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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:RO)
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & BW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With ML20210R6421999-08-13013 August 1999 ISI Outage Rept for A2R07 ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20216D3841999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function M990002, Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function1999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With BW990016, Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20196A0721999-03-16016 March 1999 Cycle 8 COLR in ITS Format & W(Z) Function ML20207J4371999-03-0808 March 1999 ISI Outage Rept for A1R07 ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations BW990010, Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With ML20206U9011999-02-15015 February 1999 COLR for Braidwood Unit 2 Cycle 7. Page 1 0f 13 of Incoming Submittal Was Not Included BW990004, Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with BW990001, Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20206U9081998-12-17017 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function BW980076, Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3561998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Braidwood Generating Station,Units 1 & 2.With ML20155B6711998-10-26026 October 1998 Safety Evaluation Accepting Requests for Relief Associated with Second 10-yr Interval ISI Program Plan ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154D4401998-10-0202 October 1998 Safety Evaluation Authorizing Second 10-yr Interval ISI Program Request for Relief 12R-30 for Plant,Units 1 & 2 ML20155C2601998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Braidwood Generating Station,Units 1 & 2 ML20195F5911998-09-11011 September 1998 Special Rept:On 980812,addl Unseated Wires Were Discovered. Cause Is Unknown at Present Time.Util Evaluated Number of Unseated/Ineffective Wires & Determined Effect on Containment Structural Integrity.Commitments,Encl ML20196B3711998-09-0808 September 1998 Cycle 8 Operating Limits Rept (Olr) ML20151X6671998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Braidwood Generating Station,Units 1 & 2.With ML20238F3281998-08-31031 August 1998 SER Approving Second 10-year Interval Inservice Insp Program Request for Relief 12R-14 for Braidwood Station,Units 1 & 2 ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A1091998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Braidwood Generating Station,Unit 1 & 2 ML20236N7001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Braidwood Generating Station,Units 1 & 2 ML20198A0151998-06-18018 June 1998 10CFR50.59 Summary Rept 960619 Through 980618, Vols I & Ii,Consisting of Descriptions & SE Summaries for Changes to Procedural UFSAR Changes,Tests & Experiments & FP Rept.Without Fp,Rept ML20249A5451998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Braidwood Generating Station Units 1 & 2 ML20247F7711998-05-0808 May 1998 Special Rept:On 980403 & 980503 Seismic Monitoring Sys Was Declared Inoperable.Caused by 5-volt Power Supply & Regulator Card Failure.Imd & Sys Engineering Are Continuing to Identify & Resolve Problems So Sys Can Be Operable ML20247L7591998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Braidwood Generating Station,Units 1 & 2 ML20217K6331998-04-20020 April 1998 Safety Evaluation Accepting Methodology & Criteria Used in Generating Flaw Evaluation Charts for RPV of Braidwood IAW Section XI of ASME Code ML20216C6621998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Braidwood Generating Station,Units 1 & 2 1999-09-30
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. Comm:nws:lth Edison Braidwood Nuclear Power Station Route #1, Box 84 Braceville, lilinois 60407 Telephone 815/458-2801 August 19, 1993 BW/93-0233 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555
Dear Sir:
The enclosed Licensee Event Report from Braidwood Generating ,
Station is being transmitted to you with the requirement of 10CFR50.73 (a) (2) (i) (B), which requires a 30-day written report. -
This report is number 93-005-00, Docket No. 50-457.
