ML20149K869
ML20149K869 | |
Person / Time | |
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Site: | Fermi |
Issue date: | 07/01/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20149K861 | List: |
References | |
50-341-97-03, 50-341-97-3, NUDOCS 9707300203 | |
Download: ML20149K869 (42) | |
See also: IR 05000341/1997003
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U.S. NUCLEAR REGULATORY COMMISSION
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l REG lON 3
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- Docket No
- 50-341
License No: NPF-43
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Report No: 50-341/97003
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i Licensee: Detroit Edison Company (DECO)
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Facility: Enrico Fermi, Unit 2
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Location: 6400 N. Dixie Hwy.
Newport, MI 48166
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Dates: March 20 through May 9,1997
Inspectors: G. Harris, Senior Resident inspector
C. O'Keefe, Resident inspector
I A. Walker, Reactor inspector
A. Dunlop, Reactor Inspector
S. DuPont, Project Engineer
D. McNeil, Operator Licensing Examiner
S. Stasek, Senior Resident inspector,
Davis-Besse
D. Butler, Reactor Inspector
Approved by: Michael J. Jordan, Chief
Reactor Projects Branch 5
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9707300203 970701
PDR ADOCK 05000341
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EXECUTIVE SUMMARY
- Enrico Fermi, Unit 2
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NRC Inspection Report 50-341/97003
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This inspection included aspects of licensee operations, engineering, maintenance, and l
plant support. The report covers a 7-week period of resident inspection.
Ooerations
- The inspector concluded that plant restart was performed in a coordinated and
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controlled manner. Equipment problems were adequately resolved using
i appropriate support personnel. Management oversight was effective in resolving
i problems, allowing the operating shift to operate the plant with minimum
distractions. Each problem was resolved in a methodical and conservative manner
before resuming startup. Operator performance was focussed and error-free.
(01.1)
e The inspectors identified that a reactor building ventilation isolation (ESF actuation)
was caused by a lack of attention to detailin review of an electrical print. (01.2)
- The inspectors concluded that current administrative controls for the backseating of
valves were weak in tthat they did not specify controls and necessary evaluations
prior to backseating motor operated valves. (01.3)
- The inspectors concluded that the licensee's drywell cleanup and closecut activities !
were largely effective based on drywell cleanliness and equipment condition. I
(O2.3) i
Maintenance I
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- The licensee identified that two failures of the Reactor Core Isolation Cooling
inboard Steamline Isolation Valve (E5150-F007) were caused by maintenance
workers. The inspectors identified that the second failure was initially not detected
and the system was unknowingly returned to service in an abnormal lineup. The
inspectors concluded that these problems were indicative of lack of attention to
detail and lack of sensitivity to potential equipment damage by station personnel,
lack of questioning attitude by operators during the surveillances and subsequent
system restoration, and procedures that were inadequate to ensure the system was
tested and restored to a proper lineup following testing. A violation was issued.
(M1.4)
- The licensee identified numerous examples of lack of attention to detail during
performance of maintenance work. These resulted in restoring equipment to
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i service without fuses, unrecognized damage, and rework. The inspectors
concluded that these examples were indicative of an adverse trend in personnel
performance during the conduct of maintenance. (M1.4, M1.6)
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- The inspectors identified an apparent violation pertaining to the failure to recognize
i the significance of the problem with hardening grease associated with the MCC
fused disconnect switches and take prompt actions to prevent recurrence.
(M 2.1.1 )
- The inspectors identified an apparent violation pertaining to the lack of establishing
preventive maintenance (PM) activities for the MCC fused disconnect switches.
The licensee narrowly interpreted the requirement for PM activities to not include
devises such as the disconnect switches. (M2.1.2)
- Tne inspectors identified an apparent violation for failure to implement corrective
actions in a timely manner for a 1988 industry problem with motor operated valve
(MOV) actuators. Following failure of the High Pressure Coolant Injection Valve
actuator, the licensee inspected 67 safety related and important to safety MOV
actuators because this problem involved a potential common mode failure
mechanism. The population inspected was large because poor maintenance
documentation prevented the licenses from determining which actuators had
corrective actions completed in the past. (M2.2)
- The inspectors identified a violation concerning inadequate work instructions and
procedures to ensure new battery cells were fully charged and installed in a
condition to support the function of the Division 124/48 Volt Battery. (M2.3)
e The inspectors identified a violation for inadequate work instructions that led to an
emergency diesel generator starting air compressor being left in the OFF position.
Weak configuration control practices during work activities contributed to this <
event, which unnecessarily challenged the operability of the associated engine.
(M3.1)
e The inspectors concluded that the On-Site Review Organization was initially slow in
resolving issues associated with MCC fused disconnect switches. Corrective l
actions were implemented on a substantial portion of the affected population before
the adequacy of the corrective actions were adequately assessed. (M7.1)
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Enaineerina l
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e The licensee identified and corrected several Emergency Equipment Cooling Water l
(EECW) System design deficiencies. These included lack of redundant power for
containment isolation valves, susceptibility to high energy line breaks inside primary
containment, and an interlock with Reactor Building Closed Cooling Water System
isolation valves which could have prevented initiating EECW during remote
shutdown conditions. The inspectors concluded that the licensee appeared to have
adequately addressed these issues prior to plant restart. (E2.1)
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! Plant Sucoort
- The inspectors identified a violation of radiological requirements concerning workers
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that did not follow procedures and notify Radiological Protection personnel before
accessing a work area greater than 8 feet above the floor. This resulted in the
! workers not receiving a briefing on radiological conditions in the entire work area.
(R1.2)
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! Honort Details
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Summarv of Plant Status
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Unit 2 began this inspection period in a forced outage to repair the main generator. During
the outage, Motor Operated Valve (MOV) inspections and Motor Control Center (MCC)
- fused disconnect switch inspections and lubrication were conducted on a significant
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number of pieces of equipment. Also during this outage, engineering identified and
corrected several Emergency Equipment Cooling Water (EECW) System design issues
through system modifications. The plant was restarted on May 2 and the main generator
was synchronized to the grid on May 6.
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l. Operations
01 Conduct of Operations
01.1 General Comments and Startuo Observations (717071
a. Insoection Scope (71707)
Using Inspection Procedure 71707, the inspectors conducted frequent reviews of
plant operations. Specific events and noteworthy observations are detailed in the
sections below.
Fermi 2 unit was restarted on May 2. The inspectors observed activities in the
control room and in the plant associated with starting up the plant. This included
reactor startup, Reactor Core Isolation Coolant (RCIC) and High Pressure Coolant
injection System (HPCI) surveillance testing, turbine roll and segments of power !
ascension. Inspectors reviewed design basis documents and other design data and !
discussed several equipment problems with engineering to assess equipment
operability and the adequacy of licensee response,
b. Findinas and Observations.
The licensee consequently delayed startup about one day while repairs were made
to a controller for the Combustion Turbine Generator 11-1. Startup was further )
delayed when post-modification testing of the RCIC steam admission valve (E5150- i
F045) indicated that the valve opened faster than the acceptance criteria. Actual l
speed was analyzed for existing bus voltage and found to be acceptable.
Control room operations during the startup were observed to be conducted in a
professional and controlled manner. Reactivity manipulations were particularly well
controlled. The inspectors observed good communications and coordination
between Operations personnel and maintenance and engineering personnel. Station
management oversight of critical startup activities was effective in coordinating
efforts between operations and other departments. This coordination increased the
availability of the control room supervisor to manage activities within the control
room. The inspectors observed that briefings were frequently held and were l
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sufficiently detailed. Operations worked effectively with Reactor Engineering to l
resolve an operator concern that two control rods had higher than average notch i
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worth near the expected critical position.
c. Conclusions
The inspector concluded that plant restart was performed in a coordinated and
controlled manner. Equipment problems were adequately resolved using l'
appropriate support personnel. Management oversight was closely involved in
resolving problems, allowing the operating shift to operate the plant with minimum
distractions. Each problem was resolved in a methodical and conservative manner
before resuming startup. Operator performance was focussed and error-free.
01.2 Reactor Buildina Ventilation (RBHVAC) Trio with Resultina Momentary Loss of
Secondarv Containment
a. Insoection Scone (93702)
The inspectors conducted an event followup and independent assessment of the
circumstances surrounding the loss of secondary containment. The licensee's
cause determination and corrective actions were reviewed for adequacy.
Secondary containment integrity during the event was evaluated by reviewing
operator logs, annunciator response procedures, and technical specifications. The ,
event and corrective actions were discussed with plant management. l
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b. Observations and Findinas i
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' On March 25, RBHVAC System alarms were received for Reactor Building High j
Pressure. Control room operators identified that the West RBHVAC Exhaust Fan
Damper (T41-F014) failed shut. This resulted in a positive pressure in the reactor
building for about 2 minutes before a normal ventilation lineup and building pressure I
could be restored. The maximum recorded reactor building pressure during the
event was +0.5 inches of water. The licensee reported this event in accordance 4
with 10 CFR 50.72 because the TS for secondary containment required that the
Reactor Building be maintained at greater than or equal to 0.125 inches of water ;
vacuum.
While response time testing (see E2.2 below) was being performed, the solenoid
operated valve (T41-F056) that controls air to damper (T41-F014) began to leak
sufficient air that the force of the actuator spring shut the damper. The inspectors
determined that a low flow trip of the fans associated with the failed damper did
not occur because the logic was not satisfied by an exhaust fan operating under j
shutoff conditions. As a result, the supply of air into the reactor building exceeded ;
the exhaust flow, causing a pressure increase.
Upon recognition of the equipment problem, control room operators tripped the l
affected supply and exhaust fans and started the idle set of fans to restore the !
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reactor building to a negative pressure. The licensee then replaced the failed
soleno;d operated valve (T41-F056).
Corrective actions included sending the failed valve offsite for failure analysis and
performing a system review to determine whether the no-flow trip should have
prevented this event. Preventive maintenance for this type of valve was also under
review.
c. Conclusions
The failure of T41-F056 resulted in a brief loss of secondary containment and a
violation of TS 3.5.2, Action b. The safety significance of this event was negligible
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because RBHVAC effluent monitoring was maintained, and no release of radioactive
material occurred during this brief event. The licensee is reviewing the design
adequacy which will be documented in Licensee Event Report (LER) 97-07.
