ML17264A994

From kanterella
Revision as of 13:13, 18 May 2018 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr
ML17264A994
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/19/1997
From: MECREDY R C, ST MARTIN J T
ROCHESTER GAS & ELECTRIC CORP.
To: VISSING G
NRC (Affiliation Not Assigned), NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-97-002, LER-97-2, NUDOCS 9708270015
Download: ML17264A994 (16)


Text

0CATEGORY1REGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)ACCESSIONNBR:9708270015DOC.DATE:97/08/19NOTARIZED:NODOCKETFACIL:50-244RobertEmmetGinnaNuclearPlant,Unit1,RochesterG05000244AUTH.NAPEAUTHORAFFILIA.IONST.HARTIN,J.T.RochesterGas&ElectricCorp.MECREDY,R,C.RochesterGas&ElectricCorp.RECIP.NAMERECIPIENTAFFILIATIONVISSING,G.

SUBJECT:

LER97-002-00:on970720,34.5KVoffsite.powercircuit751waslost.Causedbyautoma;icactua"ionof"B"emergencyDGduerounder;oitageonsafeguardsbuses16&17.0ffsir.epowerrestoredtosafeguardsbuses16&17.W/970819ltr.DISTRIBUTIONCODE:IE22TCOPIESRECEIVED:ITRJENCILSIZE:TITLE:50.73/50.9LicenseeEventReport(LER),IncidentRpt,etc.NOTES:LicenseExpdateinaccordancewith10CFR2,2.109(9/19/72).c'50002446INTERNAL:RECIPIENTIDCODE/NAMEPD1-1PDILECENTENRR/DRCH/HHFBNRR/DRCH/HOLBNRR/DRPM/PECBNRR/DSSA/SRXBRGN1FILE01COPIESLTTRENCL112211111111111111RECIPIENTIDCODE/NAMEVISSING,G.AEOD/SPD/RRABNRR/DE/ECGBNRR/DE/EMEBNRR/DRCH/HICBNRR/DRCH/HQMBNRR/DSSA/SPLBRES/DET/EIBCOPIESLTTRENCL1111111111111111RDEXTERNAL:LSTLOBBYWARDNOACPOORE,W.NRCPDR111111LITCOBRYCE,JHNOACQUEENER,DSNUDOCSFULLTXT111111CUNNOTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATIONREMOVEDFROMDISTRIBUTIONLISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION,CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION415-2083FULLTEXTCONVERSIONREQUIREDTOTALNUMBEROFCOPIESREQUIRED:LTTR24ENCL24

ANDo~("iv.igqgclap('rip+~/~i~<<l:"~~wv~hp'g~co'E)r~<v(+ofCQc<of01;sAugust19,1997U.S.NuclearRegulatoryCommissionDocumentControlDeskAttn:GuyS.VissingProjectDirectorateI-1Washington,D.C.20555

Subject:

LER97-002,Lossof34.5KVOffsitePowerCircuit751,DuetoExternalCause,ResultsinAutomaticStartof"B"EmergencyDieselGeneratorR.E.GinnaNuclearPowerPlantDocketNo.50-244

DearMr.Vissing:

Inaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"Anyeventorconditionthatresultedinamanualorautomaticactuationofanyengineeredsafetyfeature(ESF),includingthereactorprotectionsystem(RPS)",theattachedLicenseeEventReportLER97-002isherebysubmitted.Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,RobertC.Mecredyxc:Mr.GuyS.Vissing(MailStop14B2)PWRProjectDirectorateI-1Washington,D.C.20555U.S.NuclearRegulatoryCommissionRegionI475AllendaleRoadKingofPrussia,PA19406GinnaSeniorResidentInspector97082700i59708i9PDRADQCK05000244SPDRlllllllllilllilllllllllllllillllllll

