ML20129E933

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Insp Rept 50-341/96-06 on 960629-0802.Violations Noted. Major Areas Inspected:Operations,Engineering,Maint & Plant Support
ML20129E933
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 09/26/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20129E922 List:
References
50-341-96-06, 50-341-96-6, NUDOCS 9610040005
Download: ML20129E933 (35)


See also: IR 05000341/1996006

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U.S. NUCLEAR REGULATORY COMISSION ,

REGION 3

Docket No: 50-341 l

License No:

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NPF-43

Report No: 50-341/96006

Licensee: Detroit Edison Company (Deco) .

Facility: Enrico Fermi, Unit 2

Location: 6400 N. Dixie Hwy.

Newport, MI 48166

Dates: June 29 - August 2, 1996

Inspectors: A. Vegel, Senior Resident Inspector

C. O'Keefe, Resident Inspector  :

P. Lougheed, Lead Engineering Inspector, RIII

A. Dunlop, Reactor Inspector, RIII

J. Neisler, Reactor Inspector, RIII

R. Jickling, EP Analyst, Region III

A. McQueen, EP Analyst, Region IV

L. Cohen, EP Specialist, NRR

J. Lusher, EP Specialist, Region I

R. Glinski, RP Specialist, Region III

R. Doornbos, Operator Examiner, Region III

Approved by: Mike Jordan, Chief, Branch 7

Division of Reactor Projects

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9610040005 960926

PDR

G ADOCK 05000341

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EXECUTIVE SUMMARY

Enrico Fermi, Unit 2

NRC Inspection Report 50-341/96006

This integrated inspection

ing, maintenance, included aspects of licensee operations, engineer-

and plant support.

resident inspection; in addition, it includes the results of an evaluatedThe report

the service water systems, and inspections by regional special .

Operations

e

during an Emergency Diesel Generator 12 surveillance.A near mis

to

(01.2)detail and the absence of a pre-job brief contributed to the event. Lack of attention

e

Inspectors identified an example of an inadequate system operating

procedure for Residual Heat Removal Service Water in that all system

valves were not included in the system lineup verification. Inadequate

procedures continued to be an area of concern.

e (03.1 and E7.1.1)

Control room operators and a chemistry technician were unaware of the

draw a sample for the emergency exercise. abnormal Post Accident Sam

When flow could not be

shut for almost 2 months. established, operators discovered that the flow path had

(04.1)

e

and good coordination and teamwork in the simulator dur

session and the Fermi Emergency Preparedness Exercise. (05.1)

Maintenance

o

Preparation

of for outages,

safety system and execution

declined. of work, particularly during performance

between organizations. assignment of outage managers, parts availabilit

(M1.3)

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has had a positive impact on the corrective maintenance b

other maintenance groups adherence to the maintenance schedule.

o (M1.2)

A series of general service water pump problems resulted in having one

pump unavailable or in reduced status, during most of the inspection

period.

Lack of coordination within maintenance and among supporting

groups

reducedcontributed

capability. to the extended period this important system was at a

(M2.2 and M2.3)

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EXECUTIVE SUMMARY

Enrico Fermi, Unit 2

NRC Inspection Report 50-341/96006

This integrated inspection included aspects of licensee operations, engineer-

ing, maintenance, and plant support. The report covers a 5-week period of

resident inspection; in addition, it includes the results of an evaluated

emergency preparedness exercise, followup of the licensee's self-assessment of

the service water systems, and inspections by regional specialist inspectors.

Ooerations

e A near miss occurred on Technical Specification action statement entry

during an Emergency Diesel Generator 12 surveillance. Lack of attention

to detail and the absence of a pre-job brief contributed to the event.

(01.2)

e Inspectors identified an example of an inadequate system operating

procedure for Residual Heat Removal Service Water in that all system

valves were not included in the system lineup verification. Inadequate

procedures continued to be an area cf concern. (03.1 and E7.1.1)

e Control room operators and a chemistry technician were unaware of the

abnormal Post Accident Sampling System lineup when they attempted to

draw a sample for the emergency exercise. When flow could not be

established, operators discovered that the flow path had been tagged

shut for almost 2 months. (04.1)

P

e Inspectors observed proper use of procedures and emergency declarations,

and good coordination and teamwork in the simulator during a training

session and the Fermi Emergency Preparedness Exercise. (05.1)

Maintenance

e Preparation for and execution of work, particularly during performance

of safety system outages, declined. Problems were identified in timely

assignment of outage managers, parts availability, and coordination

between organizations. (M1.3)

e The recent establishment of the Fermi Integrated Resource Support Team

has had a positive impact on the corrective maintenance backlog and

other maintenance groups adherence to the maintenance schedule. (M1.2)

e A series of general service water pump problems resulted in having one

pump unavailable or in reduced status, during most of the inspection

period. Lack of coordination within maintenance and among supporting

groups contributed to the extended pericd this important system was at a

reduced capability. (M2.2 and M2.3)

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valve testing resulted in a delay in returning HPCI back to service.-

Two bolts were not installed on the valve actuator cover housing. This

required the valve actuator to be disassembled to check for damage and -

to restore the actuator to a normal operation. No damage was detected.

'(M4.2)  !

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Enaineerina ,

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e A drain line for the Division 1 safety related_ service water common  :

return line to the mechanical draft cooling towers was found by the  !

inspectors to be partially plugged for the second time in four monta;. 1

Corrective actions for Violation 341/96004-03 failed to identify this  ;

repeat occurrence. (E2.1) j

e The root cause investigation of the fire in the Reactor Water Cleanup

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Filter Demineralizer control panel was timely and thorough, and j

supported a prompt repair and return to service without adversely j

impacting reactor water chemistry. (E2.2) l

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j e NRC followup inspection of the licensee-performed Service Water System

l Operational Performance Inspection found some creas which were not

l covered by the licensee team. However, the NRC identified no additional

l concerns and concluded that the licensee self assessment was adequate.  ;

l~ (E7.1)  ;

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L Plant Suncort  ;

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e Instrumentation and Controls workers performed surveillance' activities

l on the scram discharge volume instruments under the wrong Radiation Work

Permit, and a radiation protection supervisor missed an opportunity to  ;

catch the error. (RI.1) i

e Two instances were identified where personnel new to the site violated  !

site radiological controls. While the consequences of the events were l

minor, the adequacy of radiation worker trair.ing was of concern, _!

especially in light of the upcoming refueling outage. (R5.1) o

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e The spent fuel pool cleanout project was performed conservatively.

Planning and coordination for the project was meticulous. (R2.1) l

e Overall performance during the 1996 emergency preparedness exercise was

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very good and as indica +ed by the following observations. Emergency  ;

l classifications and notifications to offsite authorities were made in a -

timely manner. Technical Support Center staff rapidly evaluated plant

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conditions and made appropriate emergency classifications. Command and -

control and offsite communications were very good in the Emergency  ;

Operations Facility. (P4.1) l

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Report Details

So-ary of Plant Status

Unit 2 operated between 85 and 89 percent power throughout this inspection

period, except for power reductions on June 28-29 and August 2, for control

rod pattern adjustments.

I. Operations

01 Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. In general, the conduct of opera-

tions was professional and safety-conscious; specific events and

noteworthy observations are detailed in.the sections below.

Operations observed in the control room and out in the plant were

performed well. The focus on procedure adherence has resulted in the

identification of a number of corrections. However, the inspectors

noted that the majority of the problems identified during evolutions

monitored by the inspectors were found during performance, rather than

during the pre-job review.

The inspectors noted that on July 5, the control room log entry for

Surveillance 44.020.232, "NS4 Reactor Coolant Injection System (RCIC)

Steam Line Flow Division 2 Functional Test," was incomplete in that only

one of the three Technical Specification (TS) action statements

applicable was listed. This gave the appearance that RCIC system was

not recognized as inoperable during that surveillance until it was found

that the Nuclear Shift Supervisor (NSS) log entry was complete regarding

the TS action statements entered. Inattention to detail was evident in

this instance, and was of concern because the control room practice was

that frequently the NSS log is updated from the control room log ,

entries. l

On July 18, inspectors observed the pre-job brief and performance of

Surveillance 24.202.01, "High Pressure Coolant Injection (HPCI) Pump

Time Response and Operability at 1025 PSI." The brief was detailed and '

thorough, including expected radiological conditions and As Low As

Reasonably Achievable (ALARA) consid0 rations. Operators were assigned

in pairs to provide peer checking, which contributed to a fairly smooth

surveillance run. During the brief, a licensed operator alertly

questioned whether a change in plan to calibrate an instrument if

necessary during the surveillance would invalidate the surveillance

results. This question was resolved prior to beginning. Several minor

procedure problems were identified during the surveillance which were

appropriately resolved by operating shift supervision.

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01.2 Near-miss on Technical Soecification Entry for Fearaency Diesel

Generator (EDG) 12

a. Insoection Scone (61726) l

The inspectors observed the shift turnover brief for the day shift on

July 11. The

cycling drywe?.-torus pre-job brief and

vacuum performance

breakers of thein surveillance

was observed for

the control room;

during this time the below events transpired. Follou p discussions with

the operators involved and the EDG system engineer were conducted

following initial problem identification. The condition of equipment

and course of action were discussed with the system engineer and the

NSS.