01.3 Backseatina of MOVs
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a. Insoection Scooe (92901)
The inspectors reviewed administrative and valve lineup procedures. The ,
inspectors held discussions with operations and station management. I
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b. Findina and Observationg l
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While reviewing the startup schedule, the inspector noted, as was done during the
previous cycle, that the reactor recirculation pump isolation valves were backseated
to reduce potential packing leakage. The discharge valves are closed during low
pressure coolant injection.
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The inspector was concerned that although an engineering evaluation had been
conducted, the valves were being placed in a position other than that described in
the current valve lineup procadures for an extended period while operating at
power. The inspector noted that the current operations procedures (MOP 03,
" Operations Policies and Practices") lacked formal controls and management
expectations concerning the backseating of valves, such as specifying the hanging
of caution tags for a configuration different than that specified by the current
system operating procedure (SOP) lineup. Operations management agreed to
review their administrative controls to ensure better control of backseating motor
operated valves.
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- c. Conclusions
- The inspector concluded that current administrative controls for the backseating of I
l valves were weak. Procedures did not specify controls and evaluations necessary
l prior to backseating motor operated valves. )
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02 Operational Status of Facilities and Equipment
O 2.1 Enaineered Safetv Feature System Walkdowns (71707)
- The inspectors used inspection Procedure 71707 to walk down accessible portions
) of the following ESF systems. The inspectors observed the condition of the
j equipment, visually verified that the systems were in the required lineup, and l
confirmed that system instrementation indicated values appropriate to the plant I
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- e Division 2 Non-interruotible Air Supply System
o High Pressure Coolant injection System (HPCI)
e Reactor Core Isolation Cooling System (RCIC) !
i e Division 2 Core Spray System )
I e Containment Vacuum Breakers i
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l e Division 1 and 2 24/48V Batteries
e Division 1 and 2 EECW
] e Division 1 Residual Heat Removal System (RHR)
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j Equipment operability, material r,ondition, system lineups, instrument indications, 1
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and housekeeping were acceptable in all cases. Several minor discrepancies were l
i brought to the licensee's attention, including:
- A spring can support for Core Spray System above the torus appeared to be l
} loaded more heavily than it should have been, based on hot and cold load 1
- markings. Engineering produced a construction-era analysis which showed ;
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the current load was acceptable, but the markings had not been changed. )
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! * The A RHR pump motor had a very small oilleak from the lower motor
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reservoir.
I e Safety relief valve J vacuum breaker had a small quantity of foreign material
inside the protective screen. (See 02.4)
The foreign material was promptly removed from the vacuum brea~ker assembly,
! and work requests were written for the oil leak.
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02.2 Licensee Reoorted Potential Habitability Issue with Dedicated Shutdown Procedure
a. Insoection Scone (92700)
The inspectors conducted an independent reviewed of the licensee's report that the
Dedicated Shutdown procedure did not account for potential habitability problems
during a specific fire scenario. The inspectors interviewed engineering personnel
and conducted field walkdowns of the Dedicated Shutdown procedure.
b. Observations and Findinas
The licensee determined during review of the Dedicated Shutdown Procedure
(20.000.18) that certain fire and carbon dioxide system dampers may not close or
would reopen during a fire requiring the use of the Dedicated Shutdown Procedure.
The dampers could open with loss of Division 2 AC power and the loss of control
air. The open dampers could create a hazardous atmosphere in a room which is
adjacent to the Division 2 battery room and required for entry while performing
20.00.18. This was reported to the NRC Operations Center in accordance with the
operating license on April 11.
The licensee corrective action was to place Self Contained Breathing Apparatus in )
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the Radwaste Building Switchgear Room to be used if required during a Dedicated i
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Shutdown.
c. Conclusion
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The inspectors concluded that the licensee corrective action for this issue was
acceptable.
02.3 Insoectors identifv Drvwgli Eauioment Discrenancies
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a. Insoection Scoce (71707)
On April 24, the inspectors conducted a walkdown of the drywell to observe the
cleanliness and equipment condition after the licensee had conducted a drywell
closeout inspection. j
b. Observations and Findinas i
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The inspectors noted that the general condition of the drywell was very good, with l
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no debris from outage work.
The inspectors identified a small quantity of an orange substance on the inside of
the protective screen covering the "J" safety relief valve vacuum breaker. Because
of the valve orientation, the inspectors were concerned that the substance might
drop inside the vacuum breaker and prevent reseating following valve actuation.
The licensee was notified, and the substance was promptly removed from the
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valve. It was subsequently identified to be room temperature vulcanizer (RTV)
material, although the source could not be identified.
The inspectors also identified a small oil leak coming from the "A" Reactor
Recirculation Pump motor upper thrust bearing resistance temperature detector.
The pump was not running at the time. The inspectors reported this oil leak to the
Nuclear Shift Supervisor (NSS). Deviation Event Report 97-0647 was initiated to
evaluate the leak.
On April 25, the system engineer and maintenance personnel inspected the leak and
found that the oil had seeped down into an electrical terminal box, and potentially
down into conduits exiting the bottom of the terminal box. The terminal box was
found to contain considerable debris in addition to standing oil. The licensee
believed the terminal box had not been opened since construction. The debris was
removed and the oil was wiped up.
System engineering subsequently performed an evaluation which stated that the oil
leakage was acceptably small to defer repair until a future outage, when parts could
be obtained. The oil leak was presumed to have existed for a long time, on the
order of years, due to the amount of oil present on the outside of the motor. The
pump was determined to be operable. Because the insulation on wiring inside the
affected terminal box was all oil-resistant, no additional electrical checks were
performed. The inspectors discussed the assessment with senior licensee
management and the electrical maintenance engineer, who agreed with the system
engineering assessment.
c. Conclusions
The inspectors were concerned that the operability determination for the "A"
Reactor Recirculation Pump was based on analysis, when electrical checks could
have been performed while the pump was accessible to confirm the analysis. The
inspectors agreed that the leak rate was small and were satisfied that the "A"
Reactor Recirculation Pump remained operable due to the small size of the leak and
the non-critical location on the motor. Each of the conductors exposed to the oil
leaking out was oil-resistant and performed only indication functions. The inspector
determined by reviewing drawings, that the leak was above the minimum
acceptable oillevel for the bearing and did not affect operability. The inspectors
concluded that the licensee's drywell cleanup and closeout activities were effective
based on the cleanliness and equipment condition.
08 Miscellaneous Operations issues (92902)
08.1 (Ocen) Unresolved item 50-341/96016-07: Condensate Storage Tank Freeze
Protection. The inspectors reviewed control room logs, conducted interviews and
reviewed design basis documentation associated with freezing of sense lines for
condensate stora0e tank level indication on January 17,1997.
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While conducting routine control board monitoring, operators noted that control
room CST levelinstrumentation was off scale high. Further investigation by the
licensee and inspectors revealed that the door to the CST instrument panel, located
outside the plant, had been bent open to obtain surveillance readings because the
cabinet lock had frozen. The inspectors reviewed control room logs and determined
that the operators declared CST levelinstrumentation inoperable and took what
was believed to be the correct actions in accordance with TS 3.3.3.
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The inspectors reviewed design basis documentation that stated that CST
instrumentation provide signals to initiate automatic suction path swapover to the ,
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torus for the HPCI and RCIC systems on a low CST level condition. In addition,
annunciators that provide signals to alert control room operators of the need to
perform manual realignment on low level may not be available when the instrument
freezes because this causes transmitter output to indicate offscale high. The
inspector was concerned that degradation of these features could complicate the
i response to an accident.
. The inspectors noted that a similar freeze related event had occurred in 1992.
During that event, the inspector noted that control room operators declared standby ;
feedwater systam inoperable and immediately took actions to align HPCI and RCIC l
to the torus. In the January 1997 event the inspector noted that the licensee l
declared the CST low level actuation feature inoperable and began to take actions l
to restore the instrumentation within operable status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. In one case,
the licensee took prompt action while during the second event, the licensee used
i the TS Limiting Condition of Operation allowed time of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to fix the
- instrumentation. The inspector was concerned with the difference in the licensee's
actions to address similar problems.
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. The inspector reviewed the applicable TS and held subsequent discussions with
- Operations management concerning the differences in the implementation of the
i TS actions. The inspector did not complete the inspection and this item will remain
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open pending inspector's review of the licensee's corrective actions.
fl. Maintenance
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M1 Conduct of Maintenance ;
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M 1.1 General Comments
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a. Insoection Scoce (62703)
The inspectors observed all or portions of the following surveillance and work
activities:
e Division 124/48V Battery Cell Replacement
e Calibration of Division 1 EECW Pump Discharge Pressure Transmitter
e General Service Water (GSW) Intake Dredging
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- Sequence of Events Testing for Destaged GSW Pumps
- Power Supply Modification to P44-F607A and F607B
e MCC Fused Disconnect Switch Lubrication and Disassembly
e Computer Room Chiller Maintenance Activities
e Post Accident Sampling Surveillance
e Reactor Building-Torus Vacuum Breaker Operability Surveillance
e Reactor Flow Unit Functional Check
e HPCI Auxiliary Oil Pump Troubleshooting Maintenance Activities
e Recharging Hydraulic Control Unit Weekly Surveillance
e Reactor instrumentation Reference Leg Backfill Functional Surveillance
e Drywell Cooling Modification Work
b. Observations and Findinas
Maintenance workers and supervisors indicated that work packages had been
getting to the shops at least a week in advance of the scheduled work date, thus
allowing better walkdowns and work preparation. The resulting familiarity of work
scope and system configuration allowed for better pre-job briefs. The inspectors
observed these improvements during several briefs.
The inspector observed portions of the Reactor Protection System response time
testing, noting the testing procedure required the use of a strip chart recorder
capable of recording data at both 4 inches per second and 40 inches per second.
However, the recorder used by the technicians was calibrated in metric units. The
inspectors determined that the use of the different strip chart recorder did not have
a significant impact on the accuracy of the results of the response time testing.
However, the inspector was concerned that the technicians failed to fully execute a
procedure change or question procedure compliance given this discrepancy with
written requirements. The inspector discussed the observation with Maintenance
and plant management, and determined that licensee management expectations
were that the correct scale should have been used or the procedure changed to
permit using an equivalent device. The procedure was revised.
