ML20125A336

From kanterella
Revision as of 06:39, 3 September 2020 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search

STP Presubmittal Meeting Exigent Accumulator LAR 2020-05-05 Presentation L-2020-LRM-0039
ML20125A336
Person / Time
Site: South Texas STP Nuclear Operating Company icon.png
Issue date: 05/04/2020
From: Dennis Galvin
NRC/NRR/DORL/LPL4
To:
Dennis Galvin - NRR/DORL 301-415-6256
References
L-2020-LRM-0039
Download: ML20125A336 (9)


Text

Pre-Submittal Meeting on Proposed Exigent LAR Regarding Accumulator Pressures for Unit 1 Cycle 23 May 5, 2020

STP Participants

  • Lance Sterling, Regulatory Affairs Manager
  • Jason Tomlinson, Plant Engineering Manager
  • Drew Richards, Licensing Supervisor
  • Safdar Hafeez, Reactor Analysis Engineer
  • Roland Dunn, Engineering General Manager
  • Fatma Yilmaz, NF&A Manager
  • Jeff Atkins, Operations Manager 2

Discussion Topics

  • Problem Description
  • Proposed License Amendment
  • Preliminary Technical Evaluation
  • Planned Submittal Schedule 3

Problem Description

  • Leakage identified on Safety Injection (SI) Train 1A following startup from recent Unit 1 refueling outage
  • Maintaining volume and pressure requires frequent RHR venting and refilling of SI Accumulator 1A
  • Challenge to safety-related components due to component cycling
  • Lowering pressure of all accumulators to less than RHR relief valve pressure will eliminate need for cycling safety-related components 4

Proposed License Amendment

  • Modify TS 3/4.5.1, Accumulators to allow Unit 1 to operate with all three Safety Injection (SI) System Accumulators at reduced pressure
  • Resolves valve leakage issue while maintaining all three SI accumulators operable and having no significant adverse impact to the RHR or Low-Head Safety Injection (LHSI) systems
  • One-time change would support deferral of repairs until the next Unit 1 refueling outage
  • Need for exigency - necessary to avoid a reactor shutdown without a commensurate increase in safety 5

Preliminary Technical Evaluation

  • Large-Break LOCA Peak Clad Temperature (PCT) impact
  • Containment Analysis Peak Pressure impact
  • Large Break LOCA limiting
  • Containment Analysis Peak Temperature impact
  • Containment Equipment Qualification Peak Pressure and Temperature
  • Containment subcompartment analysis
  • Leak-Before-Break (LBB) methodology
  • Post-LOCA hot leg recirculation switchover time
  • Plan to evaluate small break LOCA, post-LOCA long-term cooling and subcriticality, Main Steam Line Break Hot Zero Power DNBR analysis 6

Planned Submittal Schedule

  • STP will receive results of analysis from vendor on May 11, 2020
  • Planned amendment request submittal on May 14, 2020
  • Approval of the amendment requested by May 28, 2020
  • Amendment will be implemented prior to the expiration of the Risk-Informed Completion Time on May 29, 2020 7

Questions?

8