ML17262A863

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LER 92-005-00:on 920420,determined That 242 Tubes in a SG & 216 Tubes in B SG Required Corrective Action Due to Tube Degradation.Affected Tubes Either Sleeved or Plugged.W/ 920520 Ltr
ML17262A863
Person / Time
Site: Ginna Constellation icon.png
Issue date: 05/20/1992
From: BACKUS W H, MECREDY R C
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-92-005, LER-92-5, NUDOCS 9205280129
Download: ML17262A863 (22)


Text

ACCELERATEDDIS~BUTIONDEMONS+ATIONSYSTEMREGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)ACCESSIONNBR:9205280129DOC.DATE:92/05/20NOTARIZED:NODOCKET.izFACIL:50-244RobertEmmetGinnaNuclearPlant,Unit1,RochesterG05000244AUTH.NAMEAUTHORAFFILIATIONBACKUS,W.H.RochesterGas&ElectricCorp.MECREDY,R.C.RochesterGas&'lectricCorp.RECIP.NAMERECIPIENTAFFILIATION

SUBJECT:

LER92-005-00:on920420,annualmaintenanceexamperformedonbothS/G"A"&"B."242tubesin"A"&216tubesin"B"S/GrequiredC/Aduetotubedegradation.CausedbyrecurringIGA/SCC&PWSCC.S/Greturntonormal.W/920520ltr.DISTRIBUTIONCODE:IE22TCOPIESRECEIVED:LTRl.ENCLQSIZE:TITLE:50.73/50.9LicenseeEventReport(LER),IncidentRpt,etc.DNOTES:LicenseExpdateinaccordancewith10CFR2,2.109(9/19/72).05000244'ARECIPIENTIDCODE/NAMEPD1-3LAJOHNSON,AINTERNAL:ACNWAEOD/DSP/TPABNRR/DET/EMEB7ENRR/DLPQ/LPEB10NRR/DREP/PRPB11NRR/DST/SICB8H3NRR/DST/SRXB8ERES/DSIR/EIBEXTERNAL:EG&GBRYCE,J.HNRCPDRNSICPOOREiW~COPIESLTTRENCL1111221.111112211111.133111.1RECIPIENTIDCODE/NAMEPD1-3PDAEOD/DOAAEOD/ROAB/DSPNRR/DLPQ/LHFB10NRR/DOEA/OEABNRR/DST/SELB8DNRRDST/SPLB8D1R&02RGN1FIE01LSTLOBBYWARDNSICMURPHY,G.ANUDOCSFULLTXTCOPIESLTTRENCL11DDS,RDNOTETOALL"RIDS"RECIPIENTS:ADDPLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOiv1P1-37(EXT.20079)TOELIMINATEYOURNAMEFROMDISTRIBUTIONLISTSFORDOCUMENTSYOUDON'TNEED!FULLTEXTCONVERSIONREQUIREDTOTALNUMBEROFCOPIESREQUIRED:LTTR30ENCL30 tI

'OCHESTERGASANDELECTRICCORPORATIONROBERTCMECREDYVicePresidentCinnaNuclearPsoducRoni;coenaeaee~e9EASTAVENUE,ROCHESTERN.K14649-0001aTECEPHOkEAREACODE7165462700May20,1992U.S.NuclearRegulatoryCommissionDocumentControlDeskWashington,DC20555

Subject:

LER92-005,SteamGeneratorTubeDegradationDuetoIGA/SCC,CausesQ.A.ManualReportableLimitstobeReachedR.E.GinnaNuclearPower.PlantDocketNo.50-244Inaccordancewith10CFR50.73,LicenseeEventReportSystem,item(other),andtheGinnaStationQualityAssuranceManualAppendixB,whichrequiresthat,"Ifthenumberoftubesinageneratorfallingintocategories(a)or(b)belowexceedsthecriteria,thenresultsoftheinspectionshallbeconsideredareportableeventpursuantto10CFR50.73,"theattachedLicenseeEventReportLER92-005'isherebysubmitted.Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,RobertC.MeredXC'.S.NuclearRegulatoryCommissionRegionI475AllendaleRoadKingofPrussiaPA19406GinnaUSNRCSeniorResidentInspector9205280129920520PDRADOCK050002448PDR~@PE,<7~EW/~gag'l<

