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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:RO)
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & BW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With ML20210R6421999-08-13013 August 1999 ISI Outage Rept for A2R07 ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20216D3841999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function M990002, Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function1999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With BW990016, Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20196A0721999-03-16016 March 1999 Cycle 8 COLR in ITS Format & W(Z) Function ML20207J4371999-03-0808 March 1999 ISI Outage Rept for A1R07 ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations BW990010, Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With ML20206U9011999-02-15015 February 1999 COLR for Braidwood Unit 2 Cycle 7. Page 1 0f 13 of Incoming Submittal Was Not Included BW990004, Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with BW990001, Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20206U9081998-12-17017 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function BW980076, Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3561998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Braidwood Generating Station,Units 1 & 2.With ML20155B6711998-10-26026 October 1998 Safety Evaluation Accepting Requests for Relief Associated with Second 10-yr Interval ISI Program Plan ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154D4401998-10-0202 October 1998 Safety Evaluation Authorizing Second 10-yr Interval ISI Program Request for Relief 12R-30 for Plant,Units 1 & 2 ML20155C2601998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Braidwood Generating Station,Units 1 & 2 ML20195F5911998-09-11011 September 1998 Special Rept:On 980812,addl Unseated Wires Were Discovered. Cause Is Unknown at Present Time.Util Evaluated Number of Unseated/Ineffective Wires & Determined Effect on Containment Structural Integrity.Commitments,Encl ML20196B3711998-09-0808 September 1998 Cycle 8 Operating Limits Rept (Olr) ML20151X6671998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Braidwood Generating Station,Units 1 & 2.With ML20238F3281998-08-31031 August 1998 SER Approving Second 10-year Interval Inservice Insp Program Request for Relief 12R-14 for Braidwood Station,Units 1 & 2 ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A1091998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Braidwood Generating Station,Unit 1 & 2 ML20236N7001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Braidwood Generating Station,Units 1 & 2 ML20198A0151998-06-18018 June 1998 10CFR50.59 Summary Rept 960619 Through 980618, Vols I & Ii,Consisting of Descriptions & SE Summaries for Changes to Procedural UFSAR Changes,Tests & Experiments & FP Rept.Without Fp,Rept ML20249A5451998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Braidwood Generating Station Units 1 & 2 ML20247F7711998-05-0808 May 1998 Special Rept:On 980403 & 980503 Seismic Monitoring Sys Was Declared Inoperable.Caused by 5-volt Power Supply & Regulator Card Failure.Imd & Sys Engineering Are Continuing to Identify & Resolve Problems So Sys Can Be Operable ML20247L7591998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Braidwood Generating Station,Units 1 & 2 ML20217K6331998-04-20020 April 1998 Safety Evaluation Accepting Methodology & Criteria Used in Generating Flaw Evaluation Charts for RPV of Braidwood IAW Section XI of ASME Code ML20216C6621998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Braidwood Generating Station,Units 1 & 2 1999-09-30
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November 29,1989 t
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Dear Sir:
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The enclosed Licensee Event Report from Braidwood Generating Station is '.
u , ; being transmitted to you as a Supplemental Report to LER 89-002-00.
- This report is number 89-002-01; Docket No. 50-456. ,
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1.Very truly yours, ;
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. R.- E. Querlo ,
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Enslosure:- Licensee Event Report'No. 89-002-01 4
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4 PART 1 TITLE W EVDrf OCCURRED
' Reactor Trip Safety Injection and Main 4~
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-Steamline Isolation during Plant Heatup 04/16/89 1640
'due to Management rand Procedural Deficiencies. myg ggg
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REASW FM SUPPLDG3ffAL REPET This supplemental report is being submitted to enhance the cause of
' Event.
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1 PART 2-L Acc ProcE = smI. umn wP& dd.4,.2& dpem ,
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SUPPLDGNTAL REPORT APPROVED AnD Aurn =1 ZED rom DISTRIBifr1m / g/UM. // [ %> M
' STATIN MANAGER Date
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L 1 l 7048P(061086)
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( * -1.!CENSEE EVENT REPORT (LER) g l Facil.ity' Name (1) Docket Number (2) .fage (3) !