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b. Observations and Findinas

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On July 11, operators and maintenance personnel prepared to perform a

Fast Start of EDG 12, Surveillance Procedure 24.307.15. The shift had

planned to perform this surveillance following the cycling of drywell-

torus vacuum breakers. The latter surveillance was in progress while

personnel in the field made preparations for the EDG surveillance. The

i vacuum breaker surveillance required the attention of the Nuclear

l Assistant Shift Supervisor (NASS). When he began to review the EDG

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surveillance procedure he identified that Precaution 2.8 indicated that

Swing Bus 72CF automatic throw-over would be disabled during the

surveillance, which was required to be operable per TS 3.8.3.1.a.3. At

about the same time, operators in the field radioed the control room

that the diesel was being pre-lubricated, allowed by TS, and requested

an announcement for starting the EDG.

The NASS ordered the operators in the field not to start the EDG and

discussed the situation with the NSS and the system engineer. The

action statement for TS 3.8.3.1 wa entered and the surveillance was

l performed without further inddent.

The inspectors determined that no pre-evolution briefing was conducted. I

Operators stated that EDG surveillance runs were performed every week, i

and no briefing was necessary.

The operators routinely reviewed the impact statements attached to the

surveillance procedures to determine TS actions required. In this case,

the impact statement did not include TS 3.8.3.1.a.3. l

c. Conclusions

The inspectors considered this event to be a near-miss avoidance of

I recognizing an entry into a TS requirement. Considering the

surveillance to be routine, operators did not perform a briefing or

review of the procedure sufficiently in advance to identify all the

required actions. Additionally, the operating shift deviated from the

plan to perform the two surveillances sequentially; operators making

preparations in the field progressed into the time-critical starting

sequence tefore the containment vacuum breaker surveillance was

complete.

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02 Operational Status of Facilities and Equipment

02.1 Enaineered Safety Feature (ESF) System Walkdowns (71707) r

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The inspectors used Inspection Procedure 71707 to walk down accessible

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portions of the following ESF systems:

. EDGs 11, 12, 13, and 14

. Standby Liquid Control System j

. Residual Heat Removal (RHR) System

. RHR Service Water (RHRSW) System

. Core Spray System ,

. HPCI System  ;

. Primary Containment Nitrogen Inerting System  ;

Equipment operability and material condition were acceptable in all

cases. Several minor discrepancies were brought to the licensee's ,

attention and were corrected.' The inspectors identified no substantive  ;

concerns as a result of these walkdowns.

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Housekeeping in the HPCI room following the system outage was poor.

Several days after the outage, the inspectors identified outage related

debris in the HPCi room, a ; mall valve packing leak in E41-F031, and two  :

valves in series with seat leakage (E41-F055 and E41-F056).

Additionally, a hose directing oil leakage to a container did not reach

the container, and a spare step-off pad was loosely taped to the back of

the safety related HPCI room cool' r just above the cooler suction, such

that it could fall and bloch m i cs to the cooler. Once notified of -

the discrepancies, the liceria u prompt corrective action. The ,

inspectors concluded that furt..er attention to post maintenance i

housekeeping was required.

03 Operations Procedures and Documentation ,

03.1 Procedural Inadeauacies (TI 2515/118 Item 03.02.el)  !

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a. Inspection Scope (40501)

NRC temporary instruction (TI) 2515/118 ites 03.02.el required that the {

reviewers walk through the system operating procedures and the system

piping and instrument diagrams with engineering and operations staff.

As this item was not performed during the service water, self-

assessment, the inspectors performed the walk through.

b. Observations and Findinas

The inspectors, together with an engineer and operations support person,

reviewed System Operating Procedure (SOP) 23.208 "RHR Complex Service

Water System" and Functional Operating Sketch 6M721-5706-3 "RHR Service

Water Makeup, Decant and Overflow Systems. The valve lineups and

procedure steps were traced out on the drawing and the rationale for the

step order was discussed. One discrepancy was identified: vent valve

E1100-F258, although shown on the drawing, was not identified in the

procedure. The operations staff initiated a DER, walked down the system

and initiated a temporary procedure change to incorporate that valve,

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and two others identified during the walkdown, into the procedure.

Based on the walkdown results, the operations staff also requested l

labels for several components. i

10 CFR Part 50, Appendix B, Criterion V, requires, in part, that

activities affecting quality be prescribed by documented instructions,

procedures or drawings, of a type appropriate to the circumstances.

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Failure to include all valves in the system lineup verification j

procedure in 50P 23.208 resulted in the procedure being inadequate and

was considered a violation of Criterion V (50-341-96-06-01).

c. Conclusions

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The inspectors identified that 50P 23.208 was inadequate in that it did

not ensure system configuration was maintained by including all system

valves in the system lineup verification. Another example of procedural

inadequacies was identified by plant operators, as discussed in Section

01.2. In this case, the inspectors were concerned that the problem was

, found during performance of the procedure rather during a pre-

performance review, where the problem could be more easily remedied.

. As previously documented in Inspection Report 96002, 96004, and 96005, a

number of procedure inadequacies have been identified. The inspectors

l were concerned that corrective actions to improve procedure quality have

yet to be completely effective.

04 Operator Knowledge and Performance

04.1 Post Accident Samolina System (PASS) Samole Attemoted with System

Isolated and Taaaed

On July 16 during the biennial emergency exercise, chemistry personnel

attempted to obtain a sample from the Post Accident Sampling System.

When proper flow could not be established, control room operators

realized that the sample flow path was isolated by tagged and locked

shut manual valve P34-F004. The manual valve was closed because of

problems with operating solenoid-operated valve P34-F401B " Division 1

Pressurized Reactor Coolant Sample Isolation Valve" in the same line.

This condition was identified by Limiting Condition for Operation 96-

0322, Safety Tagging Record C96-0884, and Control Room Instrument System

dot 111, all dated May 25, 1996.

Despite the available indications and paperwork, neither the chemistry

technician nor the control room operators were aware of the status of

the PASS system. Deviation Event Report (DER) 96-0809 documented this

event. For additional discussion of PASS system operation, see section

P4.1. The occurrence of this event indicated a weakness in control room

operator and chemistry technician cognizance of the status of plant

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equipment.

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04.2 Non-Licensed Doerator Knowledae of Service Water Reauirements (TI

2515/118 Ites 03.02.e)

a. Insoection Scone (40501)

TI 2515/118 ites 03.02.e also required verification that service water

system components and equipment were accessible for normal and emergency

operation, including determination that any special equipment required

to perform the procedures was available and in good working order. It

further required verification of the operators' knowledge of equipment

location and operation.

b. Observations and Findinas

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The inspectors accompanied a nuclear power plant operator (nonlicensed)

on a tour of the general service water (GSW), residual heat removal

service water (RHRSW), diesel generator service water (DGSW) and

emergency equipment service water (EESW) systems. During the tour, the

operator explained what equipmot would be locally operated and under

what conditions. The operator described how he would obtain the

necessary equipment (ie ladders) to perform the procedures. The

operator independently confirmed information discussed in the training

lesson plans and was knowledgeable of a recent emergency equipment

cooling water system modification.

c. Conclusions

The nonlicensed operator was very knowledgeable of service water system

requirements and equipment locations. Besides knowing where equipment

was located, he understood why it needed to be operated and the purpose

of the equipment. No problems were identified during this walkdown.

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05 Operator Training and Qualification

05.1 Simulator Observations l

The inspectors observed simulator training sessions on July 11 and July

16 during the Fermi Emergency Preparedness Exercise.

One scenario run for training was the loss of one reactor recirculation  !

pump. This was intended as refresher training due to having one of the

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reactor recirculation motor generator lube oil pumps out of service for '

repairs. The inspectors considered this training to be timely and

pertinent to current operating conditions of the plant.

The balance of simulator scenarios observed were plant casualty i

sessions. Use of procedures and emergency declarations were proper, and

communication and teamwork among operators was excellent. Crews ,

observed did a good job discussing priorities, options, and

recommendations. For additional discussion of operator performance

during the exercise, see section P4.1.  !

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05.2 Ooerator Trainino on Service Water (TI 2515/118 Item 03.02.c)

a. Inspection Scone (40501)

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TI 2515/118 item 03.02.c required that the reviewers evaluate operator

training for the service water systems, focusing on the technical

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completeness and accuracy of the training manual and lesson plans. It

further required verification that the lesson plans reflect system

modifications and that the licensed operators have been trained on these j

modifications. I

b. Observations and Findinas

The inspectors reviewed the lesson plans for both licensed and l

nonlicensed operators for initial and continuing training. The lesson  !

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plans were determined to be complete and accurate. The inspectors l

reviewed the lesson plan for a recent EECW modification and discussed  ;

the modification with the training instructors. The lesson plan  !

, appeared to adequately address the modification. '

The inspectors also observed several simulator scenarios where the

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operators had to respond to various service water related transients )

such as failure of a general service water pump, start of the EECW and {

EESW systems and start of the DGSW pumps. The operators responded to  !

the various service water alarms appropriately. '

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c. Conclusions

The technical adequacy of the operator training on service water

appeared satisfactory. Lesson plans adequately covered operation of the i

systems under normal and abnormal conditions and were updated to address

i system modifications and that operators were appropriately trained.