~l NRCFORM366(4.95)U.S.NUCLEARREGULATORYCOMMISSIOLICENSEEEVENTREPORT(LER)(Seereverseforrequirednumberofdigits/charactersforeachblock)APPROVEDBYOMBNo.3150-0104EXPIRES04/30/96ESTIMATEDBURDENPERRESPONSEToCOMPLYWITHTHISMANDATORYINFORMATIONCOLLECTIONREQUEST:50.0HRS.REPORTEDLESSONSLEARNEDAREINCORPORATEDINTOTHELICENSINGPROCESSANDFEDBACKToINDUSTRY.FORWARDCOMMENTSREGARDINGBURDENESTIMATEToTHEINFORMATIONANDRECORDSMANAGEMENTBRANCHIT-6F33).U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555-000t,ANDToTHEPAPERWORKREDUCTIONPROJECTFACILITYNAMEIIIR.E.GinnaNuclearPowerPlantOOCKEfNUMBERI2)05000244PAGEI3)1OF8TITLEI4ILossof34.5KVOffsitePowerCircuit751,DuetoExternalCause,ResultsinAutomaticStartof"B"EmergencyDieselGeneratorEVENTDATE(5)LERNUMBER(61REPORTDATE(7lOTHERFACILITIESINVOLVED(BlDOCKETNUMBERMONTHDAY0720YEAR97SEQUENTIALREVISIONNUMBERNUMBER97-002-00MONTH08DAY19YEAR97FACILITYNAMEFACILITYNAMEDOCKETNUMBEIIOPERATINGMODE(9)POWERLEVEL(10)100THISREPORTISSUBMITTEDPUR20.2201(b)20.2203(al(1)20.2203(al(2)(i)20.2203(a)(2)(iil20.2203(a)(2)(iii)SUANTTOTHEREQUIREMENTSOF10CFRE:(Checkoneormore)(11)20.2203(a)(2)(v)50.73(a)(2)(viii)50.73(a)(2)(i)50.73(a)(2)(x)50.73(a)(2)(ii)20.2203(a)(3)(i)73.7150.73(a)(2)(iii)20.2203(a)(3)(ii)OTHERX50.73(al(2)(iv)50.73(a)(2)(v)20.2203(a)(4)50.36(c)(1)SpecityinAbstractbeloworinNRCFoim366A20.2203(a)(2)(iv)50.36(c)(2)LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(vii)NAMETELEPHONENUMBER(IneiudeAresCodeiJohnT.St.Martin-TechnicalAssistant(716)771-3641COMPLETEONELINEFOREACHCOMPONENTFAILUREDESCRIBEDINTH(SREPORT(13lCAUSESYSTEMCOMPONENTMANUFACTURERToNPRDSCAUSESYSTEMCOMPONENTMANUFACTURERREPORTABLEToNPRDSEACBL5XOOONSUPPLEMENTALREPORTEXPECTED(14)YES(Ityes,completeEXPECTEDSUBMISSIONDATE).XNoEXPECTEDSUBMISSIONDATE(15)MONTHDAYYEARABSTRACT(Limitto1400spaces,i.e.,approximatelY15single.spacedtypewrittenlines)(16)OnJuly20,1997,atapproximately0043EDST,theplantwasinMode1atapproximately100%steadystatepower.PowerfromCircuit751(34.5KVoffsitepowersource)waslost.Thisresultedindeenergizationof4160Voltbus12Band"B"train480Voltsafeguardsbuses16and17.The"B"EmergencyDieselGenerator(D/G)automaticallystartedandreenergizedbuses16and17asperdesign.Therewasnochangeinreactorpowerorturbineload.ImmediatecorrectiveactionwastoperformtheappropriateactionsofAbnormalProcedureAP-ELEC.1(Lossof12AAnd/Or12BBuses)tostabilizetheplantandtoverifythatthe"B"EmergencyD/Ghadstartedandreenergizedbuses16and17.ThecauseofthelossofpowerfromCircuit751wasdeterminedtobeaphase-to-phasefaultcausedbyaraccoon.ThisfaultcausedtheinsulatorsonanoffsitepoleforCircuit75'ltofail.ThiseventisNUREG-1022CauseCode(C).CorrectiveactiontopreventrecurrenceisoutlinedinSectionV.B.NRCFORM366(4.95)