l NACFORM368(64)9)LICENSEEEVENTREPORT(LERIAPPROVEDOMBNO.31504)104EXPIRES:4(30(92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F630).V.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON.DC20555,ANDTOTHEPAPERWORKREDUCTIONPROJECT(31500104),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON.DC20503.'ACILITYNAME(1IR.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)PAE3050002441OF09""""SteamGeneratorTubeDegradationDueTo1GA/SCCCausesQ.A.ManualReportableLimitsToBeReachedEVENTDATEIS)LERNUMBER(6I>>REPORTDATE(7)OTHERFACILITIESINVOLVED(8)MONTHDAYYEARYEARBEOUENTIALergNUMBERNUMBERREYIBONMONTHOAYYEARFACILITYNAMESDOCKETNUMBER(S)05000042092920050005209205000OPERATINGMODE(9)POWERLEVEL(10)@P)CP@&m(r'.a)P20A02(B)20.405(sI(I)ill20.405(sIllI(III20.405(el(1llill)20A05(sI(1)(lv)20.405(s)(II(vl20A05(c)50.38(cl(1)50.38(cl(2)50.73(sIl2)(l)50.73(el(2)(li)50.73(sl(2)BillLICENSEECONTACTFORTHISLER(12)50.73(s)(2)(irl50.73(sl(2)(vl50,73(sl(2)(vill50,73(sI(2I(riIII(Al50,73(s)(2)(rilll(B)50,73(sl(2)(slTHISREPORTISSUBMITTFOPURSUANTT0THERLQVIREMENTSOF10CFR()IICnec>>OneormoreolthelollowinPI(1173.71(BI73.7((clXOTHERISpecllyInAottrectBelowendlnTenet,HRCForm366A)NAMEWesleyH.Backus.TechnicalAssistantto-theOperationsManagerTELEPHONENUMBERAREACODE315524-4446COMPLETEONELINEFOAEACHCOMPONENTFAILUREDESCRIBEDINTHISREPORT(13)CAUSESYSTEMCOMPONENTMANUFAC.TUREREPORTABLETONPRDSSYSTEMCOMPONENTMANUFACTUREREPORTABLETONPRDSXABTBGH314IR4$e($BW@~NIINA!r.k45%4:SUPPLEMENTALREPORTEXPECTED(14)EXPECTEDSU6MISSIONDATE115)MONTHDAYYEARYESIIIyer,completeEXPECTEDS(IB4IISSIONDATEINOABSTRACTILlmltto1400rpecsLi,e.,epproslmerelyIrfteentinplespreetypewrittenlinn)(18)Duringthe1992AnnualRefuelingandMaintenanceOutage,subsequenttotheEddyCurrentExaminationperformedonboththe'"A"and"B"WestinghouseSeries44SteamGenerator(S/G).,242tubesinthe"A"S/Gand2'16tubesinthe"B"'S/Grequiredcorrectiveactionduetotubedegradation.-TwoadditionaltubesineachS/Gwerestabilizedandpluggedaspreventiveaction,duetoanti-vibrationbar(AVB)concerns.Theimmediatecauseoftheeventwasthatthe"A"and"B"S/GtubedegradationwasinexcessoftheGinnaQualityAssuranceManualReportabilityLimits.TheunderlyingcauseofthetubedegradationisacommonS/G'roblemofapartiallyrolledtubesheetcrevicewithrecurringintergranularattack/stresscorrosioncracking(IGA/SCC)andPrimaryWater-StressCorrosionCracking(PWSCC)attack.onS/Gtubing.Correctiveactiontakenwastoeithersleeve'rplugtheaffectedtubeswithacceptedindustryrepairmethods.NRCForm366(64)9) tI NRCFORM38SA(589)tUS.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDOMBNO.3150010OEXPIRES:O/30/92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREQUESTI50/)HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F430),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1HEPAPERWORKREDUCTION.PROJECT(315041(H),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(1IDOCKETNUMBERl2)LERNUMBER(5)PAGE(3)YEARg)SEQUENTIALNUMBERREVISIONNUM854R.E.GinnaNuclearPowerPlantTEXT///II>>>><<>>cobJoqokaLUood/I/ooo/HRCFeIIR3SSAB/(17)osooo244920050002o"09PRE-EVENTPLANTCONDITIONSTheplantwasintheCold/RefuelingShutdownconditionfortheAnnualRefuelingandMaintenanceOutage.ReactorCoolantSystem(RCS)wasdepressurizedandRCStemperaturewasapproximately65F.SteamGenerator(S/G)EddyCurrentInspectionwas'inprogress.DESCRIPTIONOREVENTA.DATESANDAPPROXIMATETIMESORMAZOROCCURRENCES:0April20,1992,1200EDST:EventDateandTime0April20,1992,1200EDST:DiscoveryDateandTime0April21,1992,1330EDST:OralNotificationmadetotheNRCOfficeofNuclearReactorRegulation(NRR)..0April26,1992,1742EDST:repairscompleted.SteamGenerator0May5,1992:Follow-upwrittenreportsenttoNRCOfficeofNRR.B.EVENTDuringthe1992AnnualRefuelingandMaintenanceOutage,anEddyCurrentExaminationwasperformedinboththe"A"and"B"WestinghouseSeries44DesignRecirculatingSteamGenerators.ThepurposeoftheEddyCurrentExaminationwastoassessanycorrosionormechanicaldamagethatmayhaveoccurredduringthecyclesincethe1991examination.TheexaminationwasperformedbypersonnelfromRochesterGasandElectric(RG&E)andAllenNuclearAssociates,Inc.(ANA).AllpersonnelweretrainedandqualifiedintheEddyCurrentExaminationmethodandhavebeencertifiedtoaminimumofLevelIfordataacquisitionandLevelIIfordataanalysis.NRCForm355A(609)