_praidwood Unit 1 el El 01 01 01 41 51 6 1lofl0l6 Title (4) Reactor Trip, Safety Injection and Main Steamline Isolation During Plant Heatup due to Management Deficiency Event Date (5) LER Nygibar (6) Report DAlt (7) Other Facilities Involved (8)
Year Sequential f/j/j/ Revision Month Day Year Facility Names Docket Number (s)
Month. Day Year /
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j_ _ Number /// _ Number None 01 Sl 01 01.,D] 1 1
-01 4 11 6 81 9 81 9
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01012 7 0l 1 111 21_2 Bl 9 01 51 Ol 01 01 l l l THIS REPORT IS SUBMITTED PUR$UANT TO THE REQUIREMENTS OF 10CFR iCheck one or more of the followina) (11)
MDOE (9) 73.7)(b) 3 20.402(b) __ 20.405(c) .1 50.73(a)(2)(iv)
POWER' __ 20.405(a)(1)(1) _ 50.36(c)(1) 50.73(a)(2)(v) ___ 73.71(c)
LEVEL'- ._._ 20.405(a)(1)(ll) __ 50.36(c)(2) ___ $0.73(a)(2)(vii) ___ Other (Specify (101 _0l 0 ._ 20.405(a)(1)(iii) _X. 50.73(a)(2)(1) 50.73(a)(2)(viii)(A) in Abstract
/ /,/ / /,/,/,/,/,/ /,/,// /,/,/,/,/,/ /,/,/,/ / / __ 20.405(a)(1)(iv) _., $0.73(a)(2)(ii) _ 50.73(a)(2)(viii)(B) below and in
- 20.405( a)(1 )(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) Text)
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LIC{NJEE CONTACT FOR THIS LER (12)
Name: TELEdQNE NUPSER AREA CODE Jerald Waaner. Reaulalgry As1EAD.ge Ext. 2497 8l115 4l 51 Bl l 218101 COMPLETE ONE LINE FOR EACH COMPON N FAlltlRLQ{l(RISID_ IN THIS REPORT (13)
SYSTEH COMPONENT MANUFAC-- REPORTABLE CAUSE SYSTEH COMPONENT HANUFAC- REPORTABLE CAUSE TURER TO NPRDS TURER TO NPRDS_
l I l' I I I I I I I I I I I I I I I l-I l l I l l l l l SUPPLEMENTAL REPORT EXPECTED (141' Expected tienth l Dav l Year Submission
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lyes (If ves. complete EXPECTED SWISSION DATE) X l NO l ll ll ABSTRACT (Limit to 1400 spaces, i.e. approximately fif teen single-space typewritten lines) (16)
At 1450 on April 16, 1989 a plant-heatup was being monitored using a graph display on a Control Room monitor (CRT). At 1601 the Nuclear Station Operator (NS0) attempted to repair a failed recorder. At 1640 a Main Steamline (MS) Low pressure Reactor Trip. Safety Injection (SI), and MS Isolation occurred due to RCS
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t- -pr ssure being above 1930 (P-11) psig and MS pressure less than 640 psig. At 1646 the SI signal was reset.
At 1648 SI flow was terminated. This event was caused by management and procedural deficiencies. A formal policy on the use of the extra NSO during startup and heatup operations has been developed. The Plant Heatup procedure will be revised to add a hold point to verify that all Steam Generator pressures are greater than 640 prig before RCS pressure exceeds P-?). This event will be included in Reactivity Hanagement training I sessions. The CRT graph display will be modified to include an alarm for p-11. There was a previous cccurrence of inadvertent safety injection. This was due to testing the wrong channel during the performance of a surveillance. The corrective actions addressed both root and contributing causes for the event.
Prsvious corrective actions are not applicable.
2717A(112889)/2
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Form Rev 2.0 h LIEENSEE EVENT REPORT fLER) TEXT CONTINLIATION
_LER NutgER f 61 - Pane (3)
- FACILITY,N4fE (1) DOCKET NUPSER (2)'
[ , Year. / Sequential ff/j// Revision
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armi n i e l's'l o 1 0: 1 o'l '41 51 6 819 eIo12 o11 el 2 or el s ;
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c TEXTi Energy Industry, Identification System (EIIS) codes are identified in the text es [KX)
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l A. PLANT CONDITIONS PRIOR TO EVENT '
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- Unitt ' Braidwood li =
-- Event Date: April 16,1989; Event Time: 1640; .
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.Modet! 3 - Hot Standby; Rx Power: 0%;
!RCS (AB). Temperature / Pressure 500 degrees-F/1935 psig_
8 DESCRIPTIONOFEVENT5 .
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, ;ThIre were no systems cricomponents inoperable at the beginning of the event which contributed to the severity of
- the event.
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At 1450 on' April. 16, 1989 the'af ternoon shif t Nuclear Station Operator (NS0) (Licensed Reactor Operator) relieved 1
. the day shif t NS0_ on Unit-1. ' A plant heatup and pressurization were in progress'in accordance with IBwGP.100-1, .
