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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:RO)
MONTHYEARML20029D6301994-05-0505 May 1994 LER 94-003-00:on 940405,reactor Tripped Due to Main Power Transformer Failure.Corrective Actions:Detailed Investigation Performed for Collateral Damage & Isophase Bus Cleaned & inspected.W/940505 Ltr ML20029D2351994-04-29029 April 1994 LER 94-006-00:on 940330,discovered That Braidwood Cooling Lake Hydrographic Survey Was Not Completed within Required Time.Cause Was Personnel Error.Corrective Action: Surveillance Was Completed within 24 hours.W/940429 Ltr ML20029D6121994-04-29029 April 1994 LER 94-002-00:on 940331,discovered 2A Auxiliary Feedwater Pump Auto Starting.Caused by Procedural Deficiency. Auxiliary Feedwater Pump 2A Secured by Placing Control Switch in Pull Out position.W/940429 Ltr ML20046D5971993-08-19019 August 1993 LER 93-005-00:on 930720,missed Surveillance on Containment Isolation Valve Occurred Due to Personnel Error & Mgt Deficiency.Enhanced Procedures,Training & Counseling. W/930819 Ltr ML20044F5531993-05-19019 May 1993 LER 93-003-00:on 930419,TS Violated Due to Source Range Reactor Trip Capability Being Blocked.Caused by Personnel Error & Procedural Deficiency.Individuals Involved Counseled & Procedure developed.W/930518 Ltr ML20044D2071993-05-14014 May 1993 LER 93-002-00:on 930414,unplanned ESF Actuation Occurred When All Four SI Accumulator Isolation Valves Closed & Accumulator Pressure Reduced.Caused by Mgt Deficiency. Training Will Be conducted.W/930514 Ltr ML20024G7411991-04-24024 April 1991 LER 91-005-00:on 910326,main Control Room Ventilation Sys Shifted to Emergency Mode of Operation Due to Momentary Fluctuation in Voltage Available to Monitor.Lightning Protection Sys Being modified.W/910424 Ltr ML20028H8631991-01-24024 January 1991 LER 90-023-00:on 901230,generator Neutral Ground Overcurrent Protective Relay Actuated & Tripped Main Generator.Caused by Internal Generator Defect.Main Generator Disassembled & Rotor Removed to Locate ground.W/910124 Ltr ML20028G9151990-09-24024 September 1990 LER 90-015-00:on 900827,auxiliary Bldg Vent Stack Grab Sample Missed.Caused by Personnel Error & Deficient Work Practices.Training Provided,Program Modified & Station Reviewing Nonroutine Surveillance process.W/900924 Ltr ML20043H4071990-06-20020 June 1990 LER 90-007-00:on 900523,pressurizer Pressure Channel 458 Failed Low & Channel 455 Deviated in Excess of Remaining Two Channels.Caused by Defective Wire on Internal Portion of Pressure Transmitter.Transmitter replaced.W/900621 Ltr ML20043G6051990-06-14014 June 1990 LER 90-008-00:on 900517,unit at Power Permissive Circuit Actuated on Train a of Solid State Protection Sys.Caused by Procedural Deficiency in That Switch Rotation Not Specified. Procedure revised.W/900614 Ltr ML20043A6571990-05-16016 May 1990 LER 90-006-00:on 891204 & 900416,diesel Generator 1B Experienced Slow Start.Caused by Crisscrossed Starting Airlines for Cylinders 6L & 9L.Starting Airlines Reconnected & Verified to correct.W/900516 Ltr ML20043A6611990-05-14014 May 1990 LER 90-004-00:on 900416,diesel Generator 2A Speed Oscillated Prior to Maint Teardown.Caused by Component Failure.Resistors Replaced & Placed on 3-yr Replacement frequency.W/900516 Ltr ML20042G7041990-05-11011 May 1990 LER 90-005-00:on 900413,determined That Pressures for MSIVs a & D Were Outside Acceptance Criteria of Procedure.Caused by Procedural Deficiencies.Procedures Being Revised to Reflect Values of 4,800 Psig to 6,000 psig.W/900511 Ltr ML20042F5441990-05-0404 May 1990 LER 90-003-00:on 900405,inadvertent Train B Safety Injection Initiation Signal Occurred Due to Programmatic Deficiency. Training Developed & Lens Evaluated for Replacement. W/900503 Ltr ML20006E4811990-02-0909 February 1990 LER 90-002-03:on 900119,discovered That Flanges Not Added to Procedure 1BwOS, Primary Containment Integrity Verification of Outside Containment Isolation Devices. Caused by Program Weakness.Training held.W/900216 Ltr ML20006E4041990-02-0202 February 1990 LER 90-001-00:on 900112,reactor Tripped During Dc Ground Isolation Activities When Auxiliary Relay Energized,Causing Turbine Governor & Reheat Interceptor Valves to Close.Caused by Increasing Steam Pressure.Valves closed.W/900206 