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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:RO)
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & BW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With ML20210R6421999-08-13013 August 1999 ISI Outage Rept for A2R07 ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20216D3841999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function M990002, Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function1999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With BW990016, Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20196A0721999-03-16016 March 1999 Cycle 8 COLR in ITS Format & W(Z) Function ML20207J4371999-03-0808 March 1999 ISI Outage Rept for A1R07 ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations BW990010, Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With ML20206U9011999-02-15015 February 1999 COLR for Braidwood Unit 2 Cycle 7. Page 1 0f 13 of Incoming Submittal Was Not Included BW990004, Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with BW990001, Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20206U9081998-12-17017 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function BW980076, Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3561998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Braidwood Generating Station,Units 1 & 2.With ML20155B6711998-10-26026 October 1998 Safety Evaluation Accepting Requests for Relief Associated with Second 10-yr Interval ISI Program Plan ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154D4401998-10-0202 October 1998 Safety Evaluation Authorizing Second 10-yr Interval ISI Program Request for Relief 12R-30 for Plant,Units 1 & 2 ML20155C2601998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Braidwood Generating Station,Units 1 & 2 ML20195F5911998-09-11011 September 1998 Special Rept:On 980812,addl Unseated Wires Were Discovered. Cause Is Unknown at Present Time.Util Evaluated Number of Unseated/Ineffective Wires & Determined Effect on Containment Structural Integrity.Commitments,Encl ML20196B3711998-09-0808 September 1998 Cycle 8 Operating Limits Rept (Olr) ML20151X6671998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Braidwood Generating Station,Units 1 & 2.With ML20238F3281998-08-31031 August 1998 SER Approving Second 10-year Interval Inservice Insp Program Request for Relief 12R-14 for Braidwood Station,Units 1 & 2 ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A1091998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Braidwood Generating Station,Unit 1 & 2 ML20236N7001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Braidwood Generating Station,Units 1 & 2 ML20198A0151998-06-18018 June 1998 10CFR50.59 Summary Rept 960619 Through 980618, Vols I & Ii,Consisting of Descriptions & SE Summaries for Changes to Procedural UFSAR Changes,Tests & Experiments & FP Rept.Without Fp,Rept ML20249A5451998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Braidwood Generating Station Units 1 & 2 ML20247F7711998-05-0808 May 1998 Special Rept:On 980403 & 980503 Seismic Monitoring Sys Was Declared Inoperable.Caused by 5-volt Power Supply & Regulator Card Failure.Imd & Sys Engineering Are Continuing to Identify & Resolve Problems So Sys Can Be Operable ML20247L7591998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Braidwood Generating Station,Units 1 & 2 ML20217K6331998-04-20020 April 1998 Safety Evaluation Accepting Methodology & Criteria Used in Generating Flaw Evaluation Charts for RPV of Braidwood IAW Section XI of ASME Code ML20216C6621998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Braidwood Generating Station,Units 1 & 2 1999-09-30
[Table view] |
Text
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- Commonweaph Edison .
1* _ Br;idwood Nucint Powir Station Rout 3 #1, B:x 84 Braceville, Illinois 80407
' - . _ Telephone 815/458 2801 -
g i
i May 3,1990 I BW/90-4484 o
i U. S. Nuclear Regulatory Commission i Document Control Desk j Washington, D.C. 20S55 j
Dear Sir:
The enclosed Licensee Event Report from Braidwood Generating !
Station is being transmitted to you in accordance with the requirements of 10CFR50.73(a)(2)(iv) which requires a 30-day written report. . j q
This report is number 90-003--00; Docket No. 50-457.
Very truly yours, !