- Plant Heatup. 3Two pressure loops associated with 1A and IB steam generators (SG). (AB) were simultaneously in test
- to facilitate Instrument Maintenance Department.(Ile) calibrations. Plant conditions at this time were:
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RCS Pressure: 1340 psig 4
, . RCS Temp: 460 degrees F SG Pressure = 431 psig ~ ~ ~ "
Pressurizer Pressure Control: Manual j_ !
!i Pressurizer Level Control: Manual SG Level Control: Manual The heatup and'pressertration'were being nonitored using a computer graph displayed on a Control Room monitor
'(CRI); 7 This graph _ displays the actual RCS Pressure and RCS Temperature over a green Target Value Line.
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Surveillances IBw0$ 4.9.2-1, Pressurizer . Temperature Limit Surveillance, and IBw0S 4.9.1.1-1, RCS . #
. Pressure / Temperature Limit Surveillance were in progress in accordance with IBwGP 100-1.
At 1530 the Unit 1 NSO observed that the IB RCS Cold leg RTD was providing erratic indication. He notified the Station Control Room Engineer (SCRE) and Technical Specification 3.3.3.5 Action Statement was entered.
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- From 1601 to 1639: .The Unit 1 NSO observed that the chart recorder pen for the failed RTD was not inking. He Cttempted to repair the'non-inking pen. During repair attempts he spilled ink on the chart, his hands, and the h . Main Control Doard. During the process of cleaning up the spilled ink, the Unit 1 NSO periodically monitored the l + hiatup'and pressurization on the CRT. He was also periodically monitoring upper norrie temperature on another
' CRT, making the ' required adjustments to the.1CV121, Pressurizer Level Control Valve, (CV) (CB) and the IFWO34A, B, L T [C, and'D,.SG Level Control Valves, (FW) (SJ) for each SG.
' . . At H1639 the-Unit 1 NSO observed that the actual Pressure versus Temperature was deviating from target value on the
, ' W htatup and' pressurization display on the CRT. After noting that pressure was higher than desired for the L temperatures he went to his desk'to refer to procedure IBwGP 100-1.
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1; hl ' 2717h(112889)/3',
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LICENSEE EVENT REPORT ILERI-TEXT CONTINUATION ' Form Rev 2.0 FACILITY NAPE (1). DOCKET NUDOCR (2) LER NUPSER (6) Pane (3) 0 Year- // Sequential / Revision
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f J 1_thlde r // Number sralt= :2 1 0is101010l41sf6 aI9 - 0l012 - 0l 1 01 J Of 01 6 TEXT: - Energy Industry Identification System (E!!S)-todes are identified in the text as (XX)
~B.- D O CRIPTION OF EVENT:. (Cont'd)
- At-1640 a Main Steamline Low Pressure Reactor Trip, Safety Injection (51) (BQ), and _ Main Steam 14ne Isolation
- occurred. _This was due to RCS pressure being above 1930 psig, the P-11 setpoint, in conjunction with Main
.Steamline (SB) pressure being less than 640 psig. Braidwood Emergency Procedure,18wtP-0, Reactor Trip or j l
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' Safety injection Unit 1, was entered. Injection of the cool Refueling Water Storage Tank (RWST) water
" resulted in an increase.in RCS pressure, a decrease in RCS temperature from 500 degrees F at the start of the .j cvent,' and a decrease in the Main Steamline pressure.
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At[1644 the' resultant insurge of relatively cooler RCS water into the Pressurizer caused the Pressurizer i
Liquid: Space water temperature to decrease from its initial value of 625 degrees F at the start of the event, i l 1At 1646 Braidwood Emergency Procedure, 19wEp ES 1.1, SI Termination Unit I was entered. The SI signal was l l
reset and termination of the SI flow was initiated.
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At 1648 the High Head Safety injection Isolation Valves were closed tennineting the safety injectio flow to the RCS. The Main Steamline. pressure reached a minimum value of 612 psig. I 1
1 At 1649 RCS pressure from,the SI achieved a maximum value of 2242 psig with a Main Steamline pressure of 612 f
.psig. ;This resulted in the Administrative Limit of 1600 psid to be exceeded by 30 psid.