Ltr ML19354E0141990-01-22022 January 1990 LER 89-020-00:on 891223,failure to Verify Safety Injection Accumulator Boron Concentration within Specified Time.Caused by Programmatic Deficiency.Procedure Revised to Include Action Requirement sheet.W/900122 Ltr ML19354E0131990-01-16016 January 1990 LER 89-008-00:on 891228,equipment Attendant Discovered Refueling Water Storage Tank Vent Line Temp Less than 35 F. Caused by Preservice Deficiency.Storage Tank Vent Path Temp Verified at 36 F.W/900119 Ltr ML20006B2081990-01-12012 January 1990 LER 89-019-00:on 891219,discovered That Procedure Did Not Adequately Test Response Times for High Steamline Pressure Rate Steamline Isolation Signal.Caused by Deficient Procedure.Procedures Re Response Time revised.W/900112 Ltr ML20005F9611990-01-0808 January 1990 LER 89-017-00:on 891206,gas Detector Channel of Process Radiation Monitor Experienced Spike,Resulting in Alert Alarm.On 891210,spike on Channel Resulted in High Radiation Alarm.Caused by Failed detector.W/900109 Ltr ML20005E8561990-01-0202 January 1990 LER 89-018-00:on 891215,as Lead on volt-ohm Meter Landed, Containment Bldg Fuel Handling Incident Area Radiation Monitor Went Into Alert Alarm & Interlock Actuation.Caused by Procedure Deficiency.Signal reset.W/900102 Ltr ML20005E7851989-12-29029 December 1989 LER 89-016-00:on 891201,RHR Pump Suction Relief Valve Premature Actuation Occurred & Failed to Reseat.Caused by Deficient Work Practices & Pesonnel Error.Maint Procedures Reviewed.Training conducted.W/891229 Ltr ML19354E1621989-12-18018 December 1989 LER 87-006-01:on 870120,4 H Fire Watch Patrol Detained by Radiation Chemistry Personnel Due to Not Signing Latest Radiation Work Permit & on 870131,did Not Start Route.Caused by Personnel Error.Personnel retrained.W/900110 Ltr ML20005D6801989-12-0808 December 1989 LER 89-007-00:on 891110,w/auxiliary Feedwater Pump 2B Pump Control Switch in Pull Out Per Stated Reasons,Automatic Initiation of Pump Sys Unavailable for 6 Minutes.Caused by Procedural Deficiency.Keys to Be Color coded.W/891208 Ltr ML19332E6261989-12-0202 December 1989 LER 89-015-00:on 891020,sample Canisters for Auxiliary Bldg Vent Stack Radiation Monitor Removed & Not Analyzed within 48 H.Caused by Programmatic Deficiencies & Personnel Error. Procedures & Training Programs revised.W/891204 Ltr ML19332E5121989-11-29029 November 1989 LER 89-014-00:on 891030,inadvertent Safety Injection Occurred on Train B During Installation of Card Holders. Caused by Personnel Error Design Deficiency.Sys Mod Request submitted.W/891129 Ltr ML19332E6411989-11-22022 November 1989 LER 89-002-01:on 890416,main Steamline Low Pressure Reactor Trip,Safety Injection & Main Steamline Isolation Occurred. Caused by Mgt & Procedural Deficiencies.Formal Policy on Use of Extra Operator During Startup developed.W/891129 Ltr ML19332C5681989-11-17017 November 1989 LER 89-006-00:on 890314,nonlicensed Operator Placed Eductor 2B Spray Additive Tank Suction Throttle Valve 2CS021B in Locked Open Position.Caused by Incorrect Valve Labeling. Valves to Be Provided W/High Visibility labels.W/891117 Ltr ML19327C2591989-11-15015 November 1989 LER 89-012-00:on 891016,momentary Loss of Power to Fuel Handling Bldg (Fhb) Area Radiation Monitor Caused Fhb Charcoal Booster Fan to Auto Start.Caused by Personnel Error.Fan Secured & Isolation Signal reset.W/891114 Ltr ML19354D4711989-11-0303 November 1989 LER 89-013-00:on 891005,discrepancy W/Design of Steam Generator Blowdown Sys Identified,Minimizing Auxiliary Feedwater Flow Requirements.Caused by Preservice Design Deficiency.Temporary Design Changes made.W/891103 Ltr ML19354D4721989-11-0101 November 1989 LER 89-005-00:on 891002,discovered That Tech Spec Action Statement Was Not Entered When safety-related Bus Was Removed from Svc.Caused by Procedural deficiency.Out-of-svc Procedure Will Be revised.W/891101 Ltr ML19325D5191989-10-20020 October 1989 LER 89-011-00:on 890920,high Head Safety Injection Valve 1SI8801A Not Capable of Being Powered by Operable Emergency Power Source.Caused by Diesel Generator 1A Being Out of Svc. Policy Statement Issued & Program revised.W/891020 Ltr ML19325D4851989-10-13013 October 1989 LER 89-010-00:on 890915,measured Leakrate of Hydrogen Analyzer Containment Isolation Valve Was Larger