The effectiveness of the training was supported by a nonlicensed

operator's understanding of the service water systems and a recent

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modification, as discussed in section 04.2.

l 07 Quality Assurance in Operations Activities

07.1 Followuo Inspection for the Service Water System Self-Assessment

a. Insoection Scope (40501)

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From February 28 through March 29, 1996, the licensee conducted a self-

assessment of the service water system in accordance with TI 2515/118

" Service Water System Operational Performance Inspection (SWSOPI)" and

inspection procedure 40501 " Licensee Self-Assessments Related to Team

Inspections." In accordance with the requirements of 40501, the

inspectors performed a followup inspection on the self-assessment in

order to evaluate (1) whether. the inspection requirements of TI 2515/118

were adequately met by the assessment team and (2) the effectiveness of

the licensee's responses to the issues raised by the assessment team.

The inspectors reviewed a draft copy of the self-assessment report and

determined that Items 03.01.e, 03.02.c, 03.02.e, 03.03.g and 03.03.h of

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the TI were either not performed or not documented. Therefore, the

inspectors performed an independent inspection of those requirements.

As documented in inspection report 96003, the inspectors had concerns

with the responsiveness of the licensee to some of the assessment team's

issues during performance of the self-assessment. For that reason, the

inspectors independently completed Item 03.04.e of TI 2515/118 to assess

the effectiveness of the assessment team.

Finally, the inspectors reviewed the licensee's responses to all the

issues raised by the assessment team to ensure that the concerns were

being adequately addressed and that no operability concerns existed,

b. Observations and Findinas

Review of the above TI inspection requirements is documented in the

following sections: TI 03.01.e - Section El.1, TI 03.02.c - Section

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. 04.2 TI 03.02.e - Sections 03.1 and 05.2, TI 03.03g - Section M4.4,

l TI 03.03h - Section M5.1, and TI 03.04.e - Section El.2. One violation

l was identified, as discussed in Section 03.1.

Review of the responses to assessment team issues is documented as

follows: maintenance and surveillance and testing - Sections M7.3 &

M7.4, engineering - Section E7.1, and operations - Section 07.2. One

inspection followup issue was identified.

The inspectors reviewed the self-assessment final report, issued

July 19, 1996, 11 weeks after the assessment team exit. While the final

report was much improved over the draft version, the inspectors noted

that there were still some problems. For example, item 03.01.e, on page

C.3, stated that pump runout was addressed by issues 5 and 41. However,

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when the inspectors reviewed these issues, they determined the subject

to be heat exchanger fouling rather than pump runout.

c. Conclusions

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Overall, the inspectors concluded that the self-assessment was

adequately performed. The assessment team covered the majority of the

areas contained in the TI, with only a few items not documented. These

areas were independently reviewed by the inspectors and only one

procedural inadequacy issue was identified. After an initial delay, the

licensee took adequate action to resolve the issues identified by the

assessment team. The inspectors identified one minor concern regarding

stroke time testing, as described in section M7.4. The self-assessment

final report was minimally satisfactory due to the length of time to

issue the report, inspector identification of missed assessment areas, l

and overall weak content of the report. However, the requirements of TI '

2515/118 were met, and the TI is closed.

07.2 Review of Service Water System Self-Assessment Issues

The inspectors reviewed the responses to the four self-assessment issues

! that were within the operations area. All four items were resolved by  ;

! procedural clarifications. The inspectors noted the documented response

to issue 31, on RHR reservoir level, did not appear complete 1,n that the

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alarm response procedure did not clearly describe how reservoir level  !

was to be verified upon failure of normal instrumentation. Per the  !

operations response team member, the intent was to have a power plant

operator measure the distance from the top of the grating to the water i

level using a standard tape measure. Following the discussion, the

liceasee revised the appropriate alarm response procedure to reflect the

above clarification. With this clarification, all of the operational

issues appeared to be resolved in a reasonable manner. The inspectors i

had no concerns with the licensee's responses to the assessment team j

issues in the operations area.

II. Maintenance

M1 Conduct of Maintenance

M1.1 General Comments

a. Inspection Scone (62703)

The inspectors observed all or portions of the following work

activities:

. HPCI Valve E4150-F004 Work

. HPCI Operability Surveillance

. Primary Containment Integrity Verification Surveillance

. Fire Wrap Installation in Control Air Compressor Room

. Drywell - Torus Vacuum Breaker Operability Surveillance

. Emergency Diesel Generator (EDG) 12 Fast Start

b. Observations and Findinos

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As discussed on section 02.1 above, housekeeping and post-maintenance

cleanup were observed to be poor following the HPCI system outage.

L Additionally, test batteries and a cart were left unattended and

l unrestrained in a safety battery room following maintenance (see Section

M4.3).  !

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M1.2 First Team Imolementation (62703)  !

Inspectors reviewed licensee documents, observed maintenance activities-

and interviewed licensee personnel to assess the effectiveness of

Fermi's Integrated Resource Support Team (F.I.R.S. Team) implementation.

The licensee developed the F.I.R.S. Team to address minor maintenance  !

issues. The goals of the team were to perform minor corrective i

maintenance tasks to reduce the maintenance backlog while reducing the l

burden on other maintenance groups. In addition, since the F.I.R.S. Team

was performing emergent corrective maintenance tasks, other maintenance

l organizations were able to focus on maintaining the maintenance

schedule. Since implementation of the F.I.R.S. Team in early June,1996,

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the corrective maintenance backlog had been reduced by approximately 100

] tasks. Also, approximately 38 percent of all work requests written in

July were addressed by the team. The inspectors concluded that the

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F.I.R.S. Team has had a positive impact on the effectiveness of the

licensee's maintenance program.

M1.3 Conclusions on Conduct of Maintenance

Performance in-the area of preparation and execution of planned

maintenance activities, particularly safety system outages, continued to

decline during this inspection period. Poor coordination and a lack of

thorough planning contributed to the continued occurrence of problems

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during the execution of planned maintenance activities.

Of particular concern was an apparent difficulty in identifying and

assigning system outage managers with sufficient lead time to set the

outage scope and coordinate preparations. For example, the RHR system

outage manager was assigned less than a week before the start of the

outage, and the planning meeting was scheduled less than four days

before the outage start date. Even though the RHR system outage was

considered by the licensee to be of greatest risk significance of all

planned system outages in 1996, the adequacy of preparations did not

appear consistent with the risk significance of the outage Most of

the system outages during this inspection period were assigned in a

similar fashion. The consequence of this late planning will be

evaluated in the next report after the completion on the outage.

Continued problems in restoring Number 2 General Service Water (GSW)

Pump to reliable service highlighted problems with work planning and

coordination, parts availability, and vendor oversight as discussed in

Section M2.1 below.

Following the system outage problems in June 1996, the licensee

instituted a new policy to enhance coordination between organizations in i

support of system outages and' ensure preparation in adequate detail. '

Changes included holding briefings attended by all appropriate

organizations prior to system outages to discuss status of preparations,

parts, tagouts, and to resolve any problems. The scope of the outage

was set at this meeting, about a week in advance of the outap. A post-

outage critique was also instituted to document problems and help

prepare for future outages. However, outage scope changes continued to

be made just prior to or during system outages.

An overall effort to improve how work was scheduled and performed was

underway, headed by the Superintendents of Work Control, Operations and

Maintenance. Some changes have been made in the process and increased  !

management attention was evident. However, the inspectors were )

concerned by the work performance problems observed this report period. j

M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 General Service Water Pumo Maintenance Problems

l

a. Inspection Scope (92903) i

The inspectors followed the progress of GSW pump maintenance

difficulties. Maintenance and engineering personnel were interviewed to

, .

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.

determine the technical and coordination difficulties and failed l

investigation results. '

b. Observations and Findinas

On June 24, the Number 2 GSW pump motor grounded and failed. It was

replaced with a new motor from a different vendor on July 5. Difficulty

in mounting and aligning the motor to the pump was encountered due to

differences in the mating surface geometry. Following return to

service, GSW Pump 2 experienced packing binding. The licensee

determined that the packing was no longer evenly distributed, which

maintenance corrected twice.

On July 14, GSW Pump Number 2 pump shaft sheared just below the motor-

pump shaft coupling. The licensee determined that the shaft failed due

to high cycle fatigue caused by shaft misalignment after about six hours

of run time. This was believed by the licensee to have been caused by

the new motor having the wrong mating surface geometry. The maintenance

l engineer believed that the initial motor to pump alignment was difficuit

l and a misalignment developed because the motor seat did not have the

proper bevel. The fact that the motor mount was different than previous

motors was not recognized until the motor was first installed.

Maintenance replaced the pump and motor using the original motor which

failed earlier. The motor had been rewound by a vendor not normally

used by the licensee. Following installation, the motor-pump

combination exhibited vibration above the acceptable range,

necessitating the use of the pump only in emergencies. Maintenance

records indicated that the licensee accepted the rewound motor with

vibration levels at the high end of the acceptable range; when coupled

l to the pump, vibration was above the acceptable range. Vendor testing

l of the motor was not observed by the licensee, as was the usual

l practice.

On August 6 the motor was replaced with the motor which previously broke i

the pump shaft. The mating surfaces of the motor had been machined to

produce a better fit and improve the ease of alignment, and the lower l

bearing had been replaced and lubricated by a vendor. During the motor

l installation, maintenance personnel discovered that two dissimilar types

of grease had been used to lubricate the lower motor bearing (DER 96-

1 0905), and that required parts were not available on site for making the

l

electrical connections. Installation was delayed several days due to

coordination problems within maintenance, and several hours due to

problems among operations, maintenance, and inservice inspection

engineers in coordinating tagging and taking vibration measurements.

l During most of the period of June 24 through August 6, Number 2 GSW Pump

l was considered in a restricted use condition. In the past hot weather

i conditions during this season required the running of all five GSW

pumps. However, conditions during this period were mild, and all five

j GSW pumps were not required.