M1.?. Foreian Material Exclusion (FME) Proaram Weakness
a. Insoection Scoce (62703)
The inspectors observed work performed on Control Center Heating, Ventilation and
Air Conditioning System (CCHVAC), including the disassembly of an air actuated
damper for the emergency equipment room cooling system. The inspector also
conducted walkdowns of plant equipment including the diesel generators. The
inspectors reviewed associated DERs and conducted interviews with appropriate
site personnel.
b. Findinas and Observations
The inspectors observed the workers performing preventive maintenance activities
on the equipment room cooling ventilation damper, including the disassembly and
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reassembly of the CCHVAC mechanical equipment room cooling ventilation damper,
and removal of air lines for the assembly.
The inspectors noted the workers did not tape the ends of several pieces of
instrument tubing to preclude the entry of foreign material. In addition, the workers
left the immediate area on at least two occasions, leaving the tubing unprotected.
Common industry practice, the inspector noted, was to tape ends of open tubing
when control of the tubing has been not ensured.
In addition, the inspectors discovered during walkdowns that dust covers were
missing from EDG air receiver gauge test fittings. The dust covers are intended to
prevent entry of foreign material that could impact instrument performance.
Further, the inspectors learned that station personnel had observed the dust covers
to be removed at least a month earlier but had not corrected the problem. The
licensee determined that the covers were not required for operability of the EDGs.
Additionally, the licensee determined that the EDGs were never rended inoperable
because of FME in the test gage test fittings.
The inspectors reviewed a recent DER that stated that the licensee continues to
identify potential weaknesses in the FME program. For example, the drywell had
been closed out even with some materials not documented as being removed from
the drywell. The inspector confirmed that some accountability sheets did not
document that items were removed from the drywell.
In inspection Report 50-341/97002, the inspectors noted that maintenance workers
failed to properly install FME barriers during activities associated with the high
pressure coolant injection valve. As a result of these and other findings in foreign i
material exclusion, the licensee initiated a review of its FME program against l
industry standards. l
c. Conclusions
The inspectors concluded that weaknesses existed in the stations foreign material
exclusion program, and were concerned that current practices in this area could
potentially impact safety related equipment. The inspectors will evaluate the
results of the 1.censee's FME program review and FME practices as an Inspection
Followup Item. (IFI)(50-341/97003-01)
M1.3 Work Performed on the Wrona Eauioment due to Lack of Self-Checkina
a. Insoection Scooe (92903)
The inspectors performed an independent review of the circumstances surrounding
the licensee's identification of the adjustment of the wrong circuit card during
calibration work and leak repairs made on an incorrect level switch. The licensee's
root cause evaluation and corrective actions were reviewed for adequacy. The
event and corrective actions were discussed with appropriate maintenance
supervisors. The inspector reviewed work packages and conducted interviews with
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Maintenance personnel. The inspectors performed walkdowns of affected
components.
b. Findinas and Observation
b.1 Mechanical maintenance personnel were assigned to perform repairs to a leak on
the barometric condenser level switch to support calibration activities. The
inspector walked down the RCIC system and noted both high and low level
switches located near each other. The inspector interviewed personnel and learned
that mechanical maintenance personnel attempted to stop the leak by adding
packing on two previous occasions. After all attempts were unsuccessful, the
licensee identified that the leak repair efforts were performed on the wrong level
switch.
The inspector reviewed the work package and noted that the work had been
treated as on emergent work item and was not walked down prior to starting the
work. Interviews with mechanical maintenance personnel revealed that the work
on the wrong level switch occurred as a result of inadequate use of self checking
and verification techniques prior to starting the work on the two occasions.
The inspector verified that the inappropriate work activities did not permanently
damage the component. The inspector verified that the correct level switch was
repaired and the calibration performed as required.
b.2 On April 2, I&C technicians performing a calibration on computer monitoring inputs I
for the general plant monitoring computer per procedure 44.030.255 inadvertently
adjusted the wrong card. The technicians discovered their error immediately when
the expected system response was not observed during an adjustment. Work was
stopped and the control room informed. The two cards involved were subsequently
re-calibrated.
The licensee concluded the event was a result of inadequate use of self-check. The
inspectors discussed the event with l&C supervision and examined the panel and
noted that the cards involved were in close proximity to each other (less than
1 inch apart), and had a similar appearance. The licensee was considering using
self-adhesive tags to mark components being worked in such situations. The
significance of the error was minimal, as it involved inputs to a monitoring
computer which was not required for plant operation.
DER 97-0501 was written to document the event and track corrective actions,
c. Conclusion
The inspectors concluded that these events were caused by lack of self checking.
The safety significance of each issue was minor. However, the inspectors were
concerned by the lack of attention to detail during work.
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M1.4 Failures of RCIC inboard Steamline Isolation Valve Caused by inadeauste
Procedures and Station Personnel Errors
a. Insoection Scoce (92903)
The inspectors conducted an independent review of the circumstances of the a
failure of the RCIC valve after corrective maintenance. Work packages for all work
on the valve during the outage were reviewed. The surveillance history was also
reviewed. The as found condition of the valve was discussed with maintenance
engineers, and the surveillance logic testing was discussed with the system
engineer. Scheduling and assignment of post-maintenance testing (PMT) was
discussed with the Work Planning Supervisor and personnel in the Surveillance
Group,
b. Observations and Findinas
The RCIC Inboard Steamline isolation Valve (E5150f007) failed to open on demand
during a surveillance run as PMT for motor pinion gear work. Following corrective
maintenance, the valve was tested and retumed to service, but was then found to
be open with an isolation signal present.
On April 17, a control room operator identified that E5150-F007 was open but
should have been closed; the valve logic had a valid isolation signal present for low
steam line pressure because the plant was in cold shutdown. The valve had been
opened two shifts earlier during performance of surveillance 44.060.001.
DER 97-0600 was written to document the issue and track corrective agtions.
Maintenance conducted troubleshooting under Work Request (WR) 000Z974252,
which identified that the 7-strand wire used to transmit automatic isolation signals
had broken conductors at a lug connection inside the limit switch cover of the
l actuator. Yhe limit switch cover had been removed twice during the outage for
maintenance activities. Maintenance concluded that the wire was inadvertently 1
damaged during one of those maintenance activities. The inspectors reviewed the !
'
PMTs on the valve worked during the current outage and confirmed that they did
not test the automatic isolation function. Maintenance engineers stated that
current PMT philosophy was to test only those portions of the circuit which were
within the work scope (i.e., were known to be disturbed). The removal of the limit
switch cover was not recognized as part of the work scope. Thus the valve was l
not tested for potential damage to the 7-wire cable. The valve was only tested for !
the remote manual operation function.
The licensee had identified that this type of conductor in MOV actuators was i
susceptible to damage during a similar problem in 1993, as documented in I
DER 93-0013. The inspectors determined that maintenance work practices had not
been changed to minimize the possibility of damage, nor was testing changed to
verify that no damage was caused during work inside the limit switch compartment i
as a result of that event. A caution was added to the MOV maintenance procedure
'
to alert workers of the potential for damage. At the conclusion of this inspection,
15
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!
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maintenance was re-evaluating the method used to determine the scope of PMT for
MOV work to include a verification of electrical continuity to the maximum practical
extent, rather than limiting testing to just check components within the work
scope.
1
The inspectors reviewed the work and surveillance history for the RCIC system, and
found that 44.060.001 had been partially performed on April 10 as PMT for valve
work, and again partially performed on April 17 following troubleshooting of
E5150 F007. The inspectors reviewed surveillance 44.060.001, and WRs
000Z974252 and 000Z974210 and identified the following deficiencies:
e Both partial surveillances performed steps which opened E5150-F007, but
no steps were performed to shut or verify it shut.
e 44.060.001 did not require verifying the position of E5150-F007 at the
conclusion of the surveillance,
o The steps performed as partial surveillance for PMTs on these WRs did not
cause the valve to be shut intentionally, and operator logs indicated no
verification of RCIC system lineup was performed at the conclusion of these
partial surveillances.
The inspectors discussed the surveillance with the system engineer, and determined
that E5150 F007 should have automatically shut when the jumper was removed
that disabled the low steam pressure isolation. However, operators and l&C
personnel performing the surveillance failed to recognize and verify that the valve
did not shut as expected.
c. Conclusions
The failure was not detected during post maintenance testing of the valve, resulting ,
in returning the system to service in an abnormal lineup. The inspectors concluded l
that this problem was indicative of lack of attention to detail, lack of questioning (
attitude by operators during the surveillances and system restoration, and
procedures that were inadequate to ensure the system was restored to a proper
lineup following testing. These problems are significant because E5150-F007 was
a safety related valve in an ESF system; this normally inaccessible valve had a
I
primary containment isolation function which was not functional. The significance
was somewhat mitigated because the plant was in cold shutdown at the time, so
the RCIC injection function and the containment isolation function were not I
required. The failure was identified by the licensee. 1
The inspectors consic'ered that Maintenance corrective actions for previous failures
of small wires inside MOVs were weak in that actions were not taken to verify that I
such wires were functionally checked during work which could have damaged
them.
l
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_ _ _ . -- . _ _ __ _
,
.
i-
The inspectors concluded that surveillance procedure 44.060.001, and work
'
request 000Z974252 were inadequate to the circumstances. Specifically,
- 44.060.01 failed to require a verification that the RCIC system was restored upon
completion of testing, and WR 000Z974252 failed to specify a PMT that
functionally tested the repaired conductor. This was considered a violation of
'
10 CFR Part 50, Appendix B, Criterion V, " Instructions, Procedures, and Drawings."
(VIO)(50-341/97003-02)
The inspectors were concerned by the licensee's practice of performing partial
surveillances by specifying selected non-sequential steps. The inspectors will
review this issue in order to assess the conformance to 10 CFR 50.59 safety
evaluation process. This will be tracked as an Unresolved Item pending further NRC
i inspections into the administrative controls rad actual practices of specifying
selected, non-sequential steps from a surveillance procedure for testing.
(URI)(50-341/97003-03)
M1.6 Conclusions on Conduct of Maintenance
The inspectors noted that equipment performance was very good at the end of this
inspection period. Plant startup went well, with few equipment problems.
