ML20204B417

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/01T-0:on 780925,during Surveillance Test,Control Rod Driveline Breaker a Failed to Trip on First Attempt. Caused by Trip Mechanism Mechanical Arm Being Out of Adjustment.Arm Adjustment Corrected
ML20204B417
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 10/06/1978
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20204B415 List:
References
LER-78-023-01T, LER-78-23-1T, NUDOCS 7810170146
Download: ML20204B417 (4)


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1. Reportabic Occurrence Report No. 50-313/78-23
2. Report Date: 3. Occurrence Date:

10/06/78 09/25/78 4 Facility: Arkansas Nuclear One - Unit '

Russellville, Arkansas 72801

5. Identification of Occurrence:

A breaker in the Reactivity Control System was not tested within time limits as prescribed by Technical Specifications.

6. Conditions Prior to Occurrence:

Steady-State Power X Reactor Power NWth 1

l Ilot Standby , Net Output MWe l

l Cold Shutdown Percent of Full Power 100 %

Refueling Shutdown ' Load Changes During Routinc Power Operation Routine Startup Operation _

Routine Shutdown Operation Other (specify) i

7. Description of Occurrence:

During surveillance testing, CRD "A" Breaker did not trip on the first attempt. The "B" Breaker was immediately tested as was the "D" Breaker. However, due to an oversight, the "C" Breaker was not tested within the eight hour period as prescribed'in Technical Specification 3.5.1.6.

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l Reportabic Occurrence Report No- 50-313/78-23

8. Designatio; of Apparent Cause of Occurrence:

Design Procedure

. Manufac ture Unusual Service Condition Including Environmental ,

Installation / l Const ruction Component Failure J (See Failure Data) -

Operator ,

l Other (specify) 1

~X Personnel error (Maintenance and Repair Personnel) .

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9. Analysis of Occurrence:

Based on other breakers operating normally and redundant breakers I being tes ted immediately, there was no danger of health or safety to the public.

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1 Reportable Occurrence Report do. '50-313/78-23 l

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10. l Corrective Action:

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.The mechanical arm of the trip mechanism was found to be out of adjustment and was corrected with vendor assistance. Subsequent 4 testing demonstrated the breaker would meet survc111ance specifi- '

ca tions.

The technicians were reinstructed on technical specifications requirements.

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11. Failure Data: l i

h Similar Reportable Occurrence Report Number 50-313/78-24 occurred on 9/16/78. l 1

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