - _ _

. _- - . _ - - - - - _ _ .

- - . . - - - - - - - - _ - - - - . . _ - _

.

21  !

reactor, turbine, and radwaste buildings to assure conformance to Final Safety

Analysis Report (FSAR) specifications. The inspector noted that the licensee ,

monitored a negative pressure only for the reactor building. (see Section R.2.3 of

'

this inspection report for details.)

During the review of selected radioactive gaseous effluent discharge permits, the

inspector determined that the discharge permits were complete and met the

Technical Specification /Offsite Dose Calculation Manual (TS/ODCM) requirements

,

. for sampling and analyses at the frequencies and lower limits of detection

established in the TS/ODCM. The inspector noted that there had been no

radioactive liquid releases from the Vermont Yankee site for several years while

pursuing effluent ALARA and plant water conservation.

The inspector also noted that there was one unplanned /unmonitored radioactive  ;

liquid or gas release since the previous inspection. The licensee found cracks in the i

radwaste building exhausting ventilation duct leading to the plant stack and the

licensee made a 10 CFR 50.72 report (ENS No. 32842) on August 29,1997. The

inspector reviewed the licensee's radiological and environmental assessment results.

The inspector determined that the licensee's actions were acceptable and that there

was no radiologicalimpact to the public safety and the environment. Unresolved

item URI 07 06 021s closed,

c. Conclusion

Based on the above reviews and observations, the inspector determined that the

licensee mainta!ned ar.d implemented effective radioactive liquid and gaseous

<

effluent control programs.

R2 Status of RP&C Facilities and Equipment

R2.1 Calibration of Effluent / Process / Area / Accident Radiation Monitorina Systems (RMS) ,

,

a. Inanection Scope (84750 01)

The inspector reviewed the most recent calibration results for the following

effluent / process / area RMS and associated flow rate monitors to determine the

implementation of the TS requirements and FSAR commitments-

  • Main Stack Noble Gas Monitors (Normal and High Ranges)
  • Main Stack Flow Rate Monitor
  • Augmented Offgas (AOG) Building Noble Gas Monitors
  • AOG Flow Rate Monitor
  • Reactor Building Monitor
  • Spent Fuel Pool Floor Monitor
  • Liquid Radwaste Discharge Monitor

l

-- -,

l

, , . -- - , - . - . .--. - . - - _

-. -.-

.

22

b. Observations and Findinas

The l&C, Chemistry, and Radiation Protection departments had the responsibility to

perform electronic and radiological calibrations for the above radiation monitors. All

reviewed calibration results were within the licensee's acceptance criteria. The

Chemistry Department performed trending analyses for the effluent RMS, which

was considered a licensee strength.

During the review of the above RMS calibration documentation, the inspector

independently calculated and compared several calibration results, including linearity

tests and conversion f actors. The inspector determined that the licensee's results

were comparable to the independent calculations,

c. Conclusions

Based on the above reviews, the inspector determined that the licensee maintained

and implemented a good calibration program and good trending analyses for effluent

radiation monitoring systems.

R2.2 Air Cleanina Systems

a. insoection Scone (84750 01)

The inspector reviewed the licensee's most recent surveillance test results (in place

HEPA and charcoalleak tests, air capacity tests, pressure drop tests, and laboratory

tests for the iodine collection efficiencies) for the standby gas treatment system

(SBGT) required by TS. In-place HEPA and charcoal surveillance tests for the

Advanced Off-Gas (AOG) system and the radwaste building air cleaning system

were also reviewed.

b. Eb3myations and Findinas

All surveillance results were either within the TS acceptance criteria or the

administrative acceptance criteria.