NRCFORM366A(4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSIONFACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERI6)YEARSEQUENTIALREVISIONNUMBERNUMBER97-,002-00PAGEI3)2OF8TEXTllfmorespaceisrequired,useadditionalcopiesofNRCForm366A/I17)PRE-EVENTPLANTCONDITIONSOnJuly20,1997,atapproximateiy0043EDST,theplantwasinMode1atapproximately100%steadystatereactorpower.Therewerenosignificantactivitiesinprogress.Theoffsitepowerconfigurationtotheplantwasinthealternate"50%/50%"offsitepowerlineup:Circuit751(34.5KVoffsitepowersource)wassupplyingpowertothe"B"train480Voltsafeguardsbuses16and17through34.5KVto4160Volttransformer12A(12Atransformer),viacircuitbreaker52/12AX,to4160Voltbus12B,andthroughthesafeguardsbus4160Voltto480Volttransformers16and17.Circuit767(34.5KVoffsitepowersource)wassupplyingpowertothe"A"train480Voltsafeguardsbuses14and18through34.5KVto4160Volttransformer12B(12Btransformer),viacircuitbreaker52/12BY,to4160Voltbus12A,andthroughthesafeguardsbus4160Voltto480Volttransformers14and18.Seetheattachedsketchoftheoffsitepowerdistributionsystem.II.DESCRIPTIONOFEVENTA.DATESANDAPPROXIMATETIMESOFMAJOROCCURRENCES:July20,1997,0043EDST:Eventdateandtime.July20,1997,0043EDST:Discoverydateandtime.July20,1997,0044EDST:ControlRoomoperatorsverifythe"B"EmergencyDieselGenerator(D/G)operationandthatsafeguardsbuses16and17areenergized.July20,1997,0114EDST:Safeguardsbuses16and17weretransferredtoCircuit767fromthe"B"EmergencyD/G.July20,1997,0124EDST:The"B"EmergencyD/Gwasstoppedandrealignedforautostandby.July20,1997,1228EDST:Circuit751wasdeclaredoperable.July20,1997,1232EDST:Offsitepowerconfigurationwasrestoredtothealternate"50%/50%"lineup.NRCFORM366AI4.95)

