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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
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Text
REQULATQRY I RMATION DISTR IHUTION BYS" 'R IDS)
,ACCESSION NHR 8704220215 DQC. DAT&: 87/09 /15 NOTAR I 2'.ED: NO DOCKET t
FACIL: 0- 44 Rob ert Emmet Ginna Nuc I eav P 1 ant> Uni 1, Roche s tev 0 05000244 AUTH. NAl }E AU I HOR AFFILIATION HACKUS> W. H. Rochestev Gas '5 Electric Corp.
KQBER> R. W. Rochestev Gas 8c Electric Corp.
RECIP. NAME REC IP I ENT AFFILIATION
SUBJECT:
LER 87-'003-00: on 870415> mayor pov tion of fiv e sos detection auto suppv ession Found inoperab le. Caused be operator
~c Failuv'e to follow pv oceduv al direction duv inire sos disconnect proceduv e. Pv ocedure updated. W/870415 ltr.
DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR TITLE; 50. 73 f icensee Event Repov't (LER) Incident Rpt> etc.
ENCL J SI NOTES: License Exp date in accov dan" e uith 10CFR2> 2. 109(9/19/72). 05000244 RECIr IENT COPIEB REC I P I EhlT COP lES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-3 LA 1 PD1-3 PD 1 BTAHLE> C 1 1 INTERNAL: ACRB MICHELSQN 1 *CRS I'}OELLER 1 AEOO/DQA 1 AEOD/DSP/RQAB 2 2 AEOD/DSP/TAPB 1 AEODIDSPITPAB 1 NRR/*Df t.'RR /DEST/ADE 1 0 NRP /DEBT/ADB 0 ti!RR/DEBT/CEH NRR/DEBT/ELB t}RR/DEBT/ ICSB 1 ERR/DEBT/MFfi i f' RR /D EST I MTH 1 1 NRR/DEBT/PSB 1 t~RR/DEBT/RSH 1 1 NHRIDEBTIBGB 1 NR R /DLP G/HFH 1 NRR/DLPG/9*B 1 t:RR/DOEA/E*H 1 1 NRR/DREPIEPB NRR/DREP/RAH 1 ERR/DREP/RPH i~!RR/PMAS/ ILRB 1 NRR/PMAS/PTBB 3 1 62 1 RES SPEIB T 1 FILE 0' 1 EXTER NAL: EQScG QROH> l'} 5 5 H ST LOHH Y WARD 1 1 LPDfk 1 t!RC PDR 1 NSlC HARRlS> J 1 1 f"S I C MAYS G 1 1 TOTAL NUMBER OF COPIES REQUIRED: LT I R 43 ENCL 41
pl f
NRC Form 255 U.S. NUCLEAR REOULA'TORY COMMISSION rte2) Afr'ROVED OMS IIO, 2)NOMIOa EXPIRES: SIS I IS5 LICENSEE EVENT REPORT tLER)
SACILITY NAME (I) DOCKET NUMSER (21 R E Ginn Nucle r Plant 0 5 0 0 0,244 1 OF1 0 E
EVENT DATE (SI Dur'm Inoperable Fire System Detection Alarms and Autanatic Suppression, LER NVMSKR (5)
Disconn c Perfo REPORT DATE (7l OTHtR SACILITIKS INVOLVtDDl)
Due To Personnel 5N Ore ENTRE AL OAY YEAR FACILITYNAMES OOCKKT NUMSER(5)
MONTH OAY YEAR YEAR HUMNNII MONTH 0 5 0 0 0 0 31 687 87 003 0 0 041 5 8 7 0 5 0 0 0 THIS RtfORT IS SVSMITTED WRSUANT TO THE RKOVIREMKNTS OS 10 CSR ()r (Crrack one or more ol tne lollorrlnf) Il'll Of ERATINO MODE (5)
N 20.e02(N) 20AOS(cl 50.7241(2)(tr) 72.7101)
SOFIER 20.OOS(a) I)HO SOM(e)III 50,724) l2) Ia) 72.71(c)
LEYEL 1 p p 20AOS la l(1) IN) 50.25(c) (2) 50,724)(2) (at I OTHER (Speclty In Aproect Oerow cart In tert, lYIIC form 20AOS(el(1)(NO 50.724I(21(0 50.724)(21(rIN)(A) JIIEAJ 20.405 Ia) Ill(lr) 50.724)(2l(tl 50.724) (2) (r(N)(~ )
20.eOSIal(11(r) 50.72(a) 12I ONI 50 72(el (2)(el LICENSES CONTACT SOR THIS LER (12)
NAME TELEPHONE NUMSER AREA CODE
'.H. Backus, Technical Assistant to the Operations Manager 31 55 24- 444 6 COMPLETE ONE LINE SOll KACH COMPONENT FAILURE OESCRISKO IN THIS REPORT Iltl MANVFAC EPORTASLE MANUFAC. EPORTASL CAVSE SYSTEM COMPONENT TO NPRDS CAUSE SYSTEM COMPONKNT TURER TURER TO NPROS eNj%j. 2( '<:;.