The GSW system was ranked the eighth most important system by the

i licensee's Probablistic Risk Assessment (PRA). During this same period,

( GSW Pumps 4 and 5 also required corrective maintenance.

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c. Conclusions

! This sequence of events represented poor work coordination and a lack of

planning and attention to detail. Inadequate oversight of vendors

, resulted in accepting motors with the wrong lubricant and with high

j vibration. Poor oversight and control of vendors was of concern with

the upcoming refueling outage and the large numbers of contract

personnel planned to be brought onsite,

i

j The inspectors considered that the coordination and planning involved in.

l this series of repairs fell short of the importance of this system from

! a PRA and Maintenance. Rule perspective. During this period of five

j weeks,. in a season which historically required all available GSW flow,

i maximum capability was not effectively maintained. Had such flow been

j required, operators would have been forced to choose between reducing

j power or running a degraded pump. I

f M2.3 GSW Pi=a Motor Work Performed by Vendor Without Authorization

} I

In an attempt to dete:mine the source of vibration in Number 2 GSW Pump,

'

l

! a representative of the vendor that rewound the motor visited the site

l on July 31. In company with licensee engineers, he went to the motor

'

expecting to find test equip;aent installed in place of the upper motor l

! bearing cover, as was arranged. When it was not installed, he asked if  ;

l the motor was tagged out, was told it was, then proceeded to remove the  !

j' cover and install the test equipment without authorization. l

l When a maintenance engineer returned from checking the status of work

i package authorization (it was not yet authorized), he found work in

j progress, he ordered work stopped and informed the control room. j

.

[ An investigation by the NSS determined that the tagout was hung but not i

! verified at the time work was performed, and the engineers involved were

i not knowledgeable in contractor control procedures. The vendor was

l directed to leave the sits, the tagout was completed, and work was

performed by licensee maintenance personnel. DER 96-0813 was written to 4

! document the event and track corrective actions. The engineers involved i

were trained on vendor control procedures and tagout requirements, and

l management expectations in this regard were stressed. i

! In response to this event, the licensee was in the process of conducting

i training on control of vendors for engineering and maintenance personnel

l at the conclusion of this inspection period.

4

Failure to follow procedures for work control and safety tagging was

l considered a violation. However, this will not be cited as the

requirements of the Enforcement Policy,Section VII were met (NCV 50-

, 341-96-06-02).

i

! M4 Maintenance Staff Knowledge and Performance

!

M4.1 HPCI Suction Path Swanoed Inadvertent 1v Durina Unrelated Maintenance

On July 19, Instrumentation and Control technicians were preparing to

i calibrate the Condensate Storage Tank (CST) level instrument. While

I

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setting up'at the CST instrument cabinet, the telephone jack was found

l to be inoperable. Radios were then used to establish communications

with the control room. At about the same time, the control room  ;

identified that the HPCI suctioni path swapped from the CST to the I

suppression pool..

1

Investigation revealed that CST water level was steady'at 22.5 feet

- during the event, which was.well above the 27 inch low water level

, swapover setpoint.

l

l Work was stopped to determine the cause of the event. The suction path l

l

was returned to normal when CST water level was verified. DER 96-0804 l

was written to document event occurrence and track corrective actions.  !

!

The NRC Operations Center was notified in accordance with 50.72 based on

l

the actuation of an ESF system.

!

A Licensee Event Report (LER) investigation was conducted for this '

event. The team concluded that keying of the maintenance worker's radio

approximately six feet away from the CST water level transmitter caused

a false low 13 vel signal four. separate times in a brief period. This

, finding was consistent with testing performed by the licensee following

L a similar event documented by DER 93-0581. Corrective actions for DER

93-0581 included posting the areas around transmitters determined to be

potentially sensitive to radio transmissions with warning signs. This

action did not include the CST level transmitter cabinet.  ;

The inspectors will follow up on this event and assess licensee

corrective actions under LER 341/96-010.

M4.2 HPCI Valve Work Error Delays System Restoration

a. Inspection Scope (92503)

The inspectors observed disassembly and inspection of the actuator for

E4150-F004, " Booster Pump CST Suction Isolation Valve ," following

actuator problems. The conditions of work leading to the problems were

discussed with maintenance personnel.

b. Observations and Findinas

On July 17, valve thrust testing on E4150-F004 was performed during a

,

planned HPCI system outage. Test equipment was removod from the

actuator, but raintenance personnel did not reinstail two bolts on the

cover housing for the actuator spring pack. When the valve was

subsequently closed, the spring pack pushed the cover off at an angle

and cocked the declutch lever. This required removing the actuator

motor and partial actuator disassembly to inspect for damage and restore

,

the actuator to normal.

The inspectors observed actuator disassembly and inspection. No damage

was identified, and subsequent testing showed no problems. The

inspectors discussed the event with maintenance personnel, and

determined that no detailed procedure was used for the thrust testing or

test equipment installation and removal. This was because of the many

.

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valve configurations in the plant and because the work was considered  :

. within the skill of the craft. '

i c. Conclusions

The inspectors consid eed that inattention to detail by sa'

'

l ince

, workers was the cause of the event, and that this work was i the

i skill of the craft. While no damage was sustained as a re the

j error, system restoration was delayed about 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

M4.3 Control of Eauinment Durina Battery Charaer Maintenance

J

'

a. Insoection Scone (92903)

On August 1, while conducting a walkdown of the Division 2 safety

related battery, inspectors identified that a metal cart and temporary

i

test batteries were left unattended and unsecured in the battery room.

Inspectors reviewed licensee documents including:

.

! . Work Request 000Z965158, Battery Charger 2B-1 Tripping on High

1 Voltage;

j . Operations Conduct Manual M0P 11, Revision 2, Fire Protection.

.

l Inspectors also discussed the' event with licensee maintenance and

operations personnel.

'

l

b. Observations and Findinas

1

'

On August 1, during a routine inspection of the Division 2 safety

related battery in the Auxiliary Building, inspectors noted that

temporary test batteries and a metal cart were being stored in the

"

Division 2 Battery Room. The inspectors were concerned that the

l temporary batteries and the cart were not properly secured to prevent

i them from damaging safety related batteries in case of a seismic event.

'

Control room operators were notified and the metal cart was removed.

The temporary batteries and the metal cart were staged in support of

corrective maintenance activities on the 28-1 battery charger. Work was

. commenced on August 1, and was completed on August 3. However, on

i August 5, inspectors noted that the temporary batteries were still

, stored in the Division 2 Battery Room. In response to the inspectors'

concerns, the temporary batteries were removed later the same day.

Operations Conduct Manual Chapter ll, " Fire Protection," required, in <

j part, that a temporary plant space request (TPSR) be initiated when

i storing or staging equipment in the Auxiliary Building unless certain

4 requirements were met. Some of the requirements included:

. staging area is roped off and properly identified;

. all materials are properly secured (seismic) in the Reactor,

Auxiliary and RHR Buildings.

l

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1 The inspectors identified that the above requirements were not met and a j

! TPSR was not utilized when the temporary test batteries were staged in

.

the Division 2 Battery Room from August I to 3. In addition,

maintenance personnel demonstrated poor housekeeping practices and
insensitivity to the potential for the metal cart to impact the

1 functionality of Division 2 battery when they left the metal cart

unrestrained on August 1.

Licensee corrective actions included performing a seismic evaluation of

i storing temporary batteries in the Division 2 battery which concluded

i that the impact was. insignificant from a seismic standpoint. In

i addition, the electrical maintenance supervisor initiated. required

reading on restraint of loose items for the electrical maintenance

i group.

! c. Conclusions

.

The inspectors were concerned that the electrical maintenance personnel

were not following site requirements for the restraint of temporarily

staged equipment in safety related rooms. Specifically, until prompted

. by the inspectors, the licensee staff did not recognize that the sei'saic

j restraining and staging requirements were not met.

1

i Failure to initiate a temporary plant space request on August 1, for

j staging of the temporary test. batteries in the Division 2 Battery Room,

as required by Operations Conduct Manual was a violation of 10 CFR Part

50, Appendix'B, Criteria V, " Instructions, Procedures, and Drawings,"

which states, in part, that activities affecting quality be accomplished

in accordance with prescribed procedures (50-341-96-06-03).

M4.4 Maintenance Personnel Knowledae of Service Water System Reautrements

(TI 2515/118 Ites 03.03.a)

TI 2515/118 item 03.02.c required that the inspectors conduct detailed

interviews with maintenance personnel to determine their technical

knowledge of how components were maintained, such as the setting of

limit switches, the alignment of pump couplings, cleaning and replacing

filters, and the maintenance of circuit breakers. The inspectors

conducted interviews; with four electrical and four mechanical

maintenance workers.

Based on the interviews, the maintenance workers were technically I

knowledgeable within their areas. All of the workers were experienced,

with an average of 8 years within their respective maintenance  !

departments. The workers were able to adequately describe the methods l

used to set valve actuator limit switches and align pumps, for example. .

The technical detail of maintenance procedures appeared adequate for the  !

craft skill. All the workers'were aware of the actions required by the

licensee's program if a procedure was unclear or incorrect.