I NRCFORM388A(IS$9)US.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORTILER)TEXTCONTINUATIONtAPPROVEDOMBNO.3)600104EXPIRES:4/30/92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHIS.INFORMATIONCOLLECTIONREQUEST:503)HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(P4)30).U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1HEPAPERWORKREDUCTIONPROJECT(31504)104),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBER(6)PAGE(3)R.E.GinnaNuclearPowerPlantTEXT(ffmoreSoeoelerfo/reer/,Iree/frfooo/HRC%%drrrr36543/(12)0s00o244YEAR$g92-SEDUENTIALNUMBER005@>REVISION.x:NUMER-0003cF09TheinitialEddyCurrentExaminationofthe"AE(and"B"SteamGeneratorswasperformed"utilizingtheZetec3-CoilMotorizedRotatingPancakeCoil(MRPC)probeandtheZetecMIZ-18DigitalDataAcquisitionSystem.The'frequenciesselectedwere400,300,100,and25KHZ.AdditionalEddyCurrentExaminationsofthe"A"'nd"B"SteamGeneratorswereperformedutilizingthe.standard0.740"or0.720"O.D.BobbinCoilProbe.Thefrequenciesselectedwere400,200,100and25KHZ.TheInletorHotLegExaminationProgramPlanincludedtheexaminationof100%ofeachopenunsleevedsteamgeneratortube.from'thetubeendtothetopofthetubesheetwithMRPC.Twentypercentofthetubeswereselectedandexaminedfortheirfulllength(20%randomsampleasrecommendedintheElectricPowerResearchInstitute(EPRI)guidelines)withabobbincoil.Inaddition,204of.eachtypeofsleevewasexaminedandtheremainder(unsleevedportion)ofthetubewasexaminedfulllength.AllRow1andRow2U-bendregionsselectedaspartofthe204randomsamplewereexaminedwiththeMRPCbetweentheg6TubeSupportPlateHotSide(TSPH)andtheg6TubeSupportPlateColdSide(TSPC)fromtheColdLegSide.Resultsoftheaboveinspectionsindicatedthat244tubesinthe"A"SteamGenerator(i.e.226-newrepairs,plus16previouslypluggedtubes,plus2tubesstabilizedforAnti-VibrationBar(AVB)concerns)and218tubesinthe"B"SteamGenerator(i.e.183newrepairs,plus3B&Wexplosiveplugs,plus30previouslypluggedtubes,plus2tubesstabilizedforAVBconcerns)requiredaction.Correctiveactionswerethereforetakenfor242tubesinthe"A"S/G,andfor216tubesinthe"B"S/G.Preventiveactions(forAVBconcerns)weretakenfor2tubesineachS/G.NRCForm368A(689)