Recently, the Office of Nuclear Reactor Regulation (NRR) identified that there was a

potential conflict regarding the charcoal testing methodology for the iodine

collection efficiency performed by the licensee / contractor laboratory. Normally, the

licensee's TS specifies Regulatory Position C,6.a of RG 1.52, Revision 2,

March 1978, as the requirement for the laboratory testing of the charcoal. RG 1.52

references ANSI N5091976," Nuclear Power Plant Air Cleaning Units and

Components." ANSI N5091970 specifies that testing is to be performed in

accordance with paragraph 4.5.3 of RDT M 161T," Gas Phase Adsorbents for

Trapping Radioactive lodine and lodine Components." The essential testing criteria

are: (1) 70% or 95% relative humidity (RH): (2) 5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> pre equilibration time, with 4

air at 25' C and plant specific RH; (3) 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> challenge, with gas at 80* C and

plant-specific RH; and (4) 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> elution time, with air at 25' C and plant specific

RH. The latest acceptable methodology for the laboratory testing of the charcoalis

.

23

ASTM D 38031989,which requires licensees to maintain 30* C during all testing

phases.

The inspector noted that the VY staff performed two separate surveillance tests for

the SBGT: (1) ANSI 5091980and ASTM D 3803 Method C-1979 (13CP C and

95% RH); and (2) ASTM D 38031989(30* C and 95% RH). The licensee

recognized that the:e was a potential problem for the iodine collection efficiency

test methodology. The licensee, therefore, added the ASTM D 38031989

methodology in May 1995 and trended iodine collection efficiencies obtained from

both methodologies. The inspector concluded that the licensee utilized an excellent

surveillance test methodology for the SBGT system, and met all regulatory

requirements.

c. Conclusions

Based on the above reviews, the inspector determined that the licensee maintained

the plant air cleaning systems in accordance with estabilshed design specification.

The licensee performed excellent iodine collection efficiency test methodologies for

the SBGT system.

R2.3 Plant Air Balance

a. Insoection Scope (84570 01)

The inspection consirted of: (1) review of the main stack exhaust flow rate; (2)

review of exhaust flo'n rate from various buildings; and (3) assessment of the plant

air balance.

b. Observations and Findinas

Procedure OP 2011, " Gaseous Radwaste" listed maximum exhausting f an

capacities of various buildings (e.g., reactor, turbine, and radwaste buildings). The

exhaust air from these buildings was released to the environment through the main

stack. The maximum exhaust air flow rate from these building was 181,900 cfm

while the main stack flow rate was about 150,000 cfm. The difference, of about

32,000 cim, potentially demonstrated that station ventilation systems were not

properly balanced. The original plant air balance data, measured in 1071(150,000

cfm), was no longer valid since the turbine building exhaust was connected to the

main stack in 1993. The licensee estimated that the main stack air flow exhaust

would be increased, from 150.000 cfm to 200,000 cim, due to addition of the

turbine building ventilation (sce inspection report Nos. 50 271/93 25and 50-

271/94 27 for details). Verification and corrections to exhaust fan capacities

(actual and maximum) listed in procedure OP 2611," Gaseous Radwaste," will be

reviewed during a subsequent inspection (IFl 97 08-02).

The licensee maintained a negative pressure in the reactor, turbine, and radwaste

buildings. The licensee monitored differential pressure daily in the control room for

the reactor building. However, the licensee maintained a negative pressure for the

24

turbine and radwaste building through damper position indications since there were

no installed delta-P gauges. The licensee planned to install delta P gauges for

turbine and radwaste buildings to assure the negative pressure was maintained.

This action will also be reviewed by the inspector during a subsequent inspection

(IFl 97 08-02),

c. Conclusions

Dased on the above reviews, the inspector made the following conclusions:

  • the actual and maximum f an capacities listed in procedure OP 2611 should

be verified to avoid a potential inaccurate projected dose calculation to the

public;

  • the licensee maintained the negative pressure for the reactor building verified

delta P daily using a installed gauge;

e the licensee maintained air balanco for turbine and radwaste buildings

through administrative means (e.g., damper position); and,

e the licensee planned to install delta P gauges for the turbine and radwaste

buildings.

