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Category:EXAMINATION REPORT
MONTHYEARML20236T8241987-10-30030 October 1987 Exam Rept 50-397/OL-87-03 on 870922-30.Exam Results:Four Out of Six Reactor Operator Candidates & Eight Out of Eleven Senior Reactor Operator Candidates Passed Exams.Sample Test & Other Supporting Info Encl ML20205G6601987-03-20020 March 1987 Exam Rept 50-397/OL-87-02.Requalification Program Evaluated as Satisfactory,Per Rev 0 to NUREG-1021 & WT Russell 860522 Memo Re Listed Requirements ML20206U7381986-09-17017 September 1986 Exam Rept 50-397/OL-86-02 on 860811-14.Exam Results:One Senior Reactor Operator Candidate Failed Simulator Portion & One Senior Reactor Operator Candidate Failed Oral & Simulator Portions of Exam.Eight Candidates Passed ML20197A5561986-04-22022 April 1986 Exam Rept 50-397/OL-86-01 on 860204-06.Exam Results:Four Senior Reactor Operator & Seven Reactor Operator Candidates Passed Written & Operating Exams ML20210V2141986-04-22022 April 1986 Rev 1 to Exam Rept 50-397/OL-86-01 on 860204-06.Exam Results:Four Senior Reactor Operator & Seven Reactor Operator Candidates Passed Written & Operating Exams.Nrc Resolutions to Facility Exam Comments Encl ML20135B5511985-08-26026 August 1985 Exam Rept 50-397/OL-85-01 of Exams Administered on 850529-30.Exam Results:Three Senior Reactor Operator Candidates Passed Exams 1987-03-20
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000397/19990011999-03-19019 March 1999 Insp Rept 50-397/99-01 on 990201-04 & 0303-05.No Violations Noted.Major Areas Inspected:Physical Security Program ML20154H7501998-10-13013 October 1998 Revised Notice of Violation from Insp on 971118.Violation Noted:In April 1996,licensee Made Changes to Procedures as Described in Safety Analysis Rept Without Seeking Prior Commission Approval & Changes Had Effect of Changing TS PNO-IV-98-025, on 980615,WNP-2 Initiated Plant Shutdown as Result of Traversing Incore Probe That Could Not Be Moved. Licensee Observed Some Drive Cable Damage & Cable Wrapped Around Some Components Under Reactor Vessel1998-06-16016 June 1998 PNO-IV-98-025:on 980615,WNP-2 Initiated Plant Shutdown as Result of Traversing Incore Probe That Could Not Be Moved. Licensee Observed Some Drive Cable Damage & Cable Wrapped Around Some Components Under Reactor Vessel ML20199E3161997-11-18018 November 1997 Notice of Violation from Insp on 971020-26.Violation Noted: on 971021,inspector Identified Gap in Vehicle Barrier Sys That Provided Path for Design Basis Vehicle to Gain Access to Unauthorized Proximity to Vital Area IR 05000397/19970071997-11-18018 November 1997 Partially Withheld Insp Rept 50-397/97-07 on 971020-26. (Ref 10CFR73.21).Violations Noted.Major Areas Inspected: Plant Support Re Vehicle Barrier Sys Which Was Consistent W/Summary Description & Accurately in Security Plan IR 05000397/19970061997-06-0909 June 1997 Insp Rept 50-397/97-06 on 970519-23.No Violations Noted. Major Areas Inspected:Insp Consisted of Review of Licensee Planned & Implemented Activities Associated W/Isi Program IR 05000397/19970021997-03-0606 March 1997 Insp Rept 50-397/97-02 on 970127-31 & 0212-14.No Violations Noted.Major Areas Inspected:Engineering & Plant Support Security IR 05000397/19960231996-12-16016 December 1996 Insp Rept 50-397/96-23 on 961118-22.No Violations Noted. Major Areas Inspected:Engineering & Plant Support ML20134Q0381996-11-21021 November 1996 EN-96-084:on 961126,notice of Proposed Imposition of Civil Penalty in Amount of $100,000 Issued to Licensee.Action Based on Several Instances Where Surveillances Not Performed & Mode Changes Made W/O Assurances That Equipment Operable PNO-IV-95-007, on 950218,plant Reactor Scrammed from 80% Power Due to Turbine Trip.News Media Was Notified of Event1995-02-21021 February 1995 PNO-IV-95-007:on 950218,plant Reactor