W/Valve Indicating Closed.Caused by Incorrect Labeling of Coil Leads.Valve Replaced W/Different Model valve.W/891012 Ltr ML19325C2851989-10-0303 October 1989 LER 89-004-00:on 890907,reactor Trip Occurred as Result of Lightning Induced Voltage Transient Affecting Rod Control Sys.Caused by Lightning Striking Containment.Rod Control Sys Devices reset.W/891006 Ltr 1994-05-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & BW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With ML20210R6421999-08-13013 August 1999 ISI Outage Rept for A2R07 ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20216D3841999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function M990002, Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function1999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With BW990016, Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20196A0721999-03-16016 March 1999 Cycle 8 COLR in ITS Format & W(Z) Function ML20207J4371999-03-0808 March 1999 ISI Outage Rept for A1R07 ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations BW990010, Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With ML20206U9011999-02-15015 February 1999 COLR for Braidwood Unit 2 Cycle 7. Page 1 0f 13 of Incoming Submittal Was Not Included BW990004, Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with BW990001, Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20206U9081998-12-17017 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function BW980076, Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3561998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Braidwood Generating Station,Units 1 & 2.With ML20155B6711998-10-26026 October 1998 Safety Evaluation Accepting Requests for Relief Associated with Second 10-yr Interval ISI Program Plan ML20207H7671998-10-0505 October 1998 Rv Weld Chemistry & Initial Rt Ndt ML20154D4401998-10-0202 October 1998 Safety Evaluation Authorizing Second 10-yr Interval ISI Program Request for Relief 12R-30 for Plant,Units 1 & 2 ML20155C2601998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Braidwood Generating Station,Units 1 & 2 ML20195F5911998-09-11011 September 1998 Special Rept:On 980812,addl Unseated Wires Were Discovered. Cause Is Unknown at Present Time.Util Evaluated Number of Unseated/Ineffective Wires & Determined Effect on Containment Structural Integrity.Commitments,Encl ML20196B3711998-09-0808 September 1998 Cycle 8 Operating Limits Rept (Olr) ML20151X6671998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Braidwood Generating Station,Units 1 & 2.With ML20238F3281998-08-31031 August 1998 SER Approving Second 10-year Interval Inservice Insp Program Request for Relief 12R-14 for Braidwood Station,Units 1 & 2 ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A1091998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Braidwood Generating Station,Unit 1 & 2 ML20236N7001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Braidwood Generating Station,Units 1 & 2 ML20198A0151998-06-18018 June 1998 10CFR50.59 Summary Rept 960619 Through 980618, Vols I & Ii,Consisting of Descriptions & SE Summaries for Changes to Procedural UFSAR Changes,Tests & Experiments & FP Rept.Without Fp,Rept ML20249A5451998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Braidwood Generating Station Units 1 & 2 ML20247F7711998-05-0808 May 1998 Special Rept:On 980403 & 980503 Seismic Monitoring Sys Was Declared Inoperable.Caused by 5-volt Power Supply & Regulator Card Failure.Imd & Sys Engineering Are Continuing to Identify & Resolve Problems So Sys Can Be Operable ML20247L7591998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Braidwood Generating Station,Units 1 & 2 ML20217K6331998-04-20020 April 1998 Safety Evaluation Accepting Methodology & Criteria Used in Generating Flaw Evaluation Charts for RPV of Braidwood IAW Section XI of ASME Code ML20216C6621998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Braidwood Generating Station,Units 1 & 2 1999-09-30
[Table view] |
Text
e _.
g -w Commonwoalth Edison
, ) Br:ldwood Nuclear Power Station
- it; l -
4 Rout)C1. Box 84
. p .1. * \ -
t Braceville, Illinob 60407 >
7 N Telephone 815/458-2801 lr'. >
November 29,1989 ,
BW/89-3080 'i t
i f
U. S. Nuclear Regulatory Commission l Document Control Desk ;
Washington, D.C. 20555 !