R. E. Querto i Station Manager i Braidwood Nuclear Station !
REQ /JDW/jfe l (7126z)
Enclosure:
Licensee Event Report No. 90-003-00 cc: NRC Region III Administrator NRC Resident Inspector INPO Record Center CECO Distribution List 9005090051 900504
,PDR ADOCK 05000437 #4%
PDC ,
I t
bt .,
LICENSEE EVENT REPORT (LER)
Form Rev 2.0 factitty,Name (1) Docket Number (2) Paos (3)
_$raithtood 2 01 51 Ql 01 01 41 51 7 1!of!O!4 Title (4)'
Inadvertant Train B Safety Injection due to Programatic Deficiency Event Date (5) LER Number (6) Report Date (7) Other Facilities Involved (B)
Honth Day Year Year // Sequential /j/j
/ Revision Month Day Year Facility Names Docket Number (s)
/j/jj/
/ Number f
/// Number None 0151010101 l l 01 4 01 5 91 0 91 0 0l0l3 Ol 0 015 01 4 91 0 0151010101 I l THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10CFR Khtch_Dat_or more of the followina) (11)
N 20.402(b) _ 20.405(c) .1. 50.73(a)(2)(iv) _ 73.7)(b)-
PUWER _ 20.405(a)(1)(i) __ 50.36(c)(1) _. 50.73(a)(2)(v) _ 73.71(c)
LEVEL 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vil) (nher (Specify
!0 !O (10) 0 _ 20.405(a)(1)(iii) _ 50.73(a)(2)(1) __ 50.73(a)(2)(viii)(A) in Abstract
///////////,///////,//,///,/,// __ 20.405(a)(1)(iv) _ 50.73(a)(2)(ii) _._ 50.73(a)(2)(viii)(B) below and in v //////////j///////}//' /j//j/'/ //
j _ 20.405(a)(1)(v) _ 50.73(a)(2)(iii) __ 50.73(a)(2)(x) Text)
LICENSEE CONTACT FOR THIS LER (12)
Name TELEP'ONE NUtEER AREA CODE Phil lau. HPES CD.D_rJ_inator Ext. 2957 841l5 415181-1218101 COMPLETE ONE LINE FOR EACH COMEDRE FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE
- IVRER TO NPRDS TURER TO NPRDS I I I I I I I i l l I I I I I I I I I I I I I I l i l I SUPPLEMENTAL REPORT EXPECTED (14) Erpected Month I Day I Year Submission lYes (If ve3. complete EXPICTED SUBMISSION DATE)
X l NO l l l_
ABSTRACT (Limit to 1400 spaces, i.e. approximately fifteen single-space typewritten lines) (16)
L At 0730 on April 6,1990 a Nuclear Station Operator (NS0) placed Train B of the Solid State Protection System I ($$PS) in test for maintenance to troubleshoot a defective test lamp. At 0905 it was identitleo that the
' voltage drop across the relay that was in series with the test lamp was greater than optimum value. This combined with a blue lens cap caused the light to appear dark in the florescent illumination of the room. At 0916 the NSO restored the Train B SSPS to normal by placing the Input Error Inhibit Switch in the " Normal" position and the Output Mode Selector Switch in the " Operate" position. This resulted in a Pressurizer Low Pressure and Main Steamine Low Pressure Safety Injection .(SI) initiation signal for Train B. Restoring inputs to normal prior to reestablishing the blocks with Psessurizer and Steamline pressures below the satpoints initiated an SI signal. The cause of this event was a programatic deficiency. Operating had no formal policy regarding manipulations of SSPS panel components following maintenance. A contributing cause to this event was personnel error. A program will be developed to provide specific guidance for restoring an SSPS train to operable status. Training will be conducted. The lens will be evaluated for replacement. A caution placard will be placed on the SSPS panels. There have been no previous similar occurrences.
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'( _ ' LICENSEE EVENT REPORT f LER)' TEXT'CQt[UMBHON Forn Rev L D_
FACI!.!TY,NAME (1)- DOCKET NUN ER (2) _LER_gggER .f 6) _ _ Pane (3)
Year // Sequential // Revision l
/j/j/j Number j//j/j
, / / NumbE_
Braldaged 2 0 1 5 1 0 1 0 l 0 1 61 51 7 g10 . 0l013 - 01 0 01 2 0F _0) A
, TEXT' Energy Industry Identification System (EIIS) codes are identified in the text as (XX]
Al PLANT CONDITIONS PRIOR TO EVENT:
Unit: Braldwood 2; Event Date: April 6, 1990; Event Time: 0916;
~Hody; N - Defueled; Rx Power: 07.;
~RCS (A0] Temperature / Pressure: Ambient / Atmospheric -
,lB. 'OESCRIPTION OF EVENT: .