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At 1650 the Pressurizer. Liquid Space temperature reached a minimum value of 518 degrees F. This indicated a
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' Pressurizer Liquid space.'cooldown of 107 degrees F in a 6 minute period which is in excess of the L -Administrative. Limit for cooldown of 100 degrees F in a one hour period. However, it was still well within ithe 200 degrees F in one hour limit allowed by the Technical Specifications. As a result of the termination
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i of -the 51 flow, the insurge flow to the pressurizer stopped and as a result the Pressurizer Liquid Space j
= water tempereture started to increase. l l
At'1651 the differential pressure between the RCS and the Main Steamlines decreased below 1600 psid with the RCS at 2155 psig and the Main Steamlines at 617 psig.
-At.1659 an Unusual Event was declared and terminated pursuant to the Generating Stations Emergency plan l
l; i(GSEP) Emergency Action Level (EAL) 2.g - ECCS initiation signal and resulf, ant injection to the vessel (Not
- . spurious).
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' At' 1704 the Nuclear Accident Reporting System (NARS) notification was made to declare and tenninate the
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. Unusual Event. l 1
1 At 1726 the Pressurizer Liquid Space temperature reached a peak value of 623 degrees F. This indicated a l- prsssurizer Liquid Space temperature increase of 105 degrees F in 36 minutes which is in excess of the l' ' Technical Specification Limiting Condition for Operation (LCO) of 100 degrees F in any one hour period.
Stable. plant tonditions were achieved.
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LICENSEE EVENT REPORT fLER) TEXT CONTINUATION Tore Rev 2.0 DOCKET NUPSER (2) ~LER NUPBER f6) Pane (3 FACILITY NAPE (1) s Year! /// Sequential /// Revision fff fff
/// Number /// Number s
raras.x.d1 o I s 1 0 1 o I o I di 51 6 e19 - oIo12 - ol 1 01'4 0F cl 6 Energy Industry Identification System (E!!$) codes are' identified in the text as (XX)
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- TEKT J
8.1 DESCRIPTION
OF EVENT:" (Cont'd)~
, The' appropriate'NRC notification via the ENS phone system was;made at 1732 pursuant to:
O -10CFR50.72(b)(2)(iv) .- Any event that results or should have resulted in Emergency Core Cooling System discharge .into the reactor coolant system as a result of a valid signal.
10CFR50.72(a)(1)-- The declaration of. any of the Emergency Classes specified -in the. Licensee's approved ,
Emergency Plan.
10CFR50.72(c)(1)(11() - A termination of the Emergency Class.
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The NRC notification vl's the ENS phone system was also made incorrectly pursuant to 10CFR50.36(c)(1)(ii)(A) based on a deficient Administrative Procedure for identifying and classifying events. The $1 automatically
' actuated at* the : correct setpoint.f Therefore, this reporting requirement is' inappropriate.
At approximatelyl2200 while reviewing the Pressuriser Temperature Limit Surveillance, it was discovered that
,th) bestup of the Pressurl er Liquid Space was in excess of the Technical Specificetion Limit of 100 degrees
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'T in a one hour period. The_LCO action statement was entered. An engineering evaluation was initiated to d;termine the ef fects of the heatup on the Pressurizer in accordance with the Technical. Specifications. +
4 (At0556'on. April 17,'1989[the.OnsiteReviewoftheengineeringevaluationwascompleted. The evaluation
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concluded that the structural integrity of the Pressurizer was ecceptable for continued operation.
- This event-is being reported pursuant to:
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10CFR50.73(a)(2)(iv).- Any event or condition that resulted in manual or automatic actuation of any 1: Engineered Safety Feature, including the Reactor Protection System.
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Any operation or condition prohibited by the plant's Technical Specifications.
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h :10CFR50'.73(a)(2)(1)
. Bdsed 'en che initta'l information associated with this event a "Braidwood Station Error Evaluation h - Presentation" was held to review this event with the personnel directly involved and their supervisor. The p 'ccrrective. actions addressing both root and contributing causes are detailed below. ,
ChCAUSEOFEVENT:
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Th2' root cause of the event was a Management deficiency. The responsibility for assessing, prioritizing, and
reassigning available personnel is a Management function. The SCRE is the Control Room Supervisor. He has the ultimate responsibility to ensure that Control Room work assignments are properly prioritized and that cdaquete personnel are assigned to tasks in progress. The SCRE was aware of the ink spill and cleanup iefforts but determined that prioritization or assigning additional personnel was not required. Cleaning up the spilled ink became a significant increase in the workload for the Unit 1 NSO.
L .The Operating Organizational scheme requires the HS0 position to share in the Management functions of prioritizing and personnel assignment for both control room and in plant work activities. The Unit 1 NSO centinued with cleanup efforts while monitoring the heatup. He did not request assistance.