Dear Sir:
The enclosed Licensee Event Report from Braidwood Generating
- Station is being transmitted to you in accordance with the requirements of 10CFR50.73(a)(2)(iv) which requires a 30-day written report.
This report is number 89-014-00; Docket No. 50-456.
Very truly yours, ;
d R. E. Quer o Station Manager Braidwood Nuclear Station j
! REQ /JDW/jfe ;
(7126z) a j u
Enclosure:
Licensee Event Report No. 89-014-00 l
1.
l cc: NRC Region III Administrator ;
NRC Resident inspector i INPO Record Center L CECO Distribution List ;
1,
., 0 *
.e , ,
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- t.!CENSEE EVENT REPORT (LER) facility Name (1) Docket Number (2) ,fgge_(31
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0_J 0 111 21 9 81 9 01 5}Jj_.01 01 I l THl$ REPORT 15 $UBMITTED PURSUANT 10 THE REQUIREMENi$ OF 10CIR 9pg 1(b.ttk one er more of ibs_.{ellowino) (11) 20.dO2(b) 20.405(c) 2. 50.73(a)(2)(tv) __ 73.7)(b)
POWER _ 20.405(a)(1)(i) __ 50.36(c)(1) _. 50.71(a)(2)(v) _. 73.71(c)
LEVEL 20.405(a)(1)(li) 50.36(c)(2) __ 50.73(a)(2)(vil) __ Other (Specify 0l0 (10) 0 ___. 20.40$(a)(1)(111) 50.73(a)(2)(1) __ 50.73(a)(2)(viii)(A) in Abstract
////////////////////////// 20.40$(a)(1)(iv) ___ 50.73(a)(2)(11) _ 50.73(a)(2)(viii)(B) below and in
////////////////////////// _._ 20.405(a)(1)(v) _ 50.73(a)(2)(iii) _.__ 50.73(a)(2)(x) Text)
Ll(18$[E CONTACT fjR THIS LER (12) iELEpHONE NLPSEp Name AREA CODE
._Jerrv Waant.r. Regulalerr_Asivunce E t _2497 8l115 41 51 81 l 21 81 01 COMPi[li_Qt4121NL LQJLEACH COMPON N FAIWEE DESCRigiDJN Jgl$ REPORT (13)
REPORTABLE CAUSE SYSTEM COMPONENT MANUTAC- REPORTABLE CAUSE SY$i[M COMPONENT MANUFAC-TURER TURER TO NPRD.$,
___TO NPRDS I _
l i 1. 1 I l_ N l _.] l l l I 1 I I I I i 1 1 I I I I I I l
$UPPLEMENI AL RifDE.LL)(PL(JED (141 Espected Month l D.ty_}_hti Submission Date (15) ' '
-lytal}L.3fL_IDeplelt MPEllD }VHMi$$10N DATE) X l N0 l l l l l_
ABSTRACT (Limit to 1400 spaces, i.e. approximately fif teen single-space typewritten lines) (16)
On October 30, 1999 Contractor personnel were installing card holders on lever-type switches in the Main Centrol Room. At 1105 a lever was removed from a switch and placed on the control panel near the Pressuriser
( Low Pressure Safety Injection (SI) Block / Reset switch for Train B. At 1107 the Train B Pressuriser Low pressure $1 Logic Circuit reset. A Train B $1 occurred. The IB Diesel Generator started, the Auxiliary Building Ventilation realigned and a charging pump suction va?ve opened. All other $1 components were removed froe service. The $1 initiated actuation signals for Fuel Handling Building Ventilation. Containment Phase A ! solation. Containment Ventilation Control Room Ventilation, and feedwater Isolation. The root cause of this event was personnel error. It is believed that the contracted electrician inadvertently bumped ,
l the 51 Block / Reset Switch while reaching f or the lever handle that was laying on the control board by the Block / Reset switch. A contributing cause of this event was a design deficiency. The automatic functions
! sere verified upon receipt of the actuation. The equipment was returned to its original status. This event l
was discussed with the Contracted electricians. A method will be devised to block protective functions not l rsquired during Cold Shutdown and Refuel /Defuel modes. No previous occurrences.