SUPPLEMENTAL REPORT EXPECTED I(el MONTH OAY YEAR EXfECTED SUSMISSION DATE (15)
YKS (II yer, c<<rrprere EXPECTED SVEMISSION DATEI NO ASSTRACT (Llmlt to IOOO rpecee, I 5, epprorimerely Rrreen rlnple~e typerrrrlnen liner) (I ~ I On March 16, 1987 at 1100 EST, with the unit at 100% reactor power, a major portion of the Fire System Detection and Auto Suppression was found inoperable. This inoperability was due to an "Alarm Off" pushbutton in the Relay Room Fire Panel being inadvertently left depressed during the earlier performance of a Fire System Disconnect procedure.
Operations and the Instrument and Control Technician who initially observed the problem, immediately restored the "Alarm Off 0 pushbutton to normal, thus restoring the Fire System to operable status again.
The event was caused by the failure of the operator to follow procedural direction while performing the Fire System Disconnect procedure.
Corrective Acti'on planned to prevent recurrence will be the upgrading of the disconnect procedure to have a second verification by a Fire Control and Safety person or a Licensed Operator.
870422021 5 87041 5 PDR ADOCK 05000244 8 PDR NRC Form 255 (Se2)
NRC Fo<M 300A U.S. NUCLEAR REGULATORY COMMISSION (9.83 I LICENSEE EVEN EPORT ILER) TEXT CONTINUATION APPROVEO OMB NO, 3150 0104 EXPIRES: 8/31/85 FACILITY NAME (ll OOCXET NUMBER (3( LER NUMBER (El ~ AGE (3I TFI 5EGUENTIAL Py@ REVISION NUM0 0 II NUMBER R.E. Ginna Nuclear Power Plant 0 S 0 0 0 2 4 4 7 0 0 3 000 2OF 1 0 TEXT /// INNO Ope(o /I /OookoIL ooo aAWonel HRC FooII 3850'e/ ((TI PRE-EVENT PLANT CONDITIONS The unit was at 100% reactor power and a Fire System Disconnect had been performed on Fire Zone Z-35 at 0940 EST per procedure SC-3. 16. 2. 4 (Fire Signaling/Component (s)
Disconnection - Reconnection). This disconnect was done so that personnel could perform work in the Fire Zone Z-35 area without inadvertently actuating the Fire Detection System due to dust, grinding, etc. A firewatch had been assigned to the Fire Zone Z-35 area prior to disconnect.
At 1045 EST, an Instrument and Control (I&C) Technician
~
began work on the Fire System Tamper Switch Panel in Satellite Station C (SSC) in the Relay Room.
DESCRIPTION OF EVENT A. EVENT:
On March 16, 1987 at 1100 EST, while the I&C Technician was working on the Tamper Switch in SSC, he observed a "Trouble Alarm" on Satellite Station A (SSA). SSA and SSC are very close together in the Relay Room.
The I&C Technician immediately checked SSA for the source of the "Trouble Alarm" and observed the "Alarm Off" button depressed. Knowing that, with this button depressed, a major portion of the Fire Systems Detection Alarms and Auto Suppression was rendered inoperable, the I&C Technician notified the Control Room.
The Ginna Station Technical, Specifications (TS)
Section 3. 14. 3. 1 requires that system is inoperable, except during emergency condi-if a spray/sprinkler tions which prohibit access, or for testing, within one hour, establish a continuous firewatch with backup fire suppression equipment for those areas in which redundant systems or components necessary for safe-shutdown could be damaged; for other areas, establish a firewatch patrol to inspect the zone with the inoperable system at least once per hour and NRC FORM 300A (9 83l
~ NRC FeIm SSSA U.S. NUCLEAR REOULATORY COMMISSION
~ 19 81I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVEO OM8 NO, SISOWIOI EXPIRE&i 8111185 FACILITY NAME III OOCKET NUMEER 111 LER NUMSER ISI ~ AOE IS)
SEOVENTIAL REVISION YEAR @ NVM ER : NVM ER R E TExT III mern eee1e H eeeeeed. eee ~
Ginna Nuclear Power Plant HAc femI 40&A'eI IITI 0 S 0 0 0 2 4 4 8 70 0 3 00 03 OF 1 0 place backup fire suppression equipment in the unprotected area(s). Because from 0940 EST on March 16, 1987, until 1100 EST on- March 16, 1987 (a lapsed time of approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 20 minutes) with many of the spray/sprinkler systems inoperable without a firewatch and backup fire suppression being established, the requirements of Section 3.14.3.1 of TS was exceeded.