Scrammed from 80% Power Due to Turbine Trip.News Media Was Notified of Event PNO-V-93-021, on 931201,chemical Spill in Radwaste Building. Caused by Addition of Oxidizing Agent,Hydrogen Peroxide. Employees Working on Floor Were Moved to Different Part of Plant1993-12-0202 December 1993 PNO-V-93-021:on 931201,chemical Spill in Radwaste Building. Caused by Addition of Oxidizing Agent,Hydrogen Peroxide. Employees Working on Floor Were Moved to Different Part of Plant ML20059D2141993-10-15015 October 1993 Notice of Violation from Insp on 930402-0517.Violation Noted:Licensee Determined That Records Required to Be Maintained by NRC Not Complete & Accurate in All Matl Respects IR 05000397/19930281993-08-26026 August 1993 Insp Rept 50-397/93-28 on 930809-13.No Violations Noted. Major Areas Inspected:Emergency Preparedness Program, Emergency Detection & Classification,Notification & Communication PNO-V-93-004, on 930121,automatic Reactor Scram Received Due to Low Level in Reactor Pressure Vessel.Licensee Estimates That Plant Will Be Shut Down for Repairs & Maint for 3 to 5 Days.Inspector Onsite During Event.Press Release Issued1993-01-21021 January 1993 PNO-V-93-004:on 930121,automatic Reactor Scram Received Due to Low Level in Reactor Pressure Vessel.Licensee Estimates That Plant Will Be Shut Down for Repairs & Maint for 3 to 5 Days.Inspector Onsite During Event.Press Release Issued IR 05000397/19920341992-12-30030 December 1992 Insp Rept 50-397/92-34 on 921207-11.No Violations Noted. Major Areas Inspected:Emergency Preparedness Program PNO-V-92-024, on 920711,while Retesting Main Steam SRV at Approx 14% Reactor Power,Srv 3B Opened When Operated from Control Room But Would Not Close.Reactor Operators Reduced Reactor Pressure in Effort to Reseat Valve1992-07-13013 July 1992 PNO-V-92-024:on 920711,while Retesting Main Steam SRV at Approx 14% Reactor Power,Srv 3B Opened When Operated from Control Room But Would Not Close.Reactor Operators Reduced Reactor Pressure in Effort to Reseat Valve PNO-V-91-031, on 911119,licensee Declared Unusual Event Following Low Reactor Pressure Vessel Level Condition W/Eccs Injecting.Reactor Tripped on Turbine Trip.All ECCS Sys Responded as Designed1991-11-19019 November 1991 PNO-V-91-031:on 911119,licensee Declared Unusual Event Following Low Reactor Pressure Vessel Level Condition W/Eccs Injecting.Reactor Tripped on Turbine Trip.All ECCS Sys Responded as Designed ML20203C2231991-06-14014 June 1991 PNO-V-91-04B on 910614,Region V Issued Rev 3 to CAL Concerning Actions to Be Taken by WPPSS Subsequent to Unsuccessful Simulator Requalification Retake Exam Performed 910605-06 PNO-V-90-049, on 901207,w/plant Operating at Full Power, Explosion Occurred in Area of B Phase Insulator of Plant Main Transformer,Which Caused Turbine & Reactor Trip.Unusual Event Was Declared Due to Explosion1990-12-0707 December 1990 PNO-V-90-049:on 901207,w/plant Operating at Full Power, Explosion Occurred in Area of B Phase Insulator of Plant Main Transformer,Which Caused Turbine & Reactor Trip.Unusual Event Was Declared Due to Explosion PNO-V-90-041, on 901024,licensee Declared Unusual Event After Determining That Vital & non-vital Instrument Power Supplies Interconnected Through Certain Sys Instrumentation1990-10-25025 October 1990 PNO-V-90-041:on 901024,licensee Declared Unusual Event After Determining That Vital & non-vital Instrument Power Supplies Interconnected Through Certain Sys Instrumentation PNO-IV-90-028, on 900603,while Attempting to Energize Station Normal Auxiliary Power Transformers,Short Circuit Failure in Bus Works for 25 Kv Sys.Fire Brigade Responded But No Fire Was Reported.Event Under Investigation1990-06-0404 June 1990 PNO-IV-90-028:on 900603,while Attempting to Energize Station Normal Auxiliary Power Transformers,Short Circuit Failure in Bus Works for 25 