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l 2931s(112989)/2
. Lggt($LL.LyENT ktPORT (Ltti TEXT ggtingpH F tw Rev 2.e.
FACILITY NAME (1) DOCKET NVPSER (2) ..LER.Nupe.ER (6) Pane (3)
Year //
fj/j Sequential // Ri'i'"
/// Number /j/u/
/ Number _
araidwood 1 eisIeIeie 1 41 51 6 819 -- ei114 - eie el 2 or el_4 TERT Energy Industry Identification System (E!!$) codes are identified in the text as (KK)
A. PLANT COND; TION $ PR102 TO EVENT:
Unit: Braidwood I; Event Date: October 30, 1989; Event Time: 1107; Cbde: . N-Defurled; Rx Power: 0%;
RC$ (AB) Temperature / Pressure: Amblent/ Atmospheric B. DESCRIPTION Or EVENT:
s There were no systems or components inoperable at the beginning of the event which contributed to the severity t,f ;
=the event.
The $olid State Protection System ($$PS) (JE) had been maintained functional for various surveillance testing even i though the Reactor was defueled.
On October 30, 1989 Electrical Contr6ctor personnel were installing control switch Out of Service Card holders.
These holders were being installed on all lever-type switches on the Main Control panels of Unit 1. This was part
$f the planned activities for the refueling outage. 10 install the holder the outer portions of the switch were disassembled. The holder device was then placed on the panel. The switch was then reassembled. The installation i process required about 3 minutes to complete.
At 1105 holder installation was initiated on the Pressuriser level Select switch. The switch lever was removed ,
and placed on the control panel about 8 inches from the Pressuriser low Pressure $afety Injection ($1) Block / Reset switch for.frain B.
At 1107'the contractors were at the point in the process where switch lever replacement was the next step to be !
performed. At this time the Train B Pressurizer low Pressure $afety injection Logic Circuit reset. The
- Fressurl er was completely depressurited. This was bslow the 1829 psig Pressurizer to Pressure $1 setroint. A
' Train B Safety Injection occurred within a fraction of a second after the logic circuit reset. The IB Diesel Generator (CK) started. The Centrifugal Charging Pump (CB) Refueling Water Storage Tank (BQ) saction valve, [
ICV 112E, opened. The Auxiliary Building Charcoal Booster f ats (VA) (Vf) started and dampers repositioned to
- provide flow through the charcoal absorbers. All other components that receive an actuation signal as the result cf a Train B $1 signal were removed from service.
The Safety injection initiated the following actuations signals:
- 1. Containment Phase A Isolation - No components repositioned because all Phase A components were already isolated.
- 2. Containment Ventilation (VA) Isolation - This isolated the Containment purge which was in progress.
- 3. Control Room Ventilation (VC) (VI) Actuation - This caused the B frain of VC to shift to the Mabeup Mode and started the B Hakeur Fan, DVC03CB.
2931 (112989)/3
. LliLM31L.LY[N_ T REPORT (LER) TEXT [0 tin!6E110N igm _l(ty_2J, TACIT!TY NAME (1) 00CKET NUPSIR (e) ,,_LLIL)lUtfER f 6i Page f3)
Year /// Sequential /// Revision fff fff
/// Numb 3r /// Number _ [
.prale = 1 0Is10l0Io141516 e19 - 0l114 - 61.'0 01 3 0F 01 4 f IERT Energy Industry Identification System ([Il$) codes are identified in the text as (KK) 1
- 5. DE$CRIPi!ON OF [ VENT: (Continued) ;
4 Feed =ater Isolation (5J) $1gnal - No components repositioned because the feedwater system was isolated.
}; 5. Tuel Handling Building Vent 41stion (VA) (VG) Actuation-This caused f an OVA 04CB to start and repositioned dampers to direct flow through the charcoal adsorbers beds.
Nuclear Statien Operators (Licensed Reactor Operators) verifled automatic actions. The actuation signals were reset. Components that had auto started / repositioned were returned to thvir stendby allynment.
The appropriate NRC notification via the [N$ phone system was made At 124$ pursuant to 10CfR50.72(b)(2)(ll).