, 1 K. L. Ko ton Station Manager Braidwood Power Station Encl: Licensee Event Report No. 50-457/93-005-00 cc: NRC Region III Administrator NRC Resident Inspector INPO Record Center CECO Distribution List 9
i
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9308250062 930819 PDR ADOCK 05000457 !w 8 / 1 S PDR id V '
N3C FORM 366 U.S. CIJCLEAR CILOJLATEDtY Cup 04]SSION AFP30tfLD BY OMB CJ0. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH II LICENSEE EVENT REPORT (LER) $4,3"'O$^mgNIsfEcADIG 3 c BURDEN ESil ATE O THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, (See reverse for required ruber of digits / characters for each block) WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY WAME (1) DOCKET NtMBER (2) PAGE (3)
Braidwood 2 05000457 1 OF 6 TilLE (4) ciissed surveillance on containment isolation valve due to personnet error and management deficiency FVINT DATF (5) ifR NUMRER (6) REPORT DATE (7) OTHER F ACIllTIES INV0tVED (8)
E AL R FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR MONTH DAY YEAR None 05000 FAC NAM C ET B 07 20 93 93 -- 005 -- 00 08 19 93 9 0
(&fRATING y THIS RFPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CIR i: (Check one or more) (11)
MCDE (9) 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b) payr" " *" "
LEVEL (10) 100 20.405(a)(1)(li) 50.36(c)(2) 50.73(a)(2M vii) OTHER
[ 20.405(aM1)(lii) X 50.73(a)(2)(i) 50.73(a)(2)(viii)( A) (Specify in a w 20.405(aM1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) 20.405(a)(1)(v) 50. 73(a)(2)(i i i ) 50.73(a)(2)(x) NRC Form 366A) llCENSEE CONT ACT FOR THlS (f R (12)
AAME TELEPHONE NUMBER (include Area Code)
P. Lau, Regulatory Assurance (815)458-2801 x2957 i
- CCMPlf TF ONE t INE FOR E ACM COMPOWINT F AllORE DESCRIBED IN THIS RFPORT (13) ,
CAUSE SYSTEM COMPOWENT 0 B MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER g No s
1 SUPPt f ME NTAL REPORT [KPECTfD (14) EXPECTED O TH DAY YEAR YES SUBMISSION (If yes, complete EXPECTED SUBMISS!ON DATE).
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single spaced typewritten lines) (16)
On June 11, 1993, Operations Department performed the RC Drain Tank l Containment Isolation Valve Stroke Test satisfactorily. On July 1, the Inservice Testing Coordinator (ISTC), after reviewing test results,
- initiated a Surveillance Request (GSRV) to increase the test frequency for valve 2RE9159B (RE). The ISTC incorrectly had Nuclear Group entered as the responsible department. On July 20, the RE system surveillance was late.
i The Nuclear Group leader contacted Primary Group, responsible for the RE system. The Primary Group Leader informed Operationc of the missed surveillance which was then completed the same day. The causes of the event were: work group misassignment, the GSRV item not reviewed by the Station Surveillance Coordinator, Nuclear Group leader assumed the GSRV item appeared on Primary Group's list, and no proceduralized routing process or formal _ training for station surveillance requests. The l corrective actions include procedural enhancements, training, and counseling. There have been previous reportable missed surveillances, however, the previous causes and corrective actions are not applicable to this event.
MC FORA 366 (5-92) idRC FORM 366A U.S. WUCLEAR RE0UULTORY C0MMISSION APPROVED BY OMB No. 3150-0104 (5-92) . EXPIRES 5/31/95 ;
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MNES 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET WlmBER (?) LER WLMBER (6? PAGE (3)
Braidwood 2 YEAR SEQUENTIAL REVISION m en w wer e 2 OF 6 05000457 93
-- 005 -- 00 TEXT (If more space is reevired. use edditional copies of NDC Form 366A) (17)
A. PLANT CONDITIONS PRIOR TO EVENT:
Unit: Braidwood 2; Event Date: July 20, 1993; Event Time: 0950; Mode: 1 - Power Operation; Rx Power: 100%;
RCS [AB] Temperature / Pressure: NOT/NOP <
B. DESCRIPTION OF EVENT:
There were no components or systems unavailable that contributed to this event.
On June 11, 1993, Braidwood Operations Department personnel performed surveillance BWVS 6.3.3-9, Reactor Coolant Drain Tank Containment Isolation 3 Valve Stroke Test. The surveillance met required acceptance criteria. The i completed surveillance was routed, and was reviewed on June 11, 1993, by the Operating Shift Supervisor, and by the Assistant Technical Staff Supervisor on June 18, 1993. On July 1, 1993, the surveillance was reviewed for trending by the Inservice Testing (IST) Coordinator. During the review, the IST Coordinator determined that the stroke time for valve 2RE9159B showed an increasing trend and was required to be placed on increased test frequency. The IST Coordinator initiated a General Surveillance Program (GSRV) Request form to have the valve entered in GSRV t for increased test frequency. The IST Coordinator then carried the form to the GSRV data entry clerk for entry into the GSRV computer program. A discussion ensued concerning four fields of the form that were not completed. These fields were: Responsible Department, Required By, Plant Condition, and Priority. Based upon the recommendations of the IST Coordinator, the GSRV data entry clerk entered the following information in l the fields: Department - TN (Systems Engineering Nuclear Group); Required '
By - BWVP 200-2; Plant Condition - 1,2,3,4; Priority - 1. The form was !
not reviewed by the responsible Department Head or the Station Surveillance Coordinator, contrary to BwAP 1400-2, Surveillance Request Form Completion.
i This.is partially due to the fact that the Station Surveillance Coordinator had been assigned other duties for an extended period of time. Upon completion of the form, the GSRV data entry clerk entered the information into the GSRV computer program with a date due of July 12, 1993, and a !
