ML19256G496

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LER 79-089/03L-0:on 791124,during Mode 3 Operation,Emergency Feedwater Flow Control Valve 2CV-1025-1 Failed to Close on Demand from Control Room.Caused by Trash in Valve Operator Hydraulic Sys & Hydraulic Snubber Out of Adjustment
ML19256G496
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 12/21/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19256G491 List:
References
LER-79-089-03L, LER-79-89-3L, NUDOCS 7912310393
Download: ML19256G496 (1)


Text

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NRC F ORM 366 U. S. NUCLE AR REGUL ATORY COMMIS$10N LICENSEE EVENT REPORT EXHIBIT A (PLE ASE PRINT OR TYPE ALL REOutRED INFORMATION)

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60 6, 68 69 EVENT DATE 74 75 HEPORT DATE 80 7 DOCstET N' Jut ER EVENT DESCRIPTION AND PROB ABLE CONSEOUENCES h o 2 1 Durino Mode 3 operation, with the electric driven Emercacy Feed. water i e i pump, 2P7B, in service as an auxiliary feedwater pump for normal startup i o . I Steam Generator feed. EFW flow control valve. 2CV-1026-1. failed tn clnsel e s i on demand from the Control Room. The valve failed in the EFW. or safe. I lo is i l position. All redundant EFW valves were su cessfully stroked from th9 I a i l Control Room. This occurrence is similar to LER 50-368/79-088 and 79-043L o e i Other ocqyrrences involvino 2CV-1025-1 are co-168/79-06R.74-094. 70 ns1 1

' a9 79-035, j,M028 anA.J8-0%,' Reportable per T.S. 6 4..l.9.h ,,

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I,lilI the hydraulic snubber out of adiustrnent. restricting oil flow in one i

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