.

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M5 Maintenance Staff Training and Qualification  !

!

M5.1 Maintenance Trainino Pertainina to the Service Water System (TI 2515/118

Ites 03.03.h) i

TI 2515/118 ites 03.03.h required that the inspectors determine if

maintenance personnel received adequate training pertaining to the

service water system and if the degree of training provided is

consistent with the amount of technical detail in the procedures. 1

During the interviews with maintenance workers, the inspectors

questioned them about the amount of training received. The licensee ,

normally only provided maintenance workers with a brief system overview 1

during the initial "new worker" training. One electrician, who was

recently traresferred to the Fermi site, noted that the system training

covered a lot of systems in a very short period of time, such that he

would not really feel comfortable describing the systems. However, all

of the workers considered that the training they received for their jobs

was extensive and thorough. The workers stated that they received

frequent refresher training, especially in t. heir " specialty" area.

Discussions with the mechanical workers revealed that they were well

aware of microbiological 1y induced corrosion and piping locations and

system conditions that contributed to it.

The inspectors also reviewed sample lesson plans and discussed the j

continuing training program with a training instructor. The Fermi 1

maintenance training appeared to provide a good mixture of classroom l

training with hands-on applications. The instructor noted that there '

was a strong management emphasis on continuing maintenance training.

The inspectors concluded that the maintenance workers received adequate

training to perform maintenance on the service water systems.

M7 Quality Assurance in Saintenance Activities

M7.1 Licensee Self-Assessment of Safety System Outaaes

a. Inspection Scone (40500)

As discussed in Inspection Report 96005, system outages in June 1996 for

the control center heating ventilation and air conditioning (CCHVAC) and

diesel fire pump (DFP) systems encountered difficulties. At the

conclusion of that inspection period, licensee self assessments of these

outages were in progress.

The inspectors discussed the outages and licensee self-assessments with

responsible engineers,. and maintenance personnel, root cause evaluators,

and work control personnel, as well as reviewing system engineering

lessons learned and overall licensee investigation results.

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b. Obser"ations and Findinas f

l

(1) Diesel Fire Pump outage Self Assessment Results j

As documented in Inspection Report 96005, during performance of the 18 ,

month surveillance on the diesel driven fire pump a number of

difficulties were encountered that challenged maintenance, operations,  :

and engineering. t

The safety engineering root cause investigation of problems with the DFP t

system outage was detailed and thorough. It identified that i

coordination among groups was lacking. Maintenance and work planning r

groups were unaware that a temporary pump was required, and as a result,  :

the outage was scheduled for the day before the critical date. System l

engineering did not begin to prepare a temporary modification package

until 4 days before the' start of the outage, and the initial design was

found to be inadequate upon review. The late start on the modification

and procedure changes resulted in a number of changes to correct errors

prior to implementation of the modification, and contributed to work

being started with the previous revision of the surveillance procedure l

(NOV341/96002-21). Another safety system outage, Primary Containment

'

Monitoring System, was delayed about two months because planners had to

support the DFP scope change to include the installation of temporary

DFPs. Document changes required were not all identified during the

license change request process to allow performing the surveillance on

line. Despite the DFP being equipment covered by TS requirements, the

outage was handled as a balance of plant equipment outage. The lessons

learned included raising future DFP outages to the level of attention

given to safety systems.

DERs 96-0651, 96-0655 and 96-0656 were written to document and track  !

corrective actions for problems related to this system outage.

(2) CCHVAC Outage Self-Assessment Results

The investigation into CCHVAC system outage problems was headed by work

control and supported by the Independent Safety Engineering Group. This

self assessment effort was slow to reach conclusions, although some

corrective actions were implemented promptly.,to support upcoming system

outages. These included:

. Getting system engineers more involved in preparation for outages

on their systems, including acting as outage manager in some

cases;

. Initiating system outage briefing meetings to discuss

preparations, tagouts, parts availability, plant impact, status,

contingencies, etc., among all concerned disciplines;

. Adding a backshift outage ::ianager to each system outage.

Lessons learned by system ongineering were developed promptly, and

appeared to be a good review. Engineering identified that the test

procedure for CCHVAC makeup filters was inadequate (NCV in 96005), test

equipment could be improved, and additional personnel required training

19

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to run that type of test. A review of inflatable damper boot seal

failures in CCHVAC dampers showed several failures in the previous year,

with none prior to that time. The seals were original equipment, with

no planned replacement interval and no spares on site. System

engineering was evaluating the seal failures as possibly age-related, t

and consideration was being given to establishing a planned interval for

periodic replacement of these seals based on discussions with the

vendor.

A problem identified in the original testing was the lack of sufficient

system flow. The system engineering assessment identified that, if

, additional system leakage were required to establish required flows, the

door to the CCHVAC mechanical equipment room could be opened without the

,

'

security precautions associated with holding open a door to the control

room. System engineering also informed the inspectors that the retest

performed was not required following removal of the sample canister and

capping of the hole, and that past tests had found no problems; system  ;

engineering had required the test as a conservative means to prove the

, main filter was not being bypassed, even though the vendor did not

i

specifically recommend such a test.

c. Conclusions j

, The inspectors noted that many of the problems exhibited during these i

system outages continued to be problems during this inspection period,

. as discussed in section M1.3 above. Coordination and execution of  !

high-visibility maintenance activities declined during this and the

previous inspection period. Self assessment efforts and improvements in

how work is planned and executed were focussed on fixing the process,

and will, therefore, be assessed as changes are implemented. The

assessments were self-critical and thorough.

M7.2 Comorehensive Intearated Technical Assessment (CITA) of Maintenance i

4

!

a. Insoection Scope (62703)

The inspectors reviewed the licensee's Maintenance CITA report and

discussed the results with the Director of Quality Assurance and i

Maintenance Superintendent. l

b. Observations and Findinas

This self assessment was performed by a multi-disciplined team which was

comprised of site personnel and industry peers. The CITA covered the

entire maintenance functional area.

The CITA team concluded that plant equipment was being maintained

appropriately. However, lingering issues, such as inadequate impact

statements and work instructions, procedure adherence, and lack of

sensitivity to housekeeping, which were previously identified still

remain. Improvements in the quality of maintenance technical procedures

were underway, and the focus on procedure adherence had reduced the

number of problems in this area.

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4  !

Adherence to the planned work schedule was identified as a problem.

'

Four-week look ahead scheduling meetings were found to be ineffective: +

organizational attendance was poor, attendees were not prepared, and '

large numbers of activities were added or removed from the schedule

(greater than 25 percent). Late work package planning contributed to

a schedule changes and resulted in little time to walk down jobs prior to

working. -

, Staffing of craft supervisory positions was not always meeting the l

4

supervisor to worker ratio goal. As a result, pre-job briefings were

j suffering and priorities slipped.  :

$

l c. Conclusions

4

The inspectors considered the Maintenance CITA to be a start at ,

3 identifying probleias in the maintenance functional area, which had not  :

had a recent self-assessment. However, this assessment primarily
reiterated previously identified problems, did not identify many new

! areas of concerns, and provided few recommendations for improvements.

j Recent CITAs in Operations and Engineering had provided more detailed

i assessments and recommendations. As discussed in this report, the

{ inspectors concluded that concerns in maintenance and work control

4

continue to exist.

i

,

M7.3 Review of Service Water System Self-Assessment Maintenance Issues

4

, The inspectors reviewed the responses to the eight self-assessment

i issues that were within the maintenance area and discussed them with the

i maintenance response team member. All of the assessment team's issues

! appeared to be resolved in a reasonable manner.

M7.4 Review of Service Water System Self-Assessment Surveillance & Testina

Issues

The inspectors reviewed the responses to the eighteen self-assessment

issues that were within the surveillance area. These items wera divided

roughly between issues concerning the licensee's response to Generic

Letter (GL) 89-13 " Service Water System Problems Affecting Safety-

Related Equipment" and the inservice testing (IST) program. The

inspectors had no problems with the action plans to resolve the

surveillance issues, with the exception of one IST item. The assessment

team had questioned why the RHRSW, DGSW, and EESW pump minimum flow line 1

'

isolation valves and two EESW control valves (P4400-F400A/B) were not in

the IST program. The licensee's response to this issue was to l

incorporate the valves into the program. The inspectors noted that the

licensee had not made provisions to stroke time test the control valves,

nor had they been granted relief by NRC. This will be tracked as an

inspection followup item (50-341-96-06-04).

The self-assessment identified a number of weaknesses with the

licensee's response to GL 89-13, Action III, which concerned testing and I

inspection of heat exchangers. Because of the number of issues i

identified, the inspectors concluded that the licensee had not  !

adequately addressed this portion of the GL. The inspectors reviewed

1 j

r 1

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the licensee's plan to correct the identified weaknesses and verified

that all the weaknesses were being addressed.

'

The remainder of the assessment team's issues appeared to be resolved in

a reasonable manner.

M8 Miscellaneous Maintenance Issues (92902)

M8.1 (closed) Insoection Follow-Uo Item 50-341/95011-01: Review of licensee

corrective actions in response to frequent control room indicator lamp

failure. The licensee determined the root cause failure to be due to

filament notching. The inspector ascertained that the licensee has

replaced the incandescent lamps, where possible, with light emitting

diodes in critical displays such as the full core display. Most other

ait. plays use dual lamp indicators. The licensee is continuing their

efforts to extend indicator lamp life. This item is closed.