Critical Date of July 19, 1993.
On the afternoon of Tuesday, July 6, 1993, the GSRV data entry clerk 1 printed out the weekly surveillance schedules and routed them to the i appropriate departments. Upon receipt of the schedules for the Systems Engineering groups, the System Engineering clerk placed the schedules for i each group in their respective routing boxes. Upon receipt of the schedule for the Nuclear Group, the group leader reviewed the weekly schedule, and
N3C FORD 366 (5-92)
CRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5 92) EXPIRES 5/31/95 ESTIMATED BURDEN PER kESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS RECARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFcaMATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MhBB 7714), U.S. NUCLEAR REGULATORY COMMIS$10N, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150 0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. DC 20503.
TACitITY NAME (1) DOCKFT NtMBER (2) LER NtMBER (6) PAGF (3)
Braidwood 2 YEAR SEQUENTIAL REVISION 05000457 93 0 3 OF 6
- 005 -
TEXT (If more space is reovired. use additional copies of NRC Form 3664) (17) noticed that there was a surveillance on his sheet for the RE (Reactor Equipment Drains) System. He determined that since this surveillance concerned the RE system, it did not belong to the Nuclear Group, and assumed that it was also on the responsible department's schedule.
On the afternoon of July 12, 1993, the GSRV data entry clerk printed out the weekly surveillance schedules and routed them to the appropriate departments. On the morning of July 13, 1993, upon receipt of the schedule for the Nuclear Group, the group leader reviewed the weekly schedule, and determined that the RE system surveillance was still on the schedule. The group leader assumed that the GSRV computer program had not been updated to reflect that the surveillance had been completed.
On July 19, 1993, the Nuclear Group surveillance schedule for July 12, 1993 was returned to the GSRV data entry clerk with the surveillance for valve 2RE9159B lined out with no explanation. The GSRV data entry clerk took no action concerning the line out. On the afternoon of July 19, 1993, the GSRV data entry clerk printed out the weekly surveillance schedules and routed them to the appropriate departments. On the morning of July 20, 1993, upon receipt of the schedule for the Nuclear Group, the group leader reviewed the weekly schedule, and determined that the RE system surveillance was still on the schedule and was in fact past the critical date. The Nuclear Group leader then contacted the Primary Group leader '
concerning the missed surveillance. The Primary Group Leader informed the Assistant Technical Staff Supervisor and the Operating Engineer of the ,
missed surveillance. The missed surveillance was completed by the Operations Department on July 20, 1993.
Emergency Notification System (ENS) notification was not required per 10CFR50.'72.
C. CAUSE OF THE EVENT:
The primary cause of the event was cognitive personnel error. The In- 6 Service Testing Coordinator made a misassignment of the responsible work group to perform the surveillance when it was placed on an increased test l frequency. The Systems Engineering Nuclear Group was assigned responsibility instead of the correct department, which was the Operating Department. Additionally, the new surveillance form generated for the increased frequency surveillance was not reviewed and approved by the ,
Department Head and the Station GSRV Coordinator in accordance with BwAP ,
1400-2 prior to being entered into the GSRV computer program. The required signature are to indicate approval of the data supplied and acceptance of ;
the work.
Sf3C FORh 366 (5-02)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5-92) -
EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS RECARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MkBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACitITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
Braidwood 2 YEAR SEQUENTIAL REvlslON 05000457 93 4 of 6
-- 005 -- 0 TEXT (if more space i reavired use additional copies of NEC rorm 366A) (17)
One contributing cause of the event was also cognitive personnel error.
When the GSRV listing of surveillances was distributed and an unfamiliar surveillance appeared on the Nuclear Group's listing, the group leader improperly assumed that it also appeared on another group's list. When the next week's listing was received by the Nuclear Group, a questioning attitude was not exercised. When the third printout was received by the s Nuclear Group on July 20, 1993, the Primary Group Leader was finally contacted in regards to the surveillance in question.
A second contributing cause to this event was a management deficiency in the surveillance program. There is no proceduralized routing process for station surveillances after they are completed. After the valve was tested on June 11, 1993, it was not identified as being required to be placed on increased testing frequency until July 1, 1993. This resulted in a less than timely routing for the surveillance from the Operating Shift Supervisor, through Systems Engineering, and ultimately arriving at the IST Coordinator.