4 Maintenance support during startup testing and in responding to equipment
problems was very good, and Outage Management and Operations Support
- personnel helped coordinate startup testing.
'
However, this report documents a significant number of errors and problems during
,
the conduct of maintenance activities during this inspection period. The inspectors
'
noted that the licensee identified a number of maintenance related problems and
took prompt corrective actions. These issues included:
l e The Division 2 Torus Spray Valve (E1150-F027A) failed to open on demand
during a surveillance because an electrical terminal was not adequately
tightened. The valve actuator had been worked and successfully passed its
- PMT two days previously. (DER 97-0467)
e The Division 2 RBCCW Supply isolation Valve (P44-F603B) failed to stroke
due to a limit switch damaged during maintenance activities. (DER 97-0662)
e Reactor water chemistry conductivity monitor P33-R500 indicated erratically
because two wires were reversed during restoration. (DER 97-0684)
e GSW pump #3 required several pump packing adjustments and eventual
replacement. (DERs 97-0420, 97-0670)
e The Division 1 EECW Drywell Return Outboard Isolation Valve (P44-F607A)
had wiring errors made during modification work that caused blown fuses
and damaged the control transformer. (DER 97-0623)
17
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.
..
1
e The East Stator Water Cooling Pump Breaker Closing Spring Charging Motor l
togg,ie switch was found in the OFF position after it had been returned to j
service. (DER 97-0759) !
6 The MCC disconnect switch for the South Reheater Seal Tank Vent Line
isolation Valve (N2200-F701) did not have power fuses installed, causing it I
to fail to open on demand when operators attempted to place the South
Separator Seal Tank in service during plant startup. (DER 97-0758)
e MCC disconnect switch for Telephone Room Air Conditioning Unit
(X4101-B023) did not have power fuses installed. (DER 97-0617)
e RBHVAC was inadvertently tripped because of improper use of electrical
prints (DER 97-0593).
e Welding was performed in the reactor building during an SBGT surveillance
despite periodic announcements to prohibit such work. Charcoal filter
testing on April 18 confirmed that damage did not occur (DER 97-0541).
Additional examples can be found elsewhere in this report.
Self-identification of maintenance problems showed improvement during this
inspection period. However, the significant number of worker-induced equipment
problems, particularly those involving safety related equipment, was concerning.
The inspectors concluded that these examples were indicative of an adverse trend
in personnel performance during the conduct of maintenance.
During this inspection period, Maintenance worked to resolve two issues with
potentially high safety significance and a large number of components affected,
namely MCC switch lubrication / seismic qualification, and MOV motor pinion gear
inspection.s. Little assistance was initially obtained outside the Maintenance
organization on either issue. The inspectors noted that the Engineering staff
handled a number of significant issues of similar safety significance and magnitude i
in November-December 1996; inspection Report 50-341/96013 assessed those
efforts and concluded that the licensee effectively identified the significance and
magnitude of the problems and applied available resources, including industry
assistance, to resolving them. This markedly contrasted with the licensee's
performance in resolving the above two maintenance issues that were identified
during this inspection period.
M2 Maintenance and Material Condition of Facilities and Equipment
M 2.1 480 Volt MCC Disconnect Switch Problems
Significant problems had been noted with the manually operated fusible disconnect
switches used in ITE, Series 5600, motor control center (MCC) starters. For
proper operation, the switch must be closed and latched when equipment is in
operation or standby service. Opening the switches is normally required for
18
.
.
surveillances, maintenance, or other activities requiring systems or equipment
isolation. If the latching mechanism did not engage when the switch was closed,
the switch would usually reopen; however, if the switch stayed closed without
latching, as it dometimes did, the switch would open when subjected to a light tap
or vibration.
M2.1.1 Problem Descriglion and Corrective Action
a. Insoection Scoon
The inspectors reviewed records documenting problems with the fusible disconnect
switches and related MCC problems and discussed the problems with licensee
personnel,
b. Observations and Findinos
1
On April 9, following severallicensee identified instances of MCC fused disconnect
switches being found out of position open, the inspectors identified a concern with
the seismic qualification of these switches. The licensee notified the NRC per
10 CFR 50.72 on April 10. The inspectors reviewed selected DERs on the switch
problems and noted that the problems had been identified as early as 1992.
Detailed cause investigation and specific corrective actions were not taken.
Licensee personnel stated that the problems were not considered significant and the
failure rates were within the accepted failure rates for this type switch.
During the current forced outage, the licensee performed inspection, cleaning and
lubrication on all 1120 fusible disconnect switches. This was considered temporary
corrective action to allow operation of the equipment for the current operating
cycle. This action required operation of the switches and documentation of the as
found condition of the switches. Spray cleaner was then sprayed sparingly into the
switch pivot points and then was dried by air. A spray lubrication was then
sprayed into the switch pivot points and the switch was operated multiple times
untilit operated smoothly.
Problems with sluggish operation or the inability to close were noted with more
than 20 percent of the "as found" switches. Switches that would not close after
the cleaning and lubrication were removed from service and replaced. Several of
tmso replaced switches were disassembled and inspected. Hardened grease was
found in the pivot points of the disassembled switches. Grease from two of the
disassembled switches was analyzed and evaluated for the effect of mixing with
the spray lubricants and cleaner. These evaluations indicated that no problems
would be created with the mixing of the lubricants. Some problems were also
encountered during the implementation of corrective actions. These included an
ESF actuation involving safety-related ventilation caused by an inadequate work
impact review.
The cleaning and lubrication was considered to be temporary and licensee personnel
stated that permanent corrective action for the fusible disconnect switches was to
19
. _ _ _ _ _ _ - _ _ _ _ - - _ _ _ _ - _ - _ _ _ .
. 1
..
be determined at a later date. This is considered to be an unresolved item pending
review of the proposed permanent corrective actions (50-341/95003-04).
c. Conclusions
The corrective action process failed to recognize the significance of the switch
problem. The licensee was severely hampered by previous failures to document
difficulties in switch operation. In addition, there was a lack of communication and
coordination between the organizations involved in the investigation and
troubleshooting process. Systems engineers were apparently not aware of the )
sluggish operation or the inability of the switch to close that was experienced by l
plant operators. Maintenance assisted operators in getting the switches closed I
without work requests or other authorization and neither maintenance or operations
documented the problem. Inadequate communication was evidenced when
information, provided to the NRC inspectors during the temporary inspection and
cleaning of the switches was in progress, varied considerably between licensee
personnel. Criterion XVI of 10 CFR Part 50, Appendix B, " Corrective Action" l
requires that, for significant conditions adverse to quality, the cause of the
condition be determined and action taken to preclude repetition. The failure to l
recognize the significance of the problem and take prompt actions to prevent
recurrence is an apparent violation.
l
M2.1.2 Inadeauate Preventive Maintenance l
l
a. Insoection Scoca
Since the lack of preventive maintenance (PM) appeared to be a significant
contributor to the cause of problems with the fusible d;sconnect switches in the ITE
Series 5600 Motor Control Centers (MCC), the inspectors reviewed selected PM
records for the MCCs and discussed MCC PM with cognizant licensee personnel,
b. Observations and Findinas
l
The inspectors noted that the ITE vendor manual for the MCCs, VME5-7.1, l
Revision D, recommended that PM, including a visual inspection and manual or
electrical operations of MCC components, be performed twice per year. The
manual also recommended that a more extensive inspection and cleaning be
performed periodically, with the period not to exceed 18 months.
The inspectors reviewed the Sections of Procedure 35.306.008, " Motor Control
Center Load Compartment," Revisions 30 through 36, that applied to the MCC
fusible disconnect switches. This procedure did not specify the periods that the PM i
should be performed. Licensee personnel stated that portions of the procedure l
were performed at different times and that the PM frequencies varied from 18 l
months to 6 years. The vendor recommendation for twice a year visualinspection !
and operation of MCC components was not addressed. Engineering justifications
for the variance in frequency or the acceptability of not performing the vendor i
recommended PM tasks did not exist. I
l
20 '
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_ _ _
- - - . . . - . .- - -- ...- -.
-
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2
4 During discussions, licensee personnel stated that, until recently, periodic operation
and cleaning of the fusible disconnect switches for the 480 volt starters was not
i performed if the individuals performing the maintenance did not consider it
i necessary. This portion of the PM task was performed at the option of the
j individuals performing the PM. Checks in the blocks for the fusible disconnect ;
~
switch portion in the record copy of the procedure could be made to indicate either l
j that the switches were cleaned and actuated or that the switches were observed
l and looked "OK." The amount of PM performed on the control switches could not
j be determined from records.
i
a
inadequate PM on these MCC fusible disconnect switches was apparent from the
"as found" conditions of the switches. Over a period of time the switches became
~
- dirty and grease became dry and hardened. This caused the switches to become
l difficult to close, sluggish to operate and, in some cases, the switches would close
'
but would not latch. As previously stated, unlatched switches would open with
- vibration or a small bump resulting in the loss of power to plant components. The
480 volt MCC breakers affected the operation many important pieces of both
- safety related and non-safety related systems and components through out the
i plant.
1
] c. Conclusions
! !
It was evident from a visual inspection of the ITE 480 Volt MCCs that preventive l
!
!
maintenance of the fusible disconnect switches was inadequate. Previous
i violations had been written on problems with these MCC starters in the recent past.
i The actions taken on the identified violations were narrowly focused and the lack of
i plant had been a significant issue during early operations of the plant. Lack of PM
i that has an effect of this magnitude on plant equipment indicates a possible overall
,
weakness in the PM program.
!
l The ITE 480 Volt MCCs affect the operation of valves and other components in
- many plant systems. The failure to perform preventive maintenance on the ITE 480
'
volt MCC fusible disconnect switches, as required by Section 4.2 of
l Procedure 35.306.008, is considered an apparent violation of 10 CFR Part 50,
j Appendix B, Criterion V.