111. Enaineerina

El Conduct of Engineering

El.1 Puma Runout Verification (TI 2515/118 Ites 03.01.e4)

TI 2515/118 item 03.01.e4 required that the inspectors verify that pump

runout conditions were not present with minimum number of pumps

operating with worst case alignment of non-safety related loads.

The inspectors reviewed the pump curves for the DGSW, EECW, EESW, and

RHRSW pumps. Of these systems, only RHRSW had the potential for a

runout condition, if operated with only a single pump running. For this

case, the inspectors determined that operator actions specified by

procedure (S0P 23.208) would prevent runout from occurring, as the

system was manually initiated and controlled. Therefore, the inspectors

concluded that the safety related service water pumps were adequately

protected against pump runout.

El.2 Inservice Test (IST) Proaram Review (TI 2515/118 Item 03.04.e)

TI 2515/118 item 03.04.e required review of the IST records for pumps

and valves in the service water systems, with an emphasis on the

technical adequacy of procedures, trending of test results and recurrent

failures and review of the IST program for completeness.

The inspectors reviewed records of recently completed IST surveillances

and noted one deficiency: On June 19, 1996, during performance an IST

surveillance on EESW pump 'B', the initial test results indicated the

pump was in the required action range for high differential pressure.

The control room personnel discussed the issue with the IST coordinator

and decided to rerun the test with the fixed reference point in the

center of its 1 percent tolerance band. These test results indicated

the pump was performing acceptably. A DER was written to document an

operability determination for the pump.

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The inspectors noted that the basis for a permitting a tolerance band

around the fixed reference value was documented in NUREG-1482, Section

5.3, and was to allow licensees some flexibility in establishing

repeatable test conditions required by the Code. The NUREG required

that the tolerance band, and the method used to establish the band, be '

documented in the licensee's IST program. Although a basis was

documented in the program, the inspectors determined that the licensee

failed to adequately evaluate the range of the tolerance band for the

EESW pump prior to implementation to ensure that test results would not

inadvertently place the pump in the required action range. The licensee

was still reviewing the issue and their intended corrective actions at

the end of this inspection.

The inspectors determined that the IST program was being adequately

implemented. One inspection followup item was identified, as discussed

in Section M7.4, with the licensee's responses to an assessment team

issue. The inspectors concluded that the assessment team acceptably

reviewed this TI item.

E2 Engineering Support of Facilities and Equipment

E2.1 Safety Related Service Water Drain Line Pluaaina

a. Inspection Scope (37551)

On July 29, the inspectors identified that a one-inch drain line on the

Division I safety related service water return line to the "A"

Mechanical Draft Cooling Tower (MDCT) was partially plugged. As 1

documented in Inspection Report 96004, inspectors had previously  !

identified a similar problem on March 31, 1996. During this inspection

period, inspectors interviewed licensee engineering and operations

personnel, and reviewed documents related to the issue.  :

b. Observations and Findinas

On July 29, when inspectors identified that one of the drain lines was

partially plugged while the Division 1 RHRSW and Emergency Equipment i

Service Water (EESW) systems were in service. The inspectors noted that j

the drain line on the "C" MDCT return line had full flow, but the "A" l

line had very little flow, indicating that some plugging was occurring. l

The inspector notified the control room operators and the abnormal

condition was confirmed. DER 96-0844 was initiated to document event

occurrence. The licensee postulated that the cause for the clogging was

loose corrosion products.

The purpose of the one inch drain lines on the return lines to the MCDTs I

was to prevent freezing. As previously documented in Inspection Report ,

96004, under cold weather conditions, the potential existed for the _'

1

return lines to the MDCT's to partially freeze if the drain lines were

plugged. Due to the failure of the licensee to adequately test the one

inch drain lines to ensure that they could perform satisfactorily, a l

violation (96004-05) was issued on June 14, 1996.

As documented in the Detroit Edison Response to Notice of Violation

96004-05, dated July 15, 1996, corrective actions taken included: "As an

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[ interim measure, the drain lines have been included in the routine

i system engiserring walkdown checklist for periodic monitoring." Since

,

May 28, 19M , the system engineer only once actually verified proper

t operation of the drain lines for each division. The systems were run on

1 a weekly basis' for chemical treatment. Though the system engineer did

1

!

conduct biweekly walkdowns of the system, and a walkdown chocklist which .

included monitoring of drain lines was utilized, systems monitoring was '

. not planned to coincide with system operation. As a result, performance

.

of the drain lines was not adequately monitored.

} c. Conclusions

j

In response to the Notice of Violation 96004-05, the licensee committed

"

to have corrective actions to. prevent recurrence of the drain line

plugging. This included a planned system modification.- Recognizing

that no possibility of freezing existed during this inspection period,

the recurrence of the drain line clogging was of minor safety

consequences. However, the failure of the licensee to adequately

monitor system performance while it was running resulted in a missed ,

opportunity to gather data to ensure that planned corrective actions

would address the plugged problem.

10 CFR Part 50, Appendix B, Criterion XVI, " Corrective Actions,"

required in part that measures be established to assure that conditions

adverse to quality, such as deficiencies, defective material and

equipment are promptly identified and corrected. Contrary to the above,

on July 29, 1996, inspectors identified partial plugging of the one inch

drain line on the Division 1 Residual Heat Removal Service Water Return

Line to the "A" Mechanical Draft Cooling Tower, a repeat occurrence (50-

341-96-06-05).

E2.2 Root Cause Investiaation of Reactor Water Cleanun (RWCU) Filter

Demineralizer Control Panel Fire

a. Inspection Scope (92902)

The inspectors reviewed the results of the investigation into an

electrical fire in the RWCU filter demineralizer control papel and

discussed the issues with the team leader and engineers.

b. Observations and Findinas

On July 7, operators identified a fire in the RWCU filter demineralizer

control panel in the reactor building. Prompt action to deenergize the

panel and put out the fire were taken. Damage from the fire, which was

limited to the local control panel, required that both filter

demineralizers be bypassed. Reactor water chemistry was maintained i

within TS limits while repairs were made.

I

At about the same time as the fire, the Sequence of Events Recorder '

(SOER) behaved erratically, then failed, and a solid ground was l

identified on the 130V balance of plant DC bus. I

'

A root cause evaluation team, headed by system engineering, promptly

investigated the event. The team determined that an AC relay (R13A)

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,

with DC monitoring power located in the RWCU panel failed and shorted  !

120V AC onto the DC bus. The superimposed AC voltage caused the faulty

operation and failure of the SOER, and also caused the failure of a  !

control room annunciator power supply. The annunciator power supply ,

failure resulted in the DC ground following the fire, but did not result  !

in the loss of any annunciators.  !

!

Failure of the relay was believed to be due to thermal aging. This j

condition was described in General Electric Service Information Letter  :

(SIL) 229, Supplement 1, so no 10 CFR 21 investigation was performed by

the licensee. Licensee evaluation of the SIL will include this failure,

but did not previously identify that affected components existed in the i

RWCU system because this panel was treated as a vendor-supplied " black  ;

box" and components were not listed in the site data base. '

Repairs were completed on July 12, and the system was restored to

service. Emineering continued to evaluate the failed relay for

reliability and other uses in the plant to determine if a replacement

part should be identified. DER 96-0755 was written to document the

event and track corrective actions.

c. Conclusions

The inspectors considered the licensee response to the fire, loss of

equipment, and repair efforts to be proper, conservative and deliberate.

The investigation was prompt and thorough, and included previous site

experience with a similar relay failure and fire. Reactor water

chemistry was maintained and closely monitored.

However, the inspectors were concerned by the failure to identify all ,

component locations in the plant affected by SIL 229, Supplement 1. The

licensee investigation to identify other " black box" components will be

tracked as an Inspection Followup Item (50-341-96-06-06).

E2.3 UFSAR Reauirement Review

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report (UFSAR) description

highlighted the need for a special focused review that compares plant

practices, procedures, and parameters to the UFSAR descriptions. While ,

performing the inspections discussed in this report, the inspectors

reviewed the applicable portions of the UFSAR that related to the areas

inspected. The inspectors verified that the UFSAR wording was

consistent with the observed plant practices, procedures, and

parameters.

E7 Quality Assurance in Engineering Activities

! E7.1 Review of Service Water System Self-Assessment Enaineerina Issues

!

, The assessment team raised 65 issues during its inspection effort, 35 of

which were in the engineering area. The inspectors discussed the issues

1 and their proposed resolutions with the system engineering and plant

'

support engineering response team mer5ers. The inspectors also reviewed

DER closure packages, calculations, drawings, and procedure revisions to

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ensure that appropriate corrective actions were being taken.  ;

Additionally, the inspectors performed a walkdown of the mechanical i

l draft cooling tower motors to confirm the response to the assessment i

team's issue.  ;

The inspectors determined that the licensee had taken appropriate

actions for those items where interim operability calls were made  :

following the assessment team exit. Specifically, all the coolers were i

cleaned during the forced outage in March 1596 and the DGSW throttle  !

valves. were reset to correspond to their des gn flow rate. Calculations  !

were redone to account for industry accepted fouling factors and to use

the design value maximum service water temperature. The modification to

resolve the EECW makeup tank deficiency was reviewed in Inspection

Report 96004 and determined to be acceptable. The inspectors noted that

this modification was an interim solution until the EECW tanks could be  !

relocated to a higher elevation.

