ML19305E358

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LER 80-006/04L-0:on 800318,average Gross Release Rate for Jan-Mar 1980 Found to Be 4.3% of Max Permissible Concentration,Exceeding Tech Specs.Major Portion Caused by Reactor Bldg Purge in Jan
ML19305E358
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 04/16/1980
From: Bramlett L
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19305E356 List:
References
LER-80-006-04L, LER-80-6-4L, NUDOCS 8004230473
Download: ML19305E358 (1)


Text

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O NRC FORM 364 U. S. NUCLE AR REGULATORY COMMIS$lON LICENSEE EVENT REPORT EXHIBIT A CONTROL 8LOCst: l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 l l i l lh 8 l AlR l Al NIO l 1 lgl 0 l0 l -l0uCENSE e4 l0 l NUM8EH 0l 0l 0 l- l 0 l0 lgl4UCkNbE 25 26 l1 [ITP&1l1 JC l 1[gl l lg bi C A T $4, 7 8 9 LICENSEE Coog CON'T fo ITl = LL_J@l015 lo 10 i 0 is i 1131GIO 68 69 i3 i EVENT 118DATE i 8i Oi@l Oi 4 HEPORT 24 ?S l 116DATE I 8i 01@ 80

> S 60 63 DOCKET 8dVMsga EVENT DESCRIPTIOPf AND PROS AOLE CONSEQUENCES h F6Til i The averace cross gas release rate for the first quarter 1980 is 4.3% of i gi the MPC. This exceeds E.T.S. 2.4.2.1. Reportable per E.T.S. 5.6.2b. ,

EE] l There were ro similar t.ccurrences. I e s l I o 6 l l gi i lo is i l I

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40 Q@ su(r@ l Z'l'979m [g 42 43 44 4s CAUSE DESCR4PTION AP.D CORREC flVE ACTIONS 27 m i The major oortion of this quarter's release was due to a reactor buildingi i,,,,i purge in January along with unit vent activity higher than previous levelp.

. 2 I These levels were higher than previous levels due to an apparent increasei gi in failed fuel (<.1% failed fuel). This fuel should be replaced within i i I two cvc19s. i ETA 5 iLPOWER HY DIS OVIH i s LE j@ l 110 l 0l@ oSk" STATUS l DES [gl Radiochemistryirve1 3!ESCHePr.Tib32ce l

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[Jij l NA @ j ; ;;;;gg;;,,,l 09 G9 30 l NAME OF PREPARER iinds' lev S. Bramlett ,,,0.m 501/968-2519

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