!
l M2.2 Failure of the Hiah Pressure Coolant Iniection Valve Resultod in Larae MOV
j Insoection Effort
a. Insoection Scoce
The inspectors reviewed the licensee's actions surrounding the failure of the HPCI
l Injection Valve (E4150-F006). This included reviewing the history of previous
j similar MOV failures, licensee's root cause determination, corrective actions, MOV
inspection results, and safety significance.
i-
21
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- - , - - , - , , - v-n- - .,-- - - . - , - - - - . - - . - - - - - - - -
. _ _ . _ _ _ _ _ _ _ _ _ . _ __ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __ _ _ _ _ _ _ _ _ _
i
-
1
)
i
s.,
j b. _ Observations and Findinas
i
i b.1 Event
s
l
During surveillance 24.202.05, "HPCI System Cold Shutdown Valve Operability
Test," on February 16,1997, while the plant was in a forced outage, the
l E4150-F006 failed to open on demand. The MOV was a 14-inch Powell flex wedge
!
gate valve equipped with an SB-3 operator. The licensee verified that the valve
.
open coil was energized and the motor was drawing current. At the valve, it was
i
noted that the motor was operating, however, there was no valve stem movement.
i The valve failure was attributed to a worn motor pinion gear set screw, such that
) the set screw no longer engaged the motor shaft to prevent the pinion gear from
- " walking" up the shaft and disengage from the worm shaft helical gear.
1
I b.2 Backaround
I During the 1980's there were a number of MOV failures in the industry due to
i problems with the motor pinion gear key and set screw. At Fermi there were two
j examples of set screw problems. These included a set screw that backed out
,
(1987) and a cross threaded set screw (1993). In 1989, Limitorque issued
Maintenance Update 89-01, which recommended a fix for the set screw problems.
This included spot drilling a hole in the motor shaft and the use of locktite or lock
wire on the set screw to prevent it from backing out. The licensee was unable to
l find any documentation on how this maintenance update was addressed at Fermi.
j The licensee, however, did revise MOV maintenance procedures 35. LIM.004,
j 35. LIM.005, and 35. LIM.006, in 1988 to include the required fixes stated in the
i update.
!
l The NRC issued several Information Notices (IN) during the 1980's and 1990's that
'
addressed the problems with the motor pinion gear problems. During the licensee's
- review of IN 94-10, " Failure of Motor-Operated Valve Electric Power Train due to
! Sheared or Dislodged Motor Pinion Gear Key," as documented in Operating
i
Experience Report Disposition Memorandum 94-76, dated August 22,1994, the
l licensee identified five issues that needed to be addressed. These issues included
! incorrect assembly of motor pinion gear to new motor shafts, inadequate strength
4 of motor pinion key stock, lack of motor pinion set screw countersink on motor
i shaft, lack of staking on end of motor shaft at keyway, and lack of lockwire holding
l the pinion set screw. The disposition indicated that "Many MOVs in the plant have
! " suspect" conditions leftover from the late 70's, early 80's inadequate assembly
,
techniques." The licensee's philosophy was that the maintenance update would be
- incorporated in the MOVs "when an opportunity presents itself," (i.e., motor
3
removed for other work). The memorandum atro concluded "there is still a risk of
l failure on many existing MOVs." The licensee 1, preventive maintenance program
3
for MOVs, however, did not require the motor to be removed on a specified
frequency. As such, for the HPCI injection valve, the motor shaft was not spot
,
drilled, nor was there a schedule in place to have the shaft spot drilled (the set
i screw was lockwired).
!
4
l 22
I
!
!
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_ _ _ _ _ _ _ _ _ _ _ _
.
.
The inspectors considered that LER 97-002, " Failure of the High Pressure Coolant
Injection System Pump Discharge Valve to Open," was misleading when it stated
"The spot drilling for pinion gear set screws is being systematically implemented at
Fermi 2, but work on valve E4150-F006 had not yet been performed..." since the
spot drilling of motor shafts was not specifically scheduled. Maintenance records
were not sufficiently detailed for the licensee to determine how many motor shafts
had been spot drilled, or set screws lockwired or used locktite. This issue
potentially affected 187 safety-related MOVs. During the inspection, the licensee
also stated for another MOV generic issue involving the key material, ANSI 4140
versus 1018, that they did not have documentation to verify that all valve keys
were of the proper material. The key material, however, did not play a part in this
failure.
b.3 Corrective Actions
The actions taken and/or planned by the licensee were considered good.
Approximately 64 safety significant valves were inspected to ensure the spot
drilling was in place. The valves were chosen based on their safety significance,
which was determined from the Probabilistic Risk Assessment or from a review of
the Maintenance Rule systems, structures and components. The licensee evaluated
the results of these inspections, and determined no subsequent inspections were
warranted prior to startup. The remaining approximately 120 safety-related and
important-to-safety MOVs were to be inspected during the following 2 outages.
b.4 Safety Sianificance
This was a generic concern for all MOVs in the plant and could have introduced a
common-mode failure that could potentially affect multiple systems. The failure of
the HPCI injection valve would prevent automatic operation of the HPCI system and
the system would not function as designed to provide a source of high pressure
flow to the core to mitigate the effects of a small break loss of coolant accident.
This valve was located in an inaccessible part of the plant during operation and
accident conditions. In the event HPCI failed, RCIC and the remaining emergency
core cooling (ECCS) systems should be available to mitigate the accident. The
Automatic Depressurization System would be available to reduce reactor pressure
such that the low pressure core spray and RHR systems would be able to inject into
the reactor system.
c. Conclusion
The licensee was not timely in resolving a known industry issue when the
corrective actions recommendations were issued by the vendor in 1989. As a
result, the HPCI E4150-F006 MOV failed to open on a demand signal from the
control room. The failure mechanism was a generic concern for all MOVs in the
plant and could have introduced a potential common-mode failure. This was
considered an apparent violation of 10 CFR Part 50, Appendix B, " Corrective
Action" for failure to implement corrective actions for a condition adverse to quality
in a timely manner.
23
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,
.
M2.3 24/48 Volt Batterv Cells Reolaced Without Beina Fully Charaed
"
a. Insoection Scoce (62703,92903)
- The inspectors reviewed the recent maintenance history for the 24/48 volt battery.
j Electrical maintenance supervision, Planning and Scheduling Supervisor, and the
- system engineer were interviewed. The design basis document, operator logs, and
- surveillance results were reviewed to determine battery operability. Administrative
procedures for work control and surveillance were reviewed to determine if proper
controls were in place, and completed work packages were then reviewed.
4
b. Observations and Findinas
The Division 124/48V battery had three cells replaced (a single jar) under
1 WR 000Z964874, but the cells were not properly charged prior to returning the
battery to service on February 12. This was not recognized until March 20, when a
,
quarterly battery check surveillance (job AB62961219) identified that the new cells
i failed to meet the minimum required individual cell voltage (ICV) of se2.13V by
i 0.01V. The system engineer recommended charging the entire battery to restore
the low ICVs, but this was unsuccessful, so the cells were replaced,
i
' The electricians assigned to install the cells determined that they required additional
! water charging before installation. From experience, they knew that batteries
should be charged following the addition of water. This work was performed and
- noted in the remarks as " shop work" in the WR 000Z964874. The inspectors
determined that the work package was not changed to include this work scope
addition.
The inspectors reviewed WR 000Z964874, and discussed the event with the
system engineer and electrical maintenance supervisors. The inspectors noted that
WR 000Z964874, which specified performing steps from maintenance procedure
- 35.310.02,"24/48 VDC Electrical System - General Maintenance," did not contain
! any instructions to perform pre-installation checks to ensure the new cells were
ready to perform their intended function, such as electrolyte level and specific
gravity checks, or charging the new cells.
,
The system engineer stated that spare cells maintained in stock offsite were
charged every 6 months. While investigating this problem, the system engineer
' identified that the new cells had last been charged 5 months previous to
installation. DER 97-0480 was written by the system engineer upon discovering
- the electricians had charged the new cells at the wrong voltage.
The vendor manual required charging at 2.33 - 2.38V per cell, but
3
WR 000Z964874 indicated that charging was performed at 2.17 volts per cell.
The inspectors determined that the electricians consulted neither the vendor manual
nor the system engineer in determining the voltage to charge the new cells, but had
instead reasoned a value from operating parameters. System engineering
l
!
4
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l
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performed an operability assessment and determined that the Division 124/48V
battery was operable.
The PMT for 000Z964874 specified performing 24/48VDC Weekly Battery Check
(47.310.03), but the inspectors identified that this procedure did not require
checking the ICVs and specific gravity for the newly installed cells (only for the
pilot cells). This deficiency was not identified by the work group supervisor or the
NSS during PMT review. In discussions with the inspectors, the Electrical
Maintenance Supervisors and the Work Planning Supervisor agreed that the PMT
specified was inadequate to verify the new cells were in a proper condition.
Licensee corrective actions planned for this event were to revise the battery
installation procedure to include cell preparation steps, including charging new cells
before installation.
The inspectors reviewed the DC Electrical System Design Basis Document and
determined that the 24/48V batteries perform support function for safety related
loads. The batteries provide backup power for four hours on loss of all AC power
to neutron monitoring and process radiation monitoring instrumentation. The
inspectors reviewed the operability determination for the as-found condition of the
battery and support documentation, and concluded that the battery retained
sufficient capacity to perform its function.
The inspectors reviewed MWC02, " Work Control," and determined that it did not
prevent performing shop work or preparation work without steps in the work
request.
c. Conclusions
The inspectors concluded that WR 000Z964874 and Maintenance Procedure
35.310.02 were inadequate to ensure new battery cells were installed in a l
condition to support the function of the battery. This was considered an example ;
of a violation of Technical Specification 6.8.1.a and Regulatory Guide 1.33,
" Quality Assurance Program Requirements (Operation)." (VIO)(50-341/97003-05)
The inspectors were concerned that this WR relied heavily on craft skill of the
workers. Previous concerns about the quality of electrical maintenance procedures
were documented in Inspection Reports 50-341/95012 and 50-341/96010, each of j
which resulted in a violation. This continued to be a concern.
1
The inspectors considered that the licensee's work control procedure was weak in l
that pre-job steps were not specified or documented in a standardized manner, in
this example, preparation steps were not specified, but were performed and
documented by workers without revising the WR for the change in scope. The
inspectors determined that this practice was not precluded by the work control
procedure, but was considered a programmatic weakness.
25
1
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.
.