There were no systems or components inoperable at the beginning of the event which contributed to the severity of
'th2 event.
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Instrument Maintenance Department Parsonnel were preparing to troubleshoot an apparent defective test lamp circuit in Train B Solid State Protection System (SSPS) (JE).
At approximately 0730 on April 6.1990 the Station Control Room Engineer (SCRE) (Licensed Senior Reactor Operator)-
authorized an Instrument Maintenance Technician (IHT) (non-licensed Instrument Technician) to troubleshot;t the ;
cause of a defective test lamp in the Train B SSPS panel, 2PA10J. The SCRE assigned an extra Nuclear. Station Operator (NS0) (Licensed Reactor Operator) to assist the IHT.
The IHT and the NSO proceeded to the Unit 2 Auxiliary Electrical Equipment room (AEER) where Panel 2PA10J was' !
-located. The INT asked the NSO to establish the conditions under which the test lamp was expected to illbainate.
Th) NSO notified the Unit 2 NSO and then pimd the Inpet Error Inhibit Switch -in the " Inhibit" position and the Output Mode Selector Switch in.the " TEST" position. The NSO provided the.IHT with a copy of Unit 2 Braidwood
(*parating Surveillance (2Bw05) 3.1.1-21 Unit Two SSPS, Reactor Trip Breaker, and Reactor Trip Bypass Breaker BI-Monthly (Staggered) Surveillance (Train B) af ter opening the procedure to the spot.where the test lamp dJficiency had been identified. The NSO then returned to the Control Room where he continued the performance of othtr unrelated activities. The INT began troubleshooting in the $$PS. Panel.
=AL,0905 the IHT completed his trouble shooting activities. The IHT Identified that the voltage drop across the
. relay that was in series with the test lamp was 9.47 VDC.. This was greater than the optimum value of 6.54 VDC.
With the slightly larger voltage drop combined with a blue lens cap the light appeared to be dark in the bright l . florescent illumination of the AEER. When the lens cap was shaded by the IHT holding his hand above the light it -
was evident that the bulb was lit, and the test circuit was functioning properly. The INT requested an NSO to perfonn the Post Maintenance Verification in accordance with his work package.
The SCRE assigned the same NSO who had performed the initial setup to assist the IHT. The extra NSD returned to ths AEER several minutes later. f At approximately 0914 the NSO verified that the lamp was illuminating when required during the testing sequence.
Tha IHT informed the NSO that he could restore the Train B $$PS to normal.
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LIEENSEE EVENT REPORT _(LERl TEXT EONTINUATION Form Rev 2.0 g~ FACILIJY NAME (1) DOCKET NUtBER (2) _LER nut 9ER (6) Page (3) j//jj/ Sequential
+
, Year //j/ Revision 4 Number fj/
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1/f Numbt.E-
.Braldwood 2 0 1 5 l 0 1 0 1 0 1 41 51 7 910 - 0l0l3 - 0l 0 01 3 0F 01 4 TEAf- Energy Industry Identification System (E!IS) codes are identified in the text as (XX)
At 0916 the extra NSO informed the Unit 2 NSO that he was, restoring the Train B SSPS to normal. The extra NSO then placed the Input Error Inhibit Switch in the " Normal" position and the Output Mode Selector $ witch in the " Operate" position. This <esulted in a Pressuriter low Pressure and Main Steamline Low Pressure Safety Injectiun (SI) initiation signal for Train B. Placing the Output Mode Selector switch in the Test
- p;sition, as the NSO did to setup the panel for trouble shooting, reset the Pressurizer low Pressure and Main Steamline Low Pressure 51 blocking circuitry for Train B. These circuits are normally blocked during shutdown when Pres?urizer pressure decreases below 1930 psig. Restoring inputs to normal prior to reestablishing the blocks with Pressurizer and Steamline pressures below the setpoints of 1829 psig and 640 psig respectively resulted in Train B $5PS initiating an 51 signal.
