ML17326A546

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LER 80-004/03L-0:on 800202,during Normal Operation,While Investigating Problem W/Test Circuit for B Main Turbine Stop Valve,Found Mounting Bracket for Proximity Switch Failed. Caused by Loosened Mounting Assembly Due to Vibration
ML17326A546
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 02/27/1980
From: RISCHLING J
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17326A545 List:
References
LER-80-004-03L, LER-80-4-3L, NUDOCS 8003040582
Download: ML17326A546 (2)


Text

)V,.+C FOSIMi366{7 77I LICENSEE EVENT REPORT I~NUCLEAR REGULATORY COMI))II SSION 7 8 CON'T CONTROL BLOCK: I f I Mti D fc C~JQ2 9 LICENSEE CODE I 2)~u~lLJ~Qs LICENSE NUIEIBER I Qi'PLEASE PRINT OR TYPE ALL REQUIREO INFORhlATIONI Olo O O"oo'"oo~LQR~05 0 0 I 0 3 I I I 0'Q)jo 2 0 2 60 61 DOCKET NUMBER 68 69 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUE)4CES QIO L-2~01 Qs 0 2 21 7 8 0/09 7 8 74 76 RCPORT DATE 80 THE"B"'AIN TURBINE STOP VALVE, IT WAS DISCOVERED THAT THE MOUN'I ING BRACKET FOR THE I PROXIMITY SWITCH HAD f:AILED.THIS PROXIMITY SWITCH PROVIDES TURBINE STOP VAlVE I O IS.CLOSURE INDICATIOII FOR THE REACTOR PROTECTION SYSTEM.THIS IS NON-CONSERVATIVE IN.RESPECT TO.-T.S.TABLE 3.3-1 iTEM 18.B.THE AFFECTED CHANNFL WAS PLACED IN THE TRIP L CONOIYIOAII AS REOUIREO.~OS 80 7 8 9 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE" SUBCODE COMPONENT CODE SUBCODESUBCODE~o)2~t>Q>>2 Q~Q~I~Y~LIIIQ LLI Q[z>Q 7 8 9 10 11 12 13 18 19 SEQUENTIAL OCCURRENCE RLPOPT REVISIOI'I LERIRQ FVENT YEAR RFPORT NO.CODE)YPE NQ.G)llo)ORT~gP~~PP O.~~[gJ~21 22 23 24 26 27 28 29, 30~31 32 ACTIOi4 FUTURE EFFECT SHVTDOENE4 ATTACHMENT NPRO 4 PRIME COMP.COMPOi'IENT TAKEN ACTION ON PLANT h'IETHOD HOURS Q22 SUBMITTED FORh1 SUB.SUPPLIFR MANUFACTURER

~OQTR~ZQER~ZQ)o~ZQst~0~00 I 0.I Y I Q22~NQ24 LAgQ>>~i~l~liQRF 33 34" 35 36 37 40 41 42 43 44 47 CAUSE OFSCRIPTICN ANO CORRECTIVE ACTIONS Q27 V*TI IITIOA lt-" ALE II I R II IELI St 2AEV:.AO~t TAI I i.IVIIEVE, I I tT Itl I il IOIIL 0"AVE: tVE~IIV EVENT STOP VALVE"B" HAD ACTUALLY SHUT.THE PROXIMITY SWITCH ITSELF DID NOT FAIL.3.THE'FAILURF.

WA IN" tI NTI G ASSEMBLY.WHICH VIBRATED I OSE.T PRF F SEE ATTACHED SUPPLEMENT.

IN Tt'J 7 8 9 FACILITY STATUS 41 PONIER oTHER STATUS 0~'E 1 0 0"9 NA METHOD OF)DISCOVERY DISCOVERY DESCRIPTION 022~A QSI[OPERATOR OBSERVATION LOCATION OF RELEASE QSB NRC USE ONLY'I I I I I I 68 69 616-465-5901 8003.{9@{6 10 Jack Risch'ting PHONc)4AME OF PREPARER CK LJQ>>j~lQ 7 8 9 10 12 13 44 ACTIVITY COI4TENT RELEASED OF RELEASE AMOUNT OF AC IVITY QSS~1e~Z 033~ZQ3.NA 7 8 9 10 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 039)~00 0 Qs)~ZQ)s NA 7 8 9 11 42 13 PERSCi4NEL INJURIES NUMBER DESCRIPTION 41~OI O O Q4oj)PA 7 8 9 11 12 LOSS OF OR DAMAGE To FACILITY Q43 7 8 9~'10 45 PUBLICI~'4 ISSUED DESCRIPTION Q g j oo.I)IJ(43 80 80 80)2 oi 30 0 SUPPLEMENT TO LFR iv'80-004/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION

.ASSEMBLY AND PROXIMITY SWITCH CONFIGURATION MAS INSTALLED AS A RESULT OF:-.-:--.A PREVIOUS ENGINEERING EVALUATION.

NO FURTHER ACTiON IS PRESENTLY PLANNED AS A RESULT OF THIS EVENT.