M 2.4 Shiocina Pluas Found in Plant Transmitters
The inspectors conducted walkdowns of various plant locations
and noted that shipping plugs were found installed in some transmitters in the .
plant. The inspector reviewed documentation that showed that shipping plugs had l
been removed from both safety and environmentally qualified transmitters. l
However, the inspectors were concerned with the scope and the application of the i
remaining transmitters with installed plugs. The concern was that the installed
plugs would degrade and allow moisture, dust or dirt to enter, potentially resulting
in transmitter failure.
The inspector noted that in some cases sealant was being used over plugs.
Moreover, the inspector noted that for some important safety transmitters it could
not readily be determined if a metal plug has been installed due to the presence of a
non-trarisparent sealant. The inspector was also concerned that shipping plugs
might remain in transmitters for nonsafety related equipment used during abnormal
and emergency operating procedures. Some of the affected transmitters include
those associated with Main Steam Leakage Detection System, Main Steam System,
and Reactor liuilding Closed Loop Cooling Water System flow indication.
The inspectom will continue to evaluate the scope and application of the
transmitters that may be affected, as well as previous corrective action for the
issue. This will be tracked as an Inspection Followup Item. (IFI)(50-341/97003-06)
M3 Malntenance Procedures and Documentation
M3.1 Emeraency D esel Generator (EDG) Station Air Comoressor (SAC) Left in Off
a. Insoection Scone (92901)
The inspectors performed an independent evaluation of the causes and corrective
actions for an EDG 11 Starting Air Low Pressure alarm. Emergency diesel
generator operability during the event was evaluated by reviewing operator logs,
annunciator response procedures, technical specifications (TS), and the system
operating procedure (SOP). Planned corrective actions were reviewed, as were the
results of subsequent findings. The surveillance procedure was reviewed and
compared with administrative controls for operation of equipment to determine the
adequacy of the procedure. The event and corrective actions were discussed with
Operations management.
b. Observations and Findinas
On April 2, a non-licensed operator performed a routine oil sample of the starting air
compressor for EDG 11. The operator knew from experience that the compressor
oil level might go below the minimum operating oil level while removing a sample,
although the surveillance sheet did not include a caution in this regard. To ensure
the compressor would not start while sampling the oil, the operator turned the
compressor off locally, without informing the control room. Several hours later, the i
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EDG 11/12 Starting Air Tank Pressure Low alarm was received in the control room.
Per the annunciator response procedures, an operator was dispatched to
investigate. The operator identified that EDG 11 air pressure was 220 psig and the
SAC local switch was out of position in OFF. The starting air pressure was
maintained above the TS minimum allowable pressure during this event (215 psig),
so EDG 11 remained operable. A valve position verification was performed for the
remainder of the EDG 11 starting air system, with no additional discrepancies
noted. The compressor was started and air pressure restored.
The I censee's investigation determined that the operator taking the oil sample had
forgotten to restart the compressor due to inadequate self-checking and a weak
procedure. By not informing the control room of the actions, the operator
prevented possible backup by other members of the shift from detecting the error.
There was no pre-job brief conducted for this work.
The inspectors determined that MOP 02, " Independent Verification," Step 3.2.1.3
required that an independent verification be performed in this situation.
Specifically, that step stated that equipment important to safety shall have
independent verification performed to ensure that equipment, valves, and switches
that were placed in an abnormal position are correctly aligned. The inspectors
identified that Surveillance Job AF11970403 did not include appropriate
instructions to turn off the SAC for equipment and personnel safety during oil
sampling, nor did it include independent verification for return to service.
The inspector discussed the event with the Operations Superintendent. Deviation
Event Report 97-0502 was written for Operations to take a broad look at the
control of equipment during work not covered by SOPS. Operations reviewed all
237 preventive maintenance events assigned to Operations and identified 32 events
that required additional instructions to properly perform the jobs, including events
which should have required independent verification steps but did not. Additional
reviews assigned to Radiation Protection (RP), Chemistry, Maintenance, and System
Engineering were stillin progress at the conclusion of this inspection.
c. Conclusions
The inspectors concluded that EDG 11 remained operable throughout this event due
to the continuous availability of an adequate supply of starting air within TS- l
required pressure limits. The inspectors considered the licensee root cause
determination to be adequate, and the corrective actions sufficiently broad to
address the larger issue; namely, the proper configuration control of safety related
equipment during evolutions which do not constitute a complete, formal procedure.
The inspectors concluded that the operator missed an opportunity to identify that
the work instructions were deficient and have the procedure changed.
Inspection report 50-341/97002 documented inspection findings of weak
configuration control during troubleshooting. The inspectors considered this event
to be an additional example of configuration control weaknesses during work ,
activities. I
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The inspectors concluded that work instructions in PST job AF11970103 were
i
inadequate to safely perform the oil sample and ensure the SAC was restored to the
proper lineup and verified as required. This was a violation of 10 CFR Part 50,
Appendix B, Criterion V. (VIO)(50-341/97003-07)
M7 Quality Assurance in Maintenance
M7.1 Licensee Self-Assessment Activities (40500)
a. Insoection Scoos (4050_Q1
The inspectors reviewed multiple licensee self-assessment activities. On-Site l
Review Organization (OSRO) review of various safety issues, including MCC fuse
disconnect switch issue, were observed for effectiveness and compliance with TS
,
requirements (see M2.1).
b. Observations and Findinas
,
The inspector questioned station management concerning the lack of an initial
review of the MCC fuse disconnect switch issue by OSRO committee before
activities were implemented to correct the unlatching problem. In response to
inspector concerns, the plant manager referred the issue to OSRO for review.
! The inspector observed the OSRO meetings and questioned the conduct and
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effectiveness of the committee. For example, the inspector observed that some
questionable laboratory results were not fully questioned to gain a complate
understanding of the issue. Specifically, the interaction of the cleaning solvent with
the existing grease accelerated the hardening of the grease. OSRO did not
,
questioned the significance of these results. Other pertinent information not initia!!y
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or fully discussed by OSRO included issues related to other failures of the fuse
disconnect switches, seismic qualification, MCC inspection findings, and the
relationship between root cause and corrective action. After the OSRO meeting, an
I anonymous DER was written discussing concerns with the effectiveness of the
OSRO meeting. Senior plant management was addressing this DER.
c. Conclusion
!
The inspectors concluded that the On-Site Review Organization was initially
ineffective in resolving issues associated with MCC Fused Disconnect Switch.
Corrective actions were implemented on a substantial portion of the affected
population before the adequacy of the corrective actions were adequately assessed.
The inspector was concerned with the effectiveness of the OSRO committee to
perform special reviews, investigations or analysis, and reports requested by the
plant manager as required by Technical Specification 6.5.1.6. This will be tracked
as an Unresolved Item pending review of licensee corrective actions for improving
OSRO effectiveness. (URI)(50-341/97003-08)
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M8 Miscellaneous Maintenance issues (92902)
M8.1 (Ocen) Follow-Uo item 50-341/96016-04: Review of licensee practices for
protecting equipment inside containment from inadvertent damage during outage
work. During this inspection, the licensee concluded that the RCIC Steamline
Inboard Isolation Valve (E5150-FOO7) became stuck in manual operation because
the declutch lever was stepped on, requiring MOV disassembly to repair the
actuator. The valve was located inside the drywell in an area that was difficult to
traverse. This was considered to be an additional example of safety related
equipment inside the drywell that was inadvertently damaged during outage work. )
The inspectors observed drywell work during this inspection period and found that l
there was little scaffolding installed for personnel access, and the scaffolds that I
were installed were only in specific work areas. Equipment in non-work areas l
which were difficult to access remained vulnerable to being stepped on. The
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vulnerable areas included the area near the main steem lines and most areas above
the main floor. In response to the latest failure, the licensee issued a site-wide
reminder to avoid stepping on plant equipment and to report any potential damage
to the control room. The inspectors noted that climbing on equipment in the certain
portions of the drywell was unavoidable if scaffolding were not installed. The
inspectors will continue to review drywell equipment performance and licensee
actions to avoid incidental damage to this equipment. This item will remain open.
M8.2 (Closed) Unresolved item 50-341/97002-04: NRC review of MOV Motor Pinion
Gear Inspection Results. Licensee inspections of 67 MOVs deemed important to
safety identified: !
e 10 motor shafts had not been spot drilled.
!
e 15 keys were not properly staked to the shaft (only one key was found
protruding from its expected position). 1 1
1
1
e All set screws were secured with either lockwire or Locktite.
- 14 set screws were found "slightly" loose. Set screws were tightened up to
half a turn.
e 1 motor pinion gear key was missing.
The deficiencies noted during the inspections were corrected and the valves
retested prior to their return to service. The licensee concluded that the corrective
actions dramatically reduced the pinion gear failure potential for the safety j
significant valves that were inspected. However, the inspection results did not I
warrant the immediate corrective actions to additional MOVs. Based on the
inspection results, the lower safety significance of the remaining affected MOVs,
and a schedule to incorporate the corrective actions over the next two refueling
cycles, the inspectors considered this acceptable to maintain MOV operability in the
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plant. The concern with failure to take proper corrective actions from previous
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identification is addressed in Section M2.2 of this report. '
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lil, Enaineerina j
E1 Conduct of Engineering l
E1.1 Inadeauate EDG Loaic Testina
a. Insoection Scone (92902)
Modifications were reviewed to ensure that safety evaluations were performed
satisfactorily, necessary approvals were obtained when required, engineering
documents and procedures were included when required, and post-modification
testing was correctly identified and completed,
b. Observations and Findinas 1
Enaineerina Desian Packaae (EDP) No. 8355
The licensee identified that non-essential EDG trips, such as tube oil high
temperature, were not automatically bypassed by the "A" start circuit if the "B" :
start circuit failed. Fermi's UFSAR stated that there were two emergency start l
circuits: either of these relays willinitiate EDG starting as well as bypass the I
unnecessary trips. This modification was field completed on June 1,1989. I
The licensee added a SEX emergency start isolation relay to each EDG start circuit.
These relays were normally de-energized during EDG operation. Normally closed
contacts (1/2) were added to the "A" start circuit and (5/6) were added to the "B" I
start circuit. The two start circuits were provided to increase reliability, and met
the requirements of the Institute of Electrical and Electronic Engineers (IEEE)
Standard 387 - 1977, "lEEE Standard Criteria for Diesel-Generator Units Applied as
Standby Power Supplies for Nuclear Power Generating Stations." If an essential .