All equipment that was operable functioned as designed.
At 0922 the Train B SI was reset.
The appropriate NRC notification via the ENS phone system was made at 1029 pursuant to 10CRF50.72(b)(2)(li).
This event is being reported pursuant to 10CFR50.73(a)(2)(lv) - any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature. including the Reactor Protection System.
C. CAUSE OF EVENT:
The root cause of this event was a programatic deficiency. Operating Department had no formal policy regarding manipulations of $$PS panel components follo.#ing maintenance or during non-routine evolutions.
While the surveillance procedures provided detailed and accurate steps for normal panel testing they were not will sulted for setup and restoration following trouble shooting activities. During previous similar cctivities Operating personnel had either used the applicable portions of these procedures as guides or had relied on their knowledge and experience. The $$PS panels are complex and require manipulations that must be performed in a specific sequence to provide for the availability of wanted functions and to avoid inadvertant actuation of. undesired functions. Manipulation of components in these panels should only be made within the bounds of a structured policy. The failure to have this policy created the event.
A contributing cause to this event was a cognitive personnel error by the extra NSO. It is the responsibility _of the NSO to verify that actions taken are correct and appropriate prior to performing those ections. The failure of the extra NSO to perform the "self check" responsibility prior to performing actions that would return the Train D SSPS to an operable status contributed to the event.
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LIEENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rev 2.0 FACILITY, NAM (1) DOCKET NUMBER (2) _LER NUteER (6) Page (3)
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fff Revision fj/
// Jumber /// Nuadi T_ ]
,Ja h wand 2 015101010141517 910 - OjjLl 3 - 01 0 01 4 07 _ _0]_4 TEXT Energy Industry Identification System (Ells) codes are identified its W text as (XX)
-D. SAFETY ANALYSIS:
This event had no ef fect on the safety of the plant or the public. All operable systems performed as d; signed. The reactor vessel was defueled.
Had this event occurred in Mode 1 at 100% power t.bere would still be no ef fect. The Intermediate Range High Flux and the Power Range High Flux Low Setpoint Reactor Trips would be re enabled and a reactor trip would occur. No S! or Main Steamline isolation would occur as Pressurizer Pressure and Main Steamline Pressure would be above the respective setpoints.
E. CORRECTIVE ACTIONS:
Automatic actions for operable systems were verified. it.e SI was reset and those components that rep;sitioned were returned to normal.
B:sid on the initial information associated with this event the personnel directly involved with this participated in a "Braidwood Station Error Evaluation Presentation" to identify root and contributing causes of this event. Based on the cc :lusions of this presentation the following actions will be taken:
- 1. A program will be daveloped to provide specific guidance for actions taken to remove an $$PS train from operable status and restoring an $$PS train to eperable status. This program will address both startup.
shutdown, and operational modes. This action will be tracked to completion by action item 457-200-90-00801.
- 2. A training tailgate session will t,e conducted to discuss this event with appropriate Operating personnel.
This action will be tracked to completion by action item 4S7-200-90-00802.
- 3. An evaluation will be conducted to determine if the blue lens on the master relsy test lamp can be replaced with a lens that provides greater visibility. This action will be tracked to completion by action item 457-200-90-00803.
V' 4. A placard will be placed on the $$PS panels cautioning the operator to ensure that the blocks are re-established prior to returning the Input Error Inhibit Switch to normal. This action will be tracked to completion by action item 4S7-200-90-00804.
- F. PREVIOUS DCCURRENCES:
Thire have been no previous similar occurrences.
G. COMPONENT FAILURE DATA:
This event was not the result of component f ailure, nor did any components fall as a result of this event.
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