E8 Miscellaneous Engineering Issues (92902) ,

E8.1 (Closed) LER 50-341/96006: Missed American Society of Mechanical.

Engineers (ASME)Section XI required inspection of an EECW check valve

due to incorrect valve grouping. EECW check valve P440F1168, an eight- '

.

inch Powell swing check, was incorrectly grouped with three six inch ,

EECW check valves'that did not meet the grouping guidance of Position 2 r

of GL 89-04. As such, the valve was not inspected during the last

refueling outage as required.

The licensee disassembled and inspected the valve during the March 1996  !

forced outage, and verified the valve showed no significant signs of

degradation. The IST disassembly / inspection procedure was revised to

i place this valve in a separate group requiring disassembly and

inspection every refueling outage, while the remaining three EECW valves

would remain in the same sampling group. The licensee was updating the

IST program such that relief request VR-48 included the three 6-inch

j check valves and a separate relief request submitted the 8-inch valve.

! These actions were considered appropriate and this item is closed.

E8.2 (Closed) Insoection Followun Item 50-341/94007-05: Failures of motor

operated valves. This issue was thoroughly investigated and is

discussed in Inspection Report 95003. The failures were traced to use

of an unapproved solvent in the auxiliary contacts and contactors. Two

violations were issued for inadequate corrective actions and use of non-

l

conforming materials. This item is closed.

!

E8.3 (Closed) Insoection Followuo Item 50-341/94009-06: This item concerned

discovery of hardened grease in 480V and 4160V breakers. This issue was

thoroughly investigated and is discussed in Inspection Report 94012.

This item is closed.

! E8.4 (Closed) Insoection Follow-un Item 50-341/95002-01: This item concerned

! the testing of pumps for the IST program using reference curves without

a relief request. The licensee incorporated single reference point

'

testing for the majority of pumps included in the IST program. The

i licensee obtained NRC approval to use reference curves for the EECW and

core spray pumps. The inspectors reviewed the implementing prccedures

26

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and associated acceptance criteria and considered them acceptable. This ,

item is considered closed. l

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E8.5 (Closed) Violation 50-341/95002-03: This item concerned the failure to  !

provide adequate acceptance criteria to verify the full flow test for i

the core spray discharge check valves as required by ASME Section XI. i

The licensee implemented corrective actions to comply with Position 2 of

GL 89-04 to satisfy the full flow test requirement. The testing i

required by the IST program included disassembly / inspection on a i

refueling outage sampling basis and a partial stroke test on a quarterly l

basis. The inspectors reviewed the applicable implementing procedures I

and considered them acceptable. This item is considered closed.

E8.6 (Closed) Insoection Followuo Item 50-341/96004-07: The inspectors were

concerned that the installed EECW modification did not match the design

calculation assumptions. The installed configuration required running

of either a DGSW or RHRSW pump in addition to an EESW pump to provide

sufficient pressure so that flow from EESW to EECW would occur. The

inspectors reviewed the licensee's analysis and determined that the

calculation was performed assuming all service water pumps on a division

were running. Therefore the installed configuration matched the design

assumptions. This item is closed.

E8.7 (Closed) Inspection Followuo Item 50-341/95011-02: Response to Generic

Letter 89-16 modification was designed for static loads only. Licensee l

performed calculations to confirm that the system would withstand

anticipated dynamic loadings. The inspector reviewed the licensee's

calculations and concluded that the hardened wetwell vent system would

,

withstand the anticipated dynamic load. This item is closed.

i

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E8.8 (Closed) Violation 50-341/95003-02A: Failure to take appropriate

corrective action to identify and resolve ITE contactor auxiliary

contact deficiencies. Contact sticking was attributed to an oil based

contact cleaner becoming sticky and impeding contact operation. The

inspector reviewed documentation indicating the licensee had cleaned or

replaced all auxiliary contacts in safety related contactors. Hon

safety related contactor were being cleaned or replaced and monitored by

an assigned tast force. Since Inspection Report 95003, the licensee

identified five contact failures. One contact contained a visual

residue from cleaner compound, all had cracked covers or bows that could

have interfered with contact operation. The licensee task force is l

continuing to monitor the performance and failure rate of ITE contactor  !

auxiliary contacts. This issue is considered closed.

IV. Plant Support

,

R1 Radiological Protection and Chemistry Controls  !

I

R1.1 Wrona Radioloaical Work Permit (RWP) Used

'

On July 9, the licensee identified instrumentation and controls (I&C)

-

workers had performed surveillances on the scram discharge volume (SDV)

i level detectors using the RWP for performing general I&C work (RWP

96-1011). However, the RWP stated "This RWP does not cover RB-1 North

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and South SDV Functional Tests and Surveillances." The workers and one

radiation protection (RP) supervisor failed to realize that the work i

should have been performed under RWP 96-1025, which was issued i

specifically to track dose accumulated for work associated with the

SDVs.

DER 96-0761 was written to document the event and track corrective

actions. The involved individuals had their access to the

radiologically restricted area revoked pending upgrading, and training

for the I&C group was planned to cover specific RWPs used by that group.

Failure to follow the requirements of RWP 96-1011 is a violation of

,

'

technical specifications. However, this violation will not be cited

because the requirements of the Enforcement Policy,Section VII were met

(NCV 341/96006-07).

l

R2 Status of Radiation Protection and Chemistry Facilities

R2.1 Soent Fuel Pool Cleanout Activities

a. InsDection Scope (71750)

The inspectors reviewed plans for removal of irradiated equipment from

the spent fuel pool and packaging for shipment to a burial facility.

'

l

The inspectors also observed various aspects of the preparation and work

over this and the previous inspection period.

b. Observations and Findinas

l This project resulted in the removal from the spent fuel pool (SFP) and l

l shipment of 4 casks which contained crushed control rod blades, local l

power range monitors, shroud head bolts, jet pump beams, hoses, and a i

source pin rack. The project was intended to remove unnecessary

l equipment stored in the SFP while a burial facility was available prior

to planned reracking of the pool.

l The project was headed by a senior line manager, ensuring adequate i

management support and attention. The group performing the work was a

l dedicated crew which included members of the RP staff, radwaste,

l engineering, and a licensed operator to coordinate efforts with the l

control room.

!

l The work was concluded with about 20 percent of the planned work

l complete due to unexpected problems. The most time-consuming problem

'

was a shipping cask which was configured for the wrong type of liner by

the supplier, causing a 2 week delay. Reactor building access was also

restricted several times due to problems with the operation of the

railroad airlock doors. This and other minor problems were resolved in

a deliberate way.

.

c. Conclusions

!

, The inspectors concluded that work was performed in a deliberate manner.

When questions were raised, work was stopped until the questions were

resolved. There was no observable schedule pressure, and management

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supported the decision to stop the partially completed project with

sufficient lead time to support preparations for the upcoming outage.

Coordination and cooperation with other organizations was smooth. This

was facilitated by having a multi-disciplined team, which frequently

updated other organizations with the status of work and required

assistance.

,

R5 Staff Training and Qualification in Radiation Protection and Chemistry

R5.1 RWP Como11ance Problems with New Workers

On June 14, a contract employee new to the site entered the control

room, a radiologically clean area, without performing the required whole

body frisk. After entering, RP questioned whether he had performed the

required frisking, which he realized he had not performed. RP then

surveyed the control room and found no contamination present. The

individual was upgraded on RP practices before having his access to the

Radiologically Restricted Area (RRA) restored.

On August 1, a relatively new security guard was found to be drinking

water and chewing tobacco inside the RRA, contrary to RP procedure. The

individual's access to the RRA was restricted, and the individual was

subsequently terminated for other reasons. DER 96-0871 was written to

document the event.

These instances were additional examples of a failure to follow

Radiation Protection procedures which is a violation of technical

specifications; however, they will not be cited because the requirements

of the Enforcement Policy,Section VII were met (NCV 341/96006-08).

RP and training were evaluating the effectiveness of radiation worker

training as a result of these events. DER 96-0926 was written to track

corrective actions for this trend. The importance of these events was

heightened by the plans to bring in large numbers of contract workers

for the upcoming refueling outage.

P3 Emergency Preparedness Procedures and Documentation

P3.1 Review of Exercise Ob.iectives and Scenario (82302)

The inspectors reviewed the 1996 exercise objectives and scenario which

arrived in sufficient time before the exercise to permit NRC review.

The scenario provided an acceptable framework for the exercise and the

objectives were appropriately in the facilities evaluated by the

inspectors.

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P4 Staff Knowledge and Performance in Emergency Preparedness l

P4.1 1996 Evaluated Biennial Emeraency Exercise ,

'

a. Inspection Scone (82301)

'

. The inspectors evaluated licensee performance in the following emergency l

response facilities during the 1996 evaluated emergency exercise, which I

was run July 16:

. Control Room Simulator

. Technical Support Center

. . Operations Support Center

] . Emergency Operations Facility

'

b. Observations and Findinas

.

b.1 The simulator control room crew was professional, and communications

i among the crew was efficient with repeat backs and acknowledgements

b'ing

e observed by the inspectors. The nuclear shift supervisor was

proactive in following plant conditions, review of emergency

classification procedures, and use of checklists.