Another contributing cause of this event was a management deficiency, with a lack of formal training for department surveillance coordinators and clerical personnel involved with the surveillance program. Several individuals involved with this event were new in their positions, and had not received any formal training on the processing of surveillances (Nuclear Group Leader and IST Coordinator).
D. SAFETY ANALYSIS:
Though 2RE9159B (RCDT to Gas Analyzer Outside Isolation Valve) was not stroked in accordance with the increased frequency requirements, this event had no effect on plant or public safety. This event was of no significance for the followir.g reasons:
- 1) The plant was stable at 100% power and no abnormal additions were ;
made to the RCDT during 7/19/93 and 7/20/93.
- 2) 2RE9159B was closed at the time the surveillance was due on 7/19/93 ,
until it was stroked for the required surveillance on 7/20/93. The valve was returned to the closed position upon completion of the required surveillance.
i
- 3) 2RE9159B receives an auto close signal on a Phase A Containment Isolation Signal to ensure Containment is isolated from the Auxiliary Building and the environment. Since this valve was i
already in the closed position, no valve movement would have been required should a Phase A have occurred.
W3C 70#C 366 (5-92)
'kRC FORM 366A U.S. NUCLEAR REGULATORY CCM ISSION APPROVED BY OMB No. 3150-0104 (5-92) EXP!RES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS lhFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESilMATE TO LICENSEE EVENT REPORT (LER) T ,< E INFoRMAiloN AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (Mas m4), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACit1TY NAME (T) DOCKET NtMBER (2) LER NtMRER (6) PA T (3)
Braidwood 2 yggp SEQUENTIAL REVISION 05000457 93 5 OF 6
-- 005 -- 0 l
t TEXT (if more space is reovired. use additional copies of NRC Form 366A) (17)
All Engineered Safeguards Features and the Reactor Protection System were operable during the time frame that 2RE9159B was inoperable due to the failure to perform the increased stroke surveillance.
E. CORRECTIVE ACTIONS:
Immediately upon identification, the missed surveillance was completed by the Operations Department on July 20, 1993. ;
A training program will be developed to train present and future Departmental Surveillance Coordinator (s) and Surveillance Scope Operator (s) l on the surveillance program procedures, in order for them to better understand the GSRV process and their functional responsibilities. This will be tracked to completion by action item 457-180-93-00501.
The importance of self checking and attention to detail were reemphasized with the Nuclear Group Leader and ISTC involved with this event. The fostering of a questioning attitude through the STAR process (Stop, Think, Act, Review) was the main focus of this discussion. This event was also the topic of a site wide In-House Operating Experience Report. This Report was made a part of required tailgate training for all site personnel.
The BwAP 1400 series procedures and tb.e Surveillance Coordinator position-cescriptions will be revised to rcilect the current site processes and functions. Improvements will be considered to increase the GSRV Program efficiency and effectiveness. A proceduralized routing process for ,
- completed surveillances will also be considered. This will be tracked to i completion by action item 457-180-93-00502.
F. PREVIOUS OCCURRENCES: ,
LER 50-456/91-009, Gas Decay Tank Sample Not Obtained Due to Procedure Deficiency LER 50-456/93-003, Missed Technical Specification Surveillance Due to Wiring Discrepancies LER 50-457/91-004, Personnel Error Results In Late Performance Of Technical Specification Surveillance t LER 50-457/91-005, Sample Required By Technical Specifications Obtained Late Due to Personnel Error ,
i LER 50-457-93-004, Core Reactivity Normalization Surveillance For Unit 2 Cycle 4 Not Performed In Required Time Frame 1
7 b
NRC FORM 366 (5-92)
ORC FORM 366A U.S. NUCLEAR RECULATORY COMMISSION APPR"VED BY OMB No. 3150-0104 (5 92) . EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQ' JEST: 50.0 HRS.
FORWARD COMMENTS REGARDlhG BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASH!hGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MAN AGEMENT AND BUDGET, WASHlWGTON, DC 20503.
FACILITY NAMF (1) DOCKE T NLMBER (2) ifR NLMBER (6) PAGE (3)
Braidwood 2 yEAg SEQUENTIAL REVISION NUpprp Nuwpre 6 Op 6 05000457 93 -- 005 -- 00 TEXT (!f more space is reovired, use additional copies of NRC Form 366A) (17)
There have been previous occurrences of failure to perform technical specification surveillances within the specified time periods. Corrective actions were implemented addressing both root and contributing causes. Previous corrective actions are not applicable to this event.
G. COMPONENT FAILURE DATA:
P None
,