R3 RP&C Procedures and Documentation

a. Inspection Scone (84570-01)

The inspection consists of a review of: (1) selected chemistry procedures to

conduct the effluent control programs; (2) secor:d hclf of the 1995 Semiannual

Report and the 1996 Annual Radioactive Effluent Release Reports;(3) the ODCM;

and (4) implementation of 40 CFR 190 requirements,

b. Observations and Findinas

The inspector noted that reviewed ef fluent control procedures were detailed, easy

to follow, and ODCM requirements were incorporated into the appropriate

procedures. The licensee had good procedures to satisfy the TS/ODCM

requirements for routine end emergency operations.

The inspector reviewed the 1995 Semiannual and the 1996 Annual Radioactive

Effluent Release Reports. These reports provided data indicating total released

radioactivity for liquid and gar.cous effluents. The assessment of the projected

maximum individual doses resulting from routine radioactive airborne and liquid

effluents were listed as required. Projected doses to the public were well below the

TS limits. The inspector determined that the e were no anomalous measurements,

omissions, or adverse trends in the reports.

.__ . - -

25

The ODCM provided descriptions of the sampling and analysis programs, which

were established for quantifying radioactive liquid and gaseous effluent

concentrations, and for calculating projected doses to the public. All necessary

parameters, such as effluent radiation monitor setpoint calculation methodologies,

and site specific dilution f actors, were listed in the ODCM. The licensee adopted

other necessary parameters (dose f actors) from Regulatory Guide 1.109.

Section 3/4.8.M of the TS requires that the licdasee shall comply with the 40 CFR

190 requirements,25 mrem / year to the total body to a member of the public with

occupancy rate at the monitoring location. The inspector reviewed the 1996

Annual Radiological Environmental Surveillance Report and Effluent Report including

projected dose calculation results to the public. The licensee has 14

thermoluminescent dosimeters (TLDs) around the site boundary and two control

TLDs ste.tions (about 15 km from the plant) to comply with 40 CFR 190

requirements. The mean measurement value at the site boundary (including

background) and control stations were 69.14 and 56.1 mrem / year, respectively,

during 1996. The difference value, which is about 13 mrem / year, would be

contributed from the plant operation. The licensee reported the maximum total

body dose from f acility direct radiation was about 14 mrem during 1996 at the west

site boundary. However, there were no residents present at that location. Total

body dose due to radioactive liquid and gaseous effluent releases was 0.05 mrem

during 1996. The total dose would be 13.05 mrom during 1996 and the licensee

met the TS requirements,

c. Conclusions

Based on the above reviews, the inspector made the following conclusions:

(1) effluerit control procedures were sufficiently detailed to f acilitato

performance of all necessary steps for routine and emergency operations;

(2) the licensee offectively implemented the TS/ODCM requirements for

reporting effluent releases and projected doses to the public; and,

(3) the licensee's ODCM contained sufficient specification, information, and

instructic,n to acceptably implernent and maintain the radioactive liquid and

gaseous effluent control programs.

R6 RP&C Organization and Administration

The inspector reviewed the organization and administration of the radioactive liquid

and gaseous effluent control programs and discussed with the licensee changes

made since the last inspection. The inspector determined that there were no

changes to the radioactive effluent control programs. The Chemistry Department

has primary responsibility for conducting the radioactive liquid and gaseous effluent

control programs. The System Engineering, Operations, Radiation Protection, and

instrumentation and Cor.trols (l&C) Departments also have responsibilities to

-support effluent control programs, such as air cleaning systems, redwaste

.

26

discharges, and radiation monitoring system calibrations (radiological and electronic

calibrations).

R7 Quality Assurance (QA)in RP&C Activities

a. laipection Scone (84750-01)

The inspection consisted of a review of: (1) the 1996 and 1997 QA audit reports;

and (2) implementation of the measurement laborato y quality control program for

radioactive liquid and gaseous effluent samples,

b. Observations and Findinas

The inspector reviewed the 1996 and 1997 QA Audit Reports (Report Nos.