B. INOPERABLE STRUCTURES, COMPONENTS OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None.
C. DATES AND APPROXIMATE TIMES FOR MOTOR OCCtG&ENCES:
o March 16, 1987, 0940 EST: Event date and time o March 16, 1987, 1100 EST: Discovery date and time o March 16, 1987, 1100 EST: SSA "Alarm Of f" button restored to normal restoring the Fire System operability.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS 'AFFECTED:
With the "Alarm Of f" button depressed in SSA, the following functions were affected on a ma)or portion of the Fire System; 0 Audible Control Room Fire System alarms were defeated 0 Automatic Fire Suppression was prevented N 0 Manual-Remote Fire Suppression from the Control
.,Room was prevented 0 Manual-Remote Fire Suppression from the area electric release stations was prevented.
NRC FOIIM SSSA IS 8SI
NRC FrrrrR OSSA V.S, NVCLEA4 4EOVLATORY COMMISSION I9.81 I LICENSEE EVENT REPORT {LER) TEXT CONTINUATION AFI ROVEO OM8 NO. 8150 OIOI EXFIRES: SISIISS FACILI'TY NAME <II OOCKET NVMSER 11l
'I LER NVMOER IS) FACE ISI YEAR SEOVENTIAL .Rrrr REVISION NUMSER :. 8 NUM ER TEXT G'
N Ituuu NMtu 8 tuFuked, l r Power Plant uuu AjtuuRAINFICFuuu 8SSAEI IITI 0 5 0 0 0 2 4 4 8 7 0 0 3 0 4 " 1 0 The major portions of the Fire System affected are as follows:
NOTE The prefix "S" denotes Fire Suppression Detection System and the prefix "Z" denotes Fire Detection only. The
- denotes Auto Actuation of a Fire Suppression System.
0 S01
- Auxiliary Building Basement East Safety Injection (SI) pumps 0 S02
- 1-G Charcoal Filter in Auxiliary Building 0 S03
- Auxiliary Building Intermediate Center Bus gl6 0 S04
- Auxiliary Building Intermediate East-Cable Tray 0 S05
- Control Building Air Handling Room 0 S07
- Turbine Driven Auxiliary Feed Pump 0 S15
- Intermediate Building Basement North Cable Trays 0 S16
- Screen House Basement - Cable Trays 0 S24 Condenser Pit NRC FORM SFSA Ol 8SI
lc J
NRC ferro 344A U.S. NUCLEAR RECULATORY COMMISSION
~ l9.83 I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION APPROVED OM8 NO, 3I50 010l r EXPIRES: 8/31/85 FACILITY NAME III DOCKET NUMEER l1l LER NUMEER (41 ~ AOE l31 VEAII SEOUENSIAL II/5 REVISION NUM E II MUM ER TEXT /I/ more SO>>e II reeueIR/. u>>
P r%MY/
POP/oooo/ HIIC Form Plant llll 0 6 0 0 0 2 4 4 8 7 0 0 3 00 05 oF l 0 o S25
- Turbine Oil Reservoir 0 S29
- Control Room/Turbine Building Wall 0 Z01 Auxiliary Building Basement East and Charging Pumps o Z02 Auxiliary Building Basement West and Residual Heat Removal (RHR) Sump area o Z03 Auxiliary Building Intermediate West o Z04 Auxiliary Building Operating Floor Bus 414 and Component Cooling Water (CCW) pumps o Z05 Cable Tunnel o Z06 Containment "A" Auxiliary Filter Charcoal Bank o Z07 Containment "B" Auxiliary Filter Charcoal Bank o ZOS Containment Basement Cable Trays o Z09 Containment "A" Post Accident Charcoal Bank o Z10 Containment "ALE Post Accident Charcoal Bank o Zll Containment "B" Post Accident Charcoal Bank o Z12 Containment "B" Post Accident Charcoal Bank 0 Z13 Containment "All RCP Cable Trays NRC POIIM 344A I9 83I
NRC form SOSA U.S. NUCLEAR REOULATORY COMMISSION l94SI LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OM8 NO. S150-OIOE EXPIRES.'8/SINS FACILITY NAME III OOCKET NUMSER ISI PACE IS)