NRCFORM366A(669)U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LERITEXTCONTINUATIONeAPPAOVED0MBNO.3)500)OEEXPIRE5I4/30/92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREQUEST.'00HRS.FORWARDCOMMENTSAEGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F430),U.S.NUCLEARAEGULATOAYCOMMISSION,WASHINGTON,OC20555,ANDTOTHEPAPERWORKREDUCTIONPROJECT(3)500104),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(1)DOCKETNUMBER(2)YEARLERNUMBERFSISEOVENTIALNVMER@rREVISIONNVMERPAGE(3)R.E.GinnaNuclearPowerPlantTEXT///momEPEEE/E/PEVked,IIEPJ/(/BRE/NRC%%dnR35663)((7)06000244920050004QF09OnApril20,1992atapproximately1200EDST,withtheRCSdepressurizedandtemperatureatapproximately65F,finalreviewofthe1992S/GInspectionEddyCurrentresultswascompleted.Resultsofthisreviewindicatedthatmorethan10percentofthetotaltubesinspectedaredegraded(i.e.imperfectionsgreaterthan20percentofthenominalwallthickness)andmorethanonepercentofthetotaltubesinspectedaredegraded(i.e.imperfectionsgreaterthantherepairlimit)..Becauseoftheabove,theresultsoftheinspectionareconsideredareportableeventpursuantto10CFR50.73perAppendixB-oftheGinnaStationQualityAssuranceManual.OnApril21,1992atapproximately1330EDST,oralnotificationwasmadetotheNRCOfficeofNRRpursuanttoAppendixBoftheGinna,StationQualityAssuranceManual.OnMay5,1992afollow-upwrittenreportoftheSteamGeneratorsInspectionandRepairswassenttotheNRCpursuantto'AppendixBoftheGinnaStationQualityAssuranceManual.C.rINOPERABLESTRUCTURESCOMPONENTS,ORSYSTEMSTHATCONTRIBUTEDTOTHEEVENT:D.None.OTHERSYSTEMSORSECONDARYFUNCTIONSAFFECTEDNone.E.METHODOPDISCOVERY:Theeventwasapparentafterthefinalreviewofthe"A"and"B"SteamGeneratorsEddyCurrentExaminationresults.NRCPARR366A(669)

NRCFORM366A(889)(LS.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONtAPPROVEDOMBNO.3(500)04EXPIRES:4(30/92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREQUESTI50.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(P430),U.S.NUCLEARREGULATORYCOMMISSION.WASHINGTON.DC20555,ANDTOTHEPAPERWORKREDUCTIONPROJECT(3150010E),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBER(6)PAGE(3)YEARoyerSEQUENTIALNUMSERREVISIONNUMBERR.EPGinnaNuclearPowerPlantTEXT(I/moreepeceJeeePJPPILIreeaB(ro'enclHRCFcnn36848)()7)0600024492-0050005QF09P.OPERATORACTION:ControlRoomoperatorscompletedthenotificationsandevaluationsrequiredbytheA-25.1(GinnaStationEventReport),submittedfortheeventbytheS/Gsupervision.G.SAFETYSYSTEMRESPONSES.None.IIICAUSEOPEVENTA.IMMEDIATECAUSE:Theimmediatecauseoftheeventwasthatthe"ALIand"BLISteamGeneratortubedegradationwasinexcessoftheGinnaStationQualityAssuranceManualReportableLimits.B.ROOTCAUSE:TheresultsoftheexaminationindicatethatIntergranularAttack(IGA)andIntergranularStressCorrosionCracking(IGSCC)continuetobeactivewithinthetubesheetcreviceregionontheinletsideofeachsteamgenerator.Asinthepast,IGA/SCCismuchmoreprevalentinthe"B"SteamGeneratorwith118newcreviceindicationsreported.Inthe"A"SteamGenerator,34newcreviceindicationswerereported.ThemajorityoftheinlettubesheetcrevicecorrosionindicationsareIGA/SCCoftheMillAnnealedInconel600tubematerial.Thisformofcorrosion'sbelievedtobetheresultofanalkalineenvironmentforminginthetubesheetcrevices.Thisenvironmenthasdevelopedovertheyearsasdepositsandactivespeciessuchassodiumandphosphate,havereacted,changinganeutralorinhibitedcreviceintotheaggressiveenvironmentthatpresentlyexists.NRCForm366A(6J)9)