Kv Sys.Fire Brigade Responded But No Fire Was Reported.Event Under Investigation PNO-V-88-054, on 880824,licensee Declared Unusual Event as Result of Increase in Unidentified Leakage to Level Above TS Limit of 5 Gpm.Reactor Was Later Shutdown & Unidentified Leakage Rate Had Correspondingly Decreased to Approx 8 Gpm1988-08-24024 August 1988 PNO-V-88-054:on 880824,licensee Declared Unusual Event as Result of Increase in Unidentified Leakage to Level Above TS Limit of 5 Gpm.Reactor Was Later Shutdown & Unidentified Leakage Rate Had Correspondingly Decreased to Approx 8 Gpm IR 05000397/19880221988-06-29029 June 1988 Insp Rept 50-397/88-22 on 880606-09.Violation Noted.Major Areas inspected:880512 Radioactive Resins Spill in Radwaste Bldg Which Resulted in Declaration of Unusual Event & Facility Tour ML20150F9771988-06-29029 June 1988 Notice of Violation from Insp on 880606-09.Violation Noted: on 880512,individual Entered Radwaste Bldg W/O Being Accompanied or Provided W/Radiation Monitoring Device & on 880608,door to Radwaste Bldg Not Locked PNO-V-88-013, on 880213,plant Experienced Condenser Tube Failure & Shut Down Manually Scramming Plant from 35% Power. on 880214,reactor Bldg Air Supply Fan Started W/O Trip Circuit Being Energized.Cause Under Investigation1988-02-16016 February 1988 PNO-V-88-013:on 880213,plant Experienced Condenser Tube Failure & Shut Down Manually Scramming Plant from 35% Power. on 880214,reactor Bldg Air Supply Fan Started W/O Trip Circuit Being Energized.Cause Under Investigation IR 07100001/20110051987-12-0404 December 1987 Notice of Violation from Insp on 871001-1105.Violation Noted:Maint Electrician Worked More than 24 H in 48 H Period & Plant Operations Committee Meeting Held W/Chairman & Three Rather than Four Members as Required IR 05000397/19870271987-12-0303 December 1987 Insp Rept 50-397/87-27 on 871001-1105.Violations Noted.Major Areas Inspected:Control Room Operations,Esf Status, Surveillance & Maint Programs,Lers,Special Insp Topics & Licensee Action on Previous Insp Findings PNO-V-87-079, on 871126,digital Voltmeter Connected to Wrong Terminal Resulting in Inadvertent Opening of Safety Relief Valve 2D.Caused by Technician Error.Position of Safety Relief Valve Identified & Shut1987-11-27027 November 1987 PNO-V-87-079:on 871126,digital Voltmeter Connected to Wrong Terminal Resulting in Inadvertent Opening of Safety Relief Valve 2D.Caused by Technician Error.Position of Safety Relief Valve Identified & Shut ML20236T8241987-10-30030 October 1987 Exam Rept 50-397/OL-87-03 on 870922-30.Exam Results:Four Out of Six Reactor Operator Candidates & Eight Out of Eleven Senior Reactor Operator Candidates Passed Exams.Sample Test & Other Supporting Info Encl ML20236G3791987-10-26026 October 1987 PNS-V-87-008:on 871024,licensed Plant Operator Reportedly Arrested by Kennewick City Police Dept & Charged W/Discharge of Firearm within City Limits & Reckless Endangerment. Licensee Suspended Employee Unescorted Access to Plant PNO-V-87-024A, on 870322,reactor Manually Tripped Due to Loss of Feedwater.Caused by Mechanical Failure of 1/4-amp Fuse in Feedwater Control Sys.Rcic Sys Operated Properly.Plant Restarted on 8703241987-03-25025 March 1987 PNO-V-87-024A:on 870322,reactor Manually Tripped Due to Loss of Feedwater.Caused by Mechanical Failure of 1/4-amp Fuse in Feedwater Control Sys.Rcic Sys Operated Properly.Plant Restarted on 870324 PNO-V-87-024, on 870322,both Main Feedwater Pumps Lost Suction Pressure & Tripped.Plant Operator Manually Tripped Reactor Upon Losing All Feedwater Flow.Reactor Vessel Level Restored & Heat Manually Removed.Investigation Pending1987-03-23023 March 1987 PNO-V-87-024:on 870322,both Main Feedwater Pumps Lost Suction Pressure & Tripped.Plant Operator Manually Tripped Reactor Upon Losing All Feedwater Flow.Reactor Vessel Level