ML17261B108

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LER 90-011-00:on 900619,fire Damper Found Missing During Surveillance Test PT-13.26 Due to Lack of Installation. Caused by Inadequate Design Info.Hourly Fire Watch established.W/900719 Ltr
ML17261B108
Person / Time
Site: Ginna Constellation icon.png
Issue date: 07/19/1990
From: CAVANAUGH M E, MECREDY R C
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-90-011, LER-90-11, NUDOCS 9007250215
Download: ML17261B108 (11)


Text

ACCELERATED D'RIBUTION DEMONSTRATION SYSTEMIREGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9007250215 DOC.DATE:

90/07/19NOTARIZED:

NODOCKETPTFACIL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester G'5000244 AUTH.NAMEAUTHORAFFILIATION CAVANAUGH,M.E.

Rochester Gas&ElectricCorp.MECREDY,R.C.

Rochester Gas&ElectricCorp.RECIP.NAME RECIPIENT,AFFILIATXON R

SUBJECT:

LER90-011-00:on 900619,fire damperfoundmissingduringSurveillance TestPT-13.26duetolackofinstallation.

W/9DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR ENCLSIZE:TITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).

D/05000244ARECIPIENT IDCODE/NAME PD1-3LAJOHNSON,A INTERNAL:

ACNWAEOD/DSP/TPAB NRR/DET/ECMB 9HNRR/DLPQ/LHFB11 NRR/DOEA/OEAB11 NRR/DST/SELB 8DNRRDSTAPLBBD1>

E'ILE01EXTERNAL:

EG&GBRYCE,J.H LPDRNSICMAYS,GNUDOCSFULLTXTCOPIESLTTRENCL11112211111,1111111111133111111RECIPIENT XDCODE/NAME PD1-3PDAEOD/DOAAEOD/ROAB/DS PNRR/DET/EMEB9H3 NRR/DLPQ/LPEB10 NRR/DREP/PRPBll NRR/DST/SICB 7ENRR/DST/SRXB 8ERES/DSIR/EIB LSTLOBBYWARDNRCPDRNSICMURPHY,G.A COPIESLTTRENCL1,111.22111122111111111111DDDNOTETOALL"RIDS"RECIPIENTS:

PLEASEHELPUSTOREDUCEiVASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMP1-37(EXT.20079)TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!DDFULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:

LTTR32ENCL32

/vga~HIIC'tOIK,v'ja$1+tLROCHESTER GASANDELECTRICCORPORATION

~89EASTAVENUE,ROCHESTER, N,Y.14649-OQP1

'TCiC0W0hgAAcAcooETlc546.2700July19,1990U.S.NuclearRegulatory Commission DocumentControlDeskWashington, DC20555

Subject:

LER90-011,Firedamperfoundmissingduringsurveillance testPT-13.26, duetonotbeinginstalled, causesacondition prohibited byTechnical Specifications.

R.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordance with10CFR50.73, LicenseeEventReportSystem,item(a)(2)(i)(B),

whichrequiresreporting of"AnyOperation orCondition Prohibited bythePlantsTechnical Specifications",

andplantTechnical Specifications, section3.14.6,whichrequiresa30dayspecialreport,theattachedlicenseeeventreportLER90-011isherebysubmitted.

Thiseventhasinnowayaffectedthepublicshealthandsafety.VerytrulyyoursRobertC.McreDivisionManagerNuclearProduction xc:U.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406GinnaUSNRCSeniorResidentInspector f3gogs7zs890072.02i5 900719PDRADDCI0000244PDCWERQIf(

~~)~-~~0~g~e~o~~~655DE~~~i~~~~~iIII~~~RARRKWNJ~KR~REWRH~REEERRRRRRK ShERRShRWRIN58ll%

~hWllllllHM55llhhh%

0..6Rllll~~~I~-~~0~~~~~~-~~~~~~-~'~~~~~~~~

II1CScow~11431LICENSEEEVENTREPORT(lER)TEXTCONTINUATION V.N.HVCLtA11COVLATOIIY COMMINCIOM ASSAOVCOOMOIIO4150&IO4JN)tSI1f5~IIBIIa%

SACILITYIIAMCIIIOOCKt'SIIVMOl1ItlLtllHVMOI1+I1IOV~llTIALMQVISIOllMSAOOIilR.E.GinnaNuclearPowerPlantVtXrIII~MSCS1~.~~SIACA~IlIIn0500024490-011-002OFNILPLANCONDIIOSTheplantwasatapproximately 984steadystatefullpowerwithnomajoractivities inprogress.

IIESCRIPTION OFEVENTA.Datesandapproximate timesformajoroccurrences:

June19,1990,1530EDST:EventdateJune19,1990,1530EDST:Discovery dateandtimeJune19,1990,1600.EDST:

Fireprotection initiated touringtheareaonceperhourincompliance withTechnical Specifications B.EVENT:OnJune19,1990atapproximately 1530EDSTwiththereactoratapproximately 984fullpower,FireProtection andSafety-alongwithHVACpersonnel wereperforming PT-13.26TestingofFire,Dampers.