LER NUMSER ISI YEAR PrX< EEQVENTIAL REVISION NVMOEII NUM E II R E Ginna Nuclear Power Plant TEXT Ilfmoro <<Mee << Ieeoeof, we PPOOe<<NP FIIIC forrrr SSSA'eI I Ill 0 5 0 0 0 2 4 ' 003 00 06 OF l 0 o Z14 Containment <<B<< RCP Cable Trays o Z15 Containment Intermediate Level Cable Trays o '16 Containment Operating Floor Cable Trays o Z19 Control Room Area o Z20' <<A<< Emergency Diesel Generator Vault Z21 <<B<< Emergency Diesel Generator Vault o Z22 Motor Driven Auxiliary Feed Pump area 0 Z23 <<A<< Containment Purge Filter o Z24 <<B<< Containment Purge Filter o Z25 Standby Auxiliary Feed Pump area o Z26 Screen House Service Water Pump area o Z35 Auxiliary Building - Spent Fuel Pit area o Z36 Intermediate Building - Sub-basement o Z37D1 Intermediate Building - Steam Header area o Z37D2 Intermediate Building - Above Steam Header o Z37D3 Intermediate Building - Top Floor area o Z38D1 Intermediate Building Basement - Hot Side o Z38D2 Intermediate Building Main Floor - Hot Side o Z38D3 Intermediate Building - Top Floor Hot Side o The Fire Pumps Auto Start Signal NRC FOIIM SEEA I9 8SI
,SC NRC Form 3SSA U.SNUCLEAR REGULATORY COMMISSION (9.83)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROV EO OMB NO 3150&(04 EXPIRES 8/31r85 FACILITY NAME (TI OOCKET NUMBER (2( LFR NUMBER (Sl PAGE (3l Y E A II SEOVENTrAL 4EYISIOrr NUM(IS 4 rrvMeeo R.E. Ginna Nuclear Power Plant TEXT ((p more epece (e rerRriNE oee ~ NRC Feem 3((BA'PI ((TI 244 87 0 0 3 000 7 OF 1 0 E. METHOD OF DISCOVERY:
The "Alarm Off" button in SSA was found depressed by an I&C Technician while he was performing maintenance on a tamper switch in SSC.
F. OPERATOR ACTION:
Operations and the I&C Technician immediately restored the Fire System to operable status.
III 'AUSE OF EVENT A. IMMEDIATE CAUSE A major portion of the Fire System Detection Alarms and Automatic Suppression rendered inoperable due to the "Alarm Off" button in SSA being depressed.
B. RCOT CAUSE:
Two root causes contributed to this event. They are as follows:
0 The operator's failure to follow procedural direction while performing the disconnect procedure, (i.e. there was a distinct step in the disconnect procedure that instructed the operator to, release the alarm off button by depressing it again and verifying the trouble light goes out").
0 There is currently n'o selective visual indication in the Control Room that alerts the operator when any of the fire zones supervised at SSA are disconnected, reconnected, or inadvertently left in trouble.
NRC FORM SSSA (8 83 I
NRC Forro'388A U.S, NUCLEAR REGULATORY COMMISSION I9 83)
LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVEO OMS NO. 3 ISO-GIOS EXPIREE: 8/3I/85 FACILITY NAME Ill OOCKET NUMSER I?I LER NUMSER ISI ~ AGE IS)
SEQUENTIAL Pgp RSVISION NVMSSII NVMSSII R E Ginna Nuclear Power Plant:
TExT ///moro opoco 8 PSrrsoor, voo PM/oonro/Hp/c Forrrr ~8/llTI 0 5 0 0 0 2 4 4 8 7 0 0 3 000 8 1 0 ANALYSTS OF EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (i) (B), which requires reporting of "any operation or condition prohibited by the Plant's Technical Specifications" in that portions of the Fire Suppression System and the Fire Detection System were inoperable for more than 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> without a firewatch and backup fire suppression being established.
An assessment was p<.rformed of the safety consequences and implications of the event with the following results and conclusions:
0 Although the above systems would not have operated as designed, the area fire detectors were still operating and if a fire in any of the areas existed a visual indication at the Fire Control Panel in the Control Room would have been received. Should indication have been received, the Station Fire Brigade would have been activated and they could have operated the suppression system locally at the hydraulic release stations. The Fire Service Pumps could have been started manually from the Control Room.