NRCFORM366AI4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSION~FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERIB)PAGEI3)YEARSEQUENTIALREVISIONNUMBERNUMBER3OF897-002-00TEXTIlfmorespaceisrequired,useadditionalcopiesofNRCForm366AII17)EVENT:OnJuly20,1997,atapproximately0043EDST,theplantwasinMode1atapproximately100%steadystatefullpower.TheControlRoomoperatorsreceivednumerousMainControlBoardannunciatoralarms.AmongthesealarmswereL-20(12AXFMROR12ABUSTROUBLE),J-5(¹11OR¹12TRANSFORMEROUTOFSYNCH),J-7(480VMAINORTIEBREAKERTRIP),J-9(SAFEGUARDBREAKERTRIP),andJ-32(EMERGENCYDIESELGEN1BPANEL).TheControlRoomoperatorsdeterminedthatthefollowingeventshadoccurred:Circuit751(34.5KVoffsitepowersource)wasdeenergized"B"train480Voltsafeguardsbuses16and17hadlosttheirpowersupplyfrom4160Voltbus12B(buses16and17hadbeenmomentarilydeenergized)The"B"EmergencyD/Ghadautomaticallystartedandwastiedtosafeguardsbuses16and17TheControlRoomoperatorsverifiedthatreactorcoolantsystemtemperatureandpressurewerestable,andthattherewasnochangeinreactorpowerorturbineload.TheyperformedtheappropriateactionsofAbnormalProcedureAP-ELEC.1(Lossof12AAnd/Or12BBuses)tostabilizetheplant.Theyverifiedthatthe"B"EmergencyD/Gwasoperatingandthatsafeguardsbuses16and17wereenergized.TheControlRoomoperatorsobservedthatCircuit751andbus128displayedzero(0)voltage.ThelossofpowerfromCircuit751resultedinundervoltageonsafeguardsbuses16and17,andthe"B"EmergencyD/Gautomaticallystartedasperdesignandreenergizedthesebuses.EnergyOperationspersonnelalsoidentifiedthelossofpowerfromCircuit751,andpromptlynotifiedGinnaControlRoomoperatorsofthelossofpowerfromCircuit751.TheControlRoomoperatorsreferredtoEquipmentRestorationprocedureER-ELEC.1(RestorationofOffsitePower)torestoreoffsitepowerto4160Voltbus12Band480Voltsafeguardsbuses16and17.TheControlRoomoperatorsclosed4160Voltcircuitbreaker52/12BXtoenergizebus12BfromCircuit767,viathe12Btransformer,atapproximately0053EDST.Atapproximately0114EDST,safeguardsbuses16and17weretransferredtoCircuit767fromthe"B"EmergencyD/G.(Circuit767hadremainedinoperation,supplying"A"train480Voltsafeguardsbuses14and18,throughouttheevent.)Atapproximately0124EDSTonJuly20,the"B"EmergencyD/Gwasstoppedandrealignedforautostandby.EnergyOperationssubsequentlycontactedtheControlRoomoperatorsandconfirmedthatthelossofpowerfromCircuit751occurredwhenaraccoonclimbedanoffsitepoleforCircuit751andcausedaphase-to-phasefault.Thefaultcausedinsulatorsonthepoletofail.(Theraccoonperished.)NRCFORM366AI4.95)

NRCFORM366A(4.95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSIONFACILITYNAMEI1)DOCKETLERNUMBERIB)PAGEI3)R.E.GinnaNuclearPowerPlant05000244YEARSEQUENTIALREVISIONNUMBERNUMBER4OF897-002-00TEXT(Ifmorespaceisreqtrired,tjseadditionalcopiesofNRCForm366AII17)Circuit751wasreenergizedanddeclaredoperableatapproximately1228EDSTonJuly20.Circuit751waslineduptosupplyplantloads,andtheoffsitepowerconfigurationwasrestoredtothealternate"50%/50%"offsitepowerlineupatapproximately1232EDST.C.INOPERABLESTRUCTURES,COMPONENTS,ORSYSTEMSTHATCONTRIBUTEDTOTHEEVENT:NoneD.OTHERSYSTEMSORSECONDARYFUNCTIONSAFFECTED:NoneE.METHODOFDISCOVERY'hiseventwasimmediatelyapparentduetonumerousMainControlBoardalarmsandotherindicationsintheControlRoomwhenpowerfromCircuit751waslost.F.OPERATORACTION:Followingtheundervoltageconditiononbuses16and17,the"B"EmergencyD/Gautomaticallystartedandreenergizedthesebuses.TheControlRoomoperatorsperformedtheappropriateactionstoverifythatthe"B"EmergencyD/Gwasoperatingandsafeguardsbuses16and17wereenergized.TheControlRoomoperatorsmanuallyrestartedthe"B"and"C"containmentrecirculationfans,whichhadtrippedduetothelossofbus16.Themomentarylossofpowertobuses16and17causedthetripofthecommonsamplepumpformonitoringofthecontainment(CNMT)atmospherebychannelsR-10A(iodine),R-11(particulate)andR-12(noblegas).TheControlRoomoperatormanuallyrestartedthecommonsamplepumpatapproximately0100EDST.TheControlRoomoperatorsrestoredoffsitepower(fromCircuit767)tobuses16and17,stoppedthe"B"EmergencyD/G,andrealigneditforautostandby.TheShiftSupervisornotifiedhighetsupervisionandtheNRCResidentInspectorofthelossofoffsiteCircuit751.Subsequently,theShiftSupervisornotifiedtheNRCper10CFR50.72(b)(2)(ii),non-emergencyfourhournotification,atapproximately0317EDSTonJuly20,1997.NACFOAM366AI495)