VY 96 02 and VY 97 02). These audits were conducted by the QA Department

staff and covered the radioactive liquid and gaseous effluent control programs,

including the implementation of the ODCM. The inspector noted that the audits

were conducted by members of QA Department with assistance from other

technical personnel. The 1996 audit team identified one finding. The 1997 audit

team identified no findings. The inspector determined that the 1996 finding was not

safety significant, but was intended for the enhancement of the effluent control

programs Prompt corrective action was performed by the Chemistry Department

staf f.

The inspector reviewed the implementation of QC for the chemistry laboratory, l

'

including control charts, inter laboratory and intra laboratory comparisons. The

inspector considered the chemistry laboratory QC program to be very good,

c. Q.gnelusion

Based on the above review and interviews, the inspector determined that the

technical depths of the audits was good and met TS requirements. The chemistry

laboratory QC program was very good.  !

R8 Miscellaneous issues

R8.1 Trair.ina

l

The inspector reviewed the training courses for the licensed operators, in the areas ,

of radioactive liquid and gaseous effluent controls and discussed this program with I

a training instructor Required training courses for operators appeared to be i

'

appropriate, and included subjects such as: solid and liquid radwaste processes;

ventilation; ODCM; HVAC; AOG; area / process / effluent RMS: and service water. To

complete these courses required about 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> in class and the use of simulator.

The licensee also had the " Response Training" and an annual re-qualification

training. The response training involved specific effluent events, such as Event

Reports or LERs.

-- - _ . . . _ _ . . - _ _ . _ - - - _ . - . . . - - _ - .- -_ - - . . - . _ - . . . . . - -

!

27

,

The inspector discussed with the plant staff the involvement of the Chemistry staff

in response training. Currently, there is no Chemistry staff involvement for the  ;

response training and the annual re qualification training. The licensee stated that t

the/ would evaluate Chemistry staff involvement in this training with respect to the

effluent ALARA program. '

R8.2 (Closed) URI 96 03-05, LER 96 03 Suo.1, and NCV 97 08 07: Removal of Reactor l

Vessel Shield Blocks et Power .

a. Insoection Scoce (92904,92700)

i

This issue was previously examined in inspection report 96 03, section 4.1, and  ;

inspection report 96-09, section R8.2 and remained open pending completion of the l

licensee's root cause evaluation. LER No. 96-03, Supplement 1, " Removed reactor  ;

shield blocks during power operations to facilitate outage scheduling due to i

personnel error," dated June 12,1997, documented the VY staff's formal root

cause evaluation results and associated corrective actions. The inspector

conducted a review of LER 96 03, Supplement 1, and verified the implementation of l

the stated corrective actions. .

c ;servations and Findinas

b.

The licensee's formal root cause of this event was personnel error, in that there was l

a lack of awareness by plant personnelin 1990 and 1992 of the consequences of l

removing all three sets of reactor cavity shield blocks while at power. A ]

contributing cause identified by the VY staff was the lack of formal procedural

guidance governing the removal of shield blocks. The inspector confirmed the l

adequacy of the licensee's corrective actions which included a revision to the

refueling preparation procedure Operating Procedure (OP) 1200," Preparation of the l

Reactor Vessel for Refueling," revision 18, dated 9/5/96) section 1.0, "Drywe!! I

I

Shield Block and Drywell Head Removal," which added the requirement that "the

first layer of shield blocks can be removed at any power level prior to shutdown, the _,

second and third layers of shield blocks cannot be removed until the reactor vessel I

is < 212 degrees F and vented." In addition, the licensee revised Plant Operations

Review Committee (PORC) member training, engineering support staff continuing '

training, and the Safety Evaluation Training lesson plans to reflect the lessons ,

'

learned from this event.