This event is being reported pursuant to 10CFR50.73(a)(2)(l*)-any event or condition that resulted in manual ,
cr automatic actuation of any Engineered $afety Feature, including the Reactor Protecilon System. l C. CAUSE Of EVENT:
The rest cause of this event was an apparent personnel error. It is believed that the contracten electrician ,
inadvertently bumped the Low Pressurizer Pressure 51 Block / Reset switch. This occurred while reaching for the lever handle that was laying on the control board approximately 8 inches to the lef t of the Block / Reset '
switch. Both contractors were interviewed. They were at the step in the installation process where picking up the lever handle would have been the next action.
The contractor who would have performed the action stated that he did not believe he had bumped anything. He tas wearing a thick flannel shirt. The cuf f was rolled up 1 fold and was hanging down appro Imately 3
- inches. From the position where the contactor was standing the Block / Reset switch would have been directly '
below the path that his right hand would have taken to reach for the lever handle. And the direction would have moved the Block / Reset switch in the Reset direction.
The Low Pressuriser Pressure SI Block / Reset switch was a Westinghouse OT2 lever type switch. Tests had been ctnducted on this type of switch as part of an investigatien of a previous non-reportable event. Based on these tests the following has been concluded about this type of switch: l
- 1. The switch will operate with a very small degree of movecent.
- 2. The awnunt of force required to operate the switch could be undetectable for an inadvertent bump especially if the bump was created by catching it on a piece of clothing.
The $$PS System Technical Expert (5TE) (non-licensed engineer) performed an evaluativn of B Train of $$PS.
Based on this evaluation it has been concluded that the SSPS train was functioning satisf actorily. And the Low Pressuriser Pressure $1 logic circuit reset s'id not occur due te any problem internal to 5$PS. The STE
- j. also operated the Block / Reset switch several times. The STE's centlutions were consistent with the OT2 switch tests results discussed above.
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-29312(112889)/4
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. _Ll(Mit EVENT PEPORf (LER) TEXT (9EI14UAT10N Fem Rev 2.0 (ACIL13Y WhME (1) 00CKLT NJ1Br.R (2) ,_LER NUMBER (6) Pane (3)
Year /// Sequential Revision ff
//j/ Number. N aber_
o I s I e I e I o I di 51 6 e19 -
ol114 - oI o el 4 L _g u hahmL1 TEXT Energy Industry Identification $ystem (E!!$) sodes are identified in the text as (KK)
C. CAUSE OF LVENT: (Continued)
A contributing cause of this event was a design deficiency. The outage activities required the $$p$ input Error Inhibit $ witch to be In " Normal" for Instrument Maintenance Surve111ance festing. The $$p$ Output Mode Selector switch was required to be (n *0perate" for Contalament Ventilation Actuation to remain operable. As ,
a result of these requirements protective functions of $$p5 that are only required for higher Modes of ,
Opstation were functional with the Reactor completely defueled.
D .' $ATETY ANALY$l$:
This event had no ef fect on the safety of the plant or its public. The systems that had not been removed from service eperated as designed. The Reactor had been completely defueled. The protective functions provided by a S.iety injection were not required and were inapproorlate for the existing plant conditions.
Discussions on redundant equipment are not appitcable. This $1 actuation was neither required nor desired.
There are not reasonsable and credible alternative conditions that would have been more severe.
E. CORRECTIVE ACTION $ ,
the automatic functions of the $1 and its associated actuations were verified upon receipt of the altre. The actuation signals were reset. The equipment that had actuated was returned to its original status.
This event was discussed with the Contracted electricians by the Superintendent of the contracting compary .
and Coasenwealth Edison Hanagement.
An evaluation of the functional requirements of the $$p$ has been conducted. Based on the results of the evaluation the following has been concluded:
- 1. The system should be modified to provide the capability to block protective functions that are inappropriate for Mode 5 and 6 while retaining those functions that are desired.
- 2. This capability could be achieved by either permanent modification or Temporary Alteration that would be installed / removed during each extended shutdown. l A Modification Request has been submitted. This will be tracked to completion by action item 456-200-89-17701.
F. PREVIOU$ OCCURRENCES:
DVR Numbsr Title 20-1-87-043/87-010 Inadvertent Loss of power to Instrument bus 111 resulting in e Reactor Trip due to personnel Error-Contractor
'20-1-89-166/89-012 Containment Vent Isolation and Fuel Handling Bldg f an Start on Homentary loss of power due to personnel Error, t
The corrective actions were implemented addressing both root end centributing causes. Previous ccrrectivt actions are not applicable to this event.
G. COMPONENT FAILURE DATA:
l This event was not the result'of component failure, nor did any components fall as a result of this event.
l 29312(112989)/5 9
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