Restored & Heat Manually Removed.Investigation Pending ML20205G6601987-03-20020 March 1987 Exam Rept 50-397/OL-87-02.Requalification Program Evaluated as Satisfactory,Per Rev 0 to NUREG-1021 & WT Russell 860522 Memo Re Listed Requirements PNO-V-87-022, on 870319,licensee Found Pressure Switch on Discharge Side of RHR Sys Pump B Isolated.Licensee Unisolated Switch & Restored Sys to Full Operability.Region V Followup Continuing1987-03-20020 March 1987 PNO-V-87-022:on 870319,licensee Found Pressure Switch on Discharge Side of RHR Sys Pump B Isolated.Licensee Unisolated Switch & Restored Sys to Full Operability.Region V Followup Continuing IR 05000397/19870031987-03-18018 March 1987 Insp Rept 50-397/87-03 on 870223-27.No Violations Noted. Major Areas Inspected:Calibr of Instrumentation,Ie Bulletin Followup,Licensee Action on Previous Insp Findings,Licensee Action on Items of Noncompliance & Part 21 Followup IR 05000397/19870011987-03-0303 March 1987 Insp Rept 50-397/87-01 on 870104-0214.No Violations or Deviations Identified.Major Areas Inspected:Control Room Operations,Esf Status,Surveillance Programs,Maint Topics, Lers,Special Insp Topics & Listed Insp Procedures PNO-V-87-015, on 870220,shutdown Commenced Due to Decreasing Lubrication Oil Pressure to Turbine Bearings.Caused by Flange or Pipe Leak Inside Lube Oil Reservoir.Shutdown Will Continue for Approx 4 to 6 Days1987-02-20020 February 1987 PNO-V-87-015:on 870220,shutdown Commenced Due to Decreasing Lubrication Oil Pressure to Turbine Bearings.Caused by Flange or Pipe Leak Inside Lube Oil Reservoir.Shutdown Will Continue for Approx 4 to 6 Days IR 05000397/19860371987-01-16016 January 1987 Insp Rept 50-397/86-37 on 861116-870103.No Violations or Deviations Identified.Major Areas Inspected:Esf Status.Lers, Surveillance Program,Maint Program,Special Insp Topics & Licensee Action on Previous Insp Findings IR 05000397/19860381987-01-0707 January 1987 Insp Rept 50-397/86-38 on 861124-26 & 1215-19.No Violations Noted.Major Areas Inspected:Gaseous Waste Sys,Liquids & Liquid Wastes,Facilities & Equipment,Followup on IE Info Notices & Enforcement Items PNO-V-86-084, on 861120,plant Shut Down Due to Inoperability of Acoustic Monitor for Safety Relief Valve 5c.Caused by Lack of Environ Qualification Documentation for Connector. Investigation Underway.Plant Will Be Restarted on 8611251986-11-20020 November 1986 PNO-V-86-084:on 861120,plant Shut Down Due to Inoperability of Acoustic Monitor for Safety Relief Valve 5c.Caused by Lack of Environ Qualification Documentation for Connector. Investigation Underway.Plant Will Be Restarted on 861125 IR 05000397/19860261986-11-19019 November 1986 Insp Rept 50-397/86-26 on 860915-20.No Violations Noted. Major Areas Inspected:Emergency Preparedness Exercise & Associated Critique & Followup on Open Items Identified During Previous Insps PNO-V-86-078, on 861107 & 09 Increased Vibration from Reactor Recirculating Water Pump a Occurred.Licensee Reduced Reactor Power & Shifted Pumps Into Low Frequency Operation, Decreasing Vibration Level1986-11-12012 November 1986 PNO-V-86-078:on 861107 & 09 Increased Vibration from Reactor Recirculating Water Pump a Occurred.Licensee Reduced Reactor Power & Shifted Pumps Into Low Frequency Operation, Decreasing Vibration Level PNO-V-86-064A, on 860918,licensee Declared Alert Due to Tornado Warnings & High Winds.Train a Svc Water Sys out-of- Svc Due to Fire in Svc Water Pump House.Licensee Also Experiencing Low Fire Main Header Pressure1986-09-18018 September 1986 PNO-V-86-064A:on 860918,licensee Declared Alert Due to Tornado Warnings & High Winds.Train a Svc Water Sys out-of- Svc Due to Fire in Svc Water Pump House.Licensee Also Experiencing Low Fire Main Header Pressure PNO-V-86-064, on 860918,licensee Declared Unusual Event Due to High Winds of 85 Mph.Svc Water