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si sq 4 LICENSEE EVENT REPORT fLER) TEXT CONTINLl& TION form Rev 2.0 DOCKET NUPSER (2) . LER NUPBER f 61- Pane (31 ;
, T FACit!TY NME (1) -
b Year /// Sequential /// Revision fff fff
/// Number /// Numbn_
aral' ' 1~ o I-s I o I o I o I di 51 6 e19 - oIo12 - oI1 01 5 or el 6 g
TEXT; ' Energy, Industry Identificaticn System (Ells) codes are identified in the text as [XX) s
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h C. CAUSE 0F EVENT: ~(continued)-
'Bhththe'SCREandtheUnit1NS0hadtheresponsibilitytoeitherensurethat1or2availableNS0swas
- assigned to Unit I until .the cleanup was completed or assign the cleanup a priority that would not interfere with the monitoring of the heatup. The deficiency of both the SCRE and the Unit 1 NSO in this Management p ,
r;sponsibility created the error.
C:ntributing causes to this event were; '
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- 1. ' An' extra NSO was specifically added to aid the Unit 1 NSO during the plant heatup and pressurization evol uti on. - Since the Operating Department had no formal policy on the use of this extra NSO, the Shif t
- Engineer (Licensed Senior Reactor Operator) assigned him to unrelated activities associated with ,
' Unit 2. The Unit 1 NSO perceived this reassignment of personnel as direction that he was to handle the-6 Unit'I heatup alone.' ;
2.1 1(2)BwGP 100-1, Plant Heatup, contained no control point te verify that all SG pressures were greater .
L than 640 psig before RCS pressure exceeded the P-11 setpoint.
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I D. . SAFETY ANALYSIS:'
Thire was no effect on plant or public safety from this event as it occurred, as the plant was in hot standby
.cnd all plant equipment operated as designed.
All engineered safety features and the-reactor protection system, including manual reactor trip, were j' ' cp2rable to mitigate the consequences of this event.
E. ' CORRECTIVE ACTIONS:
Isenedia' te corrective actions: ~
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- 1. The $1 signal was reset and stable plant conditions were established.
2 An engineering evaluation of the structural integrity of the Pressurizer was performed for the pressure
-transient. The' evaluation concluded that the structural integrity of the Pressurizer was acceptable for-continued operation.
3.- Westinghouse has performed an analysis of the effects of this event on the structural integrity of the RCS. The analysis has concluded that the impact of this event on the structural integrity of RCS components is~ insignificant.
Based on the initial information associated with this event the personnel directly involved with this event participated in a "Braldwood Station Error Evaluation Presentation" to identify the root and contributing
.causes of.this event. Based on the conclusions of this presentation the following corrective actions will be taken:
- 1. Operating Department has developed and established a formal policy on the use of the extra NSO during startup and heatup operations.
/2717:(112889)/6-1, . _ _ _ _ _ _ _ _ _ _ _ _ _
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LICENSEE. EVENT REPORT (LER) TEXT' CONTINUATION Fore Rev 2 9._
FACRITY NME (1) DOCKET NUWER (2) LER NUM ER (6) Pane (3)
Year.: /// Sequential /// . Revision ,
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, eral" 1 - oIsIoIoIoI41516 e19 - o1012 - oI1 el 6 Or el 6 1 i TERT Energy Industry Identification System (E!!$) codes are identified in the text as [KK) -
J q E.;JCORRECTIVE ACTIONS: -(continued); 1
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. 2. . l1(2) DwGP-100-1. Plant Heatup will .be revised to establish a hold point to verify that all steam.
generator. pressures are greater than 640 psig before.RCS pressure exceeds P-11 setpoint. This will be.
Etracked to completion by Action Item 456-200-89-06103.
1 This event will be reviewed with Operating Department personnel as part of the training associated with
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L iReactivity Management. This will be tracked to completion by Action Item 456-200-89-06104.
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- 4. The heatup and pressu'rlastion computer graph display will be modified to include the setpoint for P-11.
This will be tracked to completion by Action Item 456-200-89-06105.
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F.n PREVIOU$ OCCURRENCES:
Th'ere was a previous occurrence of inadvertent- safety injection, DVR 20-1-88-019/LER 50-456-88-002. However,
- th;t event was due to an Instrument Mechanic testing the wrong channel during the performance of a
, surveillance. The corrective actions were implemented addressing both root and contributing causes for this
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y -cvent. Previous corrective actions are not appitcable to this event.
G. ' COMPONENT' FAILURE DATA *
. This event was not the ' result of component failure, nor did any components fall as a result of this event.
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