NRCFORM386A(BJIS)i(LS.NUCLEARAEGULATORYCOMMISSIONLICENSEEEVENTREPORTILER)TEXTCONTINUATIONtAPPROVEDOMBNO.31500104EXPIRES'/30/$2ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFOAMATIONCOLLECTIONREQUEST:500HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(PJ)30),US.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1'HEPAPERWORKREDUCTIONPROJECT(3)500104),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBER(8)YEARPRSEQUENTIALSa~r..6%NUMER%oREVISIONNVMSERPAGE(3)R.E.GinnaNuclearPowerPlantTEXT////Sore8/reoe/e/Fr/rer/,Iree///0'ooe/HRCForIII38//AS/(IT)24492005000OFAlongwithIGA/SCCin'thecrevices,thereappearstohavebeenaslightincreasein"PrimaryWaterStressCorrosionCracking(PWSCC)attherolltransitionduringthelastoperatingcycle.Thismechanismwasfirstaddressedin1989andthisyeartherewere63rolltransitionPWSCCindicationsin"B"SteamGeneratorand189rolltransition(PWSCC)indicationsin"A"SteamGenerator.ThesenumbersincludetubesthatmayhavePWSCCincombinationwithIGAandSCCinthecrevice.XVANALYSISOPEVERTThiseventisreportableinaccordancewith10CFR50.73,LicenseeEventReportitem(other)andtheGinnaStationQualityAssuranceManualAppendixBwhichrequiresthat,."Ifthenumberoftubesinageneratorfallingintocategories(a)or(b)exceedsthecriteria,thenresultsoftheinspectionshallbeconsideredareportableeventpursuantto10CFR50.73."Thetubedegradationinthe"AL)and"B"SteamGeneratorsexceededthecriterionof(a)whichstates,"morethan10percentofthetotaltubesinspectedaredegraded(imperfections,greaterthan20percentofthenominalwallthickness)",andthecriterionof(b)whichstates,"morethan1percentofthetotaltubesinspectedaredegraded(imperfectionsgreaterthantherepairlimit).Thisrepairlimitisdefinedas,"SteamGeneratortubesthathaveimperfectionsgreaterthan40percentthroughwall,asindicatedbyEddyCurrent,shallberepairedbypluggingorsleeving."NRCForm386A(86$)

.J NRCFOAM366A(669)US.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONeAPPROVEDOMBNO.31500)04EXPIRES:6/30/92ESTIMATEDBURDENPE4RESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREQUEST:50A)HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHE4ECORDSAND4EPOATSMANAGEMENTBRANCH(F430).U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1HEPAPERWORK4EDUCTIONPROJECT(31500104).OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,OC20503.FACILITYNAME(1)DOCKETNUMBER(2)YEARLERNUMBER(6)SEOUENTIALgPNUMBERREVISIONNUMBERPAGE(3)R.E..GinnaNuclearPowerPlantTEXT/I/more<<>>ce/enrFI/rer/Beea///Noor>>lNRCForrrlJ(ISAB/((2)0500024-4920050007OF09Anassessmentwasperformedconsideringthesafety.consequencesandimplicationsofthiseventwiththefollowingresultsandconclusions:TherewerenosafetyconsequencesorimplicationsresultingfromtheSteamGeneratortubedegradationinexcessoftheQualityAssuranceManualReportableLimitsbecause:.oThe.degradedtubeswereidentifiedandrepairedpriortoanysignificantleakageorSteamGeneratortuberuptureoccurring.0EvenassumingacompleteseveranceofaSteamGeneratortubeatfullpower,asstatedintheR.E.GinnaNuclearPowerPlantUpdatedFinalSafetyAnalysisReport(Ginna/UFSAR)section15.6.3,(SteamGeneratorTubeRupture),thesequenceofrecoveryactionsensuresearlytermination.ofprimarytosecondaryleakagewithorwithoutoffsitepoweravailablethuslimitingoffsiteradiationdosestowithintheguidelinesof10CFR100.~Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywasassuredatalltimes.V.CORRECTIVEACTIONA.ACTIONTAKENTORETURNAFFECTEDSYSTEMS.TOPRE-EVENTNORMALSTATUS:o'fthe244tubesinthe"A"SteamGenerator,36tubeswererepairedusingaCombustionEngineering27"weldedsleeveintheHotLeg,plus194tubeswererepairedusingaBabcockandWilcoxexplosivelyweldedtubesheetsleeveintheHotLegandalloftheabovetubeswillremaininservice.Theremaining14tubes=wereremovedfromservicebypluggingboththeHotandColdLegtubeends.Atotalof185tubesinthe"A"SteamGeneratorarecurrentlypluggedand555tubesaresleeved.NRCForm366A(689)