Pump B out-of-svc Resulting in Emergency Diesel Generator B Being out-of-svc. Rupture in Low Pressure Fire Main Also Reported1986-09-18018 September 1986 PNO-V-86-064:on 860918,licensee Declared Unusual Event Due to High Winds of 85 Mph.Svc Water Pump B out-of-svc Resulting in Emergency Diesel Generator B Being out-of-svc. Rupture in Low Pressure Fire Main Also Reported ML20206U1861986-09-18018 September 1986 Notice of Violation from Insp on 860616-27 IR 05000397/19860311986-09-17017 September 1986 Enforcement Conference Rept 50-397/86-31.Topics Discussed: Violations Identified in Insp Rept 50-397/86-12 Re Equipment Qualification Program,Violations in Insp Rept 50-397/86-11 & Repeat Violations in Control of Combustible Matls ML20206U7381986-09-17017 September 1986 Exam Rept 50-397/OL-86-02 on 860811-14.Exam Results:One Senior Reactor Operator Candidate Failed Simulator Portion & One Senior Reactor Operator Candidate Failed Oral & Simulator Portions of Exam.Eight Candidates Passed PNO-V-86-060, on 860903,reactor Feedwater Pump B Tripped Due to Failure of Overspeed Controls.Caused by Partial Control Valve Closure Re Tripping of Hydraulic Power Units. Investigation Underway1986-09-0404 September 1986 PNO-V-86-060:on 860903,reactor Feedwater Pump B Tripped Due to Failure of Overspeed Controls.Caused by Partial Control Valve Closure Re Tripping of Hydraulic Power Units. Investigation Underway IR 05000397/19860111986-07-25025 July 1986 Insp Rept 50-397/86-11 on 860616-27.Violations Noted.Major Areas Inspected:Mgt Controls & Licensee Activities,Including Operator Recovery Actions,Qa Program,Measuring & Test Equipment & Tech Spec Surveillances & Tests PNO-V-86-034, on 860620,licensee Measured 1.3 Gpm Leakage Into RHR Sys B.Caused by Leak Through LPCI Injection Valve 53B.Util Repairing Valve.Startup Will Be Delayed Until 860629 Due to BPA Load Requirements1986-06-23023 June 1986 PNO-V-86-034:on 860620,licensee Measured 1.3 Gpm Leakage Into RHR Sys B.Caused by Leak Through LPCI Injection Valve 53B.Util Repairing Valve.Startup Will Be Delayed Until 860629 Due to BPA Load Requirements 1999-03-19
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Enclosure (1)
U. S. NUCLEAR REGULATORY COMMISSION REGION V EXAMINATION P.EPORT Examination Report No.: 50-397/0L-87-02 Facility: Washington Nuclear Project, WNP-2 Facility License No.: NPF-21 Examinations administered at Washington Nuclear Project, WNP-2, Richland, Washington Requalification Review 1987 Chief Examiner: 7 M /}l M i ~ A - w ]/'=/*7 Tho R. ead Date ign d Approved by: (/- '
, 2M W hn 0. Elin, Chief W rations Section Ostte Sfgned
- Sumary
The review of the requalification program at WNP-2 was performed in accordance with the Pilot Test Program defined in a memorandum from William T. Russell, Director, Division of Human Factors Technology, NRR, dated May 22, 1986. This memorandum stipulated the following requirements:
(1) NRC review and approval of the requalification written examinations developed by the facility.
(2) Parallel grading of the written examinaticn by the facility and NRC
- staffs.
(3) Observation of oral / simulator requalification examinations conducted by the facility staff.
Based on the criteria of NUREG-1021, Revision 0, Examiner Standards, the requalification program at WNP-2 was evaluated as satisfactory.
8703310 [j$$$97 PDR AD PDR V
! PROGRAM DETAILS
- 1. Program Evaluation The requalification program at WNP-2 was evaluated in accordance with the pilot test program defined in a memorandum from William T. Russell, Director, Division of Human Factors Technology, NRR, dated May 22, 1986,
- a. Prior Review of Facility Written Examination Required for Satisfactory Rating:
The facility written examination should follow the guidance contained in ES-601 (Rev. 2) with respect to exam format, content, and length.