DuringthetestingoffiredamperRR-113-Pwhichisthesupplyductforthe'uxroomHVACsystem,itwasnotedthat,therewasnofiredamperintheduct.TherearefiredampersintheductbetweentheMuxroomandtheRelayroom.Thisductpenetrates theRelayroomsouthwalltoastairwell whichleadstotheControlroom.Thisductisidentified asbeingatwo(2)hourTechnical Specification firewall.OnJune19,1990at,approximately 1600EST,theFireProtection sectionassignedafirewatchtoperformhourlytours.C.D~INOPERABLE STRUCTURES, COMPONENTS ORSYSTEMSTHATCONTRIBUTED TOTHEEVENT:MissingfiredamperRR-113-POTHERSYSTEMSOFSECONDARY FUNCTIONAFFECTED:

None-11CSOAIS~IIOII

~~0~~~~~~~~~~~~se~~os~~-~~~0~~II~~~~~~~$~~~~-i~~~~,g~~-~1~ggg~~s~~I~~~~~II~II~~~II~II~~~~~~~~~~~

kACform%4AIVIIILICENSEEEVENTREPORTILERITEXTCONTINUATION V.I.kVCLIAAAI4ULATOAY COMOONIIOk AffAOVIOOMIkO31IO&ICOIAflAIIInlrIIfACILITYkAMIlllOOCKITkUIOAKALTILIAkIAOIIAI~IeIOvok<rAL hlrrevrolokhrA~A4I(IIhhR.E.GinnaNuclearPowerPlantTIxTIrfmorekrooeereevveo.vooooeooohor kAcrrhvrrr~'llIITI0500024490-011-0004QF08IVLYSIEVNA11/2hourratedfiredamperwasnotinstalled inatwohourfire'wall soTechnical Specification 3.14.6couldnotbemet.Thiseventisreportable inaccordance with10CFR50.73, LicenseeEventReporting SYstem,item(a)(2)(i)(B),whichrequiresreporting of,"AnyOperation orCondition Prohibited bythePlantTechnical Specification>>,

and(Other)plantTechnical Specifications, section3.14.6,whichrequiresa30dayspecialreport.Anassessment wasperformed considering thesafetyofthiseventwiththefollowing resultsandconclusions:

FTherewerenooperational orsafetyconsequences ofimplications

~attributed tothemissingfiredamperinthefirebarrierwallbecause:ThecontrolcomplexismadeupoffirezonesAHR,RRandCR.FirezoneAHRwasnotaffectedbythemissingfiredamper.FirezoneRRandCRfireinducedeffects,safeshutdownmethodsandproposedcompliance methodsmoresimilarandaredescribed asfollows:Rectormakeupcapability

-afireintheareamaydamagecontrolcircuitry to480VACbuses14and16providing alossofchargingpumpsandsafetyinfection pumps.Thealternative shutdowncapability isprovidedbythechargingpump1Acontrolcircuitry modification.

Localtransfer, circuitisolation andcontrolofthepumpatthechargingpumproomwillbeaccomplished.

Manual,valveV-358providing RWSTsuctiontothecharging, pumpmustbemanuallyopenedinchargingpumproom.Reactorreactivity control-willbeensuredbymaintenance ofmakeupcapability asdescribed above.Decayheatremoval-Afireinthisareahasthepotential fordamagingpowerfeedstobothmotor-driven AFWpumps,bothdctrainsAandB480Vacbatterychargerfeeds,andcontrolcircuitry forthestandby,turbine-'driven andmotor-driven AFWpumps.The'lternative shutdowncapability isprovidedbyoperating theturbine-driven AFWpumpintheIntermediate BuildingkA4fOoooIIIIAII&I

<<ACtwm%4AN45l.LICENSEEEVENTREPORT{LER)TEXTCONTINUATION U.E.<<UClE*RIIEOULATISIY COMMIEEIO<<

AttlIOVEO OMI<<0,EIEO&ICNE)ctllIES I/314EOOCXETIIUaeEIIITIR.E.Ginna'NuclearPowerPlanto5ooo244TEXTIN'rrt<<<<er<<<<msst.rNN<<Ssrss<<NNC Arts~'IlIITl,I,EIIIIUIrNEII IIINNOU~STIAI.MS90-011-00tAOEIEI050Fatthepump.Theoperatorwillmanuallyisolatedcpowertotheturbinesteamadmission valvesV-3504AandV-3505Aatmaindcdistribution panels1Aand1BinfireareaBRlAandfireareaBR1B.Manualoperation ofoneofthevalveswillthenbeaccomplished tostarttheturbinedriver.DCpowerisrequiredforoperation oftheturbine'-driven AFWlubeoilpump.Powerto.thispumpissuppliedfromdctrainBthroughtheTurbinebuildingdcdistribution panel.AtransferswitchwillislocatedintheIntermediate buildingtoisolatecontrolcircuitstoCTandtoallowforlocalcontrol'f thedclubeoilpump.Manualoperation ofdischarge valvesV-3996andC-4297(orV-4298)willthenbeaccomplished topermitAFWflowtothe,appropriate steamgenerator.