The inspector considered this refueling preparation event to have been reflective of

past poor VY staff performance. This non repetitive, licensee identified and

corrected violation was treated as a non-cited violation (NCV 97 08 07), consistent

with Section Vll.B.1 of the NRC Enforcement Poliev.

c. Conclusions

Licensee actions to identify and implement corrective actions to prevent drywell

shield blocks removal during power operations were appropriate. This licensee

identified event involving the violation of regulatory requirements was not cited.

~. -- - ,, - - . , --. .----- - . - - - -.- --- -

-- - . - - _ . - . . . - . -- - - - - - - -- .. .

.

I

!

28

LER 96-03 and 96 03 Supplement 1 were closed and unresolved item URI 96 03 05

was closed.

V. Management Meetings

X1 Exit Meeting Summary

t

The inspector presented the inspection results of the radiological environmental

monitoring program to members of the licensee management at the conclusion of

the inspection on September 26,1997. The results of the MOV review were

presented to station management at the conclusion of the on site inspection on

! October 17,1997. The licensee acknowledged the findings presented. l

The resident inspectorc met with licensee representatives periodically throughout  ;

'

4

the inspection and following the conclusion of the inspection on November 20,

1997. At that time, the purpose and scope of the inspection were reviewed, and

the preliminary findings were presented. The licensee acknowledged the preliminary

inspection findings.

X2 Review of Updated Final Safety Analysis Report (UFSAR)

A recent discovery of a licensee operating their f acility in a manner contrary to the

Updated Final Safety Analysis Report (UFSAR) description highlighted the need for a i

special focused review that compares plant practices, procedures and/or parameters

'

to the UFSAR description. While performing the inspections discussed in this

report, the insp'.9 tors reviewed the applicable portions of the UFSAR that related to

the areas inspected. The inspectors verified that the UFSAR wording was

consistent with the observed practices and procedures and/or parameters.

However, the inspectors observed that the FSAR wording was questionable with

respect to the observed plant practices, procedures, and parameters involving

building air balance and flow (See Section R.2.3 of this inspection report). The

inspectors reviewed Sections 4.4, and 4.8 of the VY UFSAR to assess if VY had

,

incorporated correct UFSAR information into plant MOV procedures regarding *

reactor coolant and reactor water cleanup systems (RWCU), respectively. This

information was found to be correct and up to-date.

i

- - . , _ _ _ _ _ _ _ _ _ . . , _ _

.- . . .. .

.

29

INSPECTION PROCEDURES USED

61726 Surveillance Observations

71707 Plant Operations

92901 Follow Up Plant Operations

92903 Follow Up Engineering

84750 01 Radioactive Waste Treatment, and Effluent and Environmental Monitoring

82701 Operational Status of Emergency Preparedness Program

02700 LER review

62707 Maintenance Observations

92903 Engineering Follow up

92904 Plant Support Follow up

37551 Onsite Engineering Review

Tl 2515/109 Inspection requirements for Generic Letter 8910," Safety Related Motor-

Operated Valve Testing and Surveillance "

.

.

.

30

ITEMS OPENED, CLOSED, AND DISCUSSED

OPEN

IFl 97 08-01 Inspector follow up of the licensee's resolution of the EDG piping welds

issue.

IFl 97-08-02 Verification of exhausting actual and maximum f an capacities listed in

l'.v. vdure OP 2611, " Gaseous Redwaste."

CLOSED

LER 96-03, Sup.1

'

LER 9611

LER 9614, Sup.1

LER 96 21

LER 96 23

LER 9711

- LER 9712

LER 9714

! ER 9717

URi 96-03 05 Removal of reactor vessel shield blocks at power.

URI 97-06 02 Cracks in radwaste building vent ducting.

LER 96 29

LER 96 24 i

IFl 96 09 01 Appendix J testing deficiencies

LER 96 27

URI 9316-01 Pressure lo:: king and thermal binding

VIO 96-05 03 Failure to update and control of Program Manual

EA95 070 VIO 01013: Failure to correct a condition adverse to quality

NCV 97 08-03 LER 96 23

NCV 97 08-04 LER 96 29

NCV 97 08 05 LER 96 27

NCV 97-08-06 LER 9611

NCV 97 08 07 URI 96 03 05

DISCUSSED

LER 96-03

IFl 961101 EDG tornado protection

VIO 97 06 03 Ineffective corrective action, containment inerting event.