The WNP-2 requalification written examination was reviewed prior to its administration on February 19, 1987. Region V found this examination to be comprehensive and in general compliance with the Examiner's Standards. The NRC evaluator was present during the written examination to monitor its administration, and replaced specific examination questions addressing recent applicable Licensing Event Reports (LER's) in both the R0 and SR0 examinations. This was done to validate the security of the examinations.
Evaluation: Satisfactory
- b. Parallel Grading of the Facility Graded Written Examination Required for Satisfactory Rating:
4 Facility graded written examination results shall be within 10% per section of the results reached by NRC examiners l independently grading the same examinations.
All of the WNP-2 recualification written examinations administered by the facility staff were independently graded by NRC Region V examiners. Two Reactor Operators (RO) and five Senior Reactor Operators (SRO) participated in the February 19, 1987, requalification examinations. All NRC graded sections were within 10% of the grades determined by facility staff. On the average, the facility grades for each candidate in each section were between 1% and 2% lower than NRC grades.
Evaluation: Satisfactory
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7
- 1. c. Pass / Fail Evaluation:
Required for Satisfactory Rating:
i More than 80% of the final pass / fail determinations made by both the facility and the NRC must be in agreement.
All of the WNP-2 and NRC pass / fail determinations were in agreement.
1 Evaluation: Satisfactory
- d. Candidates Ability to Satisfactorily Complete Requalification:
Required for Satisfactory Rating:
More than 80% of the candidates pass the requalification examination with a grade of 70% or better in each section and 80% or better overall.
All of the candidates passed the February 19, 1987, examinations.
Evaluation: Satisfactory
- e. Evaluation of the Operating Examinations Required for satisfactory rating:
A subjective evaluation of the facility administered operating tests using the procedures of ES-105 for each facility examiner observed. The facility operating test should conform to an NRC administered operating test in it's comprehensiveness. More than 80% of the facility pass / fail determinations shall be in agreement with NRC determinations.
. The simulator scenarios were reviewed prior to the conduct of the simulator examinations on February 17, 1987, to ensure that they were adequate, realistic, and challenging enough for licensee evaluation. Just prior to the oral portion of the operating examination, administered on February 18 and February 20, 1987, the facility staff was presented with oral examination questions which also addressed recent LER's. The facility staff incorporated these into their oral discussions, which were subsequently monitored.
The administration of both the simulator and oral portions of the operating exams by the WNP-2 training department were evaluated for two different operating shifts. Concurrently, two experienced operator perfonnances were independently evaluated. These evaluations were subsequently compared with the parallel facility performance evaluations of these same two operators. This was done to determine the overall competence of the operating shifts, and to determine if individual operator weaknesses are properly evaluated and documented. Two facility staff instructors were independently evaluated while performing examiner duties during the operating examinations in order to determine their ability to evaluate safe operators, which in turn, reflects on the facility instructor certification program.
i The facility administered the simulator portion of the Operating examinations on February 18, 1987, and the oral portion of the Operating examinations on February 20, 1987, in accordance with the guidelines specified in NUREG-1021, Examiner Standards. All of the candidates passed the operating examinations. The facility Operating forms structure and content are virtually identical with their NRC counterparts. The NRC evaluator noted that the fccility administrated oral examinations were significantly longer than their NRC counterparts, as the facility staff examiners covered virtually all subject areas associated with the selected examination systems.
Evaluation: Satisfactory i 2. Program Strengths and Weaknesses No generic weaknesses were found in the facility licensing requalification training program. The overall evaluation of program adequacy was found satisfactory, with notable improvements in simulator fidelity. The Chief Examinar noted that the facility has implemented a continuing, aggressive Simulator Certification Plan, based on ANSI /ANS-3.5-1985 and EPRI criterion, which is committed to maintaining /
improving operational standards. Also, the facility has in place a system of requalification training on recent LER's and PMR's that effect safe plant operation.
- 3. Exit Meeting The following personnel were present at an exit meeting held on February 20, 1987.
Thomas R. Meadows, Chief Examiner, RV Roger Corcoran, Operations Manager, WNP-2 Rich Stickney, Technical Training Manager, WNP-2 John Wyrick, Nuclear License Training Manager, WNP-2
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