NRCFORM366AI4.95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSIONFACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERI6)YEARSEQUENTIALREVISIONNUMBERNUMBER97-002-00PAGE(3)5OF8TEXTilfmorespeceisrequired,useadditionelcopiesofNRCForm368A/I17)G.SAFETYSYSTEMRESPONSES:AIIsafeguardsequipmentfunctionedproperly.The"B"EmergencyD/Gautomaticallystartedduetotheundervoltageconditiononbuses16and17,displayedpropervoltageandfrequency,andreenergizedsafeguardsbuses16and17tosupplyemergencypower.Runningcontainmentrecirculationfansonbus16trippedasdesignedandweremanuallyrestartedasneededtorestorenormalcoolingtotheContainment.Runningservicewaterpumpsonbus17trippedasdesignedandthepumpselectedforautostartstartedwhenpowerwasrestoredtobus17.III.CAUSEOFEVENTA.IMMEDIATECAUSE:Theautomaticactuationofthe"B"EmergencyD/Gwasduetoundervoltageonsafeguardsbuses16and17.IB.INTERMEDIATECAUSE:The(jndervoltageonsafeguardsbuses16and17wasduetothelossofpowerfromCircuit751.C.ROOTCAUSE:TheunderlyingcauseofthelossofpowerfromCircuit751wasaphase-to-phasefaultonCircuit751.ThisfaultoccurredwhenaraccoonclimbedanoffsitepoleforCircuit751.Thefaultcausedtheinsulatorstofail.TheinsulatorfailureaffectedcircuitsatoffsiteStation204andtrippedrelaysforCircuit751,deenergizingCircuit751.ThiseventisNUREG-1022CauseCode(C),"ExternalCause".ThislossofpowerandsubsequentstartofanEmergencyD/GdoesnotmeettheNUMARC93-01,"IndustryGuidelineforMonitoringtheEffectivenessofMaintenanceatNuclearPowerPlants",definitionofa"MaintenancePreventableFunctionalFailure".IV.ANALYSISOFEVENT:Thiseventisreportableinaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"Anyeventorconditionthatresultedinamanualorautomaticactuationofanyengineeredsafetyfeature(ESF),includingthereactorprotectionsystem(RPS)",inthatthestartingofthe"B"EmergencyD/GwasanautomaticactuationofanESFsystem.NRCFORM366A(495)