EDG trip had occurred, such as high differential generator current, relay SEX would l
be energized and prevent automatic start of its associated EDG. During an I
automatic EDG start, either the ESA or ESB emergency start relays would bypass l
the non-essential EDG trips. The loss of a single start circuit would not prevent l
automatic start of it's associated EDG if a non-essential trip had occurred. l
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The licensee had identified in 1994 (LER No.94-003) that past logic testing
practices did not ensure that proper test overlap existed between procedures. A
logic test should test all components, such as relays and contacts, from the sensor
through and including the actuated device. The test may be performed by any
series of sequential, overlapping or total system steps so that the entire logic
system would be tested. As part of Fermi's corrective actions, the licensee
reviewed numerous surveillance and test procedures. Procedures were revised and
untested components were tested. No component failures were identified.
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The inspectors reviewed surveillance procedure No. 42.307.01, Revision 22, " Logic
System Functional Test of Division i EDG ECCS Emergency Start Circuits and Auto
Trip / Bypass Circuits." Since all of the EDG start circuits were similar, the start
circuits for EDG No.11 were reviewed in detail. The inspectors concluded that the
licensee was testing all circuit logic paths and components in an acceptable
manner.
The inspectors reviewed the testing performed during the implementation of
EDP 8355. This included work request No. 0058881107, the electrical scheme
chockout performed on April 26,1989, and the post-modification test perforrded on
May 25,1989. During the review of the test procedures, the inspectors
determined that 5EX relay contacts (1/2) had not been verified in their open state i
and that contacts (5/6) had not been tested in their open and closed states. These l
contacts were now appropriately tested during surveillance 42.307.01. I
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c. Cpnclusions j
The licensee's failure to appropriately test the SEX contacts during the modification
process is considered a violation. However, the licensee identified inadequate
overlap testing during routine surveillance procedure reviews. In addition, the
licensee initiated comprehensive corrective actions as identified in LER No.94-003.
This included the evaluation and implementation of necessary changes to control
plant modifications and procedure revisions to ensure test overlap was reviewed.
Therefore, this item will not be cited because the requirements of Section Vil of the !
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" General Statement of Policy and Procedure for NRC Enforcement Actions,"
NUREG-1600, were met. (NCV)(50-341/97003-09) The inspectors concluded that
the licensee had taken appropriate corrective actions to ensure electrical and
instrumentation & control test overlap would be considered during future
modifications and test procedure reviews.
E2 Engi:neering Support of Facilities and Equipment
E 2.1 LiGfLnsee Identified and Corrected Several EECW Desian Deficiencies
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During work associated with the preparation of engineering design package for the l
EECW make up tank, the licensee identified the following issues:
- Certain single failures of a divisional power source could result in loss of the
, primary containment function for EECW subsystems. All primary
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containment iso!ation valves within a division were powered from the same
source. On loss of one division of AC power, the Primary Containment
Isolation Valves (PCIVs) would fail as-is in the open position. The isolation
valves which separate EECW from RBCCW could also fail open in this
situation.
,
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e The EECW piping inside the drywell was not safety grade material. The
EECW design was such that the integrity of this piping was not relied upon
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during an accident. so it was not analyzed for the ability to withstand a high
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energy lirio br9ak (HELB). Because the PCIVs were found to be susceptible i
to failure, a high energy line break coupled with a loss of AC power could l
potentially release fission products into the secondary containment, or if the l
RBCCW isolation valves were open, to the environment.
- Also, the licensee identified that the Remote Shutdown System, for use in a i
fire which disrupts plant operation from the main control room, did not I
include controls to isolate RBCCW from Division 1 EECW. This could ;
potentially have prevented initiating EECW, because an interlock required the
RBCCW isolation valves to shut before the makeup tank isolation valve could
be opened.
The licensee reported these issues to the NRC in accordance with 10 CFR 50.72.
During this inspection period, engineering conducted analyses of the impact of
potential HELBs on the EECW system, and eliminated all potential sources except
one. A modification to protect the susceptible section of EECW piping was
installed in the drywell.
Additional modifications were installed to provide diverse power sources to EECW
PCIVs in each division in order to restore the primary containment isolation
function, and to the Remote Shutdown System to allow proper operation of the
EECW system.
These issues have been reviewed by the Resident inspectors, Region lll and NRR
personnel as the issues were developed and resolved. Additional review of the
licensee's analyses will be performed by NRR. This issue will be tracked as an
Inspection Followup Item pending the completion of reviews by NRR.
(IFI)(50-341/97003-10)
E2.2 Reactor Protection System (RPS) Resoonse Time Testina
NRR identified that a conflict existed between RPS response time testing as
described in technical specifications and the testing performed by the licensee as
documented in the Technical Requirements Manual (TRM). Specifically, TS required
testing the entire response time, while the TRM allowed using nominal sensor
response times and measuring the response time of the rest of the circuit. The
TRM had been changed with a 50.59 safety evaluation based on the Boiling Water i
Reactors Owners Group Licensing Topical Report NEDO-32291, " System Analyses l
for the Elimination of Selected Response Time Testing Requirements" as approved
by NRC Safety Evaluation Report.
The licensee then determined that response time testing of Reactor Protection
System Actuation Instrumentation, Isolation System Actuation Instrumentation, and
ECCS Actuation Instrumentation had not been conducted in accordance with
Technical Specification requirements. As a result, the licensee declared associated
ECCS systems inoperable, established secondary containment and performed l
response time testing. All equipment was found to be functioning as expected.
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The licensee requested and received a licensee amendment to modify the TS
definition to allow performance of response time testing as specified in the TRM. l
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The technical specification compliance issue and process used by the licensee to j
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make changes to technical requirements will be reviewed by Region lil inspectors.
These issues will be tracked as an Unresolved Item pending completion of Region lli
review. (URI)(50-341/9700311) l
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IV. Plant Sucoort j
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F3 Fire Protection Procedures and Documentation
F3.1 Fire Protection Surveillance Weaknesses )
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a. Insoection Scoce (61726)
The inspectors reviewed procedures associated with surveillance 28.501.04, " Fire
Suppression System Valve Operability Test." The inspectors observed both control
room and in field implementation of the fire protection surveillance. The inspector
reviewed the Updated Final Safety Analysis Report (UFSAR), and the fire protection
plan.
b. Observations and Findinas
On April 4 the inspectors observed performance of the Fire Suppression System
Valve Operability Test. The test required that various fire protection valves be
unlocked and fully closed, then fully opened. in addition, the performers were 4
required to verify the appropriate OS&Y CLOSED light Indicated correctly for valves
with tamper switches. The inspector noted the FIRE DET/ PROT System Trouble
annunciator was not received as expected for valve T80-F030,2nd Floor Cable ;
Tray Area Sprinkler System Isolation Valve. A work request was written to repair i
the alarm.
The inspector reviewed annunciator response procedure 16D28 to verify that
switch T80 N011 did input to the alarm. The inspector reviewed the UFSAR and
noted that the UFSAR did not require verification of the alarm. However, the
inspector concluded that the control board annunciator was an expected and
necessary response to ensure control room operators were alerted to problems with
the fire protection system. As a result, operations requested revising the
4
surveillance procedure to perform verification of annunciators for all valves with
alarms.
,
c. Conclusions
The inspector concluded that the lack of verification of the annunciators was a
weakness in the surveillance for fire protection system operability. The inspectors
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concluded that the licensee's decision to include the testing of the control board fire
protection trouble annunciator was acceptable.
R1 Radiological Protection and Chemistry Controls
R 1.1 Valve with Internal Contamination Released from Radioloaically Restricted Area
(RRA)
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a. insoection Scoce (71750) l
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The inspectors reviewed data concerning the release of an Offgas System valve to
the clean machine shop. The inspectors interviewed personnel and reviewed area
surveys.
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b. Observations and Findinas
Station mechanical maintenance personnel removed two valves from the Offgas
System to perform repairs. The valves were surveyed by RP, found to have no
contamination, and released to the cold machine shop. Following disassembly of
the valve, the maintenance technician requested RP to resurvey the valve internals.
The survey identified that the internals of the valve were contaminated. Radiation
protection personnel immediately returned the valve along with tools and parts to
the count room to perform additional surveys, in addition, the maintenance ,
I
technician's clothing, personal affects, and machine shop area were surveyed and
no contamination was found.
The licensee was conducting an investigation at the end of the inspection period.
The inspectors noted that the issue was raised due to the questioning attitude of a
maintenance worker.
c. Conclusions
The inspectors reviewed the licensee's immediate corrective actions and determined
that they were acceptable. This issue will be tracked as an Unresolved Item
pending review by a Region 111 specialist inspector of procedure adherence and
procedural adequacy of surveying component intervals. (URI)(50-341/97003-12)
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R 1.2 Backfill System Placed in Service Without RP Briefina on Radioloaical Conditions in
the Work Area
a. Insoection Scooe (71750,61726)
The inspectors observed performance of a surveillance which filled and vented a
potentially contaminated instrumentation system located inside a radiation area.
The inspectors observed radworker practices, compliance with radiation work
permit requirements, and exposure control measures. When a concern was I
identified, the inspectors reviewed station procedures for work outside normally l
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( surveyed areas of the plant, scaffolding procedures, and discussed the concerns
with RP supervision,
b. Observations and Findinos
On May 4, the inspector observed l&C technicians placing the Division 2 Backfill
system in service. The inspector observed that the work was done in a careful
manner, using excellent communications and radiological precautions while venting
this potentially contaminated system.
J
However, the procedure required us;ng a portable lift to operate the supply header
isolation valve (B21-F2408), which was located about 15 feet above the floor. The
inspector reviewed Radiation Work Permit (RWP) 971011, which was the Specific
RWP in use for this job. The instructions required workers to notify RP if climbing
or going above 8 feet. The inspector observed that the RWP package at the
worksite had four survey maps, none of which included the work area 15 feet !
I above the floor. The inspector asked the work group leader about the use of the
lif t, who stated that the workers had not contacted RP prior to beginning work
because the same workers had been working in the same area for the previous
3 days and were familiar with the radiological conditions.
The inspector discussed the issue with the RP Shift Supervisor, who stated that the
requirement to contact RP prior to going above 8 feet was not met in this case.