Asbefore,powerwillbeisolatedorinstrument airisolatedandbledoffbeforemanualoperation isattempted.

'ILongtermdecayheatremovalwillbeaccomplished byuseoftheRHRsystem.RHRpumpcontrolcircuitsmaybedamagedbyafireinthearea.AdequatetimeexiststoeitherrepairdamagedcontrolcircuitsortolocallycontrolRHRpumpbreakers.

Thisanalysisassumesthatrepairswillnotbemadeandthatthebreakerswillbeoperatedlocally.ReactorPressureControl-pressurecontrolisensuredbyautomatic operation ofpressurizer safetyvalvesandbymaintenance ofmakeupcapability asdescribed above.Supportsystems-ServicewaterandCCWpumpcontrolmaybeaffectedbyafireintheseareas.Emergency dieselgenerator controlmaybeaffectedbyafire.inthesesareas.However,alternative shutdownforEDG1Awillallowforcompleteisolation ofallnecessary

.controlcircuitsfromtheControlandRelayroom.EDGcoolingcanbeaccomplished bymanuallyoperating theservicewaterpumpbreakersinthe'creenhouse orviatheunderground yardfirewatersystem.AlocalEDGconnection existsthatallowsforalocalwatersupplyhookupincaseservicewaterisnotavailable.

CCWpumpcontrolisnecessary forcoldshutdown.

Adequate'ime.

existstoallowforlocalcontrolofCCWpumpbreakers.

<<1CNOAMQ4AItal

~~~~I~I~~(I$g~$~~~~II~~~~II~~~~~II~~I~~~~~~~~~II~~~~~~~~~~~~s~+~~~~~I~~~~~~~~~~~~~0~~~~II~~~~~~~~~~~~~~~~~II~~II~~~~~~0~~~~~~~~~~~~~II~~~~~~II~~~~II~~I~~~~~II II1CtensJffAIf4JI,LlCENSEEEVENTREPORT(LER)TEXTCONTINUATlON UWHUCLfA11COUlATOAY COMMlffIOII AttAOYTOOMfHQJISOWI04/frtlrffIfJI/ffI'ACICITY HAMlIIIOOCrfT1UMff1IJILfIIHUMfl1lllf~OUTHTI*l.~tMtfVISION1~AOfIJIhhR.E.GinnaNuclearPower.Plant:TCXTlit11ttMace1~tmaAaeanVSACAnn~YIIITI0500024490-.011-0007OF0dieselgenerator) andmainfusecabinet1A(trainAdcpower).Useofthisexistingintertiewillprovideforlong-term operation ofprocessmonitoring instrumentation locatedattheABELIP.Bothredundant trainsofsourcerangeneutronmonitoring maybedamagedbyafireinthisarea.Asparemonitordrawerislocatedonsitetoprovidethecapability to.bypassfiredamagedcircuits.

Aprocedure isusedtoconnectthe'existing neutronmonitorinsidethecontainment tothenewdrawer.Alocalpowersupply'willbeusedtopowerthenewdrawer.BasedontheaboveandRG&EGinnaStationAppendixRAlternative ShutdownReport,itcanbeconcluded thattheemployee's and.thepublic'shealthandsafetywasassuredatalltimes.VCOECTIVETIONSA.Actionstakentoreturninoperable components tooperablestatus:Anhourlyfirewatchwasestablished topatroltheareaonceperhourAnevaluation willbeconducted todetermine afiredamperratingandsizeAnewfiredamperwillbeinstalled intheducttobringthefirebarrierincompliance witharatedbarrierB.ACTIONSTAKENORPLANNEDTOPREVENTRECUE%ENCE:

Completeavisualinspection andperformatriptestofallTechnical Specification andAppendixRfiredampersVIADDIT0A.Failedcomponents INone81CtOAtiJfAAIf4$l 114SvIvIANNA%HIL'ICENSEE EVENTREPORT(LER)TEXTCONTINUATION VA.HVCltAAIIIOVLATOAY COMMNSOMAJP1OVTOOUIN),glgQ&lONTNPIATS'TlT1IT$NACIVITYllAMlillOOCKETHVMISAOVVTAAll1NVMOI1I~l$$4V~IITIAgUNQVINIOII U1~AOllTIR.E.GinnaNuclearPowerPlantTECTIN'NvVVMvvv1~.vMvAKenvIHNCAvtII~'llllTl0500024490011-00oso~0sB.PreviewLER'sonsimilareventsAsimilarLEReventhistorical searchwasconducted withthefollowing results:nodocumentation ofsimilarLEReventswiththesamerootcauseatGinnaStationcouldbeidentified C.SpecialCommentsNone~IACNOAMAVOCA04Tl