,~

ONRCFORM366AI4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.s.NUCLEARREGULATORYCOMMISSIONFACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBERI6)YEARSEQUENTIALREVISIONNUMBERNUMBER97-002-00PAGEI3)6OF8TEXTllfmorespaceisrequired,useadditionalcopiesofNRCForm366AlI17)Anassessmentwasperformedconsideringboththesafetyconsequencesandimplicationsofthiseventwiththefollowingresultsandconclusions:TherewerenooperationalorsafetyconsequencesorimplicationsattributedtothelossofCircuit751andstartoftheEmergencyD/Gbecause:oAllreactorcontrolandprotectionsystemsperformedasdesigned.oThe"B"EmergencyD/Gwasavailableforoperationandfunctionedasdesignedtoreenergize"B"trainsafeguardsbuses16and17.oWhileinthiscondition,theplantelectricalpowersystems(offsitepowersourcesandtheEmergencyD/Gs)remainedwithintherequirementsoftheGinnaStationImprovedTechnicalSpecifications(ITS)LimitingConditionforOperation(LCO)RequiredAction3.8.1.A.oCircuit767remainedinoperationsupplyingpowertothe"A"trainsafeguardsbuses;subsequently,Circuit767waslineduptosupplypowertothe"B"trainsafeguardsbusesalso.oRadiationmonitorchannelsR-10A,R-11,andR-12weretemporarilylost.Thecommonsamplepumpwasmanuallyrestartedwithinafewminutes.ThisresponsecompliedwiththerequirementsofITSLCORequiredAction3.3.5.B.1.Basedontheabove,itcanbeconcludedthattheplantoperatedasdesigned,andthatthepublic'shealthandsafetywasassuredatalltimes.V.CORRECTIVEACTIONA..ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUSoOffsitepowerwasrestoredtosafeguardsbuses16and17fromCircuit767,andthe"B"EmergencyD/Gwasstoppedandrealignedforautostandby.oCircuit751wasclearedforusebyEnergyOperations,protectiverelaysforCircuit751(atStation204)wereresetbyEnergyOperations,andCircuit751wasreenergizedandrestoredtooperablestatus.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:Sincethiswasanisolatedoccurrence,nocorrectiveactionisplanned.NRcFORM366AI4.95)

NRCFORM366A<4-95)LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSIONFACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKET05000244LERNUMBER(6)YEARSEQUENTIALREVISIONNUMBERNUMBER97-002-00PAGE(3)TEXTllfmorespaceisrequired,useadditionalcopiesofNRCForm866A/(17)VI.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:None8.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:LERs91-002,92-007,94-012,95-006,and95-007weresimilareventswithsimilarrootcauses(startofanEmergencyD/Gduetolossofoffsitepowerfromexternalcauses).However,noneoftheexternalcausesfortheseLERswasduetoananimal.C.SPECIALCOMMENTS:NoneNRCFORM366A<4-95)

0NRCFORM366A(4.95lLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSIONFACILITYNAME(1)R.E.GinnaNuclearPowerPlantOOCKET05000244LERNUMBER(6)YEARSEQUENTIALREVISIONNUMBERNUMBER97-002-00PAGE(3)8OF8TEXTllfmorespeceisrequired,useedditionelcopiesoflVRCForm366A1(17))I5>VI>>AS+PcIOCSIAOCWIllCII)I5A>I>AWINSSIIWIOAtttt)tt-121Sf>IIIWill~IICIC)IC$2/15252I)II)IC$2/2)IItllf~I)~CCM2A35flWII~I)O)A,SCCIIN~IIOII)O>2$III)\CvMICISf>WWICWOfOWCCI)A)I,>N~INIINIltlICOI1A>St/I2CCSl/tt5$/1It>t~tSA/lSl/ItOf$2/tttl/5I)ifOr/Milt/ltl)OCAAOWOCAAtOOc/MIWll22AIAAOWCO/ttOS2/OISI)C/I~I255IC$2/MI)O/I2$2/Ml)O/)OIASSIC~IO~Wt$2/MIWI)St/OOSIWIS~IAWICIf55IC~2/O/II)A/I~ICSSICOWOIIWCOIlSIAICWftt>ICC~INWO><tIOOSClr>A35IAICWSCWCCCWWOI>OCOI~~INACO>Atl>O)NIC>IIIIOIO~III~SIAOCWSCWCC>Off>WCONII~INWttA>WOSSCI~>SIAISWftOICt~~>INItlOISSCI~I$1/MI5/II~I~ICSl/OISI5/IICCCI~IOOICIOOSOOOWwfSWOACOIOOOfWO))CIStNCI~St/MlI/IIOI~IC52/MII/ICCCCIAIAO52/OUSI)/2)OI~ICPg)CCWIWIOO~~>OIMlfSl/OAWOCtCIC)IC$2/Of)It/1$CCCIO)WlSt/MIC/)ICtSlitICQ)CAW>AIIW~$2/O/ill/)1$I~WCNACFOAM366A(4.95)