IFl 97-04 04 RHR service water flow instrument accuracy

'

IFl 97-06-01 - Licensee's LSFT review follow up

URI 97 03-02 Cabie separation issues

<

- . _ _ , _ .. _ _ , - _ . -

-

,

)

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31 I

, t

PARTIAL LIST OF PERSONS CONTACTED -

l

.

G. Meret, Plant Manager i

F. Helin, Tech. Services Superintendent  ;

M. Balduzzi, Superintendent of Operations l

E. Lindamood, Director of Erigineering l

K. Bronson, Operations Manager  !

M. Watson, Maintenance Superintendent  !

'

G. Morgan, Security Msinager

J. Chamberlin, Sistem Engineer, instrument and Controls  ;

M. Desiletes, Radiation Protection Manager  !

,

- R. Gardes, Chemistry Manager

F. Helin, Technical Services Superintendent l

S. Jefferson, Scheduling Manager, Operations  !

i S. McAvoy, Chemistry Supervisor  !

D. Voland, Radiological Environmental Supervisor l

C. Hansen, MOV Engineer .  ;

J. Lynch, Fluids Design Engineering i

,

C. Nichols, Manager, E&C l

?

!

}

I

i

.

9

I

f

s

f

>

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>  :

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32

LIST OF ACRONYMS USED

{

!

ALARA As Low As is Reasonably Achievable  !

ARMS Area Radiation Monitoring System

GMO Basis for Meintaining Operation

CFR Code of Federal Regulation

CR control room .

J

CS core spray '

EDG emergancy diesel generator

ER Even; Report l

FSAR Final Safety Analysis Report l

01. Gener;c Letter i

W! IPA High Efficiency Particulate

,4PCI high pressur6 coolant injection j

HVAG Heating, Ventilation, and Air Conditioning ,

ifi inspecto' fol!oc item ,

IN %rmeifn Notice i

'

LCO L%thg fondition for Operation

LER Licensec Event Report

LPCI low pressure coolent injection ,

MCC -motor control center  :

NRC Nuclear Regulatory Commission l

NNS Non nuclear safety  !

ODCM Offsite Dose Calculation Manual

PO3C Plant Operations Review Committee

OA - Quality Assurance  ;

OC Ouality Cor.aol  ;

RHR residual heat removal

RMS Radiation Monitoring System

RP&C Radiation Protection

SFP Spent Fuel Pool

TS Technice! Specifications ,

UFSAR Updated Final Safety Analysis Report

URI - unresolved item

VY Vermont Yankee

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I

!

<

.. . _ -.-.____-_. _ .._ _ ___ _ _ _ _ . . . . . . _ . . , . . _ . , _ _ , . . . . . , . _ _ _ _ , _ . _ . , _

. . _ - - . _ . _ . _ . . _ . _ _ _ _ _ . _ _ . _ _ _ _ _ _ . . _ _ _ _ _ _ _ _ _ . _ _ . - - _ _ . _ - _ _ _ - _

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33

ATTACHMENT A

List of Emergerv;y Plan and implementing Procedures Reviewed

DOCUMENT TITLE REVISION

NO.

Emergency Plan Section 6.0 Emergency Facilities and Equipment 20

Emergency Plan Section 8.0 Organizatic,n 20

Emergency Plan Section 10.0 Radiological Assessment and Protectivs 20

j Measures

Emergency Plan Section 12.0 Maintaining Emergency Preparedness 19

Emergency Plan Appendix E Letters of Agreement 22

l

OP 3504 Emergency Communication DI i

97 133

OP 3509 Environmental Sample Collection During an 15 l

Emergency

OP 3535 Post Accident Sampling and Analysis of 2 i

Primary Containment  !

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