' The Emergency Director (ED) rapidly recognized and declared the Unusual

Event, and then appropriately upgraded the classification to an Alert

due to the magnitude of the simulated seismic event. Command and

control in the control room was strong as indicated by the periodic

briefings and overall awareness of the emergency conditions. State and

local notifications were made within the required 15 minutes and the NRC

notification was made within the required hour.

b.2 TSC activation was coordinated and efficient. Support staffs for

communications, administrative, and status boards provided prompt l

continuous communications, organized and distributed information copies,  !

and updated status boards continuously. The TSC staff overcame the

added challenge of the actual failure of the Emergency Response

Information System just prior to the drill. Plant conditions were

rapidly evaluated and the Site Area Emergency was appropriately

decl ared. Good teamwork was observed between the ED and his staff in  ;

looking ahead for plant condition changes which could lead to emergency i

reclassification.

Informative public address announcements were made for onsite protective

actions. Continuous communications were maintained between the TSC,

control room, and the Operations Support Center (OSC). The ED exercised

good command and control by providing frequent briefings for facility i

personnel.

The inspectors noted that control room and TSC priorities did not always

coincide. The control room requested the TSC to assign a response team

to add water to the condensate storage tank using fire hoses. When the

response was slow, the control room dispatched one of their operators to

perform the job before the TSC and OSC were able to create, brief, and '

dispatch a response team.

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' The Health Physics Network (HPN) line was not staffed in the TSC after

several requests from the NRC. The HPN line from the TSC is important

i for communication of information regarding onsite and offsite

radiological conditions and related protective action decisions. The

,

failure to staff the HPN line at the NRC's request will be tracked as an

Inspection Followup Item (50-341/96006-09).

j b.3 The OSC staff was proactive in attempts to develop solutions to actual

'

and potential plant conditions. The OSC Assistant Coordinator and

Radiation Emergency Team Leader provided effective response team

assignments. Radiological conditions and safety were emphasized to the

! teams. I

OSC Coordinator status briefings were inferquent and informal; only four

briefings were observed. During these M iefings, staff attention was

lacking, new relevant information was minimal, and no closure was

j observed for the briefings.

i

j' The Post Accident Sampling System (PASS) team was unable to obtain a

reactor water sample because the sample panel did not function properly.

.

(See Section 04.1) The sample had to be simulated for drill purposes.

The inability to obtain an actual PASS sample will be tracked as an-

l[

t

Inspection Followup Item (50-341/96006-10).

b.4 Overall performance in the Emergency Operations Facility (EOF) was

effective. Facility staffing was rapid and efficient. Activities,

j including offsite monitoring kit checks, accountability, habitability,

i emergency ventilation lineup, and radiological control were performed

j effectively and promptly.

i The Emergency Officer (EO) was in frequent communication with the TSC.

i The E0 provided frequent and concise briefings to the EOF staff and the

NRC Site Team. The Nuclear Operations Advisor provided a detailed

} briefing to the arriving NRC site team. l

i

! Dose assessors provided the E0 with timely and accurate dose projections l

and performed numerous computer runs to anticipate potential changes in

'

!

i release rates, release paths, and plant conditions.

I The inspectors determined that E0F status boards were inadequate for

!

trending plant parameters. There were no provisions for posting the

i priorities established by the ED. The EOFs protective measures status  ;

j boards contained no information from State officials. The plant i

parameter trending, TSC priorities, and offsite protective action status ,
information status board inadequacies will be tracked as an Inspection
Followup Item (50-341/96006-11).

4

b.5 Facility critiques immediately following the exercise termination were

j self critical. Several instances where controllers inappropriately  ;

'-

handled data occurred. On two occasions, misinformation was transmitted  :

offsite and had to be corrected. The impact of the misinformation
transmitted to offsite authorities was minimal and did not impact the

j outcome of the exercise.

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c. Conclusions

,

j The exercise was successful in demonstrating that the onsite emergency  :

plans were acceptable, and that the licensee was capable of-implementing

i them. Overall exercise performance was very good. Emergency

4

classifications and associated notifications to the State, local

. government, and NRC were made in a timely manner. Post exercise  !

! facility critiques involved exercise controllers and participants and

!

were very good. Three Inspection Followup Items were identified related

to failure to staff the Health Physics Network in the Technical Support
Center (TSC), problems with several status boards in the Emergency

l Operations facility, and the inability to actually obtain a post

j accident sample.

) V. Manacement Neetings i

'

X1 Exit Meeting Summiary

i

,

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on August 9, 1996. The

!

.

licensee acknowledged the findings presented.

l The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

i identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

<

S. Booker, Assistant Supervisor, Maintenance

C. Cassise, General Supervisor, Maintenance

W. Colonnello, Director, Safety Engineering

R. Delong, Superintendent, System Engineering

T. Dong, NSSS, Technical Engineering

'

P. Fessler, Plant Manager, Operations

L. Goodman, Director, Nuclear Licensing

J. Kauffman, ERS,,RERP

E. Kokosky, Superintendent, RP and Chemistry

J. Korte, Director, Nuclear Security

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R. Laubenstein, NSS, Operations

R. McKeon, Assistant Vice President / Manager, Operations

W. Miller, Technical Support '

J. Nolloth, Superintendent, Maintenance

D. Ockerman, Supervisor, Operations

J. Plona, Technical Director

W. Romberg, Assistant Vice President and Manager, Technical

33

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INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

l

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IP 40500: Effectiveness of Licensee Controls in Identifying,

Resolving, and Preventing Problems

IP 40501: Licensee Self-Assessments Related to Team Inspections

IP 61726: Surveillance Observations

IP 62703: Maintenance Observation

! IP 71707: Plant Operations

IP 71750
Plant Support Activities

l IP 82301: Evaluation of Exercises for Power Reactors

IP 82302: Review of Exercise Objectives and Scenarios for Power

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Reactors

IP 92902: Followup - Engineering

IP 92903: Followup - Maintenance

TI 2515/118: Service Water System Operational Performance Inspection

ITEMS OPENED AND CLOSED

Opened

50-341/96006-01 VIO Inadequate procedure in that all RHRSW valves were not

included in S0P

50-341/96006-02 NCV Failure to follow procedures for vendor control and

safety tagging

50-341/96006-03 VIO Temporary plant space request not initiated for staged

equipment

l

50-341/96006-04 IFI No provision to stroke time test valve in Inservice

Testing Program

l

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50-341/96006-05 VIO Partial plugging of one inch drain line on Division 1

RHRSW Return line to "A" MDCT

50-341/96006-06 IFI Failure to identify all aging thermal components as

described in SIL 229

50-341/96006-07 NCV Wrong radiological permit used on surveillance for

scram discharge volume level detectors

50-341/96006-08 NCV Three instances of failure to follow RP procedures

50-341/96006-09 IFI Failure to staff HPN line at NRCs request

50-341/96006-10 IFI Inability to obtain a PASS sample

50-341/96006-11 IFI Plant parameter trending, TSC priorities, and offsite

protective action status information status board

inadequacies

Closed

50-341/96006 LER Missed ASME Section XI required inspection of an EECW

check valve due to incorrect valve grouping

50-341/94007-05 IFI Failures of motor operated valves

50-341/94009-06 IFI Hardened grease in 480V and 4160B breakers

50-341/95002-01 IFI Testing of pumps for IST program using reference

curves without a relief request

50-341/95002-03 VIO Failure to provide adequate acceptance criteria to

verify full flow test for core spray discharge valves

l 50-341/95003-02A VIO Failure to resolve ITE contactor auxiliary contact

I

deficiencies

.

50-341/95011-01 IFI Frequent control room indicator lamp failure

l 50-341/95011-02 IFI GL 89-16, modification designed for static loads only

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50-341/96004-07 IFI Installed EECW modification did not match the design '

calculation assumptions

LIST OF ACRONYMS USED i

,

ALARA As low As Reasonably Achievable

ASME American Society of Mechanical Engineers '

, CCHVAC Control Center Heating Ventilation Air Conditioning

I

CFR Code of Federal Regulations

CITA Comprehensive Integrated Technical Assessment

CST Condensate Storage Tank

Deco Detroit Edison Company

DER Deviation Event Report

DFP Diesel Fire Pump

DGSW Diesel Generator Service Water

ED Emergency Director

EDG Emergency Diesel Generator

EECW Emergency Equipment Cooling Water

, EESW Emergency Equipment Service Water

E0 Emergency Officer

EOF Emergency Operations Facility

ESF Engineered Safety Feature

GL Generic Letter

GSW General Service Water

HPCI High Pressure Coolant Injection

HPN Health Physics Network

IFI Inspection Followup Item

IR Inspection Report

LER Licensee Event Report

MDCT Mechanical Draft Cooling Tower

NASS Nuclear Assistant Shift Supervisor

NCV Non-Cited Violation

NRC Nuclear Regulatory Commission l

NSS Nuclear Shift Supervisor

OSC Operations Support Center

PASS Post Accident Sampling System

PRA- Probable Risk Assessment

RCIC Reactor Coolant Injection System

RHR Residual Heat Removal

RHRSW Residual Heat Removal Service Water

RP Radiation Protection .

Radiologically Restricted Area

'

RRA

RWCU Reactor Water Clean-Up

RWP Radiological Work Permit

SFP Spent Fuel Pool

SIL Service Information Letter

SOER Sequence of Events Recorder '

S0P System Operating Procedure

TS Technical Specification

TSC Technical Support Center

VIO Violation

l

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