The RP expectation was that workers were expected to contact RP every time they
went above 8 feet. DER 97-0722 was written to document the event and track
corrective actions. The individuals involved had their access to the RRA removed
pending review.
The inspector further discussed the event with the workers and RP staff and
determined that the workers were knowledgeable of the work conditions because
radiological conditions had not changed since their briefing from RP the previous I
day. Additionally, workers were monitored for radiation dose. !
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c. Conclusions 1
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The inspector concluded that failure to notify Radiological Protection personnel )
before gaining access in an area greater than eight feet above the floor was a i
violation of 10 CFR 20.1101. This resulted in the radiological workers not j
obtaining a briefing on radiological conditions in the entire work area.
(VIO)(50-341/97003-13)
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R1.3 Post Accident Samole Error
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a. Insoection Scone (71750,61726)
The inspectors observed the operation of the Post Accident Sample System (PASS) 1
during a surveillance. The inspector reviewed the surveillance procedure and
training records for individuals qualified to operate the system. When the system
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chemistry supervisor.
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b. Observations and Findinas
The inspector observed a semi-annual sample obtained from the PASS on April 25.
The technician failed to obtain a sample the first time because the sample bottle
was not properly installed.
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! The licensee stated that the procedure (78.000.12) would be changed to have the
" Bottle In" light verified green, but the inspector noted that a caution on the topic
already existed in this procedure. In a discussion with the system engineer, the
, inspector learned that the microswitch which ensured that sample bottle was
correctly positioned had frequently caused difficulty obtaining a sample unless great
care was taken in inserting the sample bottle. However, the indicator light was
available to allow determination of correct alignment.
The inspector reviewed the PASS sampling procedure and determined that it
required that personnel performing PASS samples be qualified to use self contained
breathing apparatus. Respirator qualifications were checked for personnel qualified
to operate the PASS system, and the records indicated that the individual observed
and one other had expired self-contained breathing apparatus qualifications in
January,1997. The licensee subsequently determined that both individuals had
recently recertified, and that records had not yet been updated.
c. Conclusions
l, The inspector determined the chemistry technician was knowledgeable of the
sampling procedure. The PASS system functioned as designed, but operator
attention to detail had prevented obtaining a sample on the first attempt. However,
the inspectors considered that the administrative controls used to ensure proper
! training to operate the system during accident conditions were weak.
R 1.4 Untimelv Restoration of Unfettered Access for NRC Insoector
b. Observations and Findinos
During observations of performance of RCIC surveillances, an inspector lost control
of both the assi0ned dosimetry and security key-card identification badge. The
incident occurred while the inspector was exiting a vital area into an non-vital area '
within the RRA. Both the badge and dosimetry remained within the vital area while
the inspector exited the RRA. Shortly later, station personnel discovered the
uncontrolled badge and notified security parsonnel as required by procedures.
Security personnel quickly located the inspector and conducted an investigation of
l the circumstances as required by procedure MRP08, "RRA Access
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Denial / Reinstatement," Revision 1, dated October 2,1996.
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i Security personnel were able to ascertain through interview of the inspector that
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the inspector had accidently lost the badge and was unaware of the condition until
notified by security personnel. The security staff was also able to determine
through review of computer records that the badge had not been used or attempted
- to be used by any persons while it was in a uncontrolled status.
! RP personnel also conducted an investigation of the circumstances as required by
- MRP08. RP personnel were able to determine from recent surveys of the
inspector's egress path that unaccounted dose was not received by the inspector.
i After both the security and RP personnel had completed their investigation, the
- reinstatement requirements of MRP08 were verified to be met. These requirements
were verified within a half-nour of the initial incident. However, because of the late
hour on a weekend, approval for reinstatement of access was not obtained in a
< timely fashion to allow the inspector to observe the assigned activity. Although the
licensee's authorized representative for signature and approval of reinstatement of
RRA access was notified of the completed investigation in a timely fashion,
reinstatement of the NRC inspector was denied. The authorized individual, the on-
shift NSS, believed that reinstatement required at least 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or the next work
day and denied access for the inspector to conduct inspection activities. After
prompting by the inspector and the RP personnel present, approval was obtained
from offsite senior management.
1
c. Conclusions
The inspector determined that the procedure MRP08 did not allow for timely
3
compliance to 10 CFR Part 50.70 requirements. The procedure did not ensure that
l a duly authorized representative of the Commission was permitted to inspect the
assigned activity. Although the inspection was eventually complete via other
means, such as record review, the procedure MRP08 did not ensure timely access
during off-normal hours. This is an unresolved inspection activity pending further
! review of licensee actions to ensure that access can be obtained in a timely fashion
to allow inspection of licensee's activities by duly authorized NRC inspectors.
t
(URI)(50-341/9700314)
S1 Security and Safeguards Activities
S 1.1 Temocrary Backaround Checks Used Bevond 180 Davs
The licensee identified that a contract worker had exceeded 180 days on a
temporary background check. This was documented in DER 97-0606. Tha
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individual was granted temporary access at the beginning of Refueling Outage 05,
and left six weeks later. The individual came back for Forced Outage 97-01 in
January 1997, while the temporary background investigation was still valid, but the
allowed 180 day period expired on March 30. The expiration was not recognized
until April 16, at which time the individual's access was removed. The event -nas
determined to be a loggable event. A further review by security identifed three
more individuals with temporary access beyond 180 days, whose access was also
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removed. The full background checks were subsequently completed and the
individuals' access restored.
This event will be tracked as an inspection Followup Item pending review of the
circumstances surrounding the event and evaluation of licensee corrective actions
by Region 111 Security Specialist inspector. (IFI)(50-341/9700315)
V. Manaaement Meetinas
X1 Exit Meeting Summary
The inspectors presented the inspection results to members of licensee management at the
conclusion of the inspection on May 9,1997. A subsequent exit was conducted on
June 26,1997, to address resolution of issues after management review of the report.
The licensee acknowledged the findings presented.
The inspectors asked the licensee whether any materials examined during the inspection
should be considered proprietary. No proprietary information was identified.
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PARTIAL LIST OF PERSONS CONTACTED
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Licensee
! S. Bartman, Supervisor, Chemistry
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S. Booker, Superintendent, Electrical Maintenance l
P. Borer, Assistant Vice President, Nuclear Generation
C. Cassise, General Supervisor, Mechanical Maintenance l
D. Cobb, Superintendent, Operations
R. Delong, Superintendent, System Engineering
P. Fessler, Plant Manager, Operations
~
D. Gipson, Senice Vice President, Generation
T. Haberland, Superintendent, Work Control
R. Matthews, Superintendent, l&C Maintenance
J. Moyers, Director, Nuclear Quality Assurance
N. Peterson, Supervisor, Compliance
J. Plona, Technical Director
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T. Schehr, Engineer, Operations
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! None
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INSPECTION PROCEDURES USED
IP 37551: Onsite Engineering
IP 40500: Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing
Problems
IP 61726: Surveillance Observations
IP 62707: Maintenance Observation
IP 71707: Plant Operations
IP 71714: Cold Weather Preparations
IP 71750: Plant Support Activities
IP 92901: Followup - Operations
IP 92902: Followup - Engineering
IP 92903: Followup - Maintenance
IP 92700: Onsite Followup of Written Heports of Nonroutine Events at Power Reactor
Facilities
IP 93702: Prompt Onsite Response to events at Operating Power Reactors
ITEMS OPENED, CLOSED, AND DISCUSSED
Ooened
50-341/97003-01 IFl Review of FME practices
50-341/97003-02 VIO Inadequate procedure to restore RCIC to proper lineup
50-341/97003-03 URI Review safety implications of using non-sequential procedure
steps for testing
50-341/97003-04 URI Review of permanent corrective actions of MCC disconnect
switches lubrication issues
50-341/97003-05 VIO Inadequate procedure to install fully ready battery
50-341/97003-06 IFl Review transmitter shipping plugs
50-341/97003-07 VIO Inadequate procedure for EDG 11 air compressor oil sample
50-341/97003-08 URI Review OSRO effectiveness on MCC switch issue
50-341/97003-09 NCV Inadequate post-modification testing for EDG logic
50-341/97003 10 IFl NRR review of EECW design issues
50-341/97003-11 URI RPS response time testing TS compliance
50-341/97003-12 URI Release of contaminated components from RRA
j 50-341/97003-13 VIO Failure to obtain a briefing of radiological work area conditions
- 50-341/97003-14 IFl Corrective actions for prompt NRC access 1
50-341/97003-15 IFl Review temporary background check controls l
Closed
l
50-341/97002-04 URI Review of MOV motor pinion gear inspection results I
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Discussed
50 341/96016-04 IFl Protection of Equipment During Maintenance inside
Containment
50-341/96016-07 URI Condensate Storage Tank freeze protection
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1
4
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1
1
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_. _. _ _ _ _ . __ . . _ _ _ . _
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LIST OF ACRONYMS USED
'
CCHVAC Control Center Heating, Ventilation and Air Conditioning System
DER Deviation Event Report
, EDG Emergency Diesel Generator
EDP Engineering Design Package
! ECCS Emergency Core Cooling System
EECW Emergency Equipment Cooling Water
i FME Foreign Material Exclusion
GSW General Service Water
'
HPCI High Pressure Coolant injection
ICV Individual Cell Voltage
IEEE institute of Electrical and Electronic Engineers
"
IFl Inspection Followup Item
J LER Licensee Event Report
MCC Motor Control Center
- MOV Motor Operated Valves
- NCV Non-cited Violation
,
NSS Nuclear Shift Supervisor
- NRR Nuclear Reactnr Regulation
'
i PASS Post Accident Sampling System
PCIV Primary Containment isolation Valves
- PMT Post Maintenance Testing
, RBCCW Reactor Building Closed Cooling Water System
,
RBHVAC Reactor Building Heating Ventilation and Air Conditioning
l RCIC Reactor Coolant isolation System
,
f RP Radiation Protection
'
RRA Radiologically Restricted Area
l RTV Room Temperature Vulcanizer
- RWP Radiological Work Permit
'
SAC Station Air Compressor
SBGT Standby Gas Treatment System
I
SOP System Operating Procedure
TRM Technical Requirements Manual
i TS Technical Specification
, UFSAR Updated Final Safety Analysis Report i
URI Unresolved item
VIO Violation
WR Work Request
4
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