I NRCFORM3SSA(W)US.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORTILER)TEXTCONTINUATIONlAPPROVEOOMBNO.3I50010OiEXPIRES:O/30/92ESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREOUEST:50.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(PJ)30),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTOTHEPAPERWORKREDUCTIONPROJECT(31504104),OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,DC20503.FACII.ITYNAME(1IDOCKETNUMBER(2)YEARLERNUMBER(SlSEOVENTIALNVMERREVISIONNUMBERPAGE(3)R.E.GinnaNuclearPowerPlantTEXT/I/moree/>>ce/or/q/rer/Iree<<IChE/<<>>/NRC%%de3SBAB/(IT)0S00024492005000OF0Ofthe218tubesinthe"B"SteamGenerator,186tubeswererepairedusingaCombustionEngineering27"weldedsleeveintheHotLeg,plus9tubeswererepairedusingaCombustionEngineering30"weldedsleeveintheHotLegandalloftheabovetubeswillremaininservice.Theremaining23tubeswereremovedfrom=servicebypluggingboththeHotandColdLegtubeends.Atotalof313tubes.inthe"BL(SteamGeneratorarecurrentlypluggedand1134tubesaresleeved.Alltheaboverepairsonthe"A"and"BL(SteamGeneratorswerecompletedonApril26,1992atapproximately1742EDST.B.ACTIONTAKENORPLANNEDTOPRVTENTRECURRENCE:-Theoccurrence/presenceofIGA,SCC,.andPWSCCisacommonPWRSteamGeneratorproblem.UtilitieswithsusceptibletubingandpartiallyrolledcrevicesmustdealwiththisrecurringattackonSteamGeneratortubing.R.E.GinnaNuclearPowerPlantwillcontinuecarefulmonitoringofbothprimaryRCSand'econdarysidewaterchemistryparameters.Thesewaterchemistryparameterswillcontinuetobeevaluatedagainstacceptedindustryguidelinesinordertominimizeharmfulprimaryand/orsecondarysideenvironments.DegradedSteamGeneratortubesshallbesleevedorpluggedinaccordancewiththeInserviceInspectionProgramandAcceptedIndustryRepairmethods.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:Thedegradedcomponentsare:InconelGrade600tubeshavinganoutsidediameterof0.875inchesanda.nominalwallthicknessof0.050inches.ThesetubesweremanufacturedbyHuntingtonAlloyCompany.'NRCForm3SSA(589)

NRCFORM388A(669)US.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDOMBNO.3)504104EXPIRES:E/30/IQESTIMATEDBURDENPERRESPONSETOCOMPLYWTHTHISINFORMATIONCOLLECTIONREQUEST:505)HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHERECORDSANDREPORTSMANAGEMENTBRANCH(F830),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555,ANDTO1)IEPAPERWORKREDUCTIONPROJECT(3150010E).OFFICEOFMANAGEMENTANDBUDGET,WASHINGTON,OC20503.FACILITYNAME(1)DOCKETNUMBER(2)YEARLERNUMBER(6)S~SEQVENTIALNVM@ERj>gjREVISION:i.'/NVMSERPAGE(3)R.E.GinnaNuclearPowerPlantTEXT///IIRvoEPoooJIISA(RR/,vJo//I/ooo/NRCForm36643/(17)060002449005-0009"09B.PREVIOUSLERsOMSIMILAREVENTS:AsimilarLEReventhistoricalsearchwasconductedwiththe.followingresults:ThecreviceindicationsaresimilartothosereportedinA0-74-02,AO-75-07,R0-75-013,andLERs76-008,77-008,78-003,79-006,79022/80003/81009/82003/82022/83013/89=-001,90-004,and91-005.CSPECIALCOMMEHTS:Foramoreindepthreport,refertothe"1992SteamGeneratorEddyCurrentInspection"SummaryExaminationReportsenttotheNRCMay5,1992.NRCForm368A(BJ)9)

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