0 Fire barriers are located throughout the plant to separate major areas from each other and also to separate certain safety related areas from the remainder of the plant. These are designed to stop a fire from propagating frombarriers one area to another. All penetrations in these are sealed with appropriate materials to match the requirements of the barrier. Tt is reasonable to assume that even if a fire went undetected in an area, that the fire would be restricted to that area due to the installed fire barriers.
0 The Ginna Station Fire Hazard Safe Shutdown Analysis assumes achieving and/or maintaining cold shutdown status from a fire in any area of the plant. Modifi-cations have been made and procedures developed to assure this.
NRC FORM SSSA I9 83 I
NRC ForrR SOBA U.S. NUCLEAR REOULA'TORY COMMISSION IWISI LlCENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVEO OMB NO. S150&10<
EXPIRES; 8/SI/85 FACILITY NAME Ill OOCKET NUMBER ISI L'ER NUMBER IBI PACE IS)
SEOVENTIAL ru'r? REYISKIN NVM ER >Ilr NVMBER TEXT ///rrrrrr ~ rpece /P n /r/rrrrL rr>> I/h/Pr>>/h'hC frrrrR ~8/ IITI o 6 o o o 244 87 0 0 3 0 0 0 9 QF 1 0 There were no safety consequences or implications from this event because, the Fire Detection and Suppression System was only inoperable for approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 20 minutes and the above defense in depth concepts (i.e. fire barriers, and Fire Hazard Safe Shutdown Systems) were used in the plant design. Added to this Fire Detection System visual detection was still available in the Control Room, with local-manual fire suppression actuation possible.
V. CORRECTIVE ACTION A. ACTION TAKEN TO RETURN THE FIRE SYSTEM TO OPERABLE STATUS:
o Operations and the I & C Technician immediately.
restored the "Alarm Off" button to normal thus restoring the fire system to operable status.
B. ACTION TAKEN OR PLANNED 'I!0 PREVENT RECUEGU'.NCE:
o Make changes to SC-3.16.2.4 (Fire Signaling System/Component(s) Disconnection - Reconnection) procedure to have either a knowledgeable fire control and safety person or a Licensed Operator observe and verify the Fire System Disconnect-Reconnect operation.
o Implement with a high priority status, Engineering Work Request (EWR) 4280 to provide an alarm light to be located on the Control Room Fire when the Fire Display Panel to clearly indicate System has been disconnected/reconnected either by choice or inadvertently.
NRC FORM SeeA I Q.BSI
NRC F<<III 3SSA U.S. NUCLEAR REOULATORY, COMMISSION (9WI LICENSEE EVENT EPORT ILER) TEXT CONTINUATION APPROVEO OMS NO. 3150&104 EXPIRES: S/31/85 FACILITY NAME I'l DOCKET NUMSER 13l LER NUMSER ISI PACE LSI SEOVENTI*L IIE V IS IO N NVMSER NVMSFII R.E. Ginna Nuclear Power Plant TEXT //Fm<<p NMce /I mpvP<</ vpp A//I/<<M/N/ICF<<III 3SSAS/IITI 0500024487 003 0 0 1 0 1 0 VI ADDITIONAL INFORMATION A. FAILED COMPONENTS:
There were no component failures that contributed to this event.
B. PREVIOUS LER's ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results:
o LER 84-010 "Inoperable Fire Suppression System".
The LER 84-010 event was caused by operator error, (i.e. failure to restore the "Alarm Off" button on the Fire Detection Panel to normal) when restoring Fire Systems S-15 and Z-22 back to service per SC-3.16.2.4. The Corrective Action for LER 84-010 dealt w(th Reconnection and not Disconnection. It was only partially applicable and incapable of preventing the LER 87-003 event.
NIIC FORM 300A I9 93l
ROCHESTER GAS At."c r~r .>'. (.<.'tc>'.,s""7l )I' dQ EAST AVENUE, ROCHESIER, N.Y. 14649-000't ROGER W, KODt;>c vie ~seQoeur erat CTRIC 05EODVCY',Qtt April 15, 1987 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Sub) ect: LER 87-003, Inoperable Fire System Detection Alarms and Automatic Suppression Due To Personnel Error During System Disconnect Performance.
R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(i)(B) which requires a report of, "any event or condition prohibited by the Plant's Technical Specifications,"
the attached Licensee Event Report LER 87-003 is hereby submitted.
This event has in no way affected the public's health and safety.
V truly yours, Roger W. Kober xc'.S. Region I Